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On January 7,1937 at 2015, a Reactor Water Cleanup (RWCU) containment isolation occurred due to indicated high dif ferential flow. The cause of the isolation has been identified to be flow control valve problems and possible calibration inaccuracies of the flow elements used by the Leak Detection system resulting f rom teactor coolant temperature changes.
In response to the isolation, operators restored the system to its original configuration.
As a result of this and previous events an engineering design change has been implemented to provide mass and temperature compensation for the RWCU Leak Detection delta flow instrumentation. This design change has helped to reduce the magnitude of the indicated delta flow error while operating the RWCU system at low reactor power levels.
Evaluation of the results of the design change will continue during plant startup testing.
In addition, an engineering design chando has been initiated to replace five RWCU flow control va lve s.
The replacement valves will provide the flow throttling characteristics to reduce flow oscillations during startup of the RWCU system.
Due to operational constraints and parts availability, this design change is not expected to be implemented until the first refueling outage.
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m Perry Nuclear Power Plant, Unit 1 0l5jojojol4l410 81 7 0l0l 1 Ol 0 0l2 0F 0l3 TEXT ta more sp.co a revisrud, esse essneeW Ar4C Form Jests /11M On January 7,1987 at 2015, a Reactor Water Cleanup (RWCU)[CE] containment isolation occurred due to indicated high dif ferential flow.
At the time of this event, the plant was in Operational Condition 4 (Cold Shutdown) lowering reactor vessel (RPV] water level in preparation for restarting the reactor.
Reactor coolant temperature was approximately 160 degrees and reactor vessel pressure atmospheric.
On January 7 at 1950, plant operators began lowering reactor vessel water level in accordance with Integrated Operating Instruction (101)-4, " Cold Startup" by rejecting reactor vessel water via RWCU to the main coadenser.
At 2015 while adjusting the flow to the main condenser, an inboard RWCU containment isolation occurred due to indicated high dif ferential flow.
In response to the isolation, plant operators verified no actual RWCU leak existed, and reset the isolation. The RWCU system responded to the high dif ferential flow isolation signal as designed.
RWCU pump A was restarted at 2045 with the Leak Detection system (IJ] for RWCU in bypass to prevent an unnecessary isolation.
The Leak Detection system is not required in Operational Condition 4.
Af ter satisf actory system startup, the RWCU Leak Detection system was returned to normal at 2246.
Troubleshooting, system testing and investigation of this and previous events (see LERs86-039, 86-056,86-068 and 86-085) identified the cause of the isolations as the location of the blowdown flow element, oversensitive flow control valves and lack of density compensation for RWCU delta flow.
Previously, the blowdown flow element was relocated upstream of the blowdown pressure control valve (PCV] to prevent the flow element from intermittently becoming uncovered due to the lack of back pressure.
This has reduced the indicated flou oscillations while operating the RWCU system with blowdown flow.
Flow oscillations while manipulating the RWCU flow control valves during system sta-tup and subsequent flow adjustments continue to be a p roblem. The plant operators are not always able to recover from the flow oscillations before the system isolates on high dif ferential flow. A design change to replace the flow control valves was initiated prior to the January 7 event but has not been implemented.
Additionally, a contributing cause is the ef fect of the changes in reactor coolant temperature on the indicated flow rates. The flow elements are calibrated based upon operating temperature and do not compensate for temperature changes in the reactor coolant experienced during startup.
This can result in a reduced margin to the isolation setpoint a t certain operating conditions. A design change to provide mass and temperature compensation for the delta flow instrumentation was initiated prior to the January 7 event but had not been implemented.
The Leak Detection system compares RWCU suction flow to the flow returning to the reactor vessel and blowndown flow.
All three flows are summed to generate an indication of dif ferential flow.
A RWCU high dif ferential flow signal indicates the auction flow entering the system is not being discharged via no rmal flowpaths (reacto r vessel, and blowdown to radwaste or main condenser).
This could be the result of a line break in the RWCU system.
Indicated high dif ferential flow for a duration of 45 seconds generates an isolation signal
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- a Perry Nuclear Power Plant. Unit 1 0 l5 l0 l0 l0 l 4l4 l 0 81 7 0 l 0l 1 Ol0 Ol 3 OF OI 3 f tXT t# snare space a M was sahmenet 4AC perse JesA'gj {1h from the Leak Detection system. The 45 second time delay normally allows for system flow transients when changing operational configurations.
If an RWCU containment isolation were to occur at high reactor power, the loss of the RWCU system may cause reactor coolant conductivity to slowly increase until the system is returned to service.
In addition, during shutdown with little or no internal recirculation flow, reactor vessel thermal stratification may also occur. However, the time out-of-service for RWCU would be short and these ef fects minimal.
Since no actual RWCU high dif ferential flow existed and the f act that the system did respond as designed to the indicated high dif ferential flow isolation, the event is not considered safety significant.
As a result of this and previous events, an engineering design change has been implemented to provide mass and temperature compensation for the RWCU Leak Detection delta flow instrumentation. This design change has helped to reduce the magnitude of the indicated delta flow error while operating the RWCU at low reactor power levels. Evaluation of the results of the design change will continue during plant startup testing.
In addition, an engineering design change has been initiated to replace five RWCU flow control valves. The replacement valves will provide the flow throttling characteristics to reduce flow oscillations during startup of the RWCU system.
Due to operational constraints and parts availability, this design change is not expected to be implemented until the first refueling outage.
Energy Industry Identification System Codes are identified in the text as
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| 05000440/LER-1987-001, :on 870107,RWCU Containment Isolation Occurred Due to Indicated High Differential Flow.Caused by Flow Control Valve Problems.Engineering Design Change Implemented to Provide Mass & Temp Compensation for RWCU Instruments |
- on 870107,RWCU Containment Isolation Occurred Due to Indicated High Differential Flow.Caused by Flow Control Valve Problems.Engineering Design Change Implemented to Provide Mass & Temp Compensation for RWCU Instruments
| | | 05000440/LER-1987-004, :on 870127,unexpected Reactor Protection Sys Actuation Occurred Due to Upscale Trips on Intermediate Range Neutron Monitors.Caused by Personnel Error.Warning Sign Will Be Posted & Individuals Counseled |
- on 870127,unexpected Reactor Protection Sys Actuation Occurred Due to Upscale Trips on Intermediate Range Neutron Monitors.Caused by Personnel Error.Warning Sign Will Be Posted & Individuals Counseled
| | | 05000440/LER-1987-005, :on 870207,unexpected Reactor Protection Sys Actuation Occurred During Performance of APRM Surveillance Test Instruction (Svi).Caused by Deficient Svi.Svi Revised to Delete Step 5.1.61 |
- on 870207,unexpected Reactor Protection Sys Actuation Occurred During Performance of APRM Surveillance Test Instruction (Svi).Caused by Deficient Svi.Svi Revised to Delete Step 5.1.61
| | | 05000440/LER-1987-006, :on 870208,unexpected RCIC Sys Isolation Occurred Due to Indicated Min Differential Pressure from Leak Detection Sys.Caused by Steam Condensing in High Side Process Connection for Instrument Impulse Line |
- on 870208,unexpected RCIC Sys Isolation Occurred Due to Indicated Min Differential Pressure from Leak Detection Sys.Caused by Steam Condensing in High Side Process Connection for Instrument Impulse Line
| | | 05000440/LER-1987-007, :on 870213,pressure Transient Occurred within Reactor Vessel Level Instrument Rack Resulting in Redundant Reactivity Control Sys (RRCS) Alternate Rod Insertion.Caused by Design Configurations of RRCS Instruments |
- on 870213,pressure Transient Occurred within Reactor Vessel Level Instrument Rack Resulting in Redundant Reactivity Control Sys (RRCS) Alternate Rod Insertion.Caused by Design Configurations of RRCS Instruments
| | | 05000440/LER-1987-008, :on 870218,div 1,class 1E 125 Volt Dc Battery Failed to Meet Allowable Electrolyte Temp of 72 F.Caused by Personnel Error & Faulty Thermostat.Procedure Reviewed & Thermostat Replaced |
- on 870218,div 1,class 1E 125 Volt Dc Battery Failed to Meet Allowable Electrolyte Temp of 72 F.Caused by Personnel Error & Faulty Thermostat.Procedure Reviewed & Thermostat Replaced
| | | 05000440/LER-1987-009, :on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 Revised |
- on 870227,failure of Two Control Air Solenoid Valves Rendered Div I & II Diesel Generators Inoperable. Cause Unknown.Solenoid Valves Replaced & Plant Administrative Procedure PAP-1705 Revised
| | | 05000440/LER-1987-010, :on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised |
- on 870228,operators Failed to Place at Least One Reactor Protection Sys Trip Sys in Tripped Condition within 1 H.Caused by Personnel Error & Deficient Procedure. Personnel Counseled & Procedures Revised
| | | 05000440/LER-1987-011, :on 870227,during Audit,Discovered That on 861021,independent Verification of Discharge Path Valve Line Not Performed Prior to Commencing Liquid Radwaste Discharge Release.Caused by Failure to Follow Procedure |
- on 870227,during Audit,Discovered That on 861021,independent Verification of Discharge Path Valve Line Not Performed Prior to Commencing Liquid Radwaste Discharge Release.Caused by Failure to Follow Procedure
| | | 05000440/LER-1987-012, :on 870302,reactor Scram,Due to Reactor Vessel Level Less than Level 3 & NSSS balance-of-plant & RWCU Isolations,Occurred.Caused by Personnel Inadvertently Actuating lo-lo Switch 1N21-N335.Personnel Disciplined |
- on 870302,reactor Scram,Due to Reactor Vessel Level Less than Level 3 & NSSS balance-of-plant & RWCU Isolations,Occurred.Caused by Personnel Inadvertently Actuating lo-lo Switch 1N21-N335.Personnel Disciplined
| | | 05000440/LER-1987-014, :on 870305,pressure Transient in Reactor Vessel Level Instrument Rack Initiated Hpcs.Caused by Use of Incorrect Valving Sequence When Restoring Level Transmitter to Svc.Instrument Rack Tasks Rescheduled |
- on 870305,pressure Transient in Reactor Vessel Level Instrument Rack Initiated Hpcs.Caused by Use of Incorrect Valving Sequence When Restoring Level Transmitter to Svc.Instrument Rack Tasks Rescheduled
| | | 05000440/LER-1987-015, :on 870307,deenergization of Isolation Relays W/Containment Vent Exhaust Plenum Resulted in Closure of Containment Vessel Valves.Caused by Inadequate Surveillance & Work Order Preparation.Surveillance Instructions Revised |
- on 870307,deenergization of Isolation Relays W/Containment Vent Exhaust Plenum Resulted in Closure of Containment Vessel Valves.Caused by Inadequate Surveillance & Work Order Preparation.Surveillance Instructions Revised
| | | 05000440/LER-1987-016, :on 870309,partial Nuclear Steam Supply Shutoff Sys Div 2 balance-of-plant Isolation Occurred During Surveillance Test Instruction.Caused by Deficiency Involving Equipment Testability.Technicians Counseled |
- on 870309,partial Nuclear Steam Supply Shutoff Sys Div 2 balance-of-plant Isolation Occurred During Surveillance Test Instruction.Caused by Deficiency Involving Equipment Testability.Technicians Counseled
| | | 05000440/LER-1987-017, :on 870314,Tech Spec 3.6.1.3 Violated Due to Loss of Primary Containment Integrity.Caused by Leaking Valve in Upper Airlock Inner Door & Unauthorized Access of Individual Through Airlock.Security Instructed |
- on 870314,Tech Spec 3.6.1.3 Violated Due to Loss of Primary Containment Integrity.Caused by Leaking Valve in Upper Airlock Inner Door & Unauthorized Access of Individual Through Airlock.Security Instructed
| | | 05000440/LER-1987-018, :on 870316,RCIC Sys Isolation Occurred.Cause Related to Use of Ohmmeter to Monitor Status of Initiating Relay Contacts in Surveillance Test Instruction.Plant Administrative Procedure PAP-0205 Revised |
- on 870316,RCIC Sys Isolation Occurred.Cause Related to Use of Ohmmeter to Monitor Status of Initiating Relay Contacts in Surveillance Test Instruction.Plant Administrative Procedure PAP-0205 Revised
| | | 05000440/LER-1987-019, :on 870317,unexpected RCIC Sys Isolation Occurred When Technicians Connected Test Equipment Prior to Leak Detection Sys Isolation Bypass Switches Placed in Bypass.Caused by Personnel Error.Technicians Counseled |
- on 870317,unexpected RCIC Sys Isolation Occurred When Technicians Connected Test Equipment Prior to Leak Detection Sys Isolation Bypass Switches Placed in Bypass.Caused by Personnel Error.Technicians Counseled
| | | 05000440/LER-1987-020, :on 870316,backup Hydrogen Purge Inside Containment Isolation Valve Unexpectedly Isolated Due to Loss of Dc Bus D-1-A.Caused by Personnel Error.Individual Counseled on Need to Exercise Caution Around Switchgear |
- on 870316,backup Hydrogen Purge Inside Containment Isolation Valve Unexpectedly Isolated Due to Loss of Dc Bus D-1-A.Caused by Personnel Error.Individual Counseled on Need to Exercise Caution Around Switchgear
| | | 05000440/LER-1987-021, :on 870324,reactorprotection Sys Actuation Occurred Due to Indicated Reactor Vessel Water Level of Level 3.Caused by Procedure Deficiency.Operators Will Receive Training on Vessel Level Fluctuations |
- on 870324,reactorprotection Sys Actuation Occurred Due to Indicated Reactor Vessel Water Level of Level 3.Caused by Procedure Deficiency.Operators Will Receive Training on Vessel Level Fluctuations
| | | 05000440/LER-1987-022, :on 870329 & 0407,unexpected Autostarts of Diesel Generator Bldg Ventilation Sys Divs 1 & 2 Occurred. Caused by Incorrect Wiring Configuration & Unadjusted Relay Reset Setpoint.Conditions Corrected |
- on 870329 & 0407,unexpected Autostarts of Diesel Generator Bldg Ventilation Sys Divs 1 & 2 Occurred. Caused by Incorrect Wiring Configuration & Unadjusted Relay Reset Setpoint.Conditions Corrected
| | | 05000440/LER-1987-023, :on 870330,manual Reactor Protection Sys Actuation Initiated Due to Decrease in Reactor Vessel Water Level.Caused by Improper Valve Alignment Between Feedwater & Reactor Water Cleanup Sys.Personnel Retrained |
- on 870330,manual Reactor Protection Sys Actuation Initiated Due to Decrease in Reactor Vessel Water Level.Caused by Improper Valve Alignment Between Feedwater & Reactor Water Cleanup Sys.Personnel Retrained
| | | 05000440/LER-1987-024, :on 870330,reactor Protection Sys Actuation Occurred Due to Upscale Trip of Neutron Monitoring Sys Intermediate Range Monitor.Caused by Electrical Noise While Maint Outage Work in Progress.Temporary Jumpers Installed |
- on 870330,reactor Protection Sys Actuation Occurred Due to Upscale Trip of Neutron Monitoring Sys Intermediate Range Monitor.Caused by Electrical Noise While Maint Outage Work in Progress.Temporary Jumpers Installed
| | | 05000440/LER-1987-025, :on 870407,outboard Containment Isolation Valves for RHR Sys a Automatically Isolated.Caused by High Pressure Signals from Loose Signal Connection.Single Common Wire Properly Connected to Signal Common Bar |
- on 870407,outboard Containment Isolation Valves for RHR Sys a Automatically Isolated.Caused by High Pressure Signals from Loose Signal Connection.Single Common Wire Properly Connected to Signal Common Bar
| | | 05000440/LER-1987-026, :on 870411,unexpected RWCU Containment Isolation Occurred.Caused by Inaccurate Differential Flow Indication at Low RWCU Flow & Low Reactor Pressure Conditions.Bias Signal to Flow Summer Changed |
- on 870411,unexpected RWCU Containment Isolation Occurred.Caused by Inaccurate Differential Flow Indication at Low RWCU Flow & Low Reactor Pressure Conditions.Bias Signal to Flow Summer Changed
| | | 05000440/LER-1987-027, :on 870413,manual Fast Reactor Shutdown Conducted Due to Loss of Condenser Vacuum & Steam Leak in Reactor Bldg.Vacuum Loss Caused by Hole in 24-inch Main Steam Drain Manifold.Manifold Replaced |
- on 870413,manual Fast Reactor Shutdown Conducted Due to Loss of Condenser Vacuum & Steam Leak in Reactor Bldg.Vacuum Loss Caused by Hole in 24-inch Main Steam Drain Manifold.Manifold Replaced
| | | 05000440/LER-1987-028, :on 870420,determined That Jet Impingement Effects from Postulated Pipe Break in RHR Steam Line Not Considered in Piping Design Review.Caused by Failure to Follow Procedure.Design Bulletin Issued |
- on 870420,determined That Jet Impingement Effects from Postulated Pipe Break in RHR Steam Line Not Considered in Piping Design Review.Caused by Failure to Follow Procedure.Design Bulletin Issued
| | | 05000440/LER-1987-029, :on 870501,during Containment Venting,Operators Overrode Interlock to Maintain RCIC Suction Transfer W/O Reducing Suppression Pool,Violating Interlock Time Per Tech Spec.Operators Counseled.Design Change Planned |
- on 870501,during Containment Venting,Operators Overrode Interlock to Maintain RCIC Suction Transfer W/O Reducing Suppression Pool,Violating Interlock Time Per Tech Spec.Operators Counseled.Design Change Planned
| | | 05000440/LER-1987-030, :on 870501,manual Reactor Scram Initiated Due to Loss of Reactor Feedwater.Caused by Failure of Air Lines for Condensate Flow Control Valve from Vibration.Metal Air Lines,Addl Valve & Pipe Supports Will Be Installed |
- on 870501,manual Reactor Scram Initiated Due to Loss of Reactor Feedwater.Caused by Failure of Air Lines for Condensate Flow Control Valve from Vibration.Metal Air Lines,Addl Valve & Pipe Supports Will Be Installed
| | | 05000440/LER-1987-031, :on 870508,Div 3 LOCA Relay Contact Not Tested Per Tech Spec Logic Sys Functional Test Section 4.3.3.2. Caused by Inadequate Surveillance Test Instruction.Tech Spec Logic Sys Functional Test Revised |
- on 870508,Div 3 LOCA Relay Contact Not Tested Per Tech Spec Logic Sys Functional Test Section 4.3.3.2. Caused by Inadequate Surveillance Test Instruction.Tech Spec Logic Sys Functional Test Revised
| | | 05000440/LER-1987-032, :on 870509,Div 1 Leak Detection Sys Isolation Signal Resulted in RWCU Sys Outboard Containment Isolation. Caused by Momentary Power Loss.Routine Sys Performance Monitoring Will Continue as Required |
- on 870509,Div 1 Leak Detection Sys Isolation Signal Resulted in RWCU Sys Outboard Containment Isolation. Caused by Momentary Power Loss.Routine Sys Performance Monitoring Will Continue as Required
| | | 05000440/LER-1987-033, :on 870517,discovered That Performance of Surveillance Instruction Placed Both Trains of Standby Liquid Control Sys in Inoperable Condition.Caused by Inadequate Procedure.Procedure Revised |
- on 870517,discovered That Performance of Surveillance Instruction Placed Both Trains of Standby Liquid Control Sys in Inoperable Condition.Caused by Inadequate Procedure.Procedure Revised
| | | 05000440/LER-1987-034, :on 870521,RCIC Isolation Occurred.Cause Related to Use of Ohmmeter to Monitor Status of Initiating Relay Contacts in Surveillance Test Instruction.Plant Administrative Procedure PAP-0205 Revised |
- on 870521,RCIC Isolation Occurred.Cause Related to Use of Ohmmeter to Monitor Status of Initiating Relay Contacts in Surveillance Test Instruction.Plant Administrative Procedure PAP-0205 Revised
| | | 05000440/LER-1987-035, :on 870524,reactor Protection Sys Manual Reactor Scram Initiated in Response to Leak in Condensate Sys.Caused by Excessive Vibration of Condensate Sys.Design Change Under Development |
- on 870524,reactor Protection Sys Manual Reactor Scram Initiated in Response to Leak in Condensate Sys.Caused by Excessive Vibration of Condensate Sys.Design Change Under Development
| | | 05000440/LER-1987-036, :on 870525,rod Pattern Controller Surveillance Missed During Reactor Startup in Violation of Tech Spec. Caused by Personnel Error.Operator Counseled on Need for Attention to Detail |
- on 870525,rod Pattern Controller Surveillance Missed During Reactor Startup in Violation of Tech Spec. Caused by Personnel Error.Operator Counseled on Need for Attention to Detail
| | | 05000440/LER-1987-037, :on 870527,reactor Scrammed on Steam Flow/ Feedwater Flow Mismatch.Caused by Failed Resistor within Motor Driven Feedwater Pump Controller.Card Containing Resistor Replaced & Control Circuit Calibr |
- on 870527,reactor Scrammed on Steam Flow/ Feedwater Flow Mismatch.Caused by Failed Resistor within Motor Driven Feedwater Pump Controller.Card Containing Resistor Replaced & Control Circuit Calibr
| | | 05000440/LER-1987-038, :on 870529,discovered That Div III Fuel Oil Out of Spec for Approx 48 H,Beginning on 870527,w/o Required Control Room Notification.Caused by Personnel Error. Personnel Counseled |
- on 870529,discovered That Div III Fuel Oil Out of Spec for Approx 48 H,Beginning on 870527,w/o Required Control Room Notification.Caused by Personnel Error. Personnel Counseled
| | | 05000440/LER-1987-039, :on 870530,main Steam Line Inboard Isolation Valve Closed Unexpectedly.Caused by Suspected Bad Connection in Channel C NSSS Isolation Logic.Valve Closure Could Not Be Duplicated Through Troubleshooting & No Addl Action Planned |
- on 870530,main Steam Line Inboard Isolation Valve Closed Unexpectedly.Caused by Suspected Bad Connection in Channel C NSSS Isolation Logic.Valve Closure Could Not Be Duplicated Through Troubleshooting & No Addl Action Planned
| | | 05000440/LER-1987-040, :on 870604,RCIC Sys Leak Detection High Steam Flow Trip Unit Noted to Be Reading Downscale.Caused by Steam Condensing in High Side Instrument Process Line of Associated Transmitter |
- on 870604,RCIC Sys Leak Detection High Steam Flow Trip Unit Noted to Be Reading Downscale.Caused by Steam Condensing in High Side Instrument Process Line of Associated Transmitter
| | | 05000440/LER-1987-042, :on 870617,reactor Protection Sys Electrical Protection Assembly Breaker Tripped,Resulting in Deenergization of Bus A.Caused by Failure of Assembly Logic Card.Card Replaced |
- on 870617,reactor Protection Sys Electrical Protection Assembly Breaker Tripped,Resulting in Deenergization of Bus A.Caused by Failure of Assembly Logic Card.Card Replaced
| | | 05000440/LER-1987-043, :on 870622,during Annulus Exhaust Gas Treatment Sys (AEGTS) Operability Test,Aegts Exhaust Fan a Started Automatically.Caused by Instrument Drift of AEGTS Exhaust Fan B Differential Pressure Switch.Switch Setpoint Calibr |
- on 870622,during Annulus Exhaust Gas Treatment Sys (AEGTS) Operability Test,Aegts Exhaust Fan a Started Automatically.Caused by Instrument Drift of AEGTS Exhaust Fan B Differential Pressure Switch.Switch Setpoint Calibr
| | | 05000440/LER-1987-044, :on 870624 & 28,RCIC Sys Automatically Isolated.Caused by Pressure Oscillations in Rcic/Leak Detection High Flow Instrument Process Lines.Leaking Transmitter Test Connection Repaired |
- on 870624 & 28,RCIC Sys Automatically Isolated.Caused by Pressure Oscillations in Rcic/Leak Detection High Flow Instrument Process Lines.Leaking Transmitter Test Connection Repaired
| | | 05000440/LER-1987-045, :on 870630,manual Reactor Scrammed Due to Generator Bushing Failure & Resultant Increased Hydrogen Concentration.Caused by Bushing Sealing Compound Overheating & Melting.Bushings Replaced |
- on 870630,manual Reactor Scrammed Due to Generator Bushing Failure & Resultant Increased Hydrogen Concentration.Caused by Bushing Sealing Compound Overheating & Melting.Bushings Replaced
| | | 05000440/LER-1987-046, :on 870701,RWCU Sys Isolation Occurred Due to RWCU HX Room Leak Detection High Temp Signal.Caused by Technician Placing Air Sampler in Manner That Hot Air Blew Over Sensor.Technicians Counseled |
- on 870701,RWCU Sys Isolation Occurred Due to RWCU HX Room Leak Detection High Temp Signal.Caused by Technician Placing Air Sampler in Manner That Hot Air Blew Over Sensor.Technicians Counseled
| | | 05000440/LER-1987-047, :on 870702,plant Operators Failed to Demonstrate Operability of Offsite Electrical Power Sources within 8 H.Caused by Personnel Error.Personnel Will Receive Training on Correct Tech Spec Interpretation |
- on 870702,plant Operators Failed to Demonstrate Operability of Offsite Electrical Power Sources within 8 H.Caused by Personnel Error.Personnel Will Receive Training on Correct Tech Spec Interpretation
| | | 05000440/LER-1987-048, :on 870703,containment Fire Hose Reel Inboard/ Outboard Supply Isolation Valves Discovered in Open Position Since 870622.Caused by Procedural Deficiency.Integrated Operating Instructions Will Be Reviewed & Revised |
- on 870703,containment Fire Hose Reel Inboard/ Outboard Supply Isolation Valves Discovered in Open Position Since 870622.Caused by Procedural Deficiency.Integrated Operating Instructions Will Be Reviewed & Revised
| | | 05000440/LER-1987-049, :on 870704,false High Pressure Signal Caused Closure of RHR Shutdown Cooling Suction Outboard Containment Isolation Valve.Caused by Procedure Deficiency in Plant Instructions.Instructions Revised & Plant Response Reviewed |
- on 870704,false High Pressure Signal Caused Closure of RHR Shutdown Cooling Suction Outboard Containment Isolation Valve.Caused by Procedure Deficiency in Plant Instructions.Instructions Revised & Plant Response Reviewed
| | | 05000440/LER-1987-050, :on 870704,unexpected Reactor Protection Sys Actuation Occurred Due to Upscale Trip of Neutron Monitoring Sys Intermediate Range Monitor.Caused by Grounding Deficiencies in Plant Ground Grid.Design Change Initiated |
- on 870704,unexpected Reactor Protection Sys Actuation Occurred Due to Upscale Trip of Neutron Monitoring Sys Intermediate Range Monitor.Caused by Grounding Deficiencies in Plant Ground Grid.Design Change Initiated
| | | 05000440/LER-1987-051, :on 870705,primary Containment Leakage Rate Through MSIV Lines A,B & D Exceeded Tech Spec 3.6.1.2.Caused by Worn MSIV Seats Due to Component Wear & Inadequate Mating & Sealing of Bonnet Pressure Seal Ring |
- on 870705,primary Containment Leakage Rate Through MSIV Lines A,B & D Exceeded Tech Spec 3.6.1.2.Caused by Worn MSIV Seats Due to Component Wear & Inadequate Mating & Sealing of Bonnet Pressure Seal Ring
| | | 05000440/LER-1987-052, :on 870703,04 & 05,operators Failed to Place Inoperable Intermediate Range Neutron Monitor (IRM) Channels in Tripped Condition.Caused by Personnel Error.Irm Detectors Replaced.Licensed Operators Will Be Counseled |
- on 870703,04 & 05,operators Failed to Place Inoperable Intermediate Range Neutron Monitor (IRM) Channels in Tripped Condition.Caused by Personnel Error.Irm Detectors Replaced.Licensed Operators Will Be Counseled
| | | 05000440/LER-1987-053, :on 870714,discovered That Readings for Control Room Radiation & Source Range Neutron Monitors Not Recorded & Actions Required by Tech Specs 3.3.7.1 & 3.3.7.6 Not Taken on 870713.Caused by Personnel Error |
- on 870714,discovered That Readings for Control Room Radiation & Source Range Neutron Monitors Not Recorded & Actions Required by Tech Specs 3.3.7.1 & 3.3.7.6 Not Taken on 870713.Caused by Personnel Error
| | | 05000440/LER-1987-054, :on 870722,discovered That Suppression Pool Swell Deflector Shields Required by Design Not Installed for Six Limitorque Operators.Shields Installed & as-built Drawings Completed to Reflect Installation |
- on 870722,discovered That Suppression Pool Swell Deflector Shields Required by Design Not Installed for Six Limitorque Operators.Shields Installed & as-built Drawings Completed to Reflect Installation
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