:on 910101,delta Flow High RWCU Isolation Occurred While Attempting to Shift Flow from Pump B to Pump A.Caused by Personnel Error.Control Room Operator Counseled & Event Will Be Discussed During Training| ML20066J969 |
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| Site: |
Perry  |
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| Issue date: |
01/31/1991 |
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| From: |
Hegrat H CENTERIOR ENERGY |
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| To: |
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| Shared Package |
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| ML20066J967 |
List: |
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| References |
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| LER-91-001, LER-91-1, NUDOCS 9102050164 |
| Download: ML20066J969 (3) |
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On January 1, 1991 at 1935, while attempting to shift Reactor Vater Cleanup (RWCU) system flow from the B pump to the A pump, a Delta-Flow high RWCU isolation occurred.
At the time of discovery, the Plant was in Operational Condition 2 (Startup).
Reactor Pressure Vessel (RPV) temperature was 170 degrees Fahrenheit and reactor pressure was atmospheric. The Operator started the A RWCU pump for t 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run and secured the B RWCU pump. RWCU flow dropped off considerably and the B RWCU pump was restarted approximately 3 minutea later. The A RWCU pump was then secured. A Delta-Flow Righ RWCU isolation occurred within 1 minute because of flow imhalances within the RWCU system resulting from this evolution. Upon investigation, it was discovered that the A RWCU pump discharge valve was closed.
RWCU flow was then properly re-established in accordance with System Operattng Instruction S01-033, " Reactor Water Cleanup System",
using tlie B RWCU pump.
The root cause of this event was personnel error, inattention to detail, by the Control Room Operator. The operator started the A RWCU pump without first verifying that the pump discharge valve had been opened.
The corrective actions taken f or this event include counseling the operator involved and discussing the event during Operator requei ification training.
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=cs-.mvenm On January 1, 1991 at 1935, while attempting to shif t Reactor Water Cleanup (RWCU) {CE] system flow f rem the B pijmp [P) to thu A pump, a Delta Flow-High RWCU isolation occurred. At the time of discovery, the Plant was in Operational Condition 7 (Startup). Reactor Pressure Vessel {RPV) temperature was 170 degrees Fahrenheit and reactor pressure was atmospheric.
A work order was written on Decenber 18, 1990, to drain and flush the A RWCU pusp l
bearing housing as required to clean the housing. Out-of-Service tags were htmg on the A FWCU pump breaker, the breaker fuses, the control switch and the discharge valve on December 19, 1990, to allow the Operations and Maintenance personnel flexibility in running the pump following the drain amd flush oporations Out-of-Service tags are used to provide control over the operation
.f a component in situations like this when personnel safety is not in jeopardy, but control is desired.
On January 1,1991 the Control Room Operator was requested t', start the A pump j
for a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run.
The operator started the A RWCU pump at 1928 and secured the B RWCU pump 27 seconds later af ter obserring what appeared to be normal flow and
' discharge pr. essure.
RWCU flow dropped off considerably when the B RWUU pump was secured and the B RUCU pump was restarted approximately 3 minutes later. The A Rk'CU pump was then secured. A Delta Flow-High RWCU ioolation occurred within 1 minute becanoe of flow imbalances within the RWCU system resulting from this evolution. Upon investigation, it was discovered that the A RWCU pump discharge b
valve was closed.
RWCU flow was then propurly re eotablished in accordance with Syotem Operating Instruction, S01-033, " Reactor Water Cleanup Cystem", using the B RWCU pump.
Because the purap has no minimum flow racirculation capability and heceuse the pump was run sgainst shutoff head for approximately 3 minutes, an engineering 3
evaluation-was performed to dt.termine the future operobility of the pump. The bearing housing was flushed again, and the puup was run for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, The peinp was declared fully operational on Janunry 8, 1991.
The root cause of this event was personnel error, inattention to detail, by the Control Room Operator. System Operating Instruction (S01-G33), " Reactor Water Cleanup System" requires that a valve lineup be perNined prior to starting up i.
the system. Although 'the valve lineup wn wrent at the time of the ever'., the Out-of-Service tags hung for thin evolution modified the valve lineup l>y allowing the' maintenance Person in Charge to control the openjng and closing of the A RWCU putap discharge valve as needed to perform the drain and flunh evolutions. When Out-of-Service tags.are used, the Control Room operator is solely responsible for the actual pump and valve manipulations to ensure that proper lineups are maintained for the existing operating conditions.
In this case, the operator was handed the tagout which identified the A RWCU pump control switch, the pump breaker, the breaker fusas and the pump discharge valve as being under maintenance control and he was given permission to operate these components as necessary under their tags to condact the pump retest.
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position of the A RVOC pump discharge valve prior to statting the pump. The discharge valve 4a1 e osed.
The RWCU systen is nied to control reactor water chemistry, control reactor water bl inventory during sta tup ind shutdown, and minimire temperature gradients when recirculation pump: C i nat operating. The RWCU differentir1 flow instrumentation is pat-of the Leak Detection System (IJ) and in conjunction with the Nuclear Steam Suppa ' Shutof f (NSS!,. system is designed to isolate RWCU flow Jn the event of a line 5 eta i'n the system. The Leak Detection System compares t
RCD sur f 9n flow wit's he / scharge flow and generates an isolation signal when high de itial flor xists for a duration of greater than 45 seconds.
A genui-
- f ferent.a1 flow situation existed in this insto a resulting in a trip r. '.a.m of W U syntem flow for a short period of time.
'l W-loss of RWCU riow uid not have a significant offeet on plant chemist ry cont rol Eiitionally, Lt.- RWCU isolation function performed as designed to isolate the,no:t on a Delta Flow 'iigh signal. Therefore, this event is not considered safety ni p ficant.
Previous RWCU is tatM i caused by high dif ferential flow have been disunf red (see LER's99-025. 89-034,90-008 cnd 90-022).
However, none of these e g s#
were attri Nttable M perst.nel error.
The correct tve actions take s for this event include counseling t'ie Operatet involved and discussing tht. event during Operator requalification training, Energy Industry Identification System Codes are identified in the text as IXX).
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| | | Reporting criterion |
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| 05000440/LER-1991-001, :on 910101,delta Flow High RWCU Isolation Occurred While Attempting to Shift Flow from Pump B to Pump A.Caused by Personnel Error.Control Room Operator Counseled & Event Will Be Discussed During Training |
- on 910101,delta Flow High RWCU Isolation Occurred While Attempting to Shift Flow from Pump B to Pump A.Caused by Personnel Error.Control Room Operator Counseled & Event Will Be Discussed During Training
| | | 05000440/LER-1991-002, :on 910101,inadvertent Turbine Stop Valve Closure Signal Resulted in Full Scram Signal Being Generated.Cause undetermined.SVI-N31-T1151 Will Be Revised to Clarify Actions Needed to Meet All Prerequisites |
- on 910101,inadvertent Turbine Stop Valve Closure Signal Resulted in Full Scram Signal Being Generated.Cause undetermined.SVI-N31-T1151 Will Be Revised to Clarify Actions Needed to Meet All Prerequisites
| | | 05000440/LER-1991-003, :on 910106,performance of Inadequate Procedure Resulted in Main Steam Line Drain Isolations.Caused by Procedure Deficiency.Instruction Revised to Include or Ref Steps to Bypass MSL Radiation Monitors |
- on 910106,performance of Inadequate Procedure Resulted in Main Steam Line Drain Isolations.Caused by Procedure Deficiency.Instruction Revised to Include or Ref Steps to Bypass MSL Radiation Monitors
| | | 05000440/LER-1991-004, :on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified |
- on 910120,three Reactor Water level-high (Level 8) Channels Inoperable Due to Blown Fuse.Caused by Voltage Spike.Circuitry Associated W/Trip Relays Modified
| | | 05000440/LER-1991-005, :on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel Error |
- on 910129,discovered That Two Power Supplies Had Excessive Ripple Effect When All Rods Pushbutton Depressed,Resulting in Loss of Scram Accumulator Fault Indication.Caused by Personnel Error
| | | 05000440/LER-1991-006, :on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being Revised |
- on 910202,inboard Isolation Valves Closed on RWCU Delta Flow High Signal During Removal of RWCU Filter from Svc.Caused by Personnel Error.Sys Operating Instruction Being Revised
| | | 05000440/LER-1991-007, :on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper Value |
- on 910209,pressure Switch Instrument Drift Caused Automatic Start of Annulus Exhaust Gas Treatment Sys. Caused by Component Failure.Switch Recalibrated to Adjust Setpoints to Proper Value
| | | 05000440/LER-1991-008, :on 910305,trains of Control Room Heating & Air Conditioning Sys Inoperable Due to Inoperability of Both Supporting Chillers.Caused by Solenoid Valve on Thermal Purge Unit Failure to Close.Valve Replaced |
- on 910305,trains of Control Room Heating & Air Conditioning Sys Inoperable Due to Inoperability of Both Supporting Chillers.Caused by Solenoid Valve on Thermal Purge Unit Failure to Close.Valve Replaced
| | | 05000440/LER-1991-009, :on 910314,failure of Div 2 Diesel Generator Occurred During Monthly Surveillance Operability Test.Caused by Equipment Malfunction.Design & Procedural Changes Initiated to Prevent Recurrence |
- on 910314,failure of Div 2 Diesel Generator Occurred During Monthly Surveillance Operability Test.Caused by Equipment Malfunction.Design & Procedural Changes Initiated to Prevent Recurrence
| | | 05000440/LER-1991-010, :on 910401,failure of Reactor Recirculation Pump Resulted in Shutdown of Plant.Caused by Component Malfunction.Contractor Replaced & Recirculation Pump Verified to Operate Properly in Low Speed |
- on 910401,failure of Reactor Recirculation Pump Resulted in Shutdown of Plant.Caused by Component Malfunction.Contractor Replaced & Recirculation Pump Verified to Operate Properly in Low Speed
| | | 05000440/LER-1991-012, :on 910605,determined That Effluent Sys Flow Rate Monitor for Turbine/Heater Bay Bldg Inoperable Since Summer 1988.Caused by Program Deficiencies.Pitot Tube Array Calibr by Capping Individual Pitot Tubes |
- on 910605,determined That Effluent Sys Flow Rate Monitor for Turbine/Heater Bay Bldg Inoperable Since Summer 1988.Caused by Program Deficiencies.Pitot Tube Array Calibr by Capping Individual Pitot Tubes
| | | 05000440/LER-1991-013, :on 910723,tech Spec Violation Occurred Due to Missed Main Steam Line Flow High Isolation Actuation Instrumentation Surveillance.Caused by Personnel Error. Requalification Training Program Established |
- on 910723,tech Spec Violation Occurred Due to Missed Main Steam Line Flow High Isolation Actuation Instrumentation Surveillance.Caused by Personnel Error. Requalification Training Program Established
| | | 05000440/LER-1991-014, :on 910726,RWCU Isolation Occurred Due to High Differential Temp Signal During Decontamination Activity. Caused by Personnel Error.Event Discussed During Continuing Training for Health Physics Personnel |
- on 910726,RWCU Isolation Occurred Due to High Differential Temp Signal During Decontamination Activity. Caused by Personnel Error.Event Discussed During Continuing Training for Health Physics Personnel
| | | 05000440/LER-1991-015, :on 910801,liquid Radwaste Discharge Made W/O Verifying Discharge Line Valving & Channel Improperly Calibr Between 910722-0801.Caused by Personnel Error.Totalizer Recalibr & Technician Counseled |
- on 910801,liquid Radwaste Discharge Made W/O Verifying Discharge Line Valving & Channel Improperly Calibr Between 910722-0801.Caused by Personnel Error.Totalizer Recalibr & Technician Counseled
| | | 05000440/LER-1991-016, :on 910816,inadvertent Test of Radiation Monitor Results in Backup Hydrogen Purge Sys Isolation Occurred.Caused by Personnel Error.Technicians Involved Counseled & Disciplined |
- on 910816,inadvertent Test of Radiation Monitor Results in Backup Hydrogen Purge Sys Isolation Occurred.Caused by Personnel Error.Technicians Involved Counseled & Disciplined
| | | 05000440/LER-1991-017, :on 911002,high Pressure Core Spray Pump Declared Inoperable Due to Motor Bearing Oil Reservoir Drain Plug Failure.Caused by Design Deficiency.Drain Plugs Will Be Replaced W/Ball Valve Arrangement |
- on 911002,high Pressure Core Spray Pump Declared Inoperable Due to Motor Bearing Oil Reservoir Drain Plug Failure.Caused by Design Deficiency.Drain Plugs Will Be Replaced W/Ball Valve Arrangement
| 10 CFR 50.73(a)(2) | | 05000440/LER-1991-018, :on 911006,control Rod 46-23 Exceeded Max Scram Time to Position 43 & Max Scram Insertion Time to Position 43.Caused by Contaminated Valve Disc & Seats.Valves Replaced W/New Valves from Two Other Lots |
- on 911006,control Rod 46-23 Exceeded Max Scram Time to Position 43 & Max Scram Insertion Time to Position 43.Caused by Contaminated Valve Disc & Seats.Valves Replaced W/New Valves from Two Other Lots
| 10 CFR 50.73(a)(2)(i) | | 05000440/LER-1991-019, :on 911006,Tech Spec Surveillance Requirement for Rod Pattern Controller Performed Late.Caused by Personnel Error.Senior Reactor Operator Counseled & Procedures Revised Re Rod Pattern Testing Requirements |
- on 911006,Tech Spec Surveillance Requirement for Rod Pattern Controller Performed Late.Caused by Personnel Error.Senior Reactor Operator Counseled & Procedures Revised Re Rod Pattern Testing Requirements
| | | 05000440/LER-1991-021, :on 911011,preferred Source Breaker Would Not Close on Demand from Switch on Control Room Panel Since 910904.Caused by Equipment Malfunction.Spring Pins on Tooling Racks Will Be Shortened & Instruction Revised |
- on 911011,preferred Source Breaker Would Not Close on Demand from Switch on Control Room Panel Since 910904.Caused by Equipment Malfunction.Spring Pins on Tooling Racks Will Be Shortened & Instruction Revised
| | | 05000440/LER-1991-022, :on 911011,while Manipulating Front Panel Switches on Drywell Atmospheric Gaseous Monitor,Radiation Monitor Indication Spiked Upscale.Caused by Unrecognized Equipment Characteristics.Info Tag Attached to Monitor |
- on 911011,while Manipulating Front Panel Switches on Drywell Atmospheric Gaseous Monitor,Radiation Monitor Indication Spiked Upscale.Caused by Unrecognized Equipment Characteristics.Info Tag Attached to Monitor
| | | 05000440/LER-1991-023, :on 911105,misadjusted Leak Detection Instrumentation Resulted in TS Violation.Caused by Equipment Problem.Reviewed Previous Uses of Transmation Model 1010 Ref Cell.Operators Will Be Instructed on Lessons Learned |
- on 911105,misadjusted Leak Detection Instrumentation Resulted in TS Violation.Caused by Equipment Problem.Reviewed Previous Uses of Transmation Model 1010 Ref Cell.Operators Will Be Instructed on Lessons Learned
| | | 05000440/LER-1991-024, :on 911204,loss of Emergency Svc Water Sys Loop Occurred Due to Inadvertent Isolation of Keepfill Sys.Caused by Personnel Error.Valve 1P45-F720A Required Valve Position Changed to Locked Open |
- on 911204,loss of Emergency Svc Water Sys Loop Occurred Due to Inadvertent Isolation of Keepfill Sys.Caused by Personnel Error.Valve 1P45-F720A Required Valve Position Changed to Locked Open
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000440/LER-1991-025-03, :on 911213,HPCS Sys Declared Inoperable After Liquid Penetrant Testing Revealed Crack in Weld Upstream of High Point Vent Valve on HPCS Test Return Line on 911212. Schedule to Inspect Other Welds Accelerated |
- on 911213,HPCS Sys Declared Inoperable After Liquid Penetrant Testing Revealed Crack in Weld Upstream of High Point Vent Valve on HPCS Test Return Line on 911212. Schedule to Inspect Other Welds Accelerated
| | | 05000440/LER-1991-025, :on 911212,liquid Penetrant Testing Revealed Crack in Weld Upstream of High Point Vent Valve on HPCS Sys Test Return Line.Caused by Having Insufficient Weld Metal & Contour.Other Welds to Be Inspected |
- on 911212,liquid Penetrant Testing Revealed Crack in Weld Upstream of High Point Vent Valve on HPCS Sys Test Return Line.Caused by Having Insufficient Weld Metal & Contour.Other Welds to Be Inspected
| | | 05000440/LER-1991-026, :on 911216,Div I Nuclear Steam Supply Shutoff Sys Signal Resulted in Unexpected Reactor Core Isolation. Caused by Personnel Inattention to Detail.Technician Performing Surveillance Was Counseled |
- on 911216,Div I Nuclear Steam Supply Shutoff Sys Signal Resulted in Unexpected Reactor Core Isolation. Caused by Personnel Inattention to Detail.Technician Performing Surveillance Was Counseled
| | | 05000440/LER-1991-027, :on 911222, Manual Reactor Scram Inserted Due to non-isolable Break in 36 Inch Fiberglass Pipe for Cooling Water.Caused by Flow in Pipe, Degradation to Pipe Support & Improper Installation of O-ring Gasket |
- on 911222, Manual Reactor Scram Inserted Due to non-isolable Break in 36 Inch Fiberglass Pipe for Cooling Water.Caused by Flow in Pipe, Degradation to Pipe Support & Improper Installation of O-ring Gasket
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