ML20039G098

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LER 81-065/01T-0:on 811209,shutdown Commenced to Investigate a Isolation Condenser Isolation Valve V-14-30 811203 & 04 Failure to Operate Properly.Caused by Excessive Stress on Valve Backseat & Damage to Stem Nut
ML20039G098
Person / Time
Site: Oyster Creek
Issue date: 12/23/1981
From: Frederick Sullivan
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20039G095 List:
References
LER-81-065-01T, LER-81-65-1T, NUDOCS 8201150282
Download: ML20039G098 (1)


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[TTT} j On Decmber 3, 1981, the 'A' Isolation Condenser Isolation Valve V-14-30 l o ,3 j. ; failed to properly operate. The valve was successfully cycled but the g

o i4 i i next' day failed again tc operate. The valve operator stcrn nut was found l o 1s1 ; tb Le damaged. An examination of V-14-32's stcm nut proved to show the g

c r c. t i same results. Failure of these valves to close would result in degrada- ,

o1;[ tion of the reactor coolant pressure boundar.y. g

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Ju l l! 2 l5 ie i 27 40 gg el l2N rg; l3x lg 4 4 l Al 3 l 9 l14y [g 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 TF1l The station's method for backseating these valves created excessive I il 1I stress on the valve backseat. Failure of the backseat allowed the non- I ri i 21 I threaded portion of the stcm to enter the stanut and created binding ,

l3l L problems. Suspected valves will be inspected and repaired as needed.  ;

4 i l Applicable station operating procedures will be revised.

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