05000219/LER-1981-039-03, /03L-0:on 810819,during Operational Transient of Reactor Bldg Closed Cooling Water Pumps,Heat Exchanger Was Subjected to Excessive Sys Flow Causing Tube Failure.Caused by Inadequate Operating Procedures.Faulty Tubes Repaired

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/03L-0:on 810819,during Operational Transient of Reactor Bldg Closed Cooling Water Pumps,Heat Exchanger Was Subjected to Excessive Sys Flow Causing Tube Failure.Caused by Inadequate Operating Procedures.Faulty Tubes Repaired
ML20010H737
Person / Time
Site: Oyster Creek
Issue date: 09/18/1981
From: Fickeissen K
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010H736 List:
References
LER-81-039-03L, LER-81-39-3L, NUDOCS 8109290248
Download: ML20010H737 (1)


LER-1981-039, /03L-0:on 810819,during Operational Transient of Reactor Bldg Closed Cooling Water Pumps,Heat Exchanger Was Subjected to Excessive Sys Flow Causing Tube Failure.Caused by Inadequate Operating Procedures.Faulty Tubes Repaired
Event date:
Report date:
2191981039R03 - NRC Website

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