ML17263A811

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LER 94-010-00:on 940916,volt Bus 12B Inadvertenly Tripped. Caused by Defective Procedure.Normal Power Supplies Restored & B Emergency Diesel Generator Stopped & Aligned for Auto standby.W/941017 Ltr
ML17263A811
Person / Time
Site: Ginna Constellation icon.png
Issue date: 10/17/1994
From: MECREDY R C, ST MARTIN J T
ROCHESTER GAS & ELECTRIC CORP.
To: JOHNSON A R
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), Office of Nuclear Reactor Regulation
References
LER-94-010, LER-94-10, NUDOCS 9410270363
Download: ML17263A811 (17)


Text

F'RIORIY'YIACCELER.ATEDRIDSPROC!%SIXREGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9410270363DOC.DATE:94/10/17NOTARIZED:NOFACIL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterGAUTH.NAMEAUTHORAFFILIATIONSTMARTIN,J.T.RochesterGas&ElectricCorp.MECREDY,R.C.RochesterGas&ElectricCorp.RECIP.NAMERECIPIENTAFFILIATIONDOCKETN05000244

SUBJECT:

LER94-010-00:on940916,voltbus12Binadvertenlytripped.Causedbydefectiveprocedure.Normalpowersupple.esrestored&"B"emeregencydieselgeneratorstopped&alignedforautostandby.W/941017ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRENCLSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.NOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).05000244RECIPIENTIDCODE/NAMEPD1-3PDINTERNALAEOD/~GAB/DSQXHXF~02NRR/DE/EMEBNRR/DRCH/HHFBNRR/DRCH/HOLBNRR/DSSA/SPLBNRR/PMAS/IRCB-ERGN1FILE01EXTERNAL:EG&GBRYCE,J.HNOACMURPHY1GANRCPDRCOPIESLTTRENCL112211l.11111111111221111RECIPIENTIDCODE/NAMEJOHNSON,AAEOD/SPD/RRABNRR/DE/EELBNRR/DORS/OEABNRR/DRCH/HICBNRR/DRSS/PRPBNRR/DSSA/SRXBRES/DSIR/EIBLSTLOBBYWARDNOACPOORE,W.NUDOCSFULLTXTCOPIESLTTRENCL111111'111221111111111NVOTETOALL"RlDS"RECIPIENTS:PLEASEHELPL!STOREDUCEiVASTE!CONTACTTIIEDOCL'iIEiTCOiTROLDESK,ROOXIPI-37(EXT,504-2033)TOELIilliATEVOL'RRAMIEPROilDISTRIBL'TIOiLIS'I'SI'ORDOCL'iIEi'I'S5'OL'Oi"I'L'I'.I)!FULLTEXTCONVERSXONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR26ENCL26

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r10ecStAICROCHESTERGASANDELECTRICCORPORATION~89EASTAVENUE,ROCHESTERN.Y.f4649-000fROBERTC.MECREDYVicePresidentGinnedNuclearProductionTELEPHOMEAAEACQM7165462700October17,1994UPS.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonPWRProjectDirectorateI-3Washington,D.C.20555

Subject:

LER94-010,Lossof4160VoltBus12B,DuetoDefectiveProcedure,ResultsinAutomaticStartof"B"EmergencyDieselGeneratorR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"anyeventorconditionthatresultedinamanualor"automaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)",theattachedLicenseeEventReportLER94-010isherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.Mecredyxc:U.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector9410270363941017PDRADOCK05000244SPDR NRCFORH366(5-92)U.S.NUCLEARREGULATORYCOHHISSIONAPPROVEDBYOHBNO.3150~0104EXPIRES5/31/95LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/charactersforeachblock)ESTIHATEDBURDENPERRESPONSETOCOHPLYHITHTHISIHFORHATIONCOLLECTIONREQUEST:50.0HRS.FORHARDCOMMENTSREGARDIHGBURDENESTIHATETOTHEINFORMATIONANDRECORDSHANAGEMENTBRANCH(HNBB7714),U.STNUCLEARREGULATORYCOHHISSION~llASHIHGTON,DC20555-0001,ANDTOTHEPAPERNORKREDUCTIONPROJECT(3150-0104),OFFICEOFHANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244PAGE(3)10F10-TITLE(4)Lossof4160VoltBus12B,DuetoDefectiveProcedure,ResultsinAutomaticStartof"B"EmergencyDieselGeneratorMONTH09DAYYEAR1694EVENTDATE(5)YEAR94LERNUHBER(6)SEQUENTIALHUHBER--010--REVISIONNUHBERMONTH0010DAYYEAR1794REPORTDATE(7)FACILITYHAHEFACILITYHAHEDOCKETNUHBERDOCKETHUHBEROTHERFACILITIESINVOLVED(8)OPERATINGHODE(9)NTHISREPORTISSUBHITTEDPURSUANT20.402(b)e)(11)TOTHEREUIREHENTSOF10CFR5:(Checkoneormor73.71(b)50.73(a)(2)(iv)20.405(c)PNERLEVEL(10)20.405(a)(1)(i)20.405(a)(1)(ii)20.405(a)(1)(iii)20'05(a)(1)(iv)20.405(a)(1)(v)50.36(c)(1)50.36(c)(2)50.73(a)(2)(i)50.73(a)(2)(ii)50.73(a)(2)(III)LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(v)50'3(a)(2)(vii)50.73(a)(2)(viii)(A)50~73(a)(2)(viii)(0)50.73(a)(2)(x)73.71(c)OTHER(SpecifyinAbstractbelowandinText,NRCForm366A)NAMEJohnT.St.Martin-Director,OperatingExperienceTELEPHONEHUHBER(IncludeAreaCode)(315)524-4446COMPLETEONELINEFOREACHCOHPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEHCOHPONENTHANUFACTURERREPORTABLETOHPRDSCAUSESYSTEMCOHPONENTHANUFACTURERREPORTABLETONPRDSSUPPLEHENTALREPORTEXPECTED(14)YES(lfyes,completeEXPECTEDSUBHISSIONDATE).XNOEXPECTEDSUBHISSIONDATE(15)HOHTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately15single-spacedtypewrittenlines)(16)OnSeptember16,1994,atapproximately1018EDST,withthereactoratapproximately98%steadystatepower,the4160Voltcircuitbreakerthatwassupplyingpowerto4160Voltbus12Bwasinadvertentlytripped.Thisresultedindeenergizationofbus12BandmomentarylossofpowertouBntrain480Voltsafeguardsbuses16and17.ThenBnEmergencyDieselGeneratorstartedandreenergizedbuses16and17,asperdesign.Theunderlyingcauseoftheinadvertentcircuitbreakertripwasadefectiveprocedure.ThiseventisNUREG-1022CauseCode(D).CorrectiveactiontoprecluderepetitionisoutlinedinSectionV.B.HRCFORM366(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150.0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLY'NITNTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORMARDCOMHENTSREGARDINGBURDENESTIHATETOTHEINFORMATIONANDRECORDSHANAGEHENTBRANCH(MNBB7T14),U.S.NUCLEARREGULATORYCOHHISSION,llASNINGTON,DC205550001ANDTOTHEPAPERISRKREDUCTIONPROJECT(3140.0104),OFFICEOFMANAGEMENTANDBUDGETllASHINGTONDC20503.FACILITYNAME(1)DOCKETNUMBER(2)LERNUMBER(6)YEARSEQUENTIALREVISIONPAGE(3)R.E.GinnaNuclearPowerPlant0500024494010002OF10TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)PRE-EVENTPLANTCONDITIONSTheplantwasatapproximately98%steadystatereactorpower,withnomajoroperationalactivitiesinprogress.Alloffsitepowerto4160Voltbuses12Aand12BwasbeingsuppliedfromCircuit767(34.5KVoffsitepowersource).Circuit767wassupplyingpowerthrough34.5KVto4160Volttransformer12B(12Btransformer),via4160Voltcircuitbreakers52/12BY(tobus12A)and52/12BX(tobus12B).(Seetheattachedsketchoftheoffsitepowerdistributionsystem.)34.5KVto4160Volttransformer12A(12Atransformer),whichis.suppliedfromCircuit751(34.5KVoffsitepowersource),wasdeenergizedanddeclaredinoperabletopermitpreviouslyscheduledmaintenanceandtestingofthe12Atransformerandassociatedcircuitbreakers.Atthetimeofthisevent,triptestingwasinprogresson4160Voltcircuitbreaker52/12AX(alternatepowersupplyfromthe12Atransformertobus12B),inaccordancewithMaintenanceProcedurePME-50-04-52/12AX,"Bus12BAlternatePowerSource."PlantelectricianshadjustnotifiedtheControlRoomoperatorsthatcircuitbreaker12AXwouldbeclosedwhileinthe"test"position.II.DESCRIPTIONOFEVENTA.DATESANDAPPROXIMATETIMESOFMAJOROCCURRENCES:oSeptember16,1994,1018EDST:Eventdateandtime.oSeptember16,1994,1018EDST:Discoverydateandtime.oSeptember16,1994,1018EDST:ControlRoomoperatorsverifythe"B"EmergencyDieselGenerator(D/G)operationandsafeguardsbuses16and17energized.oSeptember16,1994,1120EDST:Circuit751declaredoperableatthecompletionofmaintenanceandtesting.oSeptember16,1994,1125EDST:Safeguardsbuses16and17wereresuppliedfromCircuit751.oSeptember16,1994,1142EDST:The"B"EmergencyD/Gwasstoppedandrealignedforautostandby.NRCFORM366A(5-92)

NRCFORM366A(5-92)U.S.NKLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOMBNO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYlllTHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHEIHFORHATIONANDRECORDSHANAGEMENTBRANCH(MNBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140.0104),OFFICEOFHANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)05000244LERNUMBER(6)YEARSEQUENTIAL94--010--REVISION00PAGE(3)3OF10TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)B.EVENT:OnSeptember16,1994,atapproximately1018EDST,withthereactoratapproximately98~steadystatefullpower,theControlRoomreceivednumerousannunciatoralarms.TheControlRoomoperatorsimmediatelydeterminedthat4160Voltbus12Bwasdeenergized,that"B"train480Voltsafeguardsbuses16and17hadlosttheirpowersupplyfrombus12B,andthatthe"B"EmergencyD/Ghadstartedandwastiedtosafeguardsbuses16and17.TheControlRoomoperatorsimmediatelyperformedtheappropriateactionsofAbnormalProcedureAP-ELEC.1(Lossof12AAnd/Or12BTransformer)tostabilizetheplant,andverifiedthatthe"B"EmergencyD/Gwasoperatingproperlyandthatsafeguardsbuses16and17wereenergized.TheControlRoomoperatorsobservedthatbus12Bhaddeenergizedanddisplayedzero(0)voltage,becausethecircuitbreakersupplyingpowertobus12Bhadtripped.Thelossofpowertobus12Bresultedinundervoltageonsafeguards'buses16and17,andthe"B"EmergencyD/Gstartedandreenergizedthesebuses,asperdesign.Whenthescheduledmaintenanceandtestingwascompletedonthe12Atransformerandassociatedbreakers,theControlRoomoperatorsclearedtheholdsonCircuit751andth'e12Atransformer.AswitchingorderwasusedtorestoreCircuit751,12Atransformer,andassociatedbreakerstooperablestatus.34.5KVcircuitbreaker75112wasclosed,energizingthe12Atransformer.TheControlRoomoperatorsdirectedplantelectricianstoinvestigatethefailure,andtherewerenoanomaliesnoted.Atapproximately1120EDST,usingEquipmentRestorationprocedureER-ELEC.1(RestorationofOffsitePower),theControlRoomoperatorsclosedcircuitbreaker12AX,energizingbus12Bfromthe12Atransformer.Atapproximately1125EDST,"B"trainsafeguardsbuses16and17wereresuppliedbyoffsitepower,viaCircuit751'tapproximately1142EDST,September16,1994,the"B"EmergencyD/Gwasstoppedandrealignedforautostandby.NRCFORM366A(5-92),

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150~0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPOHSETOCOHPLYWITHTHISINFORHATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMHENTSREGARDINGBURDENESTIMATETOTHEINFORHATIONANDRECORDSHANAGEHENTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOMHISSION,WASHIHGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244YEAR01000LERNUMBER(6)SEOUENTIALREVISIONPAGE(3)4OF10TEXT(tfmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)C.INOPERABLESTRUCTURESiCOMPONENTSiORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:Circuit751wasinoperableforscheduledmaintenanceofthe12Atransformer,beginningatapproximately0717EDSTonSeptember15,1994,andwasrestoredtoserviceatapproximately1120EDSTonSeptember16,1994..D.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:ThemomentarylossofpowercausedalossofprogrammemoryforradiationmonitorterminalRCT-1andassociatedchannelsR-12A(Containmentventilationeffluent),R-14A(Plantventilationeffluent),R-31(>>A>>steamlinemonitor),andR-32(B>>steamlinemonitor).E.METHODOFDISCOVERY:ThiseventwasimmediatelyapparentduetoMainControlBoardalarmsandindicationsintheControlRoomwhenbus12Bwasdeenergized.TheseincludedMainControlBoardannunciatorsJ-5(gllorgl2TransformerOutofSynch),J-6(4KVMainorTieBreakerTrip),J-7(480VMainorTieBreakerTrip),J-8(480VMCCSupplyBreakerTrip),andL-28(12BXFMRor12BBusTrouble).F.OPERATORACTION:Followingtheundervoltageconditiononbuses16and17,the>>B>>EmergencyD/Gautomaticallystartedandenergizedthesebuses.TheControlRoomoperatorsimmediatelyperformedtheappropriateactionsandverifiedthatthe>>B>>EmergencyD/Gwasoperatingproperly,andthatsafeguardsbuses16and17wereenergized.'heControlRoomoperatorsclearedtheholdsonCircuit751,restoredoffsitepowertobuses16and17,stoppedthe>>B>>EmergencyD/G,andrealigneditforautostandby.HRCFORM366A(5-92)

N NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150.0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORHATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOHHEHTSREGARDIHGBURDENESTIMATETOTHEINFORHATION.AHDRECORDSHANAGEMEHTBRANCH(MNBB7714),U.S.NUCLEARREGULATORYCOHHISSIOH~'WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3110.0104),OFFICEOFMAHAGEHEHTAHDBUDGETWASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244YEAR9401000LERNUHBER(6)SEQUENTIALREVISIONPAGE(3)5OF10TEXT(Ifmorespaceisrequired,useadditionaIcopiesofHRCForm366A)(17)Atapproximately1354EDSTonSeptember16,1994,theShiftSupervisornotifiedtheNRCper10CFR50.72(b)(2)(ii).,SAFETYSYSTEMRESPONSES:The>>B>>EmergencyD/Gautomaticallystartedduetotheundervoltageconditiononbuses16and17,displayedpropervoltageandfrequencyandclosedintosafeguardsbuses16and17tosupplyemergencypower.III.CAUSEOFEVENTIMMEDIATECAUSE:Theautomaticactuationofthe.>>B>>EmergencyD/Gwasduetoundervoltageonsafeguardsbuses16and17.B.INTERMEDIATECAUSE:Theundervoltageonsafeguardsbuses16and17wasduetobus12Bbeingdeenergizedwhencircuitbreaker12BXtrippedduetoanelectricalinterlock.C.ROOTCAUSE:Theunderlyingcauseofthetrippingofcircuitbreaker12BXwasadefectiveprocedure.Duringdevelopmentofthisprocedure(PME-50-04-52/12AX),theswitchdevelopmentofanelementarywiringdiagram(EWD)wasnotusedasareferenceindeterminingpost-maintenanceoperabilitytesting.TheprocedureisforpreventivemaintenanceofModelP-51000POWL-VACmetal-cladswitchgear,manufacturedbyPowellElectricalMfg.Co.Thereisanormallyopen>>s>>contact(52S/12AX)inthetripcircuitforbreaker12BXthatcomesfrombreaker12AX,topreventboth4160Voltcircuitbreakers(12AXand12BX)frombeingclosedsimultaneously.Contact52S/12AXislocatedinthemechanism-operatedcell(MOC)switchofthese'ircuitbreakers.These>>s>>contactschangestatewithmovementofthebreakermechanism.Technicalreviewersincorrectlyassumedthatthecellswitchwouldnotfunctionwhenin"test",andthereforeconcludedthatwithbreaker12AXin"test",contact52S/12AXwouldnotclose.NRCFORM366A(5-92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIOHLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOHHEHTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONAHDRECORDSHAHAGEMENTBRANCH(MNBB7714),U.STNUCLEARREGULATORYCOHHISSIOH,WASHINGTON,DC20555-0001AHDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGET'WASHIHGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUMBER(2)YEAR0500024494LERNUHBER(6)SEQUENTIAL--010--REVISIONPAGE3)pp6OF10~yTEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)Thereisanothercontactinserieswiththe52S/12AXcontactthatoperatesfromthesynchronizingswitchforthecircuitbreaker.Thiscontactisclosedwhenthesynchswitchisinthe"Off"position.WhenreviewingtheEWD,technicalreviewersmisinterpretedthefunctionofthiscontact,andassumedthatthecontactwasclosedwhenthesynchswitchwasinthe"On"position.Thus,thetriplogicforcircuitbreaker12BXwasmadeupwhenthesynchswitchwasinthe"Off"positionassoonasbreaker12AXclosed,causingbreaker12BXtotripperdesign.Afterfurtherinvestigation,itwasdiscoveredthatthissameincorrectinterpretationofswitchcontactstatuswasmadeforcircuitbreakers12AX,12AY,and12BY.Therewereatotalofeightdefectiveprocedures,onepreventiveandonecorrectivemaintenanceprocedureforeachofthefourcircuitbreakers.ThiseventisNUREG-1022CauseCode(D),DefectiveProcedure.ThislossofpowermeetstheNUMARC93-01,"IndustryGui'delineforMonitoringtheEffectivenessofMaintenanceatNuclearPowerPlants",definitionofa"MaintenancePreventableFunctionalFailure".IV.ANALYSISOFEVENT:Thiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"anyeventorconditionthatresultedinamanualorautomaticactuationofanyengineeredsafetyfeature(ESF),includingthereactorprotectionsystem(RPS)",inthatthestartingofthe"B"EmergencyD/GwasanautomaticactuationofanESFsystem.HRCFORM366A(5-92)

NRCFORH366A(5-92)UPS.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOHHENTSREGARDINGBURDENESTIMATETOTHEINFORMATIONANDRECORDSMAHAGEHEHTBRANCH(HHBB7714),U.STNUCLEARREGULATORYCOHHISSION,WASHINGTOH,DC20555-0001AHDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFHANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNAME(1)DOCKETNUHBER(2)LERNUHBER(6)YEAR'EQUENTIALREVISIONPAGE(3)R.E.GinnaNuclearPower'Plant0500024494010007OF10TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:oAllreactorcontrolandprotectionsystemsperformedasdesigned.oCircuitbreaker12BXoperatedasdesignedandtrippedwhenitreceivedavalidtripsignal.oThe"B"EmergencyD/Goperatedasdesignedbystartingandsupplyingemergencypowertosafeguardsbuses16and17.oCircuit767wasstillinoperationsupplyingpowertothe"A"trainsafeguardsbuses;subsequentlyCircuit751waslineduptosupplypowertothe"B"trainsafeguardsbusesaspermittedbyplanttechnicalspecifications.oRadiationmonitorsR-12AandR-14AareredundanttomonitorsR-12andR-14.R-12andR-14remainedoperableduringthisevent.oLossofradiationmonitorsR-31andR-32iscompensatedforbylocalmonitoringofsteamlineradiation,whichwouldbeperformedbyplantpersonnel,asspecifiedinemergencyoperatingprocedures.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywa'sassuredatalltimes.V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:oSafeguardsbuses16and17normalpowersupplieswererestoredviaCircuit751,andthe"B"EmergencyD/Gwasstoppedandalignedforautostandby.oCircuitbreaker12BXwascycledtoconfirmthatthebreakerrespondedasdesigned.oTheRCT-1radiationmonitorterminalandassociatedchannelsR-12A,R-14A,R-31,andR-32werereprogrammedanddeclaredoperable.HRCFORH366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPOHSETOCOHPLYMITHTHISINFORHATIONCOLLECTIOHREQUEST:50.0HRS.FORHARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORHATIOHANDRECORDSHANAGEHEHTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOHHISSION,HASHINGTOH,DC20555-0001ANDTOTHEPAPERHORKREDUCTIONPROJECT(3180-0104),OFFICEOFHANAGEHENTANDBUDGETMASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244LERNUHBER(6)YEARSEQUENTIAL94--010--REVISION00PAGE(3)8OF10TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:oAllCorrectiveMaintenanceElectrical(CME),PreventiveMaintenanceElectrical(PME),andProtectiveRelay(PRI)proceduresassociatedwithPowellcircuitbreakerswerequarantined.ThisincludedPME-50-04-52/12AXandthesevenotherproceduresforcircuitbreakers12AX,12AY,12BX,and12BY.oThequarantinedprocedureswillbereviewedagainsttheEWDsanddrawingconventionstodetermineifanyothererrorsininterpretationofswitchcontactstatusweremadeduringproceduredevelopment.Quarantinedproceduresthatarefoundtobeinerrorwillberevised.oATrainingWorkRequest(TWR)hasbeensubmittedtoincorporatedetailsofthiseventduringIndustryEventstraining,emphasizeeventdetailsduringmaintenancetrainingonPreferredPowerSources,andreinforcetherequirementtouseswitchdevelopmentinformationduringtrainingonEWDs.oElectricalEngineeringhasevaluatedthedesignoftheoffsitepowerconfiguration,andhasrecommendedamethodtoavoid4160Voltcircuitbreakertripsduringbreakertesting.oThecausesandeffectsoflossofpowertotheRCT-1radiationmonitorterminalwillbereviewed,todeterminetheneedforchangesindesignormaintenanceofthesystem.HRCFORH366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCOHHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYOHBNO.3150.0104EXPIRES5/31/95lESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISIHFORHATIONCOLLECTIOHREQUEST:50.0HRS~FORWARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORHATIONANDRECORDSHANAGEHENTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOHHISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(31400104),OFFICEOFHANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)05000244YEAR010--00LERNUHBER(6)SEQUENTIALREVISIONPAGE(3)9OF10TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:NoneB.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:NodocumentationofsimilarLEReventswiththe'samerootcauseatGinnaNuclearPowerPlantcouldbeiden-tified.However,LERs91-002and92-007weresimilarevents(startofaD/Gduetolossof4160Voltbusoroffsitepower)withdifferentrootcauses.C.SPECIALCOMMENTS:NoneNRCFORM366A(5-92)

NRCFORN366A(5-92)U.S.NUCLEARREGULATORYCONNISSIONL1CENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEOBYONBNO.3150.0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYMITHTHISINFORHATIONCOLLECTIONREQUEST:50.0HRS.FORMARDCOHHENTSREGARDINGBURDENESTINATETOTHEINFORNATIOHAHDRECORDSIIANAGEHENTBRANCH(NHBB7714)1U.S.NUCLEARREGULATORYCONHISSIONIMASHINGTON,DC20555-0001AND.TOTHEPAPERMORKREDUCTIOHPROJECT(3140.0104)1OFFICEOFHANAGENENTANDBUDGETMASHINGTONDC20503.FACILITYNAHE(1)R.E.GinnaNuclearPowerPlantDOCKETNUHBER(2)YEAR0500024494PAGE(3)010pp10OF10'ERNUHBER(6SEQUENTIALREVISIONTEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)51AIION114NN$45<VIIWtI+XNUNC5141ltWtllN7414252/ION27511$$2/751127474174AVOIIS151AWlNOICNtNNN12$$4$N41N~INV<tttICOI2$>75111CINC$4AVNISISIAAIN<<WONfOSCN114$4&i~IN~IN<<<ttt>>OOI2A>~tSO/1Sl/IC115<St/tt5$/2ItllNC~ttl/4$1/IC1151S2/tt5A/511>INO41IOl/N/212$/I~11$CANONOttONICNOI/Ntttltt/ISCANONONCANCNSt/N7511$/1$1755ICSt/OV512$/II1555IC52/S7$12$/2$~ISONOSl/OIISI24/12$2/StltIll/I5~IAWIC1155ICS2/Otlllll/141555SIAIXNI501VICCWNICAAXN1741N<tASNSNII>~IAIXN5CNVICC41~CI<<tAAOSNI4>>041II~IO41NVIll5IAlXNSCNVCCWNIISWhCN14~INNW<tl>O5541I>SIAISIN5OIVICC\CNOINNNIO~IN<t<SNSIOIS>52/NISII/II~1$ICNOIC:NOS~ONtNIXNNNCNINNIONC$2$7$144$Sl/OtltI4/ISOI~NCSt/NISIO/IICCOI~INO52/Still</ISCCCIAINO$2/WSII/2$$17I<ISC<<>>NINIOO~ItOOIIOSl/COIOlICSt/XIIII/1$CCOINNO52/OIOI5/2ICCOlitNONIXOIA~2/NISI5/21$1$ICHRCFORN366A(5-92)