05000315/LER-1979-030-03, /03L-0 on 790417:while Performing Routine Surveillance Test on AB Diesel Generator,Load Conservation Circuitry Did Not Fully Function as Design.Cause Under Investigation

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/03L-0 on 790417:while Performing Routine Surveillance Test on AB Diesel Generator,Load Conservation Circuitry Did Not Fully Function as Design.Cause Under Investigation
ML17317B210
Person / Time
Site: Cook 
Issue date: 05/16/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B209 List:
References
LER-79-030-03L, LER-79-30-3L, NUDOCS 7905220326
Download: ML17317B210 (1)


LER-1979-030, /03L-0 on 790417:while Performing Routine Surveillance Test on AB Diesel Generator,Load Conservation Circuitry Did Not Fully Function as Design.Cause Under Investigation
Event date:
Report date:
3151979030R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7-77)

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9 Qs DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 WHILE PERFORMING A ROUTINE SURVEILLANCE TEST ON THE AB DIESEL GENERATOR IN ACCORDANCE WITH T.S. 4.5.1.1.2.b.3, THE LOAD CONSERVATION CIRCUITRY OID NOT, FULLY FUNCTION AS DESIGNED.

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