ML20041D580

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LER 82-002/03L-0:on 820118,installation of Mod Could Have Led to Possible Failure to Maintain Primary Containment Integrity.Change Defeated Automatic Withdrawal Function 3 & 4 TIP Detectors.Caused by Inadequate Safety Review
ML20041D580
Person / Time
Site: Oyster Creek
Issue date: 02/19/1982
From: Riggle E
GENERAL PUBLIC UTILITIES CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20041D574 List:
References
LER-82-002-03L, LER-82-2-3L, NUDOCS 8203050431
Download: ML20041D580 (3)


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