Similar Documents at Ginna |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCELERAII=D D!S~RIBU t ION DEMONSTP 4.TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9101160181 DOC.DATE: 91/01/11 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet 'Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION
'BACKUSjW.H. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION . R
SUBJECT:
LER'90-017-00:on 901212,reactor trip relay de-energized &
reactor tripped when dc switches in distribution panel D opened. Caused by procedural inadequacy. Procedure change process being evaluated,W/910111 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
~
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A RECIPIENT COPIES. RECIPIENT COPIES ID CODE/NAME LTTR ENCL. ID CODE/NAME LTTR ENCL PD1-3 LA 1 .1 PD1-3 PD 1 1
. JOHNSON,A 1 1
'
INTERNAL: ACN W 2 2 AEOD/DOA 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DS P 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB.7E 1 ~
1 NRR/DLPQ/LHFBll 1 1 NRR/DLPQ/LPEB10 1.. - 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB SD 1 1 NRR/DST/SICB 7E 1 1 NRR/DST/SPLBSDl 1 1 NRR/DST/SRXB SE 1 1 REG F 1 1 RES/DSIR/EIB 1 '
RGN1 01 1 1 EXTERNAL EG&G BRYCE I J ~ H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MAYS,,G .1 1 R NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1' jVt/
!IYg~jl'i 9 Xr ~
D D
NOTE TO AI.I "RIBS" RECIPIENTS:
PLEASE HELP US TO REDUCE lVASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOXI P!-37 (EXT. 20079! TO ELlb IINATE YOUR NAil!E FROM DISTRIBUTION LISTS I OR DOCUb'IENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQU1RED: LTTR 31 ENCL 31
yola
$ 1k1C ROCHESTER 8AS AN'i Ef.L'RI CORPORATION 89 EAST AVENUE, ROCHESTER N.Y. 14649.0001 ROBf Rl f. s" c Tf. EPjtQN.
V<<e f're< dt" AREA cGiJf'7't6 546 270
- Cit, January 11, 1991 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 90-017, Opening of DC Switches (Procedural Inadequacy) Disables Manual and Auto Actuation of Safeguards Sequence Initiation Causing a Condition Outside the Design Basis of the Plant R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(ii)(B), which requires a report of, "any event or condition that resulted in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded, or resulted in the nuclear power plant being in a condition that was outside the design basis of the plant", the attached Licensee Event Report LER 90-017 is hereby submitted.
event has in no way affected the public's health and I'his safety.
Very ix ugly youk. 8, Robert C. Me redy
/
xc: U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector Pu g p(g.
Z(pP 9101160181 PPFy 5101ii A"tAI Y n~rirt,r " ~.i
&DR
0 HAC Arw 500
($ 441 VL NUCLCAA AIOULATOAQCOAWI~
AAYAOVIOOU! HO. SIN 0<OV LIC EN S EE EVENT REPORT tLER) CIS<ACS I/SQI 5 5ACILITY HAUC 111 OOCAIT NUMSCA Ol R 'nna Nuc1ear Power Plant 0 6 0 o 0)24410Fl Qponmq, of DC Switches Dz.sables Manual and Auto Actuation o 1 IT LC 14I Sa egu s Se ence I'nitiation Causin a Condition Outside .the Desi IVCHT OATS IN LIA NVMICA IN AtMATO*TI ITI OTHCA
'asis of the Plant IACILITICIINVOLVCO OI UOHTH OAY YCAA YIAA ~ I OUI AYIAL
>>UUYIA MY'>>
>>UUSI 1 UOHTH OAY Y CAN ~ ACILIYY>>AMIA OOCKCT HUll~ CA(ll 0 6,0 0 0 1 2 1 2 9090 0,1 7 0 0 01119 1 0 6 0 0 0 OAC AATINO THIS ACKIAT Il SUIMIIICO TUASVAHT 'I0 THI AtOVI1CMtNTI0> ISCSA $ ! ICMYA rv r rrr Al IM YA>>rr>>51 111 UOOC I~ I
- 10. 405 III TOAOII~ I N,T 54)Q I I HI TSJIWI
~ OYI C1 50.500 4(I( I II NM(alIll N.T 54( OI IVI 5 1514(
LCVIL p p 50 A00 4 II I I I I I ~ OMIAIOI OTHI1 (5Ar>>r 4 AAvvrr TOPIC 4(l I I ( W I N.T 54(O I II
~ O.T54(QI(vt(
l0254IOIIYWIIAI
~ >>or AAI M TAAL >>AC JICAI lrr 50AOS 4 I (11(HI N.T54((5(ISI N.1 5 4 l(5 llvWI I ~ I 50.50S 41(1 llrl ~ I IC4(QI IWI IO.TSNIQI(A(
LIC INC C I CONTACT SOA THIS LCA (ill HAUC TCLCTHOHC HUMSIA Wesley H. Backus AAIACOOI Technical Assistant to the Operations COM5LCTC OHC LIHC SOA CACH Mana er COMM>>tNT SAILUAC OIICAIIIOIN THI~ ACMAT (ill 31 524- 446 CAU5C SYSTSU COMMHCHT UANUYAC C~"ILC "'">'.>~~:.-,1 Ull lrSICM COMMHCHT MANVSAC CMATAIL g g>~$~(5(ÃrP A~
TVACA C TVACA TO HtAOS
~'jPi44~+'v+(+Ir rj(Q 5lO.UVIOL CAJ,. I A,IV 1+cvw SUYYLCMCHTAL ACMAT I trtCTCO II4l MONTH CAY 'YCAA CX ~ CCICO I
SV M I 55 IO H II II IllIIIrr. Y>>vU>>H CIIPTCTEO 5UCU(55(O>> OA TCI HO OATC AJCTAACT IL>>A>> N I 500 Mecr, I I, AArvsrvswr rtrvA ~YAAUYnpvrrw>>A AANI (IN
)
On December 12, 1990, at 2310 EST, with the reactor at approximately 3%
'='tc)'e ,
full power, the Control Room Foreman opened two cd by a Mainte>>.rce procedure, cav~inL) disabling of manual (pushbutton) and automatic actuation of the safeguards sequence initiation.
The two DC switches were closed, as directed by the Maintenance procedure, approximately twenty (20) minutes later, restoring manual (pushbutton) and automatic actuation initiation.'he underlying cause of the event was procedure inadequacy due to insufficient attention to detail.
A Extensive corrective actions are being taken to prevent recurrence, including communication of management expectations, HPES evalua-tions, identifying procedural'nadequacies, and a comprehensive upgrade of the procedure change process.
>>AC
.la
/rs 50C
~ ~
SRRMRRHSKHH8i%
~ ~
~ I I I ~ ~ ~
I
~ ~ ~
N
~ ~
I ~
0 ~ ~ ~ ~
~ ~ ~ ~
~ ~
~ ~ 0 0 0 0 f
~ e
~ ~ ~ - ~
~ ~
~ ~ ~
~ ~ - ~
~ ~
~ ~ ~ ~ ~
~ ~ ~ ~
~ ~
~ ~
REEHQH8895%%9PiB I ~ l ~ r y ~
$ g g $ g
~
'
~ ~ ~ o
~ - ~ 0 ~ ~ ~ ~
~
~ ~ ~
~ ~
~ ~ ~
J ~ ~ ~
~ ~ ~ ~
~ ~ ~
~ ~
~ ~ ~ ~
e
~ ~
~ ~
~ ~
~ ~
) ' ~ A
~ - ~
~ ~ ~
~ ~
~- ' ~ ~ ~
~ - ~
~ - - ~- I ~ I
~ I- - ~- ~ ~
~
~ ~ ~ ~ ~
I o ~ ~ ~ ~
s ~ ~
~ ~
~ ~
~ ~
~ ~
IIAC SIUttt SSSA V.S. IIVCLKAAASOVLATOAT COUUISSIOII 19451 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION ASSAOV50 OU9 AO 515OMIOS 5IISIA55 '9/SI I95 SACILITY IIASIC ill OOCKST IIVUSSA ITI LTA AVSSICA ICI ~ AOS ISI SSOVSIITIAL IIS U IS IO It U 1 lI U R.E. Ginna Nuclear Power Plant TTXT III'IIOIS AUSS tI ISSIUSS. USs NASOSIUS ArAC IItttlt WS'll I ITI I Ol 24 49IQQ1 7 00 Qi5oF l i5 The Control Room operators immediately .performed the applicable actions of E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response) and stabilized the plant in hot shutdown. I After completing the applicable steps of E-0 and ES-0.1, the Control Room operators completed their part of M-48.14, by closing the two DC switches that had been opened in step 5.5.1 of M-48.14. This was accomplished at approximately 2330 EST, December 12, 1990.
The oncoming SS, who had been in the Control Room during this event, resumed the evaluation of the consequences of alarm L-31 after'plant conditions had stabilized. (The cause of the alarm had already been determined. ) He performed another review of M-48. 14 and called other knowledgeable members of the plant staff at their homes (at approximately 0100 EST, December 13, 1990) to discuss his concerns about the effect of opening these two DC switches. After receiving confirmation that'his concerns were legiti-mate, he made the proper notifications to higher supervision and the Nuclear Regulatory Commission (NRC) .
3.NOPERABLL'TRUCTURAL&s COMPONEN'1'6 s OK SYSTEI'sh THA'J.
CONTRIBUTED TO THE EVENT:
None.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED-None..
E. METHOD OF DISCOVERY:
The event was made apparent during the oncoming SS review of the consequences of Control Board Alarm L-31 (Safeguards DC Failure) and subsequent discussions with knowledgeable plant staff.
~ IAC SOASS SOSA l9451
MAC lotm 9$ $ A I943I II.9. HIICLTAII1$ 4ULATOIIY CO>>AII9$ IOH LICENSEE EVENT REPORT ILERI TEXT CONTINUATION . A9PIIOVlO OM9 HO $ I$ 0WIOa XXPIA$$ 9/$ I 4$
SACILITY NA>>l III OOCrlT eu>>9$ A LTI L$ 1 HII>>9$ II ICI AAOl ITI vtAA 9 I QVl NTI AL ATVISIOH
~ tVu V TA R.E. Ginna Nuclear Polar Plant TTXT I~~>>eccl~. v>>e<<rWW+ACSn ~'IIIITI oIoI24 490 017 00 0 '6oF1 5 F. OPERATOR ACTXON:
Factors that influenced operator actions, during the event were as follows: v The Control Room operators questioned step 5.5.1 in procedure M-48.14, but information in M-48. 14, the DC switch labels, and Alarm Response procedure AR-L-31 did not provide sufficient operational information to determine the consequences of opening these two switches.
o The Control Room operators had confidence in a Plant Operating Review Committee (PORC) approved procedure that had also been reviewed by the Electrical Planner.
As the event was over prior to discovery, no operator actions other than normal were performed.
G. SAFETY SYSTEM RESPONSES:
None.
XXI. CAUSE OF EVENT A. IMHEDlATE CAUSE:
A condition outside the design basis of the plant was caused by the disabling of manual (pushbutton) and automatic actuation of the safeguards sequence initiation (i.e. auto and manual SI).
B. INTERMEDXATE CAUSE:
The disabling of manual (pushbutton) and automatic
-
actuation of the safeguards sequence initiation was-caused by switch gl2 in the 1A DC Distribution Panel and switch g9 in the 1B DC Distribution Panel being open at the same time. Both of these panels are on the back of the Main Control Board.
MAC >414 999A (9WI
~ ~
~ ~ ~ ~
~ ~ ~ ~ ~
~ ~ ~ ~
~ ~
~ ~ ~
~ ~
~ ~ ~
~ ~ ~ ~ ~
~ ~
~ ~
~ ~
~ ~ ~ ~
~ ~
~ ~
~ ~ ~ ~ ~
~ ~ ~
0 ~
~ ~ ~
~ ~ \~
~ ~ ~
~ ~
~ ~ ~
~ ~ ~ ~ ~ ~
~ ~ ~ ~
~ ~ ~ ~
a ~ t
~ ~
~ r r
~ ~ ~ ~
~ ~
~ ~
~ ~
~ ~
~ ~ 0
~ ~
~ ~ ~ ~
~ ~ ~ ~ ~ ~
~ ~
~ ~
~ o ~ ~ ~ ~ ~
~ ~ ~
,
0 HRC >wiA SAEA V.t. IIVCLEAR REOULATORY COMMISSION IE4S I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION OME HO i'ttROYEO SISO&I04 EIItIRES 'EPICS AACILITYIIAME (II COCKET iIUMEER IEI LER HVMEER Iti tAOE ISI SEQVERTiAL AtVitiOH M EA HQIJ EA R.E. Ginna Nuclear Power Plant 5Io(oIo gI4 OI1i7 0 90F15 TEXT IA'i>>itA>>i>> e ~. v>> AiAAOCrWNAC Aiiiii~'el I ITI o 4 9 0 0 The effect of the potential delay in actuating safeguards equipment upon those events analyzed in the UFSAR was evaluated. The accidents effected by this action are those accidents which result in depressurization of the primary system causing SI. These are primarily the following:
0 Feed Line Break (FLB) 0 Steam Generator Tube Rupture (SGTR) 0 Small Break Loss of Coolant Accident (SBLOCA) o Large Break Loss of Coolant Accident (LOCA) o Small Steam Line Break (Small SLB) o Large Steam Line Break (SLB)
An analysis of these accidents was performed to determine the effect of the disabling of manual (pushbutton) and automatic actuation of the safeguards sequence initiation with the following results:
Feed Line Break t
This accident was analyzed by the Ginna Updated Final Safety Analysis Report (UFSAR) as a heat up event with auxiliary feedwater available in ten (10) minutes. As a heatup event, RCS pressure never decreased below the SI setpoint, but rapidly increased above the SI pump shutoff head. Therefore, SI was not necessary and auxiliary feedwater, when available within ten (10) minutes, is sufficient to mitigate the event. Operator actions to start auxiliary feedwater within ten (10) minutes is consistent with the Ginna licensing basis. If the FLB was re-evaluated as a cooldown event from 34 power the results would be bounded by a SLB.
RRC AORM SEEA it AS I
IIAC laew 494A V.4. IIUCLSAA ASCUL*TOAY COMMI44IOII I941I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION /
A99AOYSO OM4 IIO SI SO&104 4)e+IIIK$4ISI '4$
9 ACILITY IIAM4 (Il OOCIIST IIVM44A (1I LSA MVM44II I ~ I ~ AQ4 ISI S ~ QUSHTIAL ASVIQl08 4UM A ~i Q 9A R.E. Ginna Nuclear Power Plant 90 017 00,10 oFl TEXT lll~ CWCe M ~, ~ AAAIMAMWIC AtW AM'llI Ill 0 5 0 0IO 2 4 4 5 Steam Generator Tube Ru ture SGTR is bounded by SBLOCA from the RCS depressurization standpoint. The leak rate from a SGTR is small compared to break flow for a SBLOCA. There is no significant effect due to lack of manual (pushbutton) or automatic SI since the main steps in the procedure deal with isolation of the ruptured SG, depressurization of the RCS, and termination of SI.
Small Break Loss of Coolant Accident When manual (pushbutton) and automatic SI was de-activated, the reactor was operating at 34 power. The reactor had been at 3% power for approximately ten (10) hours. Prior to that, the'eactor had been subcritical for twenty-two (22) hours following a trip.
Westinghouse Owner's Group letter WOG 90-113, dated July 2, 1990, "Shutdown LOCA Program Draf< Report", evaluated a mode 4 LOCA using a generic two (2) loop plant with a six (6) inch break assumed to occur two and a half (2.5) hours after shutdown. Acceptable results were obtained provided SI was started ten (10) minutes after the break.
Assumptions of the mode 4 LOCA analysis are compared with the Ginna Event conditions below:
WOG MODE 4 GINNA EVENT Decay Heat 1.34 Decay Heat 0.864 No accumulators available Accumulators available RCS pressure.1000 psig RCS pressure 2235 psig RCS temperature 425 F RCS temperature 547 F The availability of accumulators and the lower decay heat offset the higher RCS temperature and pressure. Sufficient time ~s available to manually start the.SI and RHR pumps and open appropriate valves from the Control Room, and to recover from the SBLOCA. In any case, SBLOCA is bounded by LOCA because less time is available for operator action during a Large Break LOCA.
4AC 90AM 994A
<9A01
MAC eOrm SSSA 114SI V.S. HVCLSAA ASOuLATOAv COMMiSSIOle LICENSEE EVENT REPORT ILER) TEXT CONTINUATION r AeeAovso OMs Ho sl so&Ice See>ASS SISI4S I'ACILITYeIAMS III OOCIIST HUMOSII (11 LSA MuMSSII ISI ~ AOS ISI SSCMSHTIAL AS Q 4 10 4 M 1 U R.E. 'Ginna Nuclear Power'Plant
~. 0 5 I0 0 io 90 017 TSxr nr eeee Meee e we eeeMeew'AC ~ Xa4 Tv I ITI 2 4 4 0 IO 1 )1 os' I 5 Lar e Break Loss of Coolant Accident An assessment of disabling manual (pushbutton) and automatic SI at 3% power was performed by Westinghouse with respect to the LOCA analysis. The assessment assumed the RCS was at 547 F, 2235 psig. The fuel rods were assumed to be at 600 F which would be the approximate pellet and clad temperature at the end-of-blowdown phase. The vessel lower plenum and the lower portion of the core would be covered with accumulator water.
that SI must be initiated when the fuel rods are at 1800 F Further, it was assumed to turn around the cladding temperature before 2200 F. Decay heat is based on an approximation of power it reaches history prior to the event, using the 1971 ANS Model. An adiabatic heatup calculation was performed using properties for a 14 x 14 array Optimum Fuel Assembly (OFA). The calculation indicated SX was necessary in 5.5 to 6 minutes.
Simulations on the Ginna specific simulator indicate a 5 to 6 minute operator response during a LOCA is achievable.
Small Steam Line Break This accident is bounded by the Large SLB because longer times are available for operator response.
Lar e Steam Li:ne Break Westinghouse assessed the effect of no manual (pushbutton) or automatic SX on the Steam Line Break analysis. Based on their experiences with Steam Line Break analysis as well as a review of the available margin to the acceptance criteria, it was judged that analyzed at 34 power with no manual (pushbutton) or if the accident were re-automatic SI, acceptable results would be obtained.
~AC eo14 sssA IS 4S I
0 MAC Sarw $ SEA 104 $ U,L MIJCLEAII AEOULATOAV COMMITEIOII 1
LICENSEE EVENT REPORT ILERI TEXT CONTINUATION I APPROVED OME IIO $ 1$ 0&IOJ E JTPi A E $ 8 JT I 4$
SACILITY IIAME III DOCKET IIU4HEA ITI LEII IILNNEII IEI PACE 1$ I SEOVS JJTJAL PEV>SIC U IvIJU 1 1 UVU SA R.E. Ginna Nuclear Power Plant TEXT JJJ eOrP JPPPP A newer. UPS PJ>>1>>MJ JTAC M Ja4'Il lltl 0 5 0 0 0 2 4 4 90 '017 00 12 OF Rochester Gas and Electric Corporation (RG&E) performed a computer analysis of the SLB using the Westinghouse LOFTRAN Code. A base case was compared to a case where SI was delayed for ten (10) minutes. The comparison indicated negligible change in, minimum DNBR. There was an insigni-ficant change in mass released to containment because mass release is dominated by initial steam generator level and auxiliary feedwater flow, neither of which are affected by delayed SI. Comparing energy out the break for both cases, showed negligible differences. Therefore, delaying SI has negligible effect on minimum DNBR and mass/energy out the break.
In conclusion, delay of manual (pushbutton) and automatic SI with the reactor at 34 power would not cause Non-LOCA events to'xceed the acceptance criteria. A delay of 5.5 to 6 minutes in the LOCA can be tolerated without unacceptable results. Based on operator training, this is sufficient time for operator response.
Based on the above, it can be concluded that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
The affected system was restored to normal when the two (2) DC switches were closed twenty (20) minutes after they were opened.
%AC SCAM SSAA I$ 431
~ ~
~ ~
~
~ ~
~ ~ ~
~ ~ ~
~ ~ ~ ~ ~ ~
~ ~ ~ ~
~ ~
~ ~
~ ~
~ ~ ~ ~ ~ ~ ~
~ ~
~ ~ ~
~ ~
~ ~ ~ ~
~ ~
~ ~
l ~ ~ r ~
~ I t
~ ~ ~
~ 0 ~ 0
~ ~ l 0 ~ ~ ~ ~
~ ~
~ ~ ~ ~
~ ~
~ ~ - ~
~ ~ ~ ~
~ ~ ~ ~
~ ~ 0
~ ~
~ 0 ~ ~ ~
~ ~
~ ~-
~ 0
~ ~
~ ~ ~
~ ~ ~
~ ~
~ ~
~ ~
~ ~ ~ ~
~ ~
~ ~
>> ~
~ s ~ i i i ~
I I I I
~ ~
~ ~ ~ ~ ~
~ ~ ~ ~ ~ ~
~ ~
II ~ ~ ~
~
~ ~ I>> ~ Ol
~ ~
~ ~ QI'
~ ~
~ ~ ~ ~ ~
~ ~
~ ~ ~ ~
~ I IB
I