ML17252A226

From kanterella
Revision as of 05:33, 19 June 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Letter Submitting Reportable Occurrence Number 050-249/1976-17 in Accordance with Technical Specifications, Section 6.6.B
ML17252A226
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 09/30/1976
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
BBS Ltr. #76-750
Download: ML17252A226 (3)


See also: IR 05000249/2019076

Text

. ' .. : . .. ,fommori'4th

Edison . . :;;.cOresden

Nuclear .Power Station. N*R.R.0#1 . ' .* Morris, Illinois 60450 Telephone

815/942-2920 *.*.* BBS Ltr. '#76-702 September

30, 1976* Mr. James G .. Keppler, Regional Director Directorate

of Regulatory

Operations

-Region III U. S. Nuclear Regulatory

Commission

799 Roosevelt

Road * * Glen Ellyn, Illinois 60137 Enclosed please find Reportable

Occurrence*report

number 50-249/1976-17.

  • This report is being'submitted

to your office in. accordance

with the Dresden .Nuclear Power Station Technical

Section 6.6.B. BBS:jo ens on Superintendent.

Dres"den Nuclear Power Station

  • cc:. Director of Inspection

& .Enforcement

Director of Management

Information

& Prog_ram Control . File/NRC . .*.; . REGULATORY.DOCKET

FILE COPV '

.-_ . t ---_ LICENSEE EVENT REPORT -. * : .

' 1.,. I I I J. . . . 'LEASE PRINT ALL REQUIRED INFORMATION)

'I>* _ , UcENSEE . < --LICENSE EVENT -NAME ' __ '_LICENSE

NUMBER* TYPE -TYPE--@E] IIILl.Pl'RISl3

I

IJ/*11It11111

101 f I --7 -8 9 -: -,;; *14 15 --.,, -'25 ---26_ --.. 30 .31 -32 REPORT REPORT

CATEGORY TYPE -SOURCE DOCKET NUMBER -:@E]coN'T

I I I tCJ lbJ

-EVENT DATE -REPORT DATE Io I c:t I / I '6 17 I C I _ I 0 I q 131 o 17 I lz.J 69 _--74 75::-;---80 . 1 -_0 57 58 59<< .. --60 61 68 ___ EVENT DESCRIPTiON

10'21.I AT 1'1l.5 -110URS ON t:tjt'lj7b

1 1)E-IN£RTrNG-

OF" THE:"DR'IWEU-

WAS-BEGUN

IN I 7 8 9 -----------80 10'31 I AA/TtCIPffflOJV

OF THE SCH£DULE:D

IJNIT SHUTDOWN FOR 1<EFU£).JNG-.

AC -I 7 -_ *-0 "9 -* . -* --_ 00 -lo141

TO SEC-T10N 3.7. A. 5. 'B OF" Tl-4£ T£CHNIGAL. .S-PEC1F1c.11.rro/IJS

])Ry-I 7 8 9 -_ _ -_ _, BO ____ . lol51 !WELL '])£*JN£"R::rtNG-

fVIAY CfJ'i>1M£NG£

J.,4 HOURS PRIOR. TO A SHUTl>OWN.

I *_ -7 8 *9 ---------80 I Tf-lc. 'D1<.'IW£LL

0'1.VGEN.

C:O.iVC.£NTRATION

E)(CEEDED .I./ Ofo AT APPROX.I MATELV f 7 -8 9 > -* * --PRIME

mt!Vni:f) .SHe::r)SD

-SYSTEM CAUSE COMPONENT

COMPONENT

--. CODE . CODE COMPONENT

CODE . SUFPUEtl -MANUFACTUF\ER

--VIOlATXlN

-[§0 ISIAI LE.J IZ.IZlZIZIZIZI -l£j IZt91'1.dqJ

_ lYJ -. -7 8 9 *10 ---11 12 -17 -43 44 47 : -48 -_ -

DESCRiP,Tl0N

_ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _ 1w ORDER io sltirsFy fYJ1N1muWJ, SY.sritM J...iYAD 'R.£QUtR£r1rc-N{S.

I.-1 8 9 ----------__ --'-.*. -. -------. -y --80 --. lol9Ll'w1ts

  • wor-*** SHUT' TJOWJJ WITHIN

HOUR'-

To J)RYWEl .. L J: -. 7 . 8 9


.* --80 --..

..

..

... J -.> .. . .-,Q .. 9. *: -. . -. -<METH*O--D-OF-


(Sef; A-rtAC.!t£D*SHcutf)

BO_* -. --*-**** -.. -* -.-. FACILITY ----" *. -.. -._ STATUS "' POWER OTHER STATUS 'DISCOVER';:

--DISCOVERY

DESCRIPT:ON

[ill] (QJ Io 17 I 3 I I Nit I lAJ -1.._ __ _._M .........

fl...__. __ -_

1 e s 10 12 13 44 45* 46 -FORM-OF ACTIVITY --cmlTENT --_ _ 11:l:l -

OF

_ _AMOUNT

,, .. , 1 ___ 1 -NALOCATION

OF RELEASE 1 1 --a * --** 10 1-1

--44 --***

..........

__ __,_.;.,,.--

___ ---'00 * 80 .' . *-:* . . PERSONNEL.E)(POSURES

  • -* --NUMBER -TYPE 0El3CRIP.TION . (!21 :j'OlD.10

I .. .'l6J I NA -..... -I . .. . _ 1 _ e s 11 12 13 80 -. PERS.ONNEL

INJURIES NUMBER DESCRIPTION

ff8 IOI OIOll _-___ M_'A __

__ ____, _________

__,I 1 e s 11 12 00 *_,......

.. .. ": _ OFFSJTE CONSEQUENCES

Elfil -Al 11 -. 7 -89 80 -LOSS 'O_R DAMAGE TO FACILITY * TYPE * DESCRIPTION

Efil *IZ.J -. NI/ 1 0* s -10 -80 .PUBLiciTY . ,-_ -./-(ill] NA 7 8 9 80 ADDITIONAL

FACTORS

.. . .. . * .. ' EVENT DESCRIPT!ON (Continued)

2030

At 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 9-19-76, the unit load drop was halted at the direction

of the Chicago load dispatcher

because of a system emergency. . .* Dr)'Weil.

inerting *was begun at 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br />; *by 0600 ,-the dr-iwell oxygen con-* * centrad.on

had d:ropped below 4%. A similar event occurred on Unit-2 in .J:une, 1975. (50-249/1976-17)

CAUSE DESCRIPTION (Continued)

the unit.had been actually shut down, since the drywell oxygen concentration

exceeded 4%

less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. As stated above, an acceptable

drywell oxygen concentration

was achieved by 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on 9-19-76. No further action was considered

appropriate.

  • -* .* ** *:< b* ..