ML17317B212

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LER 79-032/03L-0 on 790416:during Routine Channel Calibr, Bistable FB-510B Trip Point Was Nonconservative W/Respect to Tech Spec Limit.Caused by Excess Drift.Bistable Recalibr
ML17317B212
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 05/16/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B209 List:
References
LER-79-032-03L, LER-79-32-3L, NUDOCS 7905220339
Download: ML17317B212 (2)


Text

NRC FORM 366 U. S. NUCI.EAR REGULATORY COMMISSION (7-77)

LtCENSEEEEVENT REPORT CONTROL BLOCK: Q1 {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 7 8 9 M I D0 LICENSEE CODE I

0 IP200000000000Q341 14 15 6

LICENSE NUMBER 25 26 1

LICENSE TYPE 11Q4~PE 30 57 CAT 58 CON'T Eo SOURCE ~Q6 I LI~ 5 0 0 0 3 1 5 Q,,O 4 1 6 7 9 QB O 5 > 6 7 9 Qg 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES ~10 DURING A ROUTINE CHANNEL CALIBRATION OF STEAM AND FEED FLOW NISNATCH INSTRUNENTATION

'HE TRIP POINT OF BISTABLE FB-510 B WAS FOUND TO BE NON-CONSERVATIVE WITH RESPECT TO THE LIHIT IMPOSED BY T.S. TABLE 2.2-1 ITEM 14.

~O6

~os

~O7

~OS 80 7 8 9 SYSTEM CAUSE CAUSE COMPONENT CODE COMP., VALVE CODE CODE SUBCODE SUBCODE SUBCODE

~oe 7 8 9

~IA 10 QE ~EQ72 11

~G 12 p79 13 I N S T R .U 18 Q74 ~SQEE 19

~Z 20 Q16 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LERIRO REPORT ACTION FUTURE EVENT YEAR

~79 21 22 EFFECT

+

23 SHUTDOWN

~03 24 REPORT NO.

2 26 U~

27 M~~

28 ATTACHMENT CODE 29 NPRDP TYPE UL 30 PRIME COMP.

31 NO.

UD 32 COMPONENT TAKEN ACTION ON PLANT METHOD , HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER 0 0 0 0 2 0 33 Q~IQ19 34

~2Q20 35 DXQ27 36 37 40 UN 41 Q HVQ24 42

~NQ25 43 44 W 1 47 QER CAUSE DESCRIPTION AND CORRECTIVE ACTIONS F21)

THE CAUSE OF THE NON-CONSERVATIVE'TRIP POINT HAS BEEN ATTRIBUTED TO EXCESSIVE DRIFT. THE BISTABLE WAS RECALIBRATED AND OPERATION WAS MONITORED WITH NO ADDITIONAL DRIFT NOTED TO DATE.. PREVIOUS MONTHS'HANNEL FUNCTIONAL TESTS WERE CONSULTED WHICH INDICATE NO RECENT HISTORY Of DRIFT PROBLEMS. NO FURTHER ACTION IS 3

CURRENTLY PLANNED.

4 I ~p 7 8 9 80 FACILITY STATUS H

SG 0

POWER 0 0 OTHER STATUS NA Q METHOD OF DISCOVERY ROUTINE TEST DISCOVERY DESCRIPTION Q32

~BQ31 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEEASED OF RELEASE AMOUNT OF ACTIVITY, Q LOCATION OF RELEASE Q OZ LJ 7 8 9 Q33, 10 Q34 11 NA 44 45 NA 80 PERSONNEL EXPOSURES 7 8 9 11 12 13 80 PERSONNEI. INJURIES 6 ~>8 0 Qo NA 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY "Q

TYJE DESCRIPTION Q43 NA 7]~5 ZZogg(

7 8 9 10 80 o Me ISSUED PUBLICITY DESCRIPTION ~ NA NRC USE ONLY 7 8 9 10 68 69 80 ER T. P. Beilman 61 6-465-5901 0 NAME OF PREPARER PHONE:

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