ML20064H896

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LER#78-091/03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators
ML20064H896
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/19/1978
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20064H894 List:
References
LER-78-091-03L, LER-78-91-3L, NUDOCS 7812270292
Download: ML20064H896 (2)


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LER CONTISL'ATION - Ro# 1-78-91 Facility: BSEP Unit #1 Event Date: 11/20/78 reviewed by all control operators (TI-903). GP-1 will be revised to require control operators to verify a leak test has been completed before startup for each hatch recoved. Also, the drywell closure checklist will be revised to include reinstalled hatch leak rate test verification before startup. These actions should prevent similar events from occurring.

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