05000440/LER-1987-001, :on 870107,RWCU Containment Isolation Occurred Due to Indicated High Differential Flow.Caused by Flow Control Valve Problems.Engineering Design Change Implemented to Provide Mass & Temp Compensation for RWCU Instruments

From kanterella
(Redirected from 05000440/LER-1987-001)
Jump to navigation Jump to search
:on 870107,RWCU Containment Isolation Occurred Due to Indicated High Differential Flow.Caused by Flow Control Valve Problems.Engineering Design Change Implemented to Provide Mass & Temp Compensation for RWCU Instruments
ML20210F213
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 02/06/1987
From: Russ P
CLEVELAND ELECTRIC ILLUMINATING CO.
To:
Shared Package
ML20210F182 List:
References
LER-87-001, LER-87-1, NUDOCS 8702110028
Download: ML20210F213 (3)


LER-1987-001, on 870107,RWCU Containment Isolation Occurred Due to Indicated High Differential Flow.Caused by Flow Control Valve Problems.Engineering Design Change Implemented to Provide Mass & Temp Compensation for RWCU Instruments
Event date:
Report date:
4401987001R00 - NRC Website

text

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ -

  • c u Nou. a....ut a nm. t oo

,ss,,,,.

&#P% Ovid OME NO 3160 9100 LICENSEE EVENT REPORT (LER)

'"$'8'*

eacetst, naut ni ooc.Et Nuveen iri

  • ac. +

Pr*rrv Nuclent Power Plant. Unit 1 015 l 01010141410 1 IoFl 013 fl1Le t.s RWCU System Desinn Problems Cause High Differential Flow Isolation SVGN1 Daf t 191 LIR NutsetR 16.

REPOmf DaTE tri OTMt A F ACILiflE8 INVOLVED ist et v

.a6 v

MONT.e Dav vlam vtan MONtw Dav vlam pacitiv e Navas Docittf Nuwstnise a

0 l5l0 l 0 l 0l l l 0l l 0l 7 8

7 8l 7 0l 0l l 0l0 0l 2 0l6 8l7 0 1 5 to 1 0 to r l l

,,,,,,,,,o vms aleoat es suomirvio evaeua=r to val alouent=8Nrs o is Can i,Ca..

...a.

o...,, nn 4

se aert i se asei.i g

oc rs H H.i sa ri.

m ase inHis es mi.Hu sevs.H Hi ri tiai

.iei Ol o t 0 m am*in Ha' u man 8>

u ta=H Hai g,M* gsa~g,;al,*,"~;,,

u.se..in H.I.)

u,...H H,'

u,..H,u na, u.4, m ama.HtHeet to f at.Hinate oc 73.H3Hoseilisi se ame.in Het se 73i.H3llaisi oc 731.H2Hsi LICENSIS CONT ACT,Om twit 43 A (13:

Niut TiktPwCNE NuwSta aRta ci46 Paul Russ. Compliance Engineer. ext. 6472 21116 215191-131 71317 COe8PLitt ONE LINI,0R tacM ConspoNtNT rastunt OSSCnesto em twas almost its:

"$),'I

" h'g0.' [g'I Cawlt t y tt t w C0v'Cht%'

"f "E

"h'g (,' DI 0

Caulf evittu C0we0NINT I

I I I f I I I

i i i i i t i

I I I I I I I

I ! I I I I Su.*LatetNT4L Al#0Af t sPECit 0 #441 vo%tm Cav

'vtaa

$50Y 55'O%

tt$ Ist p.e.en.ee Cz9tCttO tutsttt0% 04 76 No l

l l

asev.ac,,$,-,,,.,.oe

,,4

..., n..

On January 7,1937 at 2015, a Reactor Water Cleanup (RWCU) containment isolation occurred due to indicated high dif ferential flow. The cause of the isolation has been identified to be flow control valve problems and possible calibration inaccuracies of the flow elements used by the Leak Detection system resulting f rom teactor coolant temperature changes.

In response to the isolation, operators restored the system to its original configuration.

As a result of this and previous events an engineering design change has been implemented to provide mass and temperature compensation for the RWCU Leak Detection delta flow instrumentation. This design change has helped to reduce the magnitude of the indicated delta flow error while operating the RWCU system at low reactor power levels.

Evaluation of the results of the design change will continue during plant startup testing.

In addition, an engineering design chando has been initiated to replace five RWCU flow control va lve s.

The replacement valves will provide the flow throttling characteristics to reduce flow oscillations during startup of the RWCU system.

Due to operational constraints and parts availability, this design change is not expected to be implemented until the first refueling outage.

0702110020 070206 PDR ADOCK 05000440 S

PDR

.g. c,.. w.

c...

a u.

au, m.n :ww.

LICENSEE EVENT REPORT (LER} TEXT OONTINUATION

- :m en : nm e

f remf$ 3 3t 88 FLCiteT v Naut att DUC K n i huh *S E ft Qi LER NUvesR '6 l

PAGS 43 "Mr.PI m?,T:

m Perry Nuclear Power Plant, Unit 1 0l5jojojol4l410 81 7 0l0l 1 Ol 0 0l2 0F 0l3 TEXT ta more sp.co a revisrud, esse essneeW Ar4C Form Jests /11M On January 7,1987 at 2015, a Reactor Water Cleanup (RWCU)[CE] containment isolation occurred due to indicated high dif ferential flow.

At the time of this event, the plant was in Operational Condition 4 (Cold Shutdown) lowering reactor vessel (RPV] water level in preparation for restarting the reactor.

Reactor coolant temperature was approximately 160 degrees and reactor vessel pressure atmospheric.

On January 7 at 1950, plant operators began lowering reactor vessel water level in accordance with Integrated Operating Instruction (101)-4, " Cold Startup" by rejecting reactor vessel water via RWCU to the main coadenser.

At 2015 while adjusting the flow to the main condenser, an inboard RWCU containment isolation occurred due to indicated high dif ferential flow.

In response to the isolation, plant operators verified no actual RWCU leak existed, and reset the isolation. The RWCU system responded to the high dif ferential flow isolation signal as designed.

RWCU pump A was restarted at 2045 with the Leak Detection system (IJ] for RWCU in bypass to prevent an unnecessary isolation.

The Leak Detection system is not required in Operational Condition 4.

Af ter satisf actory system startup, the RWCU Leak Detection system was returned to normal at 2246.

Troubleshooting, system testing and investigation of this and previous events (see LERs86-039, 86-056,86-068 and 86-085) identified the cause of the isolations as the location of the blowdown flow element, oversensitive flow control valves and lack of density compensation for RWCU delta flow.

Previously, the blowdown flow element was relocated upstream of the blowdown pressure control valve (PCV] to prevent the flow element from intermittently becoming uncovered due to the lack of back pressure.

This has reduced the indicated flou oscillations while operating the RWCU system with blowdown flow.

Flow oscillations while manipulating the RWCU flow control valves during system sta-tup and subsequent flow adjustments continue to be a p roblem. The plant operators are not always able to recover from the flow oscillations before the system isolates on high dif ferential flow. A design change to replace the flow control valves was initiated prior to the January 7 event but has not been implemented.

Additionally, a contributing cause is the ef fect of the changes in reactor coolant temperature on the indicated flow rates. The flow elements are calibrated based upon operating temperature and do not compensate for temperature changes in the reactor coolant experienced during startup.

This can result in a reduced margin to the isolation setpoint a t certain operating conditions. A design change to provide mass and temperature compensation for the delta flow instrumentation was initiated prior to the January 7 event but had not been implemented.

The Leak Detection system compares RWCU suction flow to the flow returning to the reactor vessel and blowndown flow.

All three flows are summed to generate an indication of dif ferential flow.

A RWCU high dif ferential flow signal indicates the auction flow entering the system is not being discharged via no rmal flowpaths (reacto r vessel, and blowdown to radwaste or main condenser).

This could be the result of a line break in the RWCU system.

Indicated high dif ferential flow for a duration of 45 seconds generates an isolation signal

..c. c.u >.

4 Gli

,. ; P w...

.. u.*..a n no:w ms..

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION

-- cw w : -

es, ins e v en F ACetif V teAMt die DOCA ti NUMBE R G6 L E R N UMB E R 166

. AG E 13-P't !.R. l OJJO

      • a Perry Nuclear Power Plant. Unit 1 0 l5 l0 l0 l0 l 4l4 l 0 81 7 0 l 0l 1 Ol0 Ol 3 OF OI 3 f tXT t# snare space a M was sahmenet 4AC perse JesA'gj {1h from the Leak Detection system. The 45 second time delay normally allows for system flow transients when changing operational configurations.

If an RWCU containment isolation were to occur at high reactor power, the loss of the RWCU system may cause reactor coolant conductivity to slowly increase until the system is returned to service.

In addition, during shutdown with little or no internal recirculation flow, reactor vessel thermal stratification may also occur. However, the time out-of-service for RWCU would be short and these ef fects minimal.

Since no actual RWCU high dif ferential flow existed and the f act that the system did respond as designed to the indicated high dif ferential flow isolation, the event is not considered safety significant.

As a result of this and previous events, an engineering design change has been implemented to provide mass and temperature compensation for the RWCU Leak Detection delta flow instrumentation. This design change has helped to reduce the magnitude of the indicated delta flow error while operating the RWCU at low reactor power levels. Evaluation of the results of the design change will continue during plant startup testing.

In addition, an engineering design change has been initiated to replace five RWCU flow control valves. The replacement valves will provide the flow throttling characteristics to reduce flow oscillations during startup of the RWCU system.

Due to operational constraints and parts availability, this design change is not expected to be implemented until the first refueling outage.

Energy Industry Identification System Codes are identified in the text as

[ XX].

.e,c. M,.

l$ $ 3 >