On June 29, 2007, at approximately 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />, with the plant in Mode 1 (i.e., Power Operation), the plant operating in single loop, and the reactor operating at approximately 58 percent rated thermal power, shutdown of the plant was initiated by a manual actuation of the Reactor Protection System.
The purpose of the shutdown was to repair, or replace reactor recirculation system (RRC) pump motor A which tripped from fast speed operation on June 27, 2007.
The cause of the RRC Pump Motor A trip was an electrical fault in the motor., The motor was past due for replacement at the time of failure. The work management preventative maintenance process for RRC motors had not yet been initiated. A contributing cause of the event was the plant accepting a less than adequate risk assessment for the large motors maintenance program.
The RRC pump motor A was replaced with a refurbished motor. PM tasks were initiated for motors to meet refurbishment frequency recommendations as stated on the motor templates. Critical motors not having spares available were identified. An assessment will determine the effectiveness of the PM .
template implementation process. Critical large motors exceeding template rewind intervals will be identified and scheduled.
This is a Voluntary Report submitted as a condition of generic interest to the industry.
NRC FORM 366 (9-2007) PRINTED ON RECYCLED PAPER 52NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (9-2007) |
LER-2007-008, . Single Recirculation Loop Operation Results In Planned Reactor ShutdownDocket Number |
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CONTINUATION SHEET
Energy Industry Identification System Codes are identified in the text as [XX].
INTRODUCTION
On June 29, 2007, at approximately 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />, with the plant in Mode 1 (i.e., Power Operation), the plant operating in single loop, and the reactor operating at approximately 58 percent rated thermal power (RTP), shutdown of the plant was initiated by a manual actuation of the Reactor Protection System (RPS) [JC]. The purpose of the shutdown was to repair or replace a reactor recirculation system (RRC) [AD] motor [MO].
Review of the regulations, guidance, and the circumstances associated with the scram has determined that the June 29, 2007, shutdown was not reportable in accordance with 10 CFR 50.72 or 10 CFR 50.73. This Voluntary Report is being submitted as a condition of generic interest to the industry.
EVENT DESCRIPTION
On June 27, 2007, at approximately 2348 hours0.0272 days <br />0.652 hours <br />0.00388 weeks <br />8.93414e-4 months <br />, while operating at 86 percent reactor power, RRC pump motor A experienced a fault and tripped. As a result, the plant entered single loop operation and power ran back to 55 percent RTP. The plant continued to operate in single loop operation in compliance with Technical Specification Limiting Condition for Operation 3.4:1, "Recirculation Loops Operating," Integrated Operating Instruction (101)-3, "Power Changes," and the Operations Requirements Manual's section, "Single Recirculation Loop Operation.
Prior to plant shutdown, a reactivity plan had been developed to operate the plant in single loop and included a contingency to shutdown if required:
In preparation for plant shutdown and in accordance with 101-8, "Shutdown By Manual Reactor. Scram," the following actions were taken by the plant operators:
o station loads were shifted to the startup transformer, o recirculation flow was lowered, o reactor water level operator setpoint was raised to 198.5 inches above top of active fuel (TAF), o hydrogen water chemistry was shut down, o ESW pumps were started, o emergency closed cooling pumps were started, o turning gear oil pump and lift pumps were started, o motor suction pump was started, o steam seal evaporator was shutdown, o automatic transfer feature of the motor feed pump controller was disabled, and o motor feed pump was started.
On June 29, 2007, at approximately 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />, with the plant in Mode 1 and the reactor operating at approximately 58 percent RTP and level and pressure stable, shutdown of the plant was completed by a manual actuation of the RPS. The mode switch was placed in shutdown to manually actuate the RPS per 101-8. The manual actuation of the RPS was inserted with "all rods in" following a pre-planned sequence in accordance with 101-8. The plant was not in a technical specification required shutdown action statement. The purpose of the shutdown was to support repairs to, or replacement of, the RRC pump motor A.
� Following the manual RPS actuation, reactor water level lowered to below level 3 (actuation scram signal at 177.7 inches above TAF) as expected. The lowest reactor water level reached was 157.6 inches above TAF. When reactor water level lowered to below reactor water level 3, containment isolation [JM] signals were appropriately received by the residual heat removal system [BO] valves [ISV]. The valves were already closed due to plant conditions. Level was recovered automatically by the feedwater system to greater than 178 inches TAF.
The turbine and generator tripped as expected. No automatic emergency core cooling system (ECCS), or reactor core isolation cooling (RCIC) system response was required and no ECCS or RCIC systems were used for level control. Overall, level control systems responded as expected and anticipated.
Control of level following the scram was performed as practiced in the training simulator, which was part of the pre-planned sequencing for the manual RPS actuation.
CAUSE OF EVENT
The cause attributed to the RRC Pump Motor A tripping was an electrical fault in the RRC pump motor (General Electric, vertical shaft, totally enclosed, air-water cooled induction motor, model number 264X776). The motor was past due for replacement at the time of failure. The work management preventative maintenance (PM) process for RRC motors had not yet been initiated.
Contributing causes of the event include the plant accepting a less than adequate risk assessment of the large motors program, and that long-range equipment and component planning is not integrated into the budget process.
EVENT ANALYSIS
The RRC system provides a forced coolant flow through the core to remove heat from the fuel to allow operation at significantly higher power than would otherwise be possible. The system consists of two recirculation pump loops external to the reactor vessel.
A bounding evaluation of the event was performed, assuming a manual reactor RPS actuation occurred with all risk significant equipment available. Configurations with a core damage probability (CDP) of less than 1.0E-06 and a large early release probability (LERP) of less than 1.0E-07 are not considered to be risk significant events. CDP of 5.5E-07, being less than 1.0E-06, and a LERP of 8.2E-08, being less than 1.0E-07 is considered to be of low risk significance.
CORRECTIVE ACTIONS
The RRC pump motor A (1B33-0001A) was replaced with a refurbished spare motor. Replacement of the RRC pump motor B will take place during the next refueling outage (number 12) scheduled to occur February to April 2009.
PM tasks were initiated for motors to ensure that the templates for the large electric motors at Perry are implemented to meet refurbishment frequency recommendations as stated on the motor templates.
Specific motors, designated as "critical" under the category of Critical Large Motor Applications, not having spares were identified. Acquisition of spare motors has been approved by the Plant Health 7 Committee (PHC) in support of the Major Equipment Reliability Program.
The PHC members performed a documented review of the PHC procedure and the value rating methodology procedure to ensure that membership understands the proper methods for identifying, ranking, approving, prioritization, value rating, and disposition of material condition issues that are submitted to the PHC. It was determined that until the equipment reliability database is fully implemented, capital spares, required to support the plant, will be identified in budget allocations and presented to the PHC with associated value ratings.
Corrective actions to be completed include: 1.) The engineering program owner will monitor the action plan for equipment reliability to ensure completion of PM template implementation. 2.) An assessment will be completed for an overall status of the work management PM program. The assessment will determine the effectiveness of the PM template implementation process and whether the templates are effective in reducing failures of critical components. 3.) Critical large motors exceeding templates for rewind intervals will be identified along with completion of PM deferrals.
PREVIOUS SIMILAR EVENTS
A review of Licensee Event Reports and the Corrective Action Program database for the past three years was completed for conditions written for RRC pumps tripping from fast speed and failure of large motors. LER 2005-001, "Manual reactor scram following unexpected RRC pump trip," describes a condition where the RRC system pumps A and B unexpectedly downshifted from fast to slow speed on January 6, 2005. While operators were inserting control rods, RRC pump A unexpectedly tripped from slow speed to off followed by a manual reactor scram initiated by operations personnel. Downshifting of the pumps was caused by a degraded optical isolator in the RRC logic circuitry. The RRC A tripping from slow speed to off was caused by a failure of an amplifier circuit on the voltage regulator card in the low-frequency motor-generator.
where both RRC pumps unexpectedly downshifted from fast to slow speed December 23, 2004. This was followed by a reactor scram due to core oscillations detected by the oscillation power range monitor. The cause was determined to be an optical isolator intermittent failure as a result of an inadequate surge suppression network in the control circuit for the RR pumps.
actuation," describes a condition where RRC pump B failed to transfer to slow speed and subsequently tripped on June 22, 2007. This was followed by shutdown of the plant by manual actuation of the RPS.
The cause of the RRC pump B failure to transfer to slow speed was a malfunction of the low-frequency motor-generator set control and interlock circuit Agastat time-delay relay.
A review of corrective action program documents over the last three years found only condition reports associated with this event (LER 2007-008) and the events reported under LER 2005-001, LER 2004 002 and LER 2007-007. The corrective actions taken for these three previous events could not reasonably be expected to prevent the occurrence of this event.
COMMITMENTS
There are no regulatory commitments contained in this report. Actions described in this document represent intended or planned actions, are described for the NRC's information, and are not regulatory commitments.
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05000498/LER-2007-001 | Turbine-Driven Auxiliary Feedwater Pump Failed to Start During Surveillance Testing (Supplement 1) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2007-001 | -f Unit 1 Automatic Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2007-001 | | | 05000266/LER-2007-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000269/LER-2007-001 | Dual Unit Trip from Jocassee Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000272/LER-2007-001 | ESF Actuation of Auxiliary Feedwater Pumps in Mode 3. | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000265/LER-2007-001 | Manual Reactor Scram on Increasing Condenser Backpressure Due to a Decrease in 2A Offgas Train Efficiency | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000278/LER-2007-001 | Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2007-001 | Unit 3 High Pressure Coolant Injection System Declared Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000282/LER-2007-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration February 28, 2007 Indian Point Unit No. 2 Docket No. 50-247 NL-07-013 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2007-001-00, "Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure" Dear Sir: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The enclosed LER identifies an event where the plant was operated in a condition prohibited by Technical Specifications, which is reportable under 10 CFR 50.73(a)(2)(i)(B). This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2007-00013. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, -Thr red R. Dacimo ite Vice President Indian Point Energy Center E Docket No. 50-247 NL-07-013 Page 2 of 2 Attachment: LER-2007-001-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 2 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104DEXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 2. DOCKET NUMBER 1 3. PAGE1. FACILITY NAME: INDIAN POINT 2 05000-247 1 OF 4 4. TITLE: Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for an Inoperable Residual Heat Removal Pump Due to an Electrical Supply Breaker Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix) | 05000483/LER-2007-001 | . Single Train Inoperability in the Essential Service Water System due to Inadequate Valve Closure Setup | | 05000286/LER-2007-001 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President June 4, 2007 Indian Point 3 Docket No. 50-286 N L-07-052 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Subject:LLicensee Event Report # 2007-001-00, "Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply" Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2007-001-00. The attached LER identifies an event where the reactor was manually tripped while critical, which is reportable under 10 CFR 50.73(a)(2)(iv)(A) . This condition has been recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2007-01775. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. T. R. Jones, Manager, Licensing at (914) 734-6670. Sincerely, Fred R. Dacimo Site Vice President Indian Point Energy Center cc:LMr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission INPO Record Center pP,c.1)-1
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 6/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReportedDlessons learned areDincorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME INDIAN POINT 3 2. DOCKET NUMBER 13. PAGE 05000-286 1 OFTD5 4. TITLE Manual Reactor Trip Due to Decreasing Steam Generator Levels as a Result of the Loss of Feedwater Flow Caused by the Failure of 32 Main Feedwater Pump Train A Control Logic Power Supply | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000293/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2007-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000309/LER-2007-001 | Uncompensated Degradation in a Security System | | 05000414/LER-2007-001 | Failure to Comply with Action Statement in Technical Specification (TS) 3.3.1 for Loss of a Channel of the Solid State Protection System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000311/LER-2007-001 | Inoperability of the Chilled Water System - (21 and 22 Chillers Inoperable) | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000331/LER-2007-011 | . Undervoltage ConditiOn Resulted in the Actuation of the Emergency Diesel Generators | | 05000346/LER-2007-001 | Station Vent Radiation Monitor in Bypass due to Faulty Optical Isolation Board | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000348/LER-2007-001 | Vire President - Farley Operating Company, Inc. Po51 Office Drawer 470 Ashford, Alabarid 36312-0470 Tel 334 814 4511 Fax 334 814 4728 SOUTHERN June 22, 2007 COMPANY Energy to Serve Your World Docket Nos.: 50-348 NL-07-1231 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Joseph M. Farley Nuclear Plant — Units 1 and 2
Licensee Event Report 2007-001-00
Technical Specification 3.8.1 Violation Due to
Failure of Breaker / Mechanism-Operated Cell Switch
Ladies and Gentlemen: Joseph M. Farley Nuclear Plant - Licensee Event Report (LER) No. 2007-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(B). This letter contains no NRC commitments. If you have any questions, please advise. Sincerely, 7e. R. Johnson Vice President — Farley Joseph M. Farley Nuclear Plant 7388 North State Highway 95 Columbia AL 36319 JRJ/CHM Enclosure: Licensee Event Report 2007-001-00 - Unit 1 U. S. Nuclear regulatory Commission NL-07-1231 Page 2 cc:� Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. J. R. Johnson, Vice President — Farley Mr. D. H. Jones, Vice President — Engineering RTYPE: CFA04.054; LC # 14596 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Ms. K. R. Cotton, NRR Project Manager — Farley Mr. E. L. Crowe, Senior Resident Inspector— Farley NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nudear Regulatory Commission, Washington, DC 2055570001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to infocolledsanrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Joseph M. Farley Nuclear Plant - Unit 1 05000 348 1 OF 4 4. TITLE Technical Specification 3.8.1 Violation Due to Failure of Breaker / Mechanism-Operated Cell (MOC) Switch | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2007-001 | As-Found Local Leak Rate Tests Not Performed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2007-001 | Unit 1 Reactor Trip Following a 345 Kv Transmission Line Lightning Strike | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2007-001 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2007-001 | S, Reactor Shutdown Due to Unidentified RCS Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2007-001 | 369 5McGuire Nuclear Station Unit 1 05000 1 OF5 | | 05000335/LER-2007-001 | Mispositioned Service Air Containment Isolation Valves | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000362/LER-2007-001 | Failure to declare Emergency Diesel Generator Inoperable and enter TS Action | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000353/LER-2007-001 | Scram Discharge Volume Vent and Drain Valves Opened Due To Fuse Removal | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000400/LER-2007-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2007-001 | Reactor Trip Due to a Loose Wire in the Main Transformer Monitoring Circuitry | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000389/LER-2007-002 | 2B2 Reactor Coolant Pump (RCP) Seal Housing Leakage | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000255/LER-2007-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000395/LER-2007-002 | Failure to Follow Administrative Controls Results in LCO 3.6.4 Violation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2007-002 | Shutdown Cooling Pump Trip Results in Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000414/LER-2007-002 | Technical Specification Violation Associated with Containment Valve Injection Water System | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2007-002 | Reactor SCRAM due to Turbine Trip caused by Loss of Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000423/LER-2007-002 | Loss of Offsite Power Caused by Transmission System Operator While Defueled | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000311/LER-2007-002 | RReactor Trip Due to a Breach in the Condensate System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2007-002 | | | 05000454/LER-2007-002 | Technical Specification Required Shutdown of Unit 1 and Unit 2 Due to an Ultimate Heat Sink Pipe Leak Common to Both Units | | 05000282/LER-2007-002 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000315/LER-2007-002 | Failure to Declare Essential Service Water Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2007-002 | Technical Specification Prohibited Condition Due to Exceeding Containment Air Temperature Limit Allowed Outage Time as a Result of Changes in Instrument Uncertainty | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2007-002 | Completion of Shutdown Required by Technical Specifications due to Inoperable Rod Position Indication for Two Control Rods in the Same Control Bank | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000353/LER-2007-002 | Automatic Actuation of Main Condenser Low Vacuum Isolation Logic During Refueling Outage | 10 CFR 50.73(a)(2)(iv), System Actuation | 05000272/LER-2007-002 | MManual Reactor Trips Due to Degraded Condenser Heat Removal | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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