ML050830489

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Confirmatory Action Letter Public Meeting Slides
ML050830489
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 03/14/2005
From:
Nuclear Management Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML050830489 (36)


Text

Point Beach Nuclear Plant Confirmatory Action Letter Public Meeting March 14, 2005 1

Introduction PBNP is attaining lasting and effective performance improvement in key areas.

Sustainable behavioral changes are driving Point Beach to Excellence.

2

Focus Areas

Ø Human Performance

Ø Corrective Action Program

Ø Emergency Preparedness

Ø Oversight and Assessment

Ø Engineering Organizational Effectiveness

Ø Configuration Management

Ø Management Effectiveness

Ø Equipment Reliability

Ø Training Organizational Effectiveness 3

CAL Action Completion Progress

Ø 88 CAL packages are ready for NRC review

Ø 33 CAL packages are in the internal review process

Ø There are 22 CAL action steps remaining to be done

Ø Our Six for Success

§ Dry Cask Storage Project - Complete

§ Unit 2 Spring Outage

§ CAL Closure

§ Unit 1 Fall Outage

§ Operations Training Program Accreditation Renewal

§ INPO 2006 E&A 4

Key CAL Accomplishments

Ø Zero modifications open greater than 90 days

Ø Human Performance Event Free Clock Improved from 28 to 73 Days

Ø Maintenance Rule (a)(1) Systems Reduced from 13 to 7

Ø Emergency Preparedness Staff has completed 104 Qualification Signoffs out of a total of 123 5

Focus Area: Human Performance Actions

Ø Human Performance Steering Committee meets monthly to provide direction on strategic issues

Ø Established departmental human performance teams and a working level Human Performance Group

Ø Held multiple human performance stand-down enhancement days and jamboree 6

Focus Area: Human Performance Actions (cont)

Ø Human Performance enhancement day scheduled for Unit 2 outage

Ø Picture of Excellence will be communicated to outage supplemental workers

Ø Utilizing Management human performance enhancement tools to reduce latent organizational weaknesses 7

Focus Area: Human Performance Results (cont)

Ø Site Human Performance Event Clock average days between resets based on 12-month rolling average is 61

Ø No significant human performance events or LERs related to human performance

Ø ACEMAN and Picture of Excellence being utilized at all organizational levels 8

Focus Area: Human Performance Challenges

Ø Identifying latent organizational weaknesses

Ø Continuing to demonstrate value of human performance tools at all levels in organization

Ø Improving critical feedback on training and job observations 9

Focus Area:

Corrective Action Program (CAP)

Actions

Ø Established Departmental Roll-Up Meeting (DRUM) process

Ø CAP Owner process 10

Focus Area:

Corrective Action Program (CAP)

Results

Ø DRUM process illuminates strengths and weaknesses

Ø Fewer CAP extensions

Ø Screen team preparation, participation and peer challenge have improved the CAP process 11

Corrective Action Program (CAP)

Results (cont)

Ø Root and apparent cause corrective actions are improving performance and reducing significance of issues

Ø Timeliness in performing corrective actions has improved

Ø Technical Review Panel (TRP) acceptance rates have improved

Ø Corrective Action Review Board (CARB) effectiveness continues to improve 12

Corrective Action Program (CAP)

Challenges

Ø More effective use of DRUM 13

Focus Area: Emergency Preparedness Actions

Ø Hired EP Coordinator with extensive EP experience

Ø EP equipment matrix completed to establish configuration control

Ø Procedures and processes enhanced

Ø Training on new Emergency Action Levels 14

Focus Area: Emergency Preparedness Results

Ø Increased experience and improved staffing

Ø Improved processes and procedures

§ PI data collection and retention improved

§ Procedure revisions and 50.54(q) reviews improved

§ Procedure use and adherence improved

§ EP equipment matrix establishes configuration control 15

Focus Area: Emergency Preparedness Challenges

Ø Implementation of approved Emergency Action Levels (EALs) and training

Ø Drill and exercise performance improvement 16

Focus Area: Oversight and Assessment Actions

Ø Trained staff on problem statement development methodology

Ø Assessors are assigned to departmental functional areas

Ø Rotational assignments from the line have been implemented 17

Focus Area: Oversight and Assessment Results

Ø Long-standing Quality Assurance findings have decreased

Ø Line recognizes value of Nuclear Oversight by requesting emergent assessment in potential problem areas

Ø Use of problem statement development sheets was a weakness turned into a strength

Ø Quarterly exit meetings are continuing to improve and are effective 18

Focus Area: Oversight and Assessment Challenges

Ø Identifying behavior gaps in performance vs. identifying the symptoms

Ø Assessing against excellence standards rather than traditional compliance 19

Engineering Organizational Effectiveness Actions

Ø Operational Decision Making Issue (ODMI) evaluation process implemented

Ø Forced Outage/Derate/Short Limiting Condition for Operation procedure initiated

Ø Station Top Equipment Issues list

Ø Increased emphasis on Maintenance Rule systems to minimize out-of-service time in emergency diesel generator and gas turbine outages 20

Engineering Organizational Effectiveness Actions (cont)

Ø Reduced corrective and elective maintenance backlog

Ø Engineering/Operations team building training

Ø Assigned station Equipment Reliability Coordinator

Ø Engineering human performance training

Ø Engineering Safety and Design Review Group (ESDRG) and Quality Review Team (QRT) directed feedback and coaching 21

Engineering Organizational Effectiveness Results

Ø Significant improvements in forced outage performance

Ø Total operator burden continues to decrease

Ø Continued use of ODMI has been effective

Ø The corrective maintenance work order backlog CAL goal was achieved in January 2005

Ø Elective maintenance work order backlog reduction

Ø Maintenance procedure corrective feedback reduction 22

Engineering Organizational Effectiveness Results (cont)

Ø Safety Injection system was returned to (a)(2) status in December 2004.

Ø No new systems added to (a)(1) status.

Ø Station cold weather preparations

Ø The quality of Engineering products continues to improve. The ESDRG has had a positive influence

Ø QRT-directed rework remains stable

Ø Human performance clock reset frequency improvement 23

Engineering Organizational Effectiveness Challenges

Ø Integration of ODMI with Other Work Processes

Ø Plant Health Committee long range effectiveness

Ø Managing Operations procedure backlog

Ø Improving equipment failure analyses 24

Actions

Ø Safety-related calculation project work is progressing

Ø Increased management oversight and challenge board reviews

Ø Station focus on modification package closeout

Ø Configuration management procedure revisions are on schedule

Ø Plan developed and support obtained for Service Water and Fire Protection Design Basis Documents 25

Focus Area: Configuration Management Results

Ø Complete review of CAL related calculations

Ø Condition of safety-related calculations is known

Ø Control of old and new calculations

Ø Project plan for calculation project revision phase developed

Ø Calculation preparation priorities established

Ø Resource loaded schedule established

Ø Several calculations are in process of revision 26

Results (cont)

Ø Modification closure backlog reduced to zero

Ø We are closing out modifications in a timely manner

Ø Change in station behavior and focus on modification closeout

Ø 38 of 51 configuration management procedures reviewed/revised 27

Challenge

Ø Calculation project progress, oversight and resource management 28

Focus Area: Management Effectiveness Actions

Ø Interim effectiveness review of the Auxiliary Feed Water cause evaluations completed Results

Ø Final effectiveness review is planned and scheduled

Ø The remaining original Auxiliary Feedwater related Operability Determination is the nonconforming condition tied to increasing the margin to safety Challenges None 29

Actions

Ø Changed evaluation software for bolted fault calculations

Ø Increased emphasis on Maintenance Rule systems to minimize out-of-service time and (a)(1) action plan resolution 30

Focus Area: Equipment Reliability Results

Ø Bolted fault modifications continue.

Project is approximately 60% complete

Ø Bolted Fault outage scope has been defined and on-line work is progressing

Ø Operable but Degraded/Non-Conforming issues 31

Focus Area: Equipment Reliability Results (cont)

Ø Maintenance Rule (a)(1) systems have been reduced from 13 to 7

Ø Maintenance Rule (a)(1) criteria has not been exceeded for any new systems

Ø IST program equipment requiring increased frequency testing has been reduced to zero 32

Focus Area: Equipment Reliability Challenges

Ø Bolted fault calculations 33

Focus Area:

Training Organizational Effectiveness Actions

Ø Weekly monitoring of core qualification progress

Ø Rotation of an engineering supervisor to engineering training Results

Ø Ownership for qualification progress has been embraced

Ø Significant progress in obtaining core qualifications 34

Training Organizational Effectiveness Results (cont)

Ø Training has improved human performance and configuration management

Ø Effectiveness review concluded program was strong with minor improvement opportunities Challenges

Ø None 35

Summary

Ø Point Beach culture is improving

Ø Multiple examples of sustainable behavior changes 36