05000316/LER-1980-039-03, /03L-0:on 800728,low Pressure Alarm Failed to Clear W/Increased Nitrogen Pressure.Cause Not Stated.Refs Encl Response to IE Insp Repts 50-315/80-15 & 50-316/80-14

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/03L-0:on 800728,low Pressure Alarm Failed to Clear W/Increased Nitrogen Pressure.Cause Not Stated.Refs Encl Response to IE Insp Repts 50-315/80-15 & 50-316/80-14
ML17331A672
Person / Time
Site: Cook 
Issue date: 03/04/1981
From: Murphy C
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A670 List:
References
LER-80-039-03L, LER-80-39-3L, NUDOCS 8103100572
Download: ML17331A672 (2)


LER-1980-039, /03L-0:on 800728,low Pressure Alarm Failed to Clear W/Increased Nitrogen Pressure.Cause Not Stated.Refs Encl Response to IE Insp Repts 50-315/80-15 & 50-316/80-14
Event date:
Report date:
3161980039R03 - NRC Website

text

U. S. NUCLEAR REGULATORY COMMISSION 7

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'9 UCENSEE CODE 14 15 LICENSEE EVENT REPORT 8

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0 Q70 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABI.E CONSEQUENCES Q10 DURIN 7

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8 QB EVENT DATE 74 75 REPORT DATE TOR TO CLEAR A LOW PRESSURE ALARM.

THE LOW PRESSURE ALARM FAILED TO CLE 4

', PRESSURE INCREASED TO 650 PSIG BEFORE THE OPERATOR STOPPED THE NI

~OS APPARENT OVERPRESSURE EXCEEDED THE TECH ~.SPEC.

LIMIT OF 644 PSIG T.S. 3.5.1 D

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THERE WAS NO REASONABLE ADVERSE SAFETY IMPLICATI

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CAUSE

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10 12 13 SEOUENTIAL LF RIRO EVENT YEAR REPORT NO.

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VALVE SUBCODE SUBCODE Q14 ~ Q15 ~ 06 18 19 20 OCCURRENCE REPORT REVISION CODE TYPE NO.

Q ATTACHMENT NPRDQ PRIME COMP.

COMPONENT 22 SUBMITTED FORM SUB.

SUPPI.IER MANUFACTURER Q23

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0 Q26 40 41 42 43 44 47 50-316/80-.14 DATED JANUARY 23,'981.

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OTHER STATUS Q NA 8

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10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY

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10 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7 ~00 0 Q37 ~ZQ38 7

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11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION 41 8

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Q40 DISCOVERY DESCRIPTION Q32 OPERATOR OBSERVATION LOCATION OF RELEASE Q NA 80 80 80 80 NA 7" NA NRC USE ONLY 80 80 68 69 80 o

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