ML20010H737

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LER 81-039/03L-0:on 810819,during Operational Transient of Reactor Bldg Closed Cooling Water Pumps,Heat Exchanger Was Subjected to Excessive Sys Flow Causing Tube Failure.Caused by Inadequate Operating Procedures.Faulty Tubes Repaired
ML20010H737
Person / Time
Site: Oyster Creek
Issue date: 09/18/1981
From: Fickeissen K
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010H736 List:
References
LER-81-039-03L, LER-81-39-3L, NUDOCS 8109290248
Download: ML20010H737 (1)


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EVENT DESCRIPTION AND PROSA8LE CONSEQUENCES h I

O l 2.t l During an operational transient of the RBCCW pumps, a RBCCW heat g ; exchanger wa's subjected to an excessive system flow. Resultant __ _ l o g ., i l tube vibration caused a tube failure. The safety significance l

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[,;ol l Inadequate operating procedu es resulted in a RBCDV System surge. ,

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