ML17331A671

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Updated LER 80-034/03X-2:on 801204,containment Isolation Valve NCR-252 Found Not Fully Seated W/Shut Indication in Control Room During Mode 5.Cause Undetermined.Valve Stroke Adjusted
ML17331A671
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/04/1981
From: Rischling J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A670 List:
References
LER-80-034-03X, LER-80-34-3X, NUDOCS 8103100566
Download: ML17331A671 (4)


Text

NTROL BLOCK: I 4~UPDATE REPORT PREVIOUS REPORT DATE l 2+gym L AR R LATDRY coMMlssloN LlCENSEE EVENT REPORT 1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 8 CON'T~01 7 8 tn I 9 I.ICENSEE CODE 14 15 LICENSE NUMBER REPORT~Q6 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 UNIT WAS SHUTDOWN IN MODE I Q3 04~Qs 25 26 LICENSE TYPE 30" 57 CAT 58 O 4 Qs 0 3 0 4 8 1 QB EVFNT DATE 74 75 REPORT DATE 80 WAS FOUND THAT CONTAINMENT ISOLATION VALVE,NCR-252 W S~O4 INDIC I 6 MODE 5 IT IS POSSIBLE NCR-252 MAY NOT HAVE BEEN FULLY OPERAB~OB ISOL~o 7 SAFETY OF THE PUBLIC WERE NOT EFFECTED.SE PP~OB 7 8 9 COMP.VALVE SUBCODE SUBCODE Q14[gJ Q16[gJ Q16 18 19 20 OCCURRENCE REPORT CODE TYPE ATTACHMENT NPRDQ PRIME COMP.SUBMITTED FORM SUB.SUPPLIER hJ Qs IJLIQ4 LaJQ>>40 41 42 43 COMPONENTCODE SYSTEM CAUSE CAUSE CODE CODE SUBCODE~S[)Qll y Q12 LLI Q13 7 8 9 10 12 13 SEOUENTIAL LERIRO EVENT YEAR REPORT NO.P>>REPORT~9P~~Q3 4 21 22 23 24 26 ACTION FUTURE EFFECT SHUTDOWN TAKEN ACTION ON PLANT METHOD HOURS~Q18~Q19~Q20 gJQ21 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o HE EXACT CAUSE FOR THE P 80 REVISION~r 32 COMPONENT MANUFACTURER 44 47 Qs DETERt1INED.

THE VALVE OPERATOR WOULD ST NOT PERMIT VALVE TO SHUT COMPLETELY.

THE VA V 3 SHUT COMPLETELY AND CYCLING TIt1E WAS ACCEPTABLE.

METHOD OF D I 5C OV E R Y LalQ31 45 46 45 Jack Rischlin NUTS ARE SEALED IN PLACE WITH ELOCTITE.7 8 9 FACILITY STATUS%POWER OTHER STATUS QBO O~Z LJQ26 LtLLOJaJQ>>

7 8 9 10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q 9~Z Q33~ZQ34 NA 7 8 9 10 11 44 4 PERSONNEI.

EXPOSURES NUMBER TYPE DESCRIPTION Q39~77~pp p Q Z Qss NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 9~pQ49 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION

,~1e~Q42 8 9 10 PUBLICITY ISSUED DESCRIPTION

~~2O~Q44 DISCOVERY DESCRIPTION Q32 LOCATION OF RELEASE Q36 NRC USE ONLY 68 69 41 80 80 80 80 80 80 49 44 O 804 g 0 0 0

~~~>')i lt SUPPLEMENT TO LER 80-034/03-L-0 ITEM 10 Ophrations Department was performing ISI Test on Check Valve PW-275 on the Primary Hater Supply to the Containment.

Air operated valve NCR-252 was placed in the shut position and the test connection between these two valves opened to verify PW-275 seats on reverse flow in system.When leak-age was observed at test connection the Operator looked at NCR-252 and found i was not fully seated,, even though Control Room indication indicated valve was'hut..A C8 I Technician found-the stroke adjusting nut improperly set and not permitting the valve to fully shut.The stroke was readjusted and the valve timing cycle was verified acceptable.

The test connection was again opened with NCR-252 in the shut position and verified NCR-252 and PW-275 were both shut with no leakage from the test connection.

A review.of maintenance and testing records revealed the last maintenance and stroke adjustment to NCR-252 were performed on February 4, 1980.Check valve PW-275 was successfully tested on July 4, 1980 with no leakage back through the check valve or through NCR-252.Valve NCR-252 had been, cycled for Surveillance Testing on July 29, 1980 with acceptable timing and correct valve position indication in the Control Room.Unit 2 had entered Mode 4 on July 12, 1980 and Mode'1 on July 13, 1980 and had operated at various power levels up to 100%until October 18, 1980 when the Unit tripped with a generator ground.Unit 2 had entered Mode 5 again on October 21, 1980.The maximum time NCR-252 could have been in a condition of not being able to fully shut as a Containment Isolation Valve was 81 days, but the exact number of days could not be determined.

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