ML17326A546

From kanterella
Revision as of 05:25, 29 October 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
LER 80-004/03L-0:on 800202,during Normal Operation,While Investigating Problem W/Test Circuit for B Main Turbine Stop Valve,Found Mounting Bracket for Proximity Switch Failed. Caused by Loosened Mounting Assembly Due to Vibration
ML17326A546
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/27/1980
From: Rischling J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A545 List:
References
LER-80-004-03L, LER-80-4-3L, NUDOCS 8003040582
Download: ML17326A546 (2)


Text

)V,.+C FOSIMi366 I~NUCLEAR REGULATORY COMI))IISSION

{7 77I LICENSEE EVENT REPORT CONTROL BLOCK: I f I Qi 'PLEASE PRINT OR TYPE ALL REQUIREO INFORhlATIONI I

7 8 9 Mti D fc LICENSEE CODE C ~JQ2 Olo O O LICENSE NUIEIBER I 2)~u~lLJ~ Qs CON'T

~01 "oo'"oo ~LQR~05 0 0 I 0 3 I I I 0 'Q)jo 2 0 2 Qs 0 2 21 7 8 0/09 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 76 RCPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUE)4CES QIO 2 L

THE "B"'AIN TURBINE STOP VALVE, IT WAS DISCOVERED THAT THE MOUN'I ING BRACKET FOR THE I PROXIMITY SWITCH HAD f:AILED. THIS PROXIMITY SWITCH PROVIDES TURBINE STOP VAlVE I O IS .CLOSURE INDICATIOII FOR THE REACTOR PROTECTION SYSTEM. THIS IS NON-CONSERVATIVE IN

.

RESPECT TO.-T.S. TABLE 3.3-1 iTEM 18.B. THE AFFECTED CHANNFL WAS PLACED IN THE TRIP CONOIYIOAII AS REOUIREO.

L

~OS 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE

~o) 2 ~t>

CODE CODE" 2 Q ~Q SUBCODE COMPONENT CODE

~I~Y~LIIIQ LLIQ SUBCODE SUBCODE

[z> Q

I Q>>

7 8 9 10 11 12 13 18 19 SEQUENTIAL OCCURRENCE RLPOPT REVISIOI'I G)

ACTIOi4 FUTURE LERIRQ llo)ORT FVENT YEAR

~gP 21 22 EFFECT

~

23 SHVTDOENE4

~PP 24 RFPORT NO.

O .

26

~~

27 28 ATTACHMENT CODE

[gJ~29, NPRO 4

)YPE 30 ~

PRIME COMP.

31 32 NQ.

COMPOi'IENT TAKEN ACTION ON PLANT h'IETHOD HOURS Q22 SUBMITTED FORh1 SUB. SUPPLIFR MANUFACTURER

~OQTR ~ZQER 33 34 " ~ZQ)o 35

~ZQst 36 37

~0~00 I 0.

40 IY 41 I Q22 ~NQ24 LAgQ>> ~i~l~liQRF 42 43 44 47 CAUSE OFSCRIPTICN ANO CORRECTIVE ACTIONS Q27 V* TI IITIOA lt-" ALE II I R I' IELI St 2AEV:.AO~

t TAI Ii . IVIIEVE, II tT Itl I il IOIIL 0 "AVE: tVE ~

IIV EVENT STOP VALVE "B" HAD ACTUALLY SHUT. THE PROXIMITY SWITCH ITSELF DID NOT FAIL.

3 .THE'FAILURF. WA IN " tI NTI G ASSEMBLY. WHICH VIBRATED I OSE. T PRF F IN Tt'J SEE ATTACHED SUPPLEMENT.

0 7 8 9

)

CK LJQ>>

7

~

8 FACILITY STATUS 9

'E ACTIVITY COI4TENT j~lQ 10 1

41 PONIER 0 0 12 "9

13 oTHER STATUS NA 44 METHOD OF DISCOVERY

~A QSI[

DISCOVERY DESCRIPTION 022 OPERATOR OBSERVATION RELEASED OF RELEASE AMOUNT OF AC IVITY QSS LOCATION OF RELEASE QSB

~1e ~Z 033 ~ZQ3. NA 7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 039

) ~00 0 Qs) ~ZQ)s NA 7 8 9 11 42 13 80 PERSCi4NEL INJURIES NUMBER DESCRIPTION 41

~OI O O Q4oj )PA 7 8 9 11 12 80 LOSS OF OR DAMAGE To FACILITY Q43 7 8 9 ~ '10 80 PUBLICI ~ '4 ISSUED DESCRIPTION 45 Q 8003.{9@{6 '

NRC USE ONLY

)2 oi g j oo. I )IJ(43 10 68 69 I I I I I I 30

)4AME OF PREPARER Jack Risch'ting PHONc 616-465-5901 0

SUPPLEMENT TO LFR iv'80-004/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION

. ASSEMBLY AND PROXIMITY SWITCH CONFIGURATION MAS INSTALLED AS A RESULT OF

.-:-- .A PREVIOUS ENGINEERING EVALUATION. NO FURTHER ACTiON IS PRESENTLY PLANNED AS A RESULT OF THIS EVENT.