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#REDIRECT [[IR 05000029/1985098]]
{{Adams
| number = ML20207F622
| issue date = 12/30/1986
| title = SALP Rept 50-029/85-98 for Feb 1985 - Oct 1986
| author name =
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| addressee name =
| addressee affiliation =
| docket = 05000029
| license number =
| contact person =
| document report number = 50-029-85-98, 50-29-85-98, NUDOCS 8701060160
| package number = ML20207F617
| document type = SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 57
}}
See also: [[see also::IR 05000029/1985098]]
 
=Text=
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                                                ENCLOSURE
                                            SALP BOARD REPORT
                                U.S. NUCLEAR REGULATORY COMISSION
                                                REGION I
                        SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
                                    INSPECTION REPORT 50-29/85-98
                                  YANKEE ATOMIC ELECTRIC COMPANY
                                    YANKEE NUCLEAR POWER STATION
                  ASSESSMENT PERIOD:        FEBRUARY 1, 1985 - OCTOBER 6, 1986
                            BOARD MEETING DATE: DECEMBER 4, 1986
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          8701060160 861230 9
          PDR ADOCK 0500
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                                          TABLE OF CONTENTS
                                                                                        PAGE
        I.    INTR 000CTION.........................................................    1
                A.  Purpose and 0verview............................................      1
                B.  SALP Board Members..............................................      1
                C.  Background......................................................      2
        II.    CRITERIA.............................................................      6
        III. SUMMARY OF RESULTS...................................................        7
                A.  Facility Performance............................................      7
                B.  Overall Facility Evaluation.....................................      8
        IV.    PERFORMANCE ANALYSIS.................................................      9
                A.  Plant Operations................................................      9
                B.  Radiological Controls...........................................    13
                C.  Maintenance and Modifications...................................    17
                D.  Survei11ance....................................................    21
                E.  Fire Protection and Housekeeping................................    24
                F.  Emergency Preparedness.. .......................................    26
                G.  Security and Safeguards................ ........ .    ...      ...  28
                H.  Refueling and Outage Management.................................    31
                I.  Assurance of Quality............................................    34
                J.  Training and Qualification Effectiveness........................    37
                K.  Licensing Activities.............................    ...... .      40
        V.    SUPPORTING DATA AND SUMMARIES........................................    43
                A.  Investigation and Allegation  Review.............................  43
                B.  Escalated Enforcement Action....................................    43
                C.  Management Conferences..........................................    43
                D.  Licensee Event Reports..........................................    43
                E.  Operating Reactors Licensing Actions............................    44
                                                TABLES
        Table 1 - Tabular Listing of LERs by Functional Area
        Table 2 - LER Synopsis
        Table 3 - Inspection Hours SuTT.sr3
        Table 4 - Enforcement Summary
        Table 5 - Enforcement Data
        Table 6 - Inspection Report Activities
        Table 7 - Reactor Trips and Unplanned Shutdowns
                                                FIGURES
        Figure 1 - Number of Days Shutdown
                                                    i
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        I.  INTRODUCTION
            A.    Purpose and Overview
                  The Systematic Assessment of Licensee Performance (SALP) is an integrated
                  NRC staff effort to collect the available observations and data on a peri-
                  odic basis and to evaluate licensee performance based upon this informa-
                  tion. SALP is supplemental to normal regulatory processes used to ensure
                  compliance to NRC rules and regulations. SALP is intended to be suffi-
                  ciently diagnostic to provide a rational basis for allocating NRC re-
                  sources and to provide me?.ningful guidance to the licensee's management
                  to promote quality and safety of plant operation.
                  The NRC SALP Board, composed of the staff members listed below, met on
                  December 4, 1986 to review the collection of performance observations
                  and data to assess license. performance in accordance with guidance in
                  NRC Manual Chapter 0516, " Systematic Assessment of Licensee Performance."
                  A summary of the guidance and evaluation criteria is provided in Section
                  II of this report.
                  This report is the SALP Board's assessment of the licensee's safety per-
                  formance at the Yankee Nuclear Power Plant for the period February 1,
                  1985 through October 6, 1986. It is noted that the summary findings and
                  totals reflect a 20 month assessment period.
            B.    SALP Board Members
                  Board
                    S. J. Collins, Deputy Director, Division of Reactor Projects (DRP) and
                    Chairman
                  *W.  F. Kane, Director, DRP
                    E. C. Wenzinger, Chief, Projects Branch No. 3, DRP
                    T. C. Elsasser, Chief, Reactor Projects Section 3C, DRP
                    H. Eichenholz, Senior Resident Inspector, Yankee Nuclear Power Station
                    T. T. Martin, Director, Division of Radiation Safety and Safeguards
                    (DRSS)
                  *R. R. Bellamy,  Chief, Emergency Preparedness and Radiological Protection
                    Branch, DRSS
i                *W.  V. Johnston, Deputy Director, Division of Reactor Safety (DRS)
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                  *L. H. Bettenhausen, Chief, Operations Branch, DRS
                    G. E. Lear, Director, PWR Project Directorate No. 1, NRR
                    E. M. McKenna, Project Manager, PWR Project Directorate No. 1, NRR
                Attendees
                G. R. Klingler, Reactor Operations Engineer, Office of Inspection and
                    Enforcement
                W. J. Lazarus. Chief, Emergency Preparedness Section, DRSS
                M. M. Shanbaky, Chief, Facilities Radiation Protection Section, DRSS
                T. F. Dragoun, Senior Radiation Specialist, DRSS
l                * Indicates part-time Board members.
 
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          C. Background
              1.    Licensee Activities
                  The facility operated at or near full power from February 1, 1985
                  .until April 26, 1985. On April 27, 1985 a load reduction to 15 MWe
                  was initiated to repair an extraction steam line leak. A second leak
                  was discovered and repaired during power ascension on April 29, 1985.
                  From April 30, 1985 until June 30, 1985 the plant was at essentially
                    full power, other than periods of minor power restrictions that re-
                  sulted from increased cooling pond water temperature.
                  The licensee determined on May 13, 1985 that a control rod movement
                  restriction was required to comply with Section I.A of Appendix K
                  to 10 CFR 50.46, that pertained to axial power distribution assump-
                  tions for the Loss of Coolant Accident analysis. Operation of the
                  core in a rodded condition (i.e., control rod Group C inserted below
                  83 inches withdrawn) continued until September 23, 1985, when the
                  restriction was removed in response to a licensee analysis that
                  provided an acceptable basis for unrodded core operations. The power
                  coastdown to the Core XVII-XVIII refueling outage began in August
                  3, 1985. Two plant milestones involving the 25th anniversary of
                  initial criticality and exceeding the previous operating record of
                  289 continuous days of operation occurred on August 19, 1985 and
                  September 1, 1985, respectively. On September 23, 1985 licensee
                  protective measures in response to Hurricane Gloria were implemented.
                  There was no impact on the facility and operations continued.
                  On October 19, 1985, with the plant in its 336th day of continuous
                  operation, the facility was shut down until December 10, 1985 for
                  its scheduled refueling and maintenance outage. Major activities
                  during the outage included refueling, steam generator tube inspec-
                  tions, installation of a new solid state reactor protection system,
                  main generator overhaul, and implementation of Systematic Evaluation
                  Program modifications (SEP). During the refueling period, the lic-
                  ensee identified degradation of a total of four fuel rods in three
                  fuel assemblies. These occurrences were partially attributed to
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                  baffle spacer flow jetting that induced fretting of the fuel clad-
                  ding. Higher than normal coolant activity levels resulted during
                  Cycle XVII operation.
                  The facility started up from the refueling outage on December 5,
                  1985, with the plant remaining in Mode 2 to facilitate contractor
                  work on turbine-related problems. A reactor scram from low power
                  occurred on December 9, 1985 as a result of a contractor employee
                  bumping a relay during post modification cleanup in the control room.
                  The plant achieved Mode 1 operation and was phased to the grid on
                  December 10, 19S5, but a nitrogen leak in the No. I station service
                  transformer required that the generator be taken offline for a
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          period of time on December 11, 1985. The plant returned to the grid
          with power escalation being halted on December 17, 1985 due to ex-
          cessive leakage from the No. I heater drain pump. A subsequent
          problem with a stuck closed No. 3 turbine control valve limited the
          plant to 97% of rated power, which was achieved on December 23, 1985.
          A plant shutdown to Mode 2 was initiated on December 28, 1985 for
          repair of the No. 3 turbine control valve, with an unplanned auto-
          matic scram occurring from a false high startup rate condition re-
          sulting from maintenance being performed on the nuclear instrumen-
          tation system. A failure of the No. 3 boiler feedwater pump (BFP)
          and motor occurred while plant operators were preparing to return
          the plant to operation from Mode 2 on December 29, 1985. The plant
          returned to the grid on December 30, 1985 and, while undergoing a
          reactor power increase, the main coolant Dose Equivalent Iodine
          (DEI) level reached 74% of the Technical Specification (TS) limit.
          Operator actions resulted in reduction of DEI levels to approxi-
        mately 5% of the TS limit. Following the return to operation of the
          failed BFP on January 4, 1986, the plant achieved full power on
        January 7, 1986 and remained at that level until January 25, 1986.
        On this date, a planned load reduction to 65% of rated power oc-
          curred for repairs to the No. 2 heater drain pump due to excess
        packing leakage and turbine valve testing. The plant returned to
          full power on January 26, 1986.
        The facility operated at or near full power from January 26, 1986
        until the end of the assessment period on October 6, 1986, with the
        exception of the following load reductions or outages. On January
        31, 1986 an unplanned load reduction to 76% of rated power occurred
        due to a leaking pump seal on the No. 3 BFP; a planned reduction
        to 70% of rated power occurred on March 22, 1986 to perform main-
        tenance on the Nos. 1 and 3 BFPs and turbine valve testing; and an
        emergency load reduction to 78% of rated power was initiated by
        plant operators when a loss of cooling water to th* generator hydro-
!        gen cooler occurred. A low steam generator level automatic scram
        occurred on June 1, 1986 due to a loss of both heater drain pumps
        during a severe lightning storm. An unplanned load reduction to 75%
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'        of rated power occurred cn June 13, 1986 in response to a leak in
l        tne packing gland of the No. 1 BFP. The licensee proceeded to cold
        shutdown on June 18, 1986 for an outage to effect repairs to a
        leaking weld in a coupling located in containment on the No. 2 steam
        generator's blowdown line.
,        During this outage that lasted until July 1, 1986, the licensee
l        identified the following anomalous conditions: 1) a main coolant
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        hot leg isolation valve (MC-MOV-325) was found to have a failed
        valve stem, and 2) four valves in the reactor coolant vent and
        emergency feedwater systems had incorrect overload trip coils in-
        stalled in their respective power supply circuit breakers. Also
,        during this outage a valving error by a plant auxiliary operator
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                                          4
                resulted in the potential for a loss of shutdown cooling and severe
                damage of the main coolant pump internals. A planned load reduction
                to 50% of rated power occurred on September 20, 1986 to perform
                maintenance on BFPs, to conduct condenser tube leak checks, and to
                conduct turbine control valve testing. On October 4,1986 a low
                control cir pressure condition occurred that subsequently resulted
                in a reactor automatic scram on low steam generator levels. During
                the plant startup later the same day, an operator error resulted
                in a reactor automatic scram occurring when a main steam line non-
                return valve trip / reset switch was inadvertently placed in the trip
                position.    The plant was at 75% of rated power at the end of the
                assessment period on October 6, 1986.
                During this assessment period the plant availability factor was 88%.
            2.  Inspection Activities
                One NRC resident inspector was assigned to the site during the en-
                tire assessment period. The total NRC resident and region-based in-
                spection hours for this 20 month assessment period was 3057 hours
                (1,834 hours on an annual basis) with a distribution in the ap-
              praisal functional areas as shown in Table 3.
              The resident inspector conducted one event-related special inspec-
              tion that involved the review of the circumstances and licensee
              corrective actions related to the discovery of inoperable motor
              operated valves in the reactor coolant vent and emergency feedwater
              systens.
              During the period, NRC team inspections were conducted of the fol-
              lowing areas:
              a.    Implementation of various items required by NUREG 0737 includ-
                      ing post-accident sampling and monitoring capabilities.
              b.    Evaluation of the annual emergency preparedness exercises con-
                      ducted May 15, 1985 and June 11, 1986.
              c.    Licensee's action to address the concerns identified in NRC
                      Generic Letter 83-28, in the areas of Equiprent Classification,
                      Post-Maintenance Testing, and Vendor Interface.
              d.    Compliance with 10 CFR 50, Appendix R safe shutdown capability.
              e.    An operational QA effectiveness inspection.
              In this period five violations, including one Severity Level III,
              were issued. Tabulations of Violations and Inspection Activities
              are presented in Tables 5 and 6, respectively.
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                                        5
    .
        This report also assessed " Training and Qualification Effectiveness"
        and " Assurance of Quality" as separate functional areas. Although these
        topics, in themselves, are assessed in the other functional areas through
        their use as avaluation criteria, the two areas provide a synopsis. For
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        example, quality assurance effectiveness has been assessed on a day-to-
        day basis by the resident inspector and as an integral aspect of special-
        ist inspections. Although quality work is the responsibility of every
        employee, one of the management tools to measure this effectiveness is
        reliance on quality assurance inspections and audits. Other major factors
        that influence quality, such as involvement of first-line supervision,
        safety committees, and worker attitudes, are discussed in each functional
        area.
                                      _ _ . . - . -
 
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                                                6
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      II.  CRITERIA
            Licensee performance is assessed in selected functional areas. Each functional
            area represents areas significant to nuclear safety and the environment, and
            are normal programmatic areas. The following evaluation criteria were used
            as appropriate to assess each functional area.
            1.    Management involvement and control in assuring quality.
            2.    Approach to resolution of technical issues from a safety standpoint.
            3.    Responsiveness to NRC initiatives.
            4.    Enforcement history.
            5.    Reporting and analysis of reportable events.
            6.    Staffing (including management).
            7.    Training effectiveness and qualification.
            However, the SALP Board is not limited to these criteria and others may have
            been used where appropriate.
            Based upon the SALP Board assessment each functional area evaluated is clas-
            sified into one of three performance categories. The definitions of these
            performance categories are:
            Category 1:    Reduced NRC attention may be approprinte. Licensee management
            attention and involvement are aggressive and oriented toward nuclear sz %ty;
            licensee resources are ample and effectively used such that a high level of
          performance with respect te operational safety is being achieved.
          Category 2: NRC attention should be maintained at normal levels. Licensee
          management attention anc involvement are evident and concerned with nuclear
          safety; licensee resources are adequate and reasonably effective such that
          satisfactory performance with respect to operational safety is being achieved.
          Category 3:    Both NRC and licensee attention should be increased. Licensee
          management attention or involvement is acceptable and considers nuclear safety,
          but weaknesses are evident; licensee resources appear strained or not effec-
          tively used such that minimal satisfactory performance with respect to opera-
          tional safety is being achieved.
          The SALP trend categories are as follows.
          Ircroving: Licensee performance has generally improved over the last part of
          the SALF assessment period.
          Declinino: Licensee performance has generally declined over the last part of
          the SALP assessment period.
          A trend is assigned only when, in the opinion of the SALP Board, the trend
          is significant enough to be considered a precursor to a change in performance
          category in the near future.
                                                                                _          _
 
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                                              7
  .
      III. SUPMARY OF RESULTS
            A.    Facility Performance
                                                Last Period          This Period
                                                (11/1/83 -          (2/1/85 -
            Functional Area                      1/31/85)            10/6/86)          Trend
      A.    Plant Operations                        1                    1
      B.    Radiological Controls                    2                    1
      C.    Maintenance and Modifications            1                    1
      D.    Surveillance                            1                    1
      E.    Fire Protection and Housekeeping        1                    1
      F.    Emergency Preparedness                  1                    2
      G.    Security and Safeguards                  2                    2
      H.    Refueling and Outage Management          1                    1
      1.    Assurance of Quality                    2#                  1
      J.    Training and Qualification
            Effectiveness                            ##                  2
      K.    Licensing Activities                    1                    1
      #Previously assessed as Design Control / Quality Assurance
      ##Not Previously addressed as separate area
                                  __                        _ _ . _            _ _ _ _  _ - . ,
 
                                                                                                      ._
  .  .
    .
                                                    8
    .
        B.          Overall Facility Evaluation
                    Our assessment confirms your strong orientation towards plant safety,
                    technical strength, and staff experience which are considered
                    licensee attributes. Additionally, we acknowledge your initiatives
                    to address plant aging concerns and to increase the oversight and
                    effectiveness of your quality programs.
                    Management attention has resulted in your continued high level of
                    performance in eight of the eleven rated functional areas, as
                    illustrated by your successful initiatives to upgrade performance in
                    the Radiological Controls area. Our evaluation indicates that this
                    aggressive approach and high level of management involvement have not
                    been evident ~in the oversight of the security program, the effective-
                    ness of the licensed operator training program, and recent implemen-
                    tation of emergency plan actions.
                    As a result of this assessment, NRC activities in Category 1 functional
                    areas are eligible for reduced inspection effort. We will consider your
                    high level of performance and initiatives to address identified short-
                    comings in our prioritization of the inspection program for your
                    facility.
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        _ _ _ _ _ .                  __ _ ___ _  ._-    ._
                                                              .  _ _ - -              _  .__ _____
 
  .    .
    .
                                                  9
    .
        IV. PERFORMANCE ANALYSIS
            A.  Plant Operations (655 hours, 22%)
                  1.    Analysis
                        The previous SALP rated plant operations as Category 1, with a con-
                        clusion that the licensee continued to demonstrate a strong and
                        effective commitment to safety in this area.
                      This functional area includes plant operations as well as opera-
                        tional support activities. During the current SALP period, there
                      was one region-based inspection of this area. Plant operations were
                      observed by the resident inspector throughout the period.
                      Plant operators and licensee management response to plant events
                      and conditions have generally demonstrated a strong and effective
                      approach to resolution of technical issues. The team effort, which
                        includes Yankee Nuclear Services Division (YNSD) project and engi-
                      neering personnel, demonstrates a clear understanding of the issues,
                      and exhibits a conservative, technically sound approach to safety
                      issues. Abnormal events during which these characteristics were
                      demonstrated included: 1) plant operations with degraded fuel clad-
                      ding, 2) the identification of a LOCA analysis deficiency, and
                      3) the discovery of an electrical loading problem. Plant staff
                      corrective actions were noted as aggressive in resolving the opera-
                      tional concerns. However, the YNSD Projects staff has at times de-
                      layed identification of impending operational problems, which has
                      resulted in unnecessary reactive conditions being imposed upon the
                      operating organization. A notable example of this was compensatory
                      measures required during 480V A-C bus cross-tie operations while
                      the plant was in a startup and shutdown condition. Management at-
                      tention to improve YNSD Projects response timeliness is warranted.
                      The general performance of the operations department reflects a
                      commitment to quality operation as evidenced by few personnel
                      errors and a low reactor scram (trip) rate of 0.15 scrams per 1000
                      critical hours while at power.    This scram rate is significantly
                      belc,w the national average of about one per 1000 critical hours.
;                    Consistent evidence of prior planning and assignment of priorities
                      were apparent. When personnel errors occur they are isolated in-
                      stances that are not reflective of a programmatic breakdown. The
                      performance level of plant operators during routine and transient
                      plant operations reflects a conscientious attitude and concern for
                      plant safety. However, one event involving the opening of all four
                      main coolant loop bypass valves by the operators in an attempt to
                      mitigate decreasing main coolant temperature was a deviation from
                      their normally conservative manner in which they respond to opera-
                                        -
 
          ,
  .    .
            ,
    .
                                                    10
    .
                  tional problems. Although their actions were contrary to Technical
                  Specifications (TS), an NRC-requested safety evaluation demonstrated
                  that the event was of minimal safety significance.
                  Continued improvement in licensed operator knowledge of equipment
                  status has been evident. Events involving failure to document equip-
                  ment malfunctions and failure to initiate corrective maintenance
                  have been essentially eliminated due to responsive management at-
                  tention to the prior SALP concerns in this area. Increased on-line.
                  maintenance to assess the consequences of off-normal indications
                  is occurring.
                  The licensee maintains a professional atmosphere in the control room
                  by prohibiting radios, television, and unrelated reading material,
                  which tends to minimize disruptive activities. In response to NRC-
                  initiatives, the licensee has developed formal administrative means
i                  for 1) effectively limiting control room access, and 2) specifying
                  expected conduct and performance policies for operational personnel.
                  A noted licensee strength is the nearly " blackboard" status for
                  control room overhead annunciators that is routinely maintained.
                  The licensee has established well-stated administrative controls      ,
                  to provide notification and event reporting as required by 10 CFR
                  50.72 and 50.73. Licensec Event Reports (LERs) are, in general, pre-
  -
                  perly identified, analyzed, and reported in a timely manner. The        .
                  NRC review of the licensee's LERs determined that they were of
                  above-average quality. Prior SALP concerns involving incorrect and
                  insufficient information in LERs have not recurred. The licensee
                  utilizes Flent Information Reports (PIRs) for addressinc non report-
                  able concerns. Quality is evident in the areas of causal analysis
      <
                  and corrective actions; however, report issuance timeliness rou-
                  tinely exceeds the licensee's established administrative controls.
                  The overall good quality of LERs is attributable to the increased
                  involvement and thorough reviews conducted by the Plant Operations
                  Review Committee (PORC) and management. Numerous meetings of the
'
                  PORC were observed by the resident inspector, with proper question-
                  ing attitudes consistently observed that resulted in active and
                  probing discussions on items of concern and plant events. However,
,                the PORC meeting minutes tend to lack an adequate level of detaii
:                to reflect the details of the discussions that occur. Station man-
                  agement instituted training for the PORC members to improve their
                  sensitivity to responsibilities associated with procedural matters
                  and 10 CFR 50.59 evaluation adequacy.
                  Some of the initiatives undertaken in this assessment period by the
i                Nuclear Safety Audit and Review Committee include 1) ensuring that
                  safety evaluations are performed in an adequate manner, and 2) im-
i
l
l
i
              , -        -,            .
                                          , . . . .    - . - . .    -- .  . . _ - -
 
    .  .
  ,!
      .
                                      11
      .
            proving committee-cognizance over the In-Plant Audit Program by
            having members participate or monitor at least one audit to provide
            a better understanding of the program.
            A January 1986 NRC review of the licensee's initial operator lic-
            ensing program found the administrative control systems to be ade-
            quate. However, the training program and its administrative con-
            trol systems have not effectively prepared large classes of candi-
            dates to operate the facility as demonstrated by the low success
            rate on NRC licensing examinations.      During this assessment period
            one class of operator candidates consisting of four reactor opera-
            tors (R0s) and tnree senior reactor cperators (SR0s) were trained
            to operate the facility, but only three of the candidates (43%)
            were issued operating licenses.
            Presently, station staffing is adequate. A five-shift rotation
            schedule is used. Early in the assessment period the licensee as-
            signed a spare shift supervisor and a senior control room operator
            to facilitate operational flexibility. However, the current number
            of licensed reactor operators requires reliance on overtime, at a
            level that is presently in compliance with NRC requirements, to meet
          watchstanding needs. The current class for R0 and SR0 licenses is
            cocprised of five and three candidates, respectively. It appears
            that even if all of the licensee's candidates are fully successful,
            the overall depth of licensed operator staffing levels may not sig-
            nificantly change because of the potential for attrition of current
          operators.
          The use of Special Orders in lieu of approved procedures was a prior
          SALP concern. Recurrence of this issue has been identified in this
          assessment period, which suggests insufficient management attention.
          A plant procedures programmatic inspection, with specific emphasis
          placed on plant operations, was conducted. This review, in conjunc-
          tion with routine observations, identified issues that involve:
          1) difficulties in determining that independent verification for
          certain systems has been performed, 2) the need to increase the
          emphasis on attention to detail as part of the procedure review
          program, and 3) the need to insure that procedures are developed
          for all planned operations. Over-reliance on special orders and
,
'
          weaknesses in procedural content may be due to the demands placed
          on the operations department support staff that is currently being
          relied upon to perform this important function, as that staff at
          times appears to be taxed by a heavy workload.
          During this assessment period, the licensee accomplished notable
          milestones related to plant performance that involved reaching the
          25th anniversary of initial criticality, the setting of a new plant
          continuous operation record of 336 days without a shutdown, and
          maintaining the olant in an on-line status for 539 out of the 613
          days contained within the period. This represents a plant availa-
l
I
            , -                  -                -.        -.    --
 
:.
_
    .
  .
                                  12                                          *
  .
          bility of 88 percent and is significantly above the national average
          of 69 percent. These accomplishments are indicative of the operat-
          ing and support staff's overall quality performance.
      2. Conclusion
          Category 1.
      3. Board Recommendation
          None.
 
.  .
  .
                                      13
  .
      8. Radiological Controls (507 hours, 14%)
        1.  Analysis
              In the previous SALP report the licensee's performance in Chemistry
              and Radiological Controls was rated as Category 2. Weaknesses were
              identified in the areas of staff development, oversight of radwaste,
              control of work in radiation areas, recordkeeping, and respiratory
              protection programs. Three minor violations were cited. SALP Board
              recommendations were made regarding: 1) supervisory staffing,
              2) staff development, 3) self evaluation, and 4) radiological pro-
              cedure review and compliance.
            During this SALP period, region-based radiation specialists conducted
              seven inspections in the following areas: radiation protection (3);
            environmental monitoring (1); radiological chemistry (1); non-radio-
              logical chemistry (1); and waste management (1). The resident in-
            spector also reviewed selected program areas. No violations were
              identified.
            Site and corporate management directed a high level of attention
            and resources towards resolving Radiological Protection (RP) program
            weakness during this period. Substantial progress was made in the
            area cf self-identification and resolution of problems. Management
            has revised existing policies and established new policies that
            firmly support a conservative approach to radiation protection. For
            example, the Radiological Work Policy requires all personnel to
            comply with all RP requirements and delineates disciplinary action
            for noncompliance.
            A major project was undertaken to replace the outdated RP procedures
            by using assistance from the corporate technical staff with input
            and review by the small highly experienced site staff. This re-
            sulted in clear, well written draft RP procedures. Management de-
            cided to enhance this effort by id ng en innovative approach of two
            tiers of procedures - one simplified ievel for use by plant workers
            with the second level providing detailed instructions for the radi-
            ation department staff. This project is nearly complete.
            Ir;wovements in planning were noted during this period. The ALARA
            reviews for all dose intensive Design Change Request work was com-
            pleted prior to the start of the refueling outage. An infrequent
            spent resin shipment was thoroughly preplanned and controlled re-
            sulting in minimal personnel exposure and no site contamination.
            Additionally, the impact of temporary changes to the radiologically
            controlled area boundary was minimized through good planning.
            Records are complete and well-maintained for routine radiation sur-
            veys, routine chemistry surveillance, radioactive liquid waste pro-
            cessing, radiological environmental monitoring and meteorological
 
,  .
  .
                                14
  ,
      monitoring. A large main frame computer and record keeping system
        dedicated to RP and chemistry has recently been installed on site
        that will enhance recordkeeping capabilities.
      The licensee routinely exhibits technical thoroughness in the resolu-
      tion of radiation safety issues. A new on-site QC function was estab-
        lished to oversee all phases of radwaste processing and radioactive
      materials shipments. The QC personnel were specifically trained and
      qualified for this dJty. Personnel exiting the radiological control
      area on site are required to self-frisk, use an automatic hand and
      foot monitor, and then pass through a sensitive portal monitor exit.
      This multistep process provides a high degree of radioactive con-
      tamination control. The Environmental Lab has conducted exhaustive
      technical studies of the behavior characteristics of the Harshaw
      TLD system used for personnel dosimetry. This approach results in
      a high confidence in the reported personnel exposures.
      Responsiveness to NRC initiatives in almost all cases has been timely,
      technically sound and thorough. Previous NRC concerns regarding RP
      department staffing levels and lines of authority have been resolved.
      The need for procedural compliance was addressed by strong management
      disciplinary action with contractor and permanent site personnel.
      The RP prooram was understaffed and lacking experience at the begin-
      ning of this period due to loss of the radiation protection manager
      and two of four supervisory personnel. The impact of this loss of
      key personnel from this small staff was aggravated by the lack of
      a staff development program and cross-training of supervisors. A
      systematic program was implemented to correct this situation, and
      by the midpoint of this assessment period, all positions had been
      refilled. New job descriptions with clearly assigned primary and
      backup responsibilities were promulgated and a staff development
      program was put in place. In addition, a permanent supervisory posi-
      tion was added to coordinate various program improvements that are
      uncerway and planned for the future such as the expanded use of com-
      puters. The increased staff size and depth resolve the concerns
      stated in the previous SALP.
      A defined but informal training program is provided to RP supervisors
      and technicians, which makes a positive contribution to understand-
      ing of the work as evidenced by adherence to procedures with few
      personnel errors. A policy change now permits only fully ANSI quali-
      fied RP technicians to implement the RP program. The trainee posi-
      tion called " tester" was abolished in a licensee initiative to
      strengthen the technician performance level. The qualification pro-
      gram for radwaste QC inspectors made a positive contribution to the
      inspection activities and adherence to procedures.
      The licensee has improved its chemistry and radiochemistry programs.
      The licensee has a strong program to insure compliance with Techni-
      cal Specification requirements for inplant and effluent sampling
                                                                    ._-
 
                                          __      .
  .  .
    .
    ,                            15
        and analysis. In particular, the licensee has paid particular atten-
        tion to meeting its Radiological Environmental Technical Specifica-
        tions (RETS), which were effectively implemented during this assess-
        ment period. The review of the licensee's implementation of the RETS
        indicated that procedures for control and monitoring of effluents
        were very effectively stated and thoroughly carried out.
        Initiatives to improve management oversight and to improve labora-
        tory instrumentation and chemistry facilities were implemented. A
        surveillance matrix, which is reviewed by two levels of management,
        tracks the required sampling of radioactive and non-radioactive sys-
        tems. However, for the nonradioactive systems that have a potential
        for an unmonitored, unplanned release, there are no action statements
        to provide guidance, if a priori criteria are exceeded. This is a
        minor discrepancy associated with an otherwise excellent program.
        Procedures for gaseous and liquid effluent controls and offsite dose
        calculations are generally implemented properly. However, an un-
        planned, unauthorized gasecus release occurred subsequent to purging
        of a main coolant icop when the activated charcoal filter failed
        to retain the gaseous iodine. Management took aggressive actions
        to prevent a similar release including: lowering the alarm setpoint,
        replacing the charcoal, and periodically determining the removal
        efficiency for the charcoal. A timely and technically sound resolu-
        tion to this issue was implemented. Previously, periodic in place
        testing of charcoal filters had not been performed with the excep-
        tion of the Control Room Emergency Ventilation System. Although not
        required by Technical Specifications, such testing is considered
        standard industry practice.
        Procedures for chemistry surveillances have been implemented and
        analyses performed as required. Technical Specifications require
        analysis of main coolant and gaseous effluents following a 15 per-
        cent per hour power change. The operators are aware of this require-
        ment, and normally take action to insure compliance. However, in
        one instance, the analyses were performed but results were not re-
        ported to the control room. The licensee implemented a timely re-
        sponse to this concern, including issuance of a written instruction
l      to chemistry technicians to report these results to the control roo~
!
        and revision to procedures to indicate appropriate notification
        requirements. This is another indication of increased management
        attention to the follow up and correction of identified problerts.
        The licensee improved its chemistry staffing and qualification pro-
I      gram during this assessment. This was demonstrated by documentation
        of on-the-job training and retraining of chemistry personnel, in-
        creased staff, and clearly defined position descriptions to address
        major responsibilities. A number of these improvements were in re-
i      sponse to industry and NRC initiatives. However, on its own initi-
l
        ative, the licensee recognized the need and initiated action, to
        develop managerial depth within the chemistry department.
 
.  .
  .
                                      16
  .
        The licensee's ability to accurately measure radioactivity in ef-
          fluents was confirmed by intercomparisons with the NRC using the
          NRC Mobile Radiological Measurements Laboratory.
        Weaknesses in the nonradiological chemistry program, identified dur-
          ing the previous assessment period, included lack of a measurement
        control program, lack of a retraining program for chemistry techni-
        cians, and an unreliable and insensitive method for determination
        of chloride in water. A new Chemistry Department Manager was assigned
        to the facility in August 1984. During the current assessment period,
          it was noted that significant improvements have been made. These
        include: the use of control charts for chemical analyses, testing
        of technicians by requiring them to analyze samples containing un-
        knowns, and an improvement in laboratory facilities through the pur-
        chase of new equipment that will provide for greater reliability
        and sensitivity.
        The licensee maintains well-stated, controlled and explicit proce-
        dures for control of radiological environmental monitoring program
        (REMP) activities and for the calibration of meteorological moni-
        toring instrumentation. Records of REMP and meteorological monitor-
        ing were complete, well-maintained and available. Procedures are
        consistently followed. REMP sainpling stations were located as stated
        by procedure, required sampling frequencies were met, and equipment
        was calibrated as required. Positions and responsibilities are well-
        defined for management of the REMP. Calibrations of meteorological
        monitoring instruments are performed more frequently than required,
        and reviewed calibration data have been satisfactory.
        During the last SALP, the NRC made several recommendations in this
        functional area to aid improvement in licensee performance. These
        recommendations, promptly implemented by the licensee, were a blue-
        print to improve radiological controls performance from consistently
        average to exceptional. By the midpoin'. of the assessment period,
        all recommendations had been fully implemented. This resulted in
        a continuous improvement in licensee performance throughout the as-
        sessment period. In the latter part of the period, the licensee also
        implemented additional programmatic improvements on their own initi-
        ative which even further improved performance in this functional
        area. Significant programmatic improvement, coupled with a lack of
        deficiencies and consistently strong performance in all associated
        activitiu , indicates a strong licensee commitment to achieve and
        sustain a high level of performance in this diverse functional area.
      2. Conclusion
        Category 1.
      3. Board Recommendation
        None.
                                .. __
 
.  .
  .
                                          17
  .
      C. Maintenance and Modifications (601 hours, 20%)
        1.    Analysis
              The previous SALP rated the licensee's performance as Category 1.
              Positive findings were made in the areas of management involvement,
              plant reliability, improved analysis of maintenance related events,
              training and qualification, responsiveness to NRC initiatives, and
              prioritization of safety-related maintenance. The licensee continues
              to demonstrate responsiveness to NRC concerns in this functional
              area by providing effective, timely corrective actions which pre-
              vented recurrence of 10 CFR 50.59 and technical specification re-
              lated problems in performing jumper and lifted lead activities.
              During the current SALP period maintenance and modification activi-
              ties were reviewed in four region-based inspections. The resident
              inspector also examined activities in this functional area as part
              of the routine inspection program.
              The maintenance program inspections conducted during this period
              identified no programmatic deficiencies and detected no trends of
            maintenance problems. Active licensee management involvement in
              the maintenance program is evident on all levels, with maintenance
                                        -
            practices being conducive to early detection of developing equiprent
            problems      In the process of planning maintenance work, the foreman
            automatically reviews the maintenance history cards for the item
            being repaired, thus detecting any developing trends. The mainten-
            ance department, instrument and control department, and maintenance
              support department continue to be staffed by experienced, qualified
            craft and supervisory personnel. The attitude that maintenance per-
            sonnel exhibit, and the generally good housekeeping conditions in-
            volved while performing their work, are indications of good main-
            tenance attitudes and practices.
            The licensee is in the process of increasing the training program
            effectiveness for I&C, mechanical and electrical maintenance per-
            sonnel, as part of obtaining INPO accreditation. Training and quali-
            fication of maintenance personnel is a noted strength, as evidenced
            by the few personnel errors that occur.
            The licensee continues to demonstrate concern for plant reliability
            and safety. Appropriate equipment upgrading is being considered and
            implemented for systems and components proving to be difficult to
            maintain either due to age, inadequate performance or unavailability
            of spare parts. A ten year plan, reviewed annually and updated or
            modified as needed, was developed to identify these licensee con-
            cerns. The licensee's initiative in this regard was evidenced by
            the installation of a new solid state Reactor Protection Systerr and
            the replacement or addition of core exit and reactor head thermo-
            couples.
                                                                        .-.        - . _ _ _
 
  .  .
    .
    .
                                  18
          During this assessment period, the licensee performed some difficult
          maintenance work. A main coolant pump suction valve stem failure
          was identified during an unplanned maintenance outage that occurred
          to perform repairs for a leak in a steam generator (SG) blowdown
          line. The NRC viewed the licensee's corrective actions in response
          to the stem failure as being representative of a conservative,
          technically sound and thorough approach to resolving conditions
        where the potential for adverse safety conditions exist.
          Nine LER's were submitted in this functional area. A review of the
          event details indicates that the corrective action implemented by
          the maintenance organization was effective in that recurrent events
        were not prevalent. No adverse trends were identified that would
        contribute to equipment unavailability or improper performance as
        a result of maintenance activities. The licensee's event analyses,
        using PIRs, provided thorough reviews involving the PORC, and de-
        scribed proper corrective actions to prevent the recurrence of non-
        reportable events.
.
        The NRC issued a Severity Level III violation in response to the
        licensee's identification of the existence of incorrect overload
        devices that resulted in the inoperability of four motor operated
        valves utilized in the reactor coolant vent and emergency feedwater
        systems. These incorrect devices were installed in October, 1985
        during the refueling outage as part of implementing a design modi-
        fication installed to address current regulatory issues and plant
        betterment efforts. The licensee assembled a task force to determine
        the root causes of the event and identify corrective actions. The
        root cauce of this event was attributed to the ambiguous description
        contained within the design and procurement documents provided by
        YNSD project engineering personnel, with contributing causes in-
        volving inadequate receipt inspection and insufficient post instal-
        lation testing of the installed equipment. A civil penalty was not
        proposed by the NRC because: 1) licensee identification and prompt
        reporting occurred; 2) the corrective actions were prompt and com-
        prehensive; and 3) good prior performance was evident.
        The prior SALP recommended that the licensee ensure that sufficient
        maintenance engineering resources in the Maintenance Support Depart-
l      ment (MSD) are available with a formalized training program estab-
!
'
        lished for these engineers. This recommendation emanated from NRC
        concerns for the need to assure that complete and timely reviews
        of quality related documentation are performed, and in recognition
        of the important functions served by this resource in maintenance
!      and modification activities. No additional resources, however, have
;
'
        been allocated to the MSD during the assessment period. Currently,
        the formalized training program for attaining, maintaining, and
        upgrading MSD personnel oualifications includes attendance at formal
        schools and seminars.    However, the program does not appear to be
        effectively implemented. The weaknesses regarding receipt inspection
,
1
            -    .                          -              _--  ___ - _. -  --
 
  .
      .
    .
                                                        19
    .
                and post-modification testing of the above event involved both MSD
                engineering and an apparent unfamiliarity with motor control center
                equipment. The licensee's task force assigned to investigate the
                Level III Violation has called for management review of the adequacy
              of resources for implementation of design change modifications. Man-
              agement attention is warranted to complete the MSD review and ad-
              dress recommendations to assure its effectiveness.
              The licensee's preventive maintenance (PM) program has been viewed
              as a licensee strength. Initiating additional PM activity in areas
              exhibited by industry experience, such as feedwater system check
              valves, should be considered.
              In general, the licensee continues to be responsive to NRC initi-
              atives involving maintenance and modifications. Replacement of
              Agastat GP series relays due to service life concerns was imple-
              mented in a timely fashion in safety-related applications in re-
              sponse to IE Information Notice 84-20. Commitments and implemented
              activity by the licensee in areas of NRC concern have involved 10
              CFR 50 Appendix R, post-accident sampling, grid undervoltage pro-
              tection, Systematic Evaluation Program, EQ program, and Generic
              Letter 83-28 modifications. The licensee also completed modifica-
              tions to centainment isolation valves resulting from leak rate
              testing identified deficiencies.
              The program for control of technical manuals, as required by Generic
              Letter 83-28, has been slow in developing. The technical information
              program formalized by the licensee's programmatic procedure has
              neither established the applicability and accuracy of manuals in
              use nor ensured their control. Management attention to fulfill com-
              mitments in this area is warranted.
              Audits performed by the YNSD Quality Audit and Engineering Group
              involving procurement, preventive and corrective maintenance, and
              post-maintenance testing were conducted on a yearly basis, with the
              use of comprehensive checklists noted. Deficiencies and observations
              were documented, with responses reflecting timely and appropriate
              corrective actions. QA/QC involvement in safety related activities
              regarding design change processes and material procurement appears
(            to be adequate. The recently established Quality Control (QC) group's
j            responsibilities include a review of all maintenance requests (MR).
l
'
              However, this QC review is performed prior to detailed planning of
              the work which limits the usefulness of the review. QC inserts hold
              points only for notification prior to the start of the work. During
              the team inspection that reviewed QA/QC effectiveness, it was de-
!            termined that proper documenting of maintenance was not being ac-
              complished, with the QC function observed not to be aggressive in
              identifying tnese deficiencies.
        ..
          .-                      . _ _ _ _ . _ _ _ -    _ .        _        _
 
                                                  I
...  ..
    .
    ,
                                    20
              In response to recurrent fuel failure problems, a task force, which
            was formed to investigate the situation during Cycle XVII operation,
            has developed plans and programs necessary to eliminate future
            failures. Initiatives included: 1) design and implementation of
            baffle spacer plugs to preclude flow-induced fretting from occurring,
            2) use of ultrasonic fuel inspection techniques to replace tradi-
            tional fuel sipping methods to identify failures in second cycle
            fuel bundles, and 3) factoring design features into future fuel to
            strengthen the resistance of the fuel bundles to previously identi-
            fled failure mechanisms. The licensee is currently monitoring Cycle
            XVIII operation indications of cladding failure (which appear to
            be second cycle fuel related) and will be assessing the need for
            additional corrective measures.
            In summary, maintenance and modification activities are observed
            to be implemented in an outstanding manner. The plant, particularly
            avith regard to equipment important to safety, performs with high
            reliability. Forced entries into TS action statements because of
            safety related equipment problems are rare. Proper regard for
            equipment concerns, such as aging, poor performance, or maintain-
            ability, and responsiveness to NRC concerns has been effectively
            demonstrated. The modification-related breakdown associated with
            the installation of incorrect overload devices for four valves was
            determined to be an isolated occurrence that was not representative
            of the normally observed high standard of licensee performance.
            Improvements are needed to: 1) provide more effective integration
            and involvement of QC in routine maintenance activities, 2) provide
            a proper level of documentation for maintenance activities being
            perforced, and 3) address resource and training issues in the MSD.
        2. Conclusion
            Category 1.
        3. Board Recommendation
            None.
 
  .
                                      21
  .
    D. Surveillance (284 hours, 10%)
      1.    Anal: *is
            Surveielance was rated Category 1 during the last SALP. Weaknesses
            in the management control and attention in the chemistry area were
            specific NRC concerns. This issue was resolved during this assess-
            ment period by continued improvements in chemistry department per-
            formance that resulted from strong management involvement at cor-
            porate, plant, and department levels. Further discussion on this
            item is contained in the Radiological Controls functional area. The
            licensee's perceived incompatibility between current steam generator
            in-service inspection sample size and Technical Specification ac-
            ceptance criteria has been the subject of their continued efforts
            in this assessment period, with the development of a Technical
            Specification amendment request nearing completion that should aid
            in resolving the issue.
            During this assessment period, operational and refueling surveil-
            lance activities were reviewed by the resident inspector during
            routine inspections. Two inspe:tions were conducted by region-based
            inspectors in the areas of surveillance testing and calibration con-
            trol program and main coolant syr, tem structural integrity surveil-
            lance requirements. NRC concerns were raised because of the opera-
            tions department failure to conduct meaningful daily required chan-
            nel checks for meteorological monitoring and steam generator blow-
          down radiation monitoring instruments, as well as a failure to im-
          plement a requirement to verify the position of the in-service main
          coolant loop bypass valve (s) while in Mode 3. Two violations were
            issued in response to the observed inadequacies. The licensee is
          conducting a review of surveillance procedures in comparison to the
          Technical Specifications to ensure that appropriate surveillance
          requirements have been addressed and are properly incorporated into
          procedures.
          The QA/QC programs appear to be well-managed in this functional area.
          The Quality Coatrol Group and the Operational Quality Group have
          defined their areas of responsibility and they have actively pur-
          sued an NRC-identified weakness that involved management review of
l          QC inspection reports.
          Management involvement and control in assuring quality was evident.
          Department managers are responsible for the performance of surveil-
          lance activities within their assigned areas. This ensures a high
          level of management involvement by dedicated individuals. When
          Technical Specifications changes occur, the plant superintendent
'
          directs the implementing activity to ensure correct incorporation
          of requirements into the program. Prior planning was consistently
:
 
  y  ,
    .
                                                                      22
    '
                                                                                                                                :
                        evident, records were complete, well-maintained and available. Sur-
                        veillance testing activities are consistently performed according
                        to test procedures.
                        Technical personnel involved with preparing changes to Technical
                        Specification surveillance requirements were fully knowledgeable-
                        of the engineering aspects of what was viewed by the NRC as somewhat
                        unique existing surveillance requirements. The licensee has been
                        aggressive in obtaining an appropriate technical approach to re-
                        solving an examination problem with eddy current inspection of steam
                        generator (SG) tubes. During the routine reviews by the resident
                        and specialist inspectors the licensee's technical staff was found
                        to be well trained and knowledgeable, in almost all cases, of ap-
                        plicable surveillance and testing requirements. Staffing is ample,
                      with training and qualification programs making a positive contri-
                        bution to properly controlled and documented testing activities.
                        Surveillance test results continue to be evaluated in a thorough
                      and accurate manner. In many cases, the maintenance department pro-
                      vides ongoing performance trending of as-found equipment performance.
                      Almost without exception, technically sound and acceptable rEsolu-
                      tions to NRC and licensee-identified concerns are provided by the
                      licensee in a timely manner.
                      The nutter of reportable events for this functional area (four) is
                      not considered to be high. One LER described a missed surveillance
                      test on two containment isolation valves because of failure to in-
                      corporate the testing requirement into an appropriate procedure.
                      Another LER involved an inadequacy in the testing method for a valve
                      that is tested per the IST program. The remaining LERs identifiec
                      equipment inoperabilities due to component failures. In all cases
                      the licensee's corrective action was prompt and effective.
                      Licensee initiatives to identify problems are frequent, and reflect
                      a conservative approach whenever the potential for safety signific-
                      ance exists. Biweekly containment inspections, although not required,
                      are conducted in a thorough manner to provide early detection of
                      potentially adverse conditions involving main coolant system integ-
                      rity and equipment performance. This is of particular significance
                      in light of degraded fuel performance exhibited during this assess-
                      ment period. Equipment failures identified during surveillance
                      testing are aggressively reviewed for root cause, and if situations
                    warrant, thc licensee will increase the frequency of testing or
                      perform additional types of tests to isolate the problem. The lic-
                      ensee consistently performs eddy current testing on more than the
                    minimum number of SG tubes required by Technical Specifications.
                    The licensee continues to exhibit strong overall performance in this
                      functional area. Management attention to resolve identified weak-
                    ness involving operations department surveillances have resulted
                    in a positive trend toward the end of the assessment period. Sur-
,
        , --..,mw.. ..w-...--  , , . . - - - , , - - , - - - - , - . ,    .y, , m . - - . , ,.. , . , . ,._ . - - , , . - . . .
 
              _    _      _ .                    .                  .-.  .
  ..  n
      .
1
      .
                                      23
            veillance testing control and performance trending used by the
            various maintenance departments are considered a significant licen-
            see strength.
          2. Conclusion
            Category 1.
          3. Board Recommendation
            None.
'I
k
i
e
!
r
I
i
',
l
 
  .  ,
    ,
                                                      24
    .
        E.  Fire Protection and Housekeeping (162 hours, 5%)
            1.    Analysis
        .
                  The previous SALP rated fire protection and housekeeping as Cate-
                  gory 1. That SALP identified the need for the licensee to provide
                  continued or additional direct management attention: 1) to encourage
                  and assure adherence to established procedures; 2) to increase first
                  line supervision in the field to direct and control work activities
                  to prevent fires; and 3) to remove non-fire protection duties from
                  the plant fire protection coordinator during refueling and major
                  maintenance outages.
                  During this assessment period, frequent observations of fire pro-
                  tection and housekeeping activities were conducted by the resident
                  inspector, with one region-based inspection performed. The licensee
                  continued to demonstrate its responsiveness to NRC concerns by pro-
                  viding effective, timely corrective actions to previous issues which,
                  with minor exceptions, prevented recurrence of the above concerns
                  during the current assessmant period. The licensee has demonstrated
                  initiative, as well as a strong and effective approach to the
                  resolution of technical issues, by instituting at the inception of
                  the 1985 refueling outage, a fire protection tour at the end of each
                  shift.          The tours, which were conducted by refueling outage co-
                  ordinators or shift supervisors, were designed to identify inade-
                  quacies in the control of combustibles. This was in addition to
                  the observed high level of involvement by the Fire Protection Co-
                  ordinator in the ongoing outage activities.
                  Throughout this assessment period, housekeeping and plant cleanli-
                  ness were maintained at an excellent level. This was the result
                  of aggressive management involvement that was evident in their
                  routine station tours, identification of areas needing attention,
                  and the allocation of resources to both maintain and upgrade the
                  site facilities.          Interdepartmental cooperation on a working level
                  has resulted in a number of previously contaminated areas becoming
                  recovered.
                  Fire brigade training in the area of tactics and hands-on equipment
                  use was viewed by the resident inspector as aggressive and well
                  defined. Backshift brigade drills were routinely conducted by the
                  Fire Protection Coordinator (FPC), with written performance ap-
                  praisal of the drill disseminated to the brigade members. A
                  training weakness in fire protection system knowledge that involves
                  the plant operators was identified on two occasions by the NRC.
                  Minimal involvement of the training department was noted regarding
                  assessment of the overall effectiveness of fire protection systems
                  training. The licensee provided timely resolution of NRC concerns
                  involving the qualification program for fire watch personnel.
:
          .              - - - -    -      - - - .            .-.          -      . , - . - _ -
 
                    ._.
  :o  ,
    ,
                                                                                              25
    .
                          During the current assessment period, an NRC team inspection took
                          place to determine compliance with the 10 CFR 50 Appendix R require-
                          ments with respect to the plant's ability to safely shutdown in the
                          event of a fire. During this inspection, the plant's corporate and
                          site management exhibited aggressiveness to the resolution of fire
                          protection issues. It was evident that priority was given to prob-
                            lems requiring hardware fixes.
                          The licensee made several modifications to achieve compliance with
                          Appendix R separation requirements, and the licensee incorporated
                          several diverse means of achieving a plant safe shutdown in the
                          event of a fire, including a new dedicated Safe Shutdown System.
                          The licensee also had developed adequate procedures, including de-
                          tailed repair procedures for cold shutdown equipment, and had
                          demonstrated competence in the use of these procedures. Good
                          planning and training were evident with respect to these procedures.
                          The inspection team's conclusion was that the licensce's fire pro-
                          tection program is adequate and a major contributing factor is the
                          rapport maintained by the fire protection staff and management and
                          the increased awareness of the plant's personnel of fire protection
                          Concerns.
                          In summary, the fire protection and housekeeping programs continue
                          to receive aggressive management attention, as evidenced by: 1) the
                          implementation of effective and timely corrective actions to arrest
                          the declining trend in the fire protection area at the end of the
                          last SALP period, and 2) the excellent level of housekeeping condi-
                          tions found throughout the facility.                                            This area remains a licensee
                          strength.
                      2. Conclusion
                          Category 1.
                      3. Board Recommendation
                          Licensee: Provide increased involvement by the training department
                                              in fire protection system training.
                          NRC:              None.
t
        . . _ _ _ .        _ _ _ . _ _
                                        _ . . . _ _ _ _ _ _ . _ _ _ . _ _ . _ _ _ . - _ _ _ .    . _ . _ .    _ ,______ , -_. - ,.  -
                                                                                                                                        _ _ - -
 
3    -
  ,
                                                    26
  s
      F. Emergency Preparedness (445 hours, 15%)
          1.      Analysis
                  During the previous assessment period licensee performance in this
                  area was rated as Category 1 (consistent), based upon performance
                  during the annual exercise, and a high degree of management involve-
                  ment in emergency preparedness, as evidenced by training, respon-
                  siveness to identifying and correcting program deficiencies, and
                  in response to actual events.
                  During the current assessment period, one partial-scale exercise
                  and one full-scale exercise were observed, a routine safety inspec-
                  tion specifically related to follow-up of previous deficiancies was            -
                  conducted, and changes to on-site and off-site emergency plans were
                  reviewed. In addition, a new Emergency Operations Facility was com-
                  pleted and fully operational ahead of schedule. Licensee management
                  undertook a rigorous training program, including drills, to ensure
                  all required personnel were familiar with facility operation.
                  For the majority of the assessment period there has not been a per-
                manently assigned site Emergency Preparedness Coordinator (EPC) for
                the Yankee Nuclear Power Station. On-site duties have been performed
                by an individual detailed from the Yankee Atomic Electric Company
                corporate office in Framingham, Massachusetts, for the purpose of
                upgrading emergency planning capabilities. A permanent site Emer-
                gency Preparedness Coordinator was assigned as of August 25, 1986.
                One LER was submitted by the licensee in this area, which involved
                a failure of PORC to review a change to the Emergency Plan. This
                item was identified during an in plant QA audit, with prompt and
                effective corrective actions taken in response to the root cause
                involving a lack of adequate corporate level administrative controls.
                During the partial-scale exercise conducted on May 15, 1985, the
                licensee demonstrated a good emergency response capability. Person-
                nel were generally well-trained and qualified in their emergency
                response roles. Command and control at each emergency response
                facility were effective. Protective action recommendations for the
              general population were accurate. No significant deficiencies were
                identified.
              A review by the resident inspector of a medical emergency drill
              conducted in September 1985 to assess the emergency medical team
              response to on-site medical emergencies, radiation protection con-
              siderations, security requirements, and interfaces with off-site
              support services (i.e., ambulance and hospital) determined that the
            activities reflected a properly planned, executed and audited drill.
            The emergency medical response capability remains a licensee
              strength.
            _ _      _ . _ _ - _ -    . _ _ _ _ - . - - _ . . - -
                                                                    . - -  --    - _ _ . _ . -.
 
          O  *
            .
                                                                                                    27
            e
                                                    During the full-scale exercise conducted on June 11, 1986, the lic-
                                                    ensee demonstrated an adequate emergency response capability. How-
                                                    ever, some significant deficiencies were identified. As the emer-
                                                    gency escalated, turnover of authority was not clear. Protective
                                                    action recommendations made to Vermont and Massachusetts were pri-
                                                    marily based upon dose projection data without consideration of
                                                    potential degradation of plant and core conditions. The licensee's
                                                    post-exercise critique was noted to be somewhat superficial and did
                                                    not cover the significant deficiencies identified by the NRC in-
                                                    spection team. Following clarification of the NRC concerns, more
  ,                                                  aggressive licensee managem?nt attention was focused on issues the
                                                    NRC believed would result in improvement of the licensee's emergency
                                                    response capabilities. However, the above previously mentioned
                                                    deficiencies suggest the need for continued management involvement
                                                    to assure that resolution is provided via the licensee's established
                                                    corrective action plan.
                                            2.      Conclusion
                                                    Category 2.
                                            3.      Board Recommendation
                                                    Nont.
.
                                                                                                                    .----.-.a . -,---_ - -- - - -- - - -.- , - , - . , , .
    ----*e      .. - - - -. , - - - . . - - , , , ,        y - ---, - - - .- - - --.-- ..--- . ~ ,    -,,-.,n ---.
 
a  u
  .
                                      28
  4
      G. Security and Safeguards (154 hours, 5%)
        1.  Analysis
              During the previous SALP period, the licensee's performance in this
              area was Category 2 (improving). An area in need of improvement was
              identified as developing a better understanding of NRC performance
              objectives in the implementation of co:spensatory measures.
              During this assessment period, two rmannounced inspections were
              performed by a region-based inspectcr. Routine resident inspections
              continued throughout the assessment period. No violations were
              identified.
            An NRC Regulatory Effectiveness Review (RER) of the security program
            was conducted on July 28 - August 1,1986. The preliminary findings
            presented to the licensee at the completion of the review included
            weaknesses in barrier features, assessment aids and detection aids
            that required the immediate implementation of compensatory actions
            by the licensee. During the RER followup inspection, a programmatic
            weakness was found in the area of security recordkeeping practices.
            Records were determined not to be readily available or easily re-
            trievable, and were not centrally stored. The majority of the
            weaknesses further derronstrated a continuing need for a better
            understanding of NRC security program objectives by licensee and
            contractor security management. The licensee should have identified
            and corrected many of the deficiencies found by the RER team and
            during' inspections (such as the records problem discussed above).
            While no violations of NRC requirements were identified during this
            assessment period, and several program improvements were implemented
            to respond to NRC-identified weaknesses, there is still room for
            additional improvement.
            The licensee's responses to NRC findings were generally prompt and
            effective. There was evidence of continuing management attention,
            both corporate and plant, to program needs in terms of facility,
            equipment, and program upgrades. While these largely involved the
            expenditure of capital resources, the program upgrades included an
            increase in maintenance support for security equipment and the de-
            velopment and implementation of a more comprehensive audit and sur-
            veillance program. The prior upgrading of some systems, and the
            continuin; in:rease in maintenance support for the systems, have
            resulted in a substantial reduction in the need for compensatory
            measures. However, management attention to overall program effec-
            tiveness was still not tiufficient, as evidenced by the large number
            of access control area door alarms. The licensee has identified the
            necessary long term hardware fixes, but plant management has not
            been aggressive in obtaining plant personnel cooperation in pre-
            cluding the need for security force response to compensate for
            equipment inadequacies.
                                        __ _  _    - _.
 
  .  .
    .
                                            29
    ,
                  The recently developed (June 1985) licensee audit and surveillance
                  program represents a substantial improvement over the previous audit
                  program, in that it focusas on compliance with the licensee's com-
                  mitments contained in the NRC-approved security program plans and
                  the licensee's implementing procedures. Improvements in the detec-
                  tion, identification, and implementation of audit deficiencies was
                  observed by the NRC.    However, the compliance-oriented nature of
                  the audit program places insufficient emphasis on overall improve-
                  ment by not measuring program effectiveness.
                  The licensee submitted three security event reports during the
                  assessment period, in accordance with 10 CFR 73.71. For one event,
                  which involved a loss of certain systems due to a power surge, an
                  amended report was requested (and received) by NRC to understand
                  better the circumstances and impact of the event. Another event,
                which involved servicing systems that had been properly compensated,
                  did not require reporting. The third event involved the loss of a
                  portion of a document that had been categorized as Safeguards In-
                  formation. It 'was later determined that the document was erroneously
                  categorized. While each event was promptly reported, each report
                  indicated deficiencies in licensee management's understanding in
                  regard to the NRC requirements. Enhanced performance by site lic-
                ensee management is required.
                The security contractor has an adequate number of supervisory per-
                sonnel on shift who appear to be well qualified. Staffing of the
                security force appears to be adequate for normal conditions. However,
                the use of overtime was required in August when it became necessary
                to man several compensatory posts unexpectedly. The security force
                was not up to its full complement, and the required working of
                overtime had a noticeably deleterious effect on the existing poor
                morale, caused by extended labor negotiations between the security
                contractor and the force. An NRC inspection at that time found that,
                despite the generally low morale condition, the force remained
                dedicated to its duties and responsibilities. Licensee management
                attention should be directed toward maintaining the force at its
                full complement to avoid complications when unexpected circumstances
                stress the security organization.
l                The training and qualification program for the security force is
i                carried out in accordance with the NRC-approved plan. The program
l                includes on-the-job evaluations of security force members by the
I
                contractor's supervisors and effective feedback to the training
                function. Members of the security force are knowledgeable of their
[
1
                duties and responsibilities and carry them out in a professional
                manner. In response to an NRC recommendation, increased emphasis
                on armed response drills was noted during this assessment period.
!
'
                These training experiences should continue in order to further en-
                hance the capabilities of the security organization.
l
t      ._ __ -.      _
                          .  _.    .        --  -_ - -      -      --- -      -    - - - - -
 
                                                                                              ._                                                _
                                                                                                                                                  q
  .  .
    .
                                                                  30
    ,
                                During the assessment period, the licensee submitted five revisions
                                to security program plans to NRC, under the provisions of 10 CFR
                                50.54(p). Some requested changes reflected a lack of understanding
                                of the provisions of the regulations; however, prompt resolution
                                was provided by the licensee upon NRC identification of unacceptable
                                conditions. Although latter submittals have shown improvement,
                                continued management attention is necessary to provide complete and
                                accurate descriptions and summaries of changes to ensure that there
                                  is no decrease in the effectiveness of previous NRC-approved plans.
                                Although the security program is adequate, program implementation
                                and oversight is compliance oriented. Neither licensee nor security
                                contractor management has demonstrated understanding of program ob-
                                jectives. As a result, program improvements have been minimal and
                                management oversight is not fully effective.
                    2.          Conclusion
J
                                Category 2.
                    3.          Board Recommendation
i                              None.
!
l
l
l
i
;
      - _ . _ - ..  . _ _ _ . .      _ _ _ _ _ _ _ __  _ _ _ _ _ . . ~ _ _ . _ . _ _ _ . _ . _ , _ _ _ . _ _ _ _ _ _ ______ _ _ _ ._ _ _ _ _ _
                                                                                                                    _
 
,
  e  4
    0
                                          31
    ,
        H. Refueling and Outage Management (142 hours, 5%)
          1.  Analysis
                The previot.; SALP rated refueling and outage management as Category
                1, with thir functional area considered to be a notable licensee
                strength.
                During this assessment period, a refueling outage began on October
                19, 1985. Preparations for refueling were reviewed by the resident
                inspector and included outage planning and procedural preparations.
                Post refueling physics testing was the subject of two region-based
                inspections.
                One unscheduled extended maintenance outage occurred between June
                18 and July 1, due to a leak on a steam generator blowdown line and
                the failure of a valve stem on a loop isolation valve. These acti-
                vities were reviewed by the resident inspector.
              Management involvement and control in this functional area continues
                to be a licensee strength. A high level of attention by both senior
              corporate and site management is provided in scheduling, planning,
              and controlling activities associated with plant outages. During
              the current refueling outage, the assistant operations manager (SRO
                licensed) was detailed to act as the refueling outage coordinator.
              A senior control room operator and a reactor engineer were assigned
              to provide back shift coordinator coverage. Proper and detailed
              shift turnovers were observed to occur. The outage planning and
              coordination organization resulted in decision making consister.tiy
              at a level that ensured adequate manapn ent review of activities.
              Daily planning meetings, held twice per day, were effective in co-
              ordinating work accomplished and identifying mechanisms to improve
              schedules.
              Activities related to refueling and outage activities were verified
              to be performed in accordance with approved procedures, with records
              being complete, well maintained and available. The assistant plant
              superintendent continues to be charged with overall outage planning
              responsibility. His high level of dedication, attention to detail,
              and proper concern for adherence to administrative policies place
              a priority on plant and personnel safety. This is a notable
              strength that contributed significantly to the licensee's excellent
              performance in this functional area.
              The license's response to unexpected problems during the outage is
              viewed as a continuing strength. Thoroughness and conservatism,
              with an ongoing attention to safety, characterized the licensee's
              approach to resolving technical issues. Identified oeficiencies in
              controlling work activities resulted in prompt corrective action.
              Problems and issues encountered during the outage were diverse. In
 
                                                                      .      -  .  ,
  a    .
    .
    ,.                                  32
                handling these problems, the inplace corrective action systems
                promptly identified the non-reportable concerns. Plant ir. formation
                reports have been utilized to assess the events with the onsite
                safety committee ensuring appropriate corrective action was identi-
                fled to prevent recurrence. During the refueling, the NRC observed
                that further-licensee action is needed to strengthen procedural
              controls associated with maintenance, surveillance and operational
              activities used to ensure that containment integrity is maintained
              when required.
              Licensee staffing levels were ample to perform the refueling acti-
              vities, with supervisory involvement in field operations evident.
              Augmentation of the station staff with appropriate contractor help
              and assistance from the Yankee Nuclear Service Division staff was
              implemented by the licensee. Effective integration occurred between
              plant and contractor personnel, especially within containment where
              aggressive supervision of contractor radiation protection techni-
              cians was provided. The training and qualification efforts of the
              licensee in preparing and conducting refueling outage activities
              made a positive contribution to the safe conduct of the refueling
              outage. Pre-refueling reviews of guidelines and procedures involving
              normal and abnormal or emergency conditions, with the use of train-
              ing check off sheets, was implemented well in advance of the initi-
              ation of the refueling outage. A general plant safety meeting was
              used to review previous refueling incidents by plant managers to
              prevent recurrence. Personnel errors were minimal, reflecting an
              understanding of the work and adherence to procedures. Effective
              feedback was provided to operating personnel when it was observed
              that nen- fuel could be lifted with only a partial latching of the
              lifting tool. Proper attention to detail and recovery operations
              by the licensed operators controlling the activity is credited with
              preventing the occurrence of a dropped fuel bundle event.
              At the completion of the refueling outage, updated drawings and
              procedures that reflect facility modifications are made available
              to support startup and subsequent plant operations. A Pre-startup
              Training manual was developed and utilized to qualify licensed plant
              operators on the various design changes and modifications made
              during the ref.aling outage.
              In summary, the licensee's performance in this area continues to
              be a noteworthy strength. Active involvement of corporate and site
              managers, with quality performance of personnel involved in outage
i
I
              activities, has resulted in safe and timely completion of outage
              activities.
        2. ' Conclusion
              Category 1.
 
  ,  o
    C
                                33
    .
        3. Board Recommendation
          None.
!
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.  .
  .
                                        34
  ,
      I. Assurance of Quality
        1.    Analysis
              During this assessmer,t period, management involvement and control
              in assuring quality is being considered as a separate functional
              area in addition to being one of the evaluation criteria for the
              other functional areas. Consequently, this discussion is a synopsis
              of the assessments relating to quality work conducted in other areas.
              In addition, the prior assessment period included as a separate area
              the topic of Design Control / Quality Assurance (QA), which was as-
              signed a Category 2 performance rating. The licensee has adequately
              addressed previous NRC concerns which included: 1) adequacy of de-
              sign control and safety evaluation review; 2) evaluation of training
              effectiveness for non-licensed training; and 3) performance of the
              Operations Quality Group (0QG). However, prior NRC concerns with
              the licensee's implementation of their quality control (QC) inspec-
              tion program, did not result in effective corrective measures.
              The emphasis for the performance of quality resides with the indi-
              viduals performing the work activities involved in operating, main-
              taining, and modifying the plant. Licensee management efforts appear
              to be directed towards QA/QC involvement that enhances quality by
              feeding bad VM related observations without removing the primary
              responsibilities of the workers in ensuring quality. To this end,
              the licensee's programs have been very effective in most areas, as
            evidenced by plant and personnel performance factors. Programmatic
            deficiencies have not been identified by the licensee or the NRC
              that have adversely impacted on the safe operation of the plant.
            Performance of onsite and offsite review committees continues to
            be viewed as a licensee strength in performing their assigned func-
            tions. The licensee uses PIRs and LERs as effective corrective
            action systems to address licensee identified deficiencies and aid
              in preventing future loss of quality performance.
            The QC group has been in existence for ten months and consists of
            a supervisor and three inspectors with plans for an additional in-
            spector by 1987. The responsibilities of the QC group include moni-
            toring of various plant maintenance, modification, surveillance,
            administrative and radwaste activities to verify adherence to qual-
            ity assurance requirements. In addition, inspectors occasionally
            accompany equipm nt shipped offsite for repairs to insure quality
            care and work are maintained at the repair facility. The licensee's
            QC group has also established provisions to in:.rease the QC staff
            during outage periods with personnel from the corporate office.
            The QC group has exhibited strong performance in the radwaste ship-
            ping area by providing 100% coverage. Another positive initiative
            was the cross-certification of permanent QC personnel on at least
            two inspection disciplines (most actually have three areas of ex-
            pertise).
 
  e
    O  s
      O
                                      35
      .
            In the previous SALP report the NRC recommended that the licensee
            review the existing quality control inspection program and proce-
            dures to identify areas of disagreement, and formally document and
            implement the desired program with appropriate controls. An opera-
          tionally oriented QA effectiveness team inspection conducted at the
          end of this assessment period found that the corrective action for
          previously identified deficiencies was not effective in some areas.
          The licensee's QC inspection of maintenance and surveillance acti-
          vities was not implemented in accordance with procedures that es-
          tablish requirements, provide acceptance' limits, and include in-
          spection responsibilities. Weaknesses in supervisory reviews for
          quality control inspection reports and establishment of hold points
          were also identified.
          The QA effectiveness team inspection had further findings which are
          indicative of a potential weakness in QA/QC management involvement.
          These included: 1) the lack of management review of all Quality
          Control Inspection Reports (QCIRs); 2) the lack of understanding
          the significance and method of completing the final review section
          of the QCIRs; 3) the excessive delay in revising procedures; 4) the
          failure to identify that inspection procedures were not implemented
          as written; and 5) management's position that the QA program did
          not apply to certain consumables. The findings of the QA team as-
          sessment are not indicative of a programmatic breakdown, but do in-
'
          dicate that more intensive management involvement in this area is
          warranted.
          The audit program is conducted in accordance with the licensee's
          procedure and published schedule. Licensee initiatives to improve
          effectiveness of the program have included: 1) improved offsite
          review committee cognizance of the audits; 2) increased staffing
          and use of plant related expertise for the audits; 3) incorporation
          of audit findings in trending reports; and 4) reports of audit de-
          ficiencies and observations that have gone uncorrected for more the-
          six months, highlight items which require management attention. The
          licensee's station staff has remarked positively about audit program
          improvements, and considers that they are providing a more meaning-
          ful self-evaluation process.
          The licensee's Quality Audit and Engineering Group has been success-
          ful in establishing a program to track, trend and evaluate NRC
          findings, LERs, nonconformance reports, PIRs, audit observations
          and deficiencies, and QA surveillance deficiencies. As of July, 1986,
          QC group inspection deficiencies were incorporated into the Quality
          Assurance Department's Trending program. Semi-annual trending re-
          ports are issued to all levels of licensee management. Other indi-
          cations of related improvements in management involvement and con-
          trol in assuring quality include the following licensee initiatives:
          1) utilization of yearly performance-oriented corporate goals in
i
 
  .        .. .
    .
                                                                              36
    ,
                                            all areas of operations; 2) development and use of plant quarterly
.
                                            performance statistical trends; and 3) comparing industry-wide plant
                                            performance.
                                            To more clearly define the fitness for duty program, the licensee
                                            has issued a revised drug and alcohol policy effective October 1,
                                            1986. This policy incorporates drug and alcohol testing of.all
                                            employees at annual physicals and a strict prohibition against the
                                            sale, use, or possession of drugs or alcohol on licensee property.
                                            Also, licensee employees are not to report for work under the in-
                                            fluence of either drugs or alcohol. The policies also cover both
                                            visitors and contractors requiring unescorted access to the plant
                                            site. In a related matter, the licensee's plant management, super-
                                            visory and senior technical personnel attend fitness for duty and
                                            behavior observation training given by a behavior observation pro-
                                            fessional on a once per year basis.
                                            In summary, management involvement and control in assuring quality
                                            continues to be aggressive in providing the proper level of over-
                                            sight.  On an overall basis, the QA and QC staffs were monitoring
                                            all licensee activities at a high degree of involvement and con-
                                            tinued positive performance trends were generally noted. The fol-
                                            lowup of identified deficiencies exhibited thoroughness as well as
                                            exceeding the frequency required by their program. The trending
                                            analysis is used to identify those areas where performance improve-
                                            ment is needed and as such it is proving to be a valuable management
4
                                            tool. Also, QA audits have gained wider worker acceptance as the
                                            type of auditing technique becomes more meaningful with respect to
                                            the evaluation of quality and performance. The only exception tc
                                            an otherwise exemplary performance is the one inadequate corrective
                                            action associated with the concerns expressed in the previous SALP
'
                                            period. In this area, focused management attention is warranted
                                            in developing and implementing program procedures for the QC in-
                                            spection activities that are responsive to NRC requirements with
                                            respect to proper documentation of inspection activities.
                      2.                    Conclusion
                                            Category 1.
                      3:                    Board Recommendation
                                            None.
.
    --n..,      , . n . . - . - - - - , . -,          - , . , -o -y ,.c - ---    , .--- --a , , . - - - _ - - , . _ . - . - , _ . - . - , - - - - - - -
 
  -
        .
  -.
      _
    ,-
                                                37
            J.  Training and Qualification Effectiveness
                1.      Analysis
                        During this assessment period, Training and Qualification Effective-
                        ness is being considered as a separate functional area for the first
                        time. Training and qualification effectiveness continues to be an
                        evaluation criterion for each functional area.
                        The various aspects of this functional area hate 1een considered
                        and discussed as an integral part of other functional areas and the
                        respective inspection hours have been included in each one. Conse-
                        quently, this discussion is a synopsis of the assessments related
                        to training conducted in other areas. Training effectiveness has
                        been measured primarily by the observed performance of licensee
                        personnel,-and to a lesser degree, as a review of program adequacy.
                        The discussion below addresses three principal areas: licensed
                        operator training, non-licensed staff training, and the status of
                        INPO training accreditation.
                                            '
                                                                                      l
                        In the area of licensed operator training, the licensee maintains
                        a relatively small training staff and relies on^ contractor support
                        to perform a large portion of initial operator instruction, all
                        simulator training and most of the candidate evaluations conducted
                        prior to NRC examinations. The review cf the licensed operator
                        training program detected significant weaknesses that have nega-
                        tively impacted on the ability of the licensee to successfully
                        prepare candidates for NRC examinations. Continued and additional
                        management attention is warranted to provjde corrective measures
                        to: 1) improve training effectiveness upon identification of can-
                      'didate weaknesses during all evaluation phases of the training
                      program, and 2) provide aggressive training department oversight
                        of training programs, including contractor involvement, to insure
                    ,
                      adequate standards of instruction are maintained.
l                        I
!
                      The licensee ha:, taken actions to improve the quality of candidates
                      entering the licensing program and to improve the screening of can-
                      didates during the training program., Candidates will be required
                        to become more involved with plant evolutions as part of their
                      training. An additional licensee initiative involves the implementa-
i                      tion of a new hiring policy that requires a Bachelor riegree in en-
                      gineering or engineering technology for an individual to be eligible
                      for vacant auxiliary operator positions. The first hire under this
                      policy occurred in August, 1986.                                  ,
                                                                                              ,
                      Training material was identified as a training weak' ness in the prior
                      SALP and no significant improvement has been noted during the as-
                      sessment period. Some recently prepared training material has become
                      out-of-date due to plant modifications. The licensee has committed
                      to have a complete and accurate set of training mateffal by March
!
l
I
l
!
          ,    - - _              - - . _ _
                                                        ,    .-
 
                                                                              _ _ .
  ee'  e
      .
      .
                                    38
            1987. The training programs for non-licensed operator, licensed
            operator, and licensed operator requalification received INPO ac-
            creditation in March 1986. Since accreditation is relatively recent,
            no candidates have completed the approved program. However, a lic-
            ensing class entered the accredited program in the summer of 1986
            and will complete the program in April, 1987.
            During this assessment period, non-licensed training proved to be
            effective as evidenced by very few personnel errors. The licensee
            relies heavily on department on-the-job training to establish and
            maintain personnel technical qualification. Notable training and
            qualification effectiveness strengths were: 1) use of department
            managers as GET/Requalification training leaders to cover those
            areas of their expertise; 2) strong performance by plant operators
            in procedural implementation of safe shutdown system use in accord-
            ance with 10 CFR 50 Appendix R; 3) quality control inspector knowl-
          edge of radwaste transportation requirements
          program to familiarize all emergency response;personnel
                                                            and 4) a vigorous
                                                                      in effective
          use of the new E0F.
          Weaknesses in training and qualification effectiveness were identi-
          fled in some areas; e.g., 1) maintenance support engineers' under-
          standing of equipment performance and receipt inspection require-
          ments, as well as ineffective implementation of their training pro-
          grams; 2) inadequate training and its effectiveness assessments for
          fire protection systems knowledge; and, 3) inattentiveness of the
          maintenance staff to completion of documentation requirements of
          MRs, in conjuction with insufficient identification by QC inspectors
          that program requirements were not being met.
          The licensee continues to aggressively pursue the training program
          accreditation with INPO. On October 17, 1986, just subsequent to
          the end of this assessment period, the licensee had submitted and
          INP0 had accepted the Self Evaluation Reports for: maintenance (I&C,
          mechanical, electrical), chemistry, radiation protection, shift
          technical advisor, and technical staff and managers. The INP0 site
          accreditation team visit is scheduled for June,1987.
!
l
;
          In summary, problems persist in preparing personnel for NRC license
'        examinations. The overall program for the candidates as well as the
          quality of training material continues to be marginal. In contrast.
i
'
          the training of licensee personnel to perform a variety of assignec
          responsibilities appears to be very effective. There is a low in-
,
          cidence of personnel errors, few of which could be directly attri-
i
          butable to shortcomings in the training program. A number of lic-
!        ensee initiative > during this assessment period indicated managerial
          interest in various aspects of training at many levels. The short-
          comings in preparing licensed operators for NRC examinations appears
          to be a notable exception to an otherwise effective overall training
          program.
                -.
 
                                                                  .
      --    .
          .
                                                                    39
          ..
                                2.          Conclusions
,'                                          Category 2.
                                3.          Board Recommendation
                                            Licensee:
                                            -
                                                  Closely monitor trainee progress in the licensing program and
                                                  provide for an assessment of the quality of instruction and
                                                  evaluation provided by contractors.
                                            -
                                                  Complete and update training material.
                                                                                                                  ,
,                                            -
  '__        _ , _ , . . , _ _ _ _ _ _ _ _        _  ...    .-        -                                    --
 
  ~  ,
    .
                                          40
        K. Licensing Activities (107 hours, 4%)
            1.  Analysis
                This evaluation represents the combined inputs of the Operating
                Reactor Project Manager, technical reviewers, and the resident in-
                spector.
                During the SALP evaluation period, YAEC continued to show excellent
                management overview in the area of licensing activities. The licen-
                see does not have a formal integrated implementation schedule plan.
                However, the licensee has a system for establishing priorities on
                issues such that both licen:ee and NRC resources are focused on the
                most significant issues. Also, the licensee has a system for co-
                ordinating manpower requirements, equipment procurement and engi-
                neering changes for outage planning. The licensee has been ogen in
                discussing their priorities for both completion of licensing issues
                and for their implementation with NRC and has been receptive to NRC
                comments. The NRC has noted evidence of prior planning, in particu-
                lar, timely submission of the incore detector operability TS pro-
                posed change and also the early submittal of a proposed change to
                the TS relating to the next reload (Spring 1987).
                Licensee management has taken an aggressive role in an effort to
                achieve resolution of long-standing issues such as the SEP reviews.  '
                Upper management involvement in establishing priorities and in
                reaching technical resolution has been evident.
                Early in the reviec perioc, some problems were experienced with
                respect to providing sufficient information to support the no sig-
                nificant hazards considerations determination and, on occasion (such
                as proposed change 192), for the proposed changes themselves. Im-
                provement has been noted in this area over the period.
                The Yankee plant is unique in many aspects and the licensee often
                relies on the long operating experience and simplicity of design
                to justify alternative approaches to resolution. Because of the age
                and size of the plant many generic resolutions of issues are not
                appropriate and thus more work is required by both the NRC and YAEC
                to complete the reviews. In general the licensee has been able to
                satisfy the intent of NRC requirements in plant-specific applica-
                tions. For example, the licensee has installed a safety parameter
                display system (SPDS) which is relatively simple, acceptable to the
                NRC and effectively used by the plant staff.
l              The licensee has developed an approach for resolution of SEP exter-
!              nal event reviews which relies on the recently installed dedicated
l              shutdown capability and on the results of their probabilistic safety
l              study. This approach should result in efficient use of resources
                to obtain maximum safety benefit.
l
l
l.
l
l
l
!
 
            .-_          .                  -                                .
      .
    .
                                  41
    ->
          Clear understanding of the issues and sound technical approaches for
          resolution have been evident in the areas of fire protection, re-
          sponse to GL83-28 concerns (Salem ATWS) and for the many proposed
          changes to the Technical Specifications.
          In the detailed control room design review, the licensee did not
          initially perform a sufficiently detailed function / task analysis
          particularly of instrumentation and control requirements. The lic-
          ensee did not appear to recognize the importance of this analysis
          in.the overall review and was reluctant to implement remedial ac-
          tions. While progress has been made recently through meetings and
          licensee submittals, this aspect is not yet resolved.
          .The issue of bus undervoltage protection has been prolonged. The
          NRC safety evaluations have clearly indicated the staff's position
          regarding testing of both the first and second level of protection.
          The licensee did not resolve the safety issues dealing with the
          first level of protection, even after they were identified by the
          staff. Several rounds of correspondence have occurred and the issue
          is still not settlec.
        A problem regarding adequacy of minimum starting voltages in the
        electrical distribution system for safety-related equipment was
        reported by the licensee some time after this generic issue had been
        originally resolved. One of the underlying reasons for this prciblem
        was an assumption by the YNSD engineering staff regarding pump motor
        rating which had not been adequately verified on site.
        Some of the issues mentioned above originated prior to the rating
        period and may have been complicated by turnover of licensing per-
        sonnel both at YAEC and the NRR organization. However, more atten-
        tion to detail, improved communication within YAEC, and enhanced
        verification activities by the licensee may be appropriate.
        In April, 1985, the licensee implemented a plant level organiza-
        tional change that impacted on existing Technical Specifications.
,
        As of the end of the current assessment period an appropriate lic-
        ensing action has not been submitted. Additionally, as indicated
        in Section G, Security and Safeguards, the licensee has not been
        fully responsive to the prior SALP's concern involving changes sub-
        mitted under Section 10 CFR 50.54 (p). Additional management atten-
        tion in these areas is warranted to prevent future inadequacies from
        developing.
        The licensee continues to respond promptly to NRC staff initiatives.
        During this performance period, the licensee worked with NRC to
        resolve a substantial number of multiplant, TMI and plant specific
        issues. Actions completed included environmental qualification of
        electrical equipment, GL83-28 issues, as well as a large backlog
        of TS changes. In addition, significant progress has been made in
!                                                                                !
                                                                                !
  .              _ _ . ,      __.
 
    w  .
      .
                                      42
    o
              the areas of SPDS, Regulatory Guide 1.97 (Post Accident Monitoring),
  e
              and SEP issues. All issues on fire protection are essentially re-
              solved and implemented.
            The licensee has been cooperative in providing information through
            conference calls, meetings, and submittals. In addition, periodic
            meetings are held between the NRC Project Manager and the YAEC
              licensing representative to discuss licensing issues. Generally,
              issues have been resolved in a timely manner.
            The licensee performs most of their engineering, including the re-
            load analysis, in-house. Staffing levels seem satisfactory for the
            level of work required.
            The analysis of the licensee's reportable events is contained in
            the plant operations section of this report. Only a single event
            (LER 85-01) was identified by the licensee where plant operations
            could have potentially been in deviation with the safety analysis.
            This event involved the identification of a LOCA analysis deficiency
            which was compensated for by the insertion of selected control rods.
            The licensee provided timely resolution of this issue in a technic-
            ally sound and thorough manner that reflects their conservative
            approach whenever the potential for safety significance exists. Re-
            views of licenset responses required by NRC I&E Bulletins have
            improved in response to management attention to previously-identi-
            fled weaknesses in this area.
            In sur. mary, the YAEC organization has performed well in the licens-
            ing area during the report period as evidenced by the large number
            of completed actions. Strong management involvement has been noted;
            however, continued management attention should be focused on the
            areas noted above to maintain the high performance level.
l
          2. Conclusion
            Category 1.
          3. Board Recommendation
l
            None.
i
,
l
 
  ,,
.
                                              43
.
    V.  SUPPORTING DATA AND SUMMARIES
        A.  Investigation and Allegation Review
              There was one allegation during this SALP period. It involved the licen-
              see's policy on use of prescription narcotic medicine by members of the
              contract guardforce while on duty. Currently, the licensee's contracted
              security force has appropriate policies covering the use of prescription
              medicines. No violation of NRC requirements was identified.
        B.    Escalated Enforcement Action
            1.    Civil Penalties
                    There were no civil penalties issued during this assessment period.
            2.    Orders
                  There were no orders involving escalated enforcement action during
                    this assessment period.
            3.    Confirmatory Action Letters
                  There were no confirmatory action letters issued during this as-
                  sessment period.
        C.  Management Conferences
            On July 22, 1986, an enforcement conference was held at the NRC Region
            I office to discuss the installation of undersized trip coils in the
            circuit breakers for motor-operated valves located in the reactor coolant
            system vents and emergency feedwater system.
        D.  Licensee Event Reports
            1.    Tabular Listing
                  Type of Events:
                  A.    Personnel Errors                  11
                  B.    Design / Man./Const./ Install      3
                  C.    External Cause                    0
                  D.    Defective Procedure                2
                  E.    Component Failure                  7
                  X.    Other                              0
                                              Totals      23
                  LERs Reviewed
                  LER No. 85-01 to 86-13
                                                                                        1
                                                                                        l
                                        -
 
                                  44
      2.  Causal Analysis
          The following sets of common mode events were identified;
          a.    LERs 85-02 and 86-11 reported missed or incorrectly performed
                surveillances.
          b.    LERs 85-09, 85-10, 86-04, 86-12, and 86-13 reported a total
              of five reactor trips (two at power and three while in startup).
              Of these, three reactor trips (all while in startup) involved
              personnel error.
          c.  LERs 85-08 and 86-06 involved inoperabilities of steam genera-
              tor blowdown monitors
          d.  LERs 85-04, 85-06, 85-07, 85-08, 86-04. 86-06, and 86-08 are
              events due to component failures.
  E. Operatino Reactors Licensino Actions
    1.  Schedular Extensions Granted
        None.
    2.  Reliefs Granted
        None.
    3.  Fva-" inns Gre.ted
        October 2, 1986 Exemptions to Section III.G of 10 CFR Part 50 Ap-
        pendix R (Fire Protection)
    4.  Orders
        A confirmatory order was issued on July 5,1985, modifying the
        license regarding additional licensee commitments on emergency
        response capability (Supplement 1 to NUREG-0737)
    5.  License Amend ents Issued
        Amendment E3 issued on July 1,1985, Technical Specifications on:
        a) typographical corrections / clarifications, b) removal of references
        to 3 loop operation, c) NUREG-0737 clarification items, d) Inte-
        grated Plant Safety Assessment Report items, and e) Radiological
,
        Effluent TS clarifications.
        Amendment 84 issued on October 1, 1985, Technical Specifications
        on a) pressurizer code safety valve capacity / snubbers, b) degraded
        grid voltage, and c) main coolant vents.
 
o
,
                          45
  Amendment 85 issued on October 31, 1985, Technical Specifications
  on pressurizer safety valve setpoint tolerance.
  Amendment 86 issued on November 8, 1985, Technical Specifications
  on containment isolation surveillance.
  Amendment 87 issued on November 18, 1985, Technical Specifications
  on ECCS surveillance intervals.
  Amendment 88 issued on November 27, 1985, Technical Specifications
  on refueling.
  Amendment 89 issued on November 30, 1985, Technical Specifications
  on degraded grid voltage (second level).
  Amendment 90 issued on December 16, 1985, Technical Specifications
  on ECCS leakage.
  Amendment 91 issued on January 15, 1986, Technical Specifications
  for train coolant system inspections.
  Amendment 92 issued on May 14, 1986, Technical Specifications for
  SIT, steam generator blowdown monitors, etc.
  On May 14, 1986, notice of denial of changes on: 1) isolated loop
  charging, 2) reference to TS 4.0.5, 3) control room ventilation TS,
  4) use of temporary door in airlock, and 5) removal of tritium
  sample requirements.
  Amenament 93 issued on May 20, 1986, Technical Specifications for
  spent fuel pit movements.
  Amendment 94 issued on May 28, 1986, Technical Specifications for
  main steam line low pressure isolation trip.
  Amendment 95 issued on June 5,1986, Technical Specifications for:
  a) containment high range radiation monitors, core exit and vessel
  head thermocouples, containment pressure and water level monitors,
  and b) containment hydrogen monitor.
  Amendment 96 issued on June 9, 1986, Technical Specifications on
  blank flange.
  Amendment 97 issued on June 17, 1986, Technical Specifications on
  containment breathing air system isolation.
  Amendment 98 issued on August 20, 1986, Technical Specifications
  on RETS Reporting Requirements.
  Amendment 99 issued on September 23, 1986, Technical Specifications
  on changes to RETS.
 
  A                                                .
  .
                                          TABLE 1
                      TABULAR LISTING OF LERS BY FUNCTIONAL AREA
                            YANKEE NUCLEAR POWER STATION
                                                          CAUSE CODES *
        Area                                      A  B      C    D    E Total
    A.  Plant Operations                          2  1                2  5
    B. Radiological Controls                      1                        1
    C. Maintenance and Modifications              4  1          1    3  9
    D. Surveillance                              1              1  2    4
    E. Fire Protection and Housekeeping              1                    1
    F. Emergency Preparedness                    1                        1
    G. Security and Safeguards                                            0
    H. Refueling and Outage Management                                    0
    I. Assurance of Quality
    J. Training and Qualification Effectiveness                            0
    K. Licensing Activities                      2    _  _    _    _
                                                                          2
                                  TOTALS:        11  3  0    2    7    23
      *LER Cause Codes (Assignea during NRC review.)
      A - Personnel Error
      B - Design, Manufacturing, Construction, or Installation Error
      C - External
      D - Defective Procedure
l      E'- Equipment Malfunction
!
,
!
 
    .
  1 e. 9 k.'
    6-
                                                TABLE 2
                                    LER SYNOPSIS (2/1/85 - 10/6/86)
                                      YANKEE NUCLEAR POWER STATION
              LER NUMBER  SUMMARY DESCRIPTION
              85-01        Determination of Inappropriate LOCA Methodology Assumption
            -85-02        CS-V-621 Not Tested in Accordance With The ISI Program
              85-03        Fuel Degradation (Assemblies B-696I, B-688 and A-679 In Core Posi-
                          tions ,,-9, H-8, and K-5)
              85-04        Pressurizer Safety Valve PR-SV-181 (S/N BW 07972) Setpoint Greater
                          Than TS
,
              85-05      Switchgear Room Fire Barrier Inadequacy
              85-06      Condensate Pump Trip Circuit Inoperable
              85-07      Nuclear Instrumentation Channels 7 & 8 Low Power Set Points In-
                          operable
              85-08      No. 4 Steam Generator Blowdown Monitor Inoperative
              85-09      Reactor Scram During Startup due to Maintenance Personnel Error.
              85-10      Inadvertent Reactor Scram During Maintenance Activity
              86-01      Technical Specification Violation Concerning the Yankee Emergency
                          Plan
              86-02      Insufficient Implementation Procedures For the Offsite Dose Calcu-
                          lation Manual
4
              86-03      Failure to Comply with a Technical Specification Action Statement
              86-04      Reactor Scram - Loss of Heater Drain Pumps
.            86-05      Dose Equivalent I-131 >1.0 Microcuries Per Gram
                                                                                                    .
              86-06      Inoperable No. 3 Steam Generator Blowdown Monitor
              86-07      480 VAC Busses Cross-Tie Electrical Loading Problem
              86-08      No. 1 Main Coolant Pump Suction Valve Stem Failure
              86-09      Incorrect Overload Devices for Four Motor-0perated Valves
                                                                      ._    -  .-          . -. ,
 
                                        _ _ - _ _ _ - _ _ _ _ _ _ _
  =  M
    i
                                                                    T-2-2
    .
        LER NUMBER          SlM4ARY DESCRIPTION
        86-10                Potential Loss Of Shutdown Cooling
        86-11                Containment Isolation Valves Missed Surveillance
        86-12                Plant Trip on Low SG Level Due to Loss of Control Air
        86-13                Reactor Scram due to Operator Error
l
l
t
t
              . _ _ _ . _ .
 
                          _
  <  -k
    .
    4
                                              TABLE 3
                              INSPECTION HOURS SUMMARY (2/1/85 - 10/6/86)
                                    YANKEE NUCLEAR POWER STATION
                                                              HOURS      % OF TIME
          A.  Plant Operations                              655                  22%
          B.  Radiological Controls                        507                  14%
          C.  Maintenance and Modifications                601                  20%
        D.    Surveillance                                  284                  10%
        E.    Fire Protection and Housekeeping              162                    5%
        F.    Emergency Preparedness                        445                  15%
        G.    Security and Safeguaras                      154                    5%
        H.  Refueling and Outage Management                142                    5%
        I.  Assurance of Quality                            NA                  NA
        J.  Training and Qualification Effectiveness        NA                  NA
        K.  Licensing Activities *                        107                    4%
                                        Total              3057              100%
        * Inspection effort only.
l
t
:
                                                        _ _      __ _      . _ .    _ . - -
 
        - - - - _ _ _ _ _                    _ _ _ _ _ _ _
<  (' k
  .
  6
                                                                    TABLE 4
                                                                                                      ed
                                                              ENFORCEMENT SUMMARY
                                                          YANKEE NUCLEAR POWER STATION
                                                                                Severity Levels
            FUNCTIONAL AREAS                                                  I II III IV V DEV  Total
          A.              Plant Operations                                                1      1
          B.              Radiological Controls
          C.              Maintenance and Modifications                              1          1
          D.              Surveillance                                                        2  2
          E.              Fire Protection and Housekeeping
          F.              Emergency Preparedness
          G.              Security and Safeguards
          H.              Refueling and Outage Management
          I.              Assurance of Quality                                            1      1
          J .'            Training and Qualification Effectiveness
          K.              Licensing Activities
                                                                                      1  2  2  5
                                                _-
 
                                                              ..
        r
      -
    7
    %
.
'-
                                                          TABLE 5
                                                ENFORCEMENT DATA
                                          YANKEE NUCLEAR POWER STATION
          Inspection      Inspection          Severity Functional
          Report No.        Date              Level          Area  Violation
            85-07        3/21-4/26/85          V              D    Failure to establish a
                                                                      written procedure that pre-
-
                                                                      scribes the required quali-
                                                                      tative assessment for in-
                                                                      strumentation channel checks
                                                                      required by the Technical
                                                                      Specifications for meteoro-
                                                                        logical monitoring system.
            86-02      1/7-2/14/86              V              D    Failure to establish a
                                                                      written procedure that prc-
                                                                      scribes the required quali-
                                                                      tative assessment for in-
                                                                      strumentation channel checks
                                                                      required by the Technical
                                                                      Specifications for steam
                                                                      generator blowdown monitors.
            86-08      6/10-10/8/86              IV              A    Failure to maintain at least
                                                                      one main coolant loop bypass
                                                                      valve closed while in Mode
                                                                      3 and failure to conduct
                                                                      a required surveillance test
                                                                      on these valves.
            86-09      6/26-7/2/86              III            C    Installation of undersized
                                                                      trip coils in circuit
                                                                      breakers for motor-operated
                                                                      valves located in the reac-
                                                                      tor coolant system and
                                                                      emergency feedwater system.
  .
            86-17      9/29-10/3/86              IV                H Failure to follow procedures
                                                                      requiring quality control
                                                                      for maintenance activities.
!
                      .- -        -_ ___            . ._        ,_              ._      -
 
  -  g
    6
    i
    u
                                                      TABLE 6
                                  INSPECTION REPORT ACTIVITIES
                                  YANKEE NUCLEAR POWER STATION
        Inspection Inspection                Areas
        Report No.  Hours                  Inspected
          85-04-      110                  Routine Resident
          85-05      160                  Post-Accident Sampling System
          85-06        30                  Startup Physics Testing
          85-07      114                  Routine Resident
          85-08      163                  Emergency Preparedness Exercise
          F5-09        72                  Radiation Protection Prorrr,
'
          85-10        40                  Radiological Environmental Monitoring Program
          85-11      141                  Routine Resident
          85-12      135                  Generic Letter 83-28, Salem-ATWS Concerns
          85-13        34                  Safe Shutdown System Building Construction
          85-14      181                  Routine Resident
          85-15      137                  Routine Resident
          85-16        7.                  Radiation Protection Program
          85-17        31                  Physical Security
          85-18      156                  Routine Resident
          85-19        12                  Licensing Review (on-site) of P.C. 186
          85-20        37                  Maintenance Program
          85-21        27                  Nonradiological Chemistry Program
          85-22        --
                                            Operator Examination
          85-23        74                  Radiation Protection Program
          85-24      126                  Routine Resident
l
f
                ,          . - - - . - - -      -e.    , , . - - - c. < -
                                                                              -,    .  --.. ., - - . , -,,
 
  .
    i    :o
      e
      *f.                                    T-6-2
            Inspection Inspection    Areas
            Report No.    Hours    Inspected
                85-25        135  Appendix R
                86-01        42    Refueling and Startup Testing
              86-02        99    Routine Resident
              86-03        18    Licensed Operator Training Program
              86-04        37    Radioactive Waste Management
              86-05      196      Routine Resident
              86-06        83    Emergency Preparedness Exercise
              66-07        --
                                  Operator Examination
              86-08      200      Routine Resident
              86-09      49      Reactor Coolant System Vents-Special Inspection
              86-10        19    Emergency Preparedness
              86-11      32      Surveillance Testing and Calibration Control Program
              86-12      74      Radiation Protection Program
              86-13      --
                                  Not Used
              86-14      35      Physical Security
              86-15      --
                                  Not Used
              86-16        58      Radiological and Chemical Confirmatory Measurements
,            86-17      124      Operational QA Effectiveness
,
l
                                                              -    _ _ _ .  - _  _ .
                                        .  .  . _ _
 
  r
    t"  'h
      I
      :
      c
                                                              TABLE 7
                                              REACTOR TRIPS AND UNPLANNED SHUTDOWNS
                                                  YANKEE NUCLEAR POWER STATION
                          Power                  Proximate        Root
            Date          Level                    Cause          Cause
            12/9/85      <2%                      Unit Trip        Personnel error        maintenance. Contractor
                                                                    employee inadvertenly bumped an RPS relay
                                                                    while cleaning within the control room's
                                                                    main control board.
            12/28/85      <2%                      Unit Trip        Personnel error - maintenance and opera-
                                                                    tions.        False high startup rate trip caused
                                                                    when maintenance personnel performed a
                                                                    functional test in conjunction with
                                                                    troubleshooting. The root cause was per-
                                                                    sonnel failure to recognize performance
                                                                    of the test while at <15% power will resuit
                                                                    in a plant scram.
            6/1/86        100%                    Unit Trip        Equipment failure - random cause.          Loss
                                                                    of both heater drain pumps resulted in a
                                                                    low steam generator level reactor scram.
                                                                    The pumps were damaged in a lightning storm.
            6/18/86      100%                    Shutdown          Equipment failure - mechanical defect
                                                                    (under review). Shutdown to repair a
                                                                    leaking weld in a coupling on the No. 2
                                                                    steam gerator's blowdown line.
            10/4/86      100%                    Unit Trip        Equipment failure - random cause.          Low
                                                                    control air pressure condition caused by
                                                                    a component failure subsequently resulted
                                                                    in a plant scram on low steam generator
                                                                    levels. A contributing cause was inade-
                                                                    quacies in guidance in a recovery procedure
                                                                    involving feedwater control valve lock-up.
            10/4/86      <2%'                    Unit Trip        Personnel error - operations. Control
                                                                    room operator error resulted in RPS trip
,                                                                  when the non-return valve trip / reset switch
;
'
                                                                    was inadvertantly placed in the trip posi-
                                                                    tion during a plant startup.
;
I
              .    . . , _ - - . _ . . . _ .            ,      _
                                                                        _ _ _ - .            .-
 
(                                                                                                          1
    c:  :o
      *
  I
      :
      c
                                                        FIGURE 1
                                              NUMBER OF DAYS SHUT DOWN
                                            YANKEE NUCLEAR POWER STATION
                              I
            February, 85    l
                              l
            March, 85        l
                              l
            April, 85        l
                              l
            May, 85          l
                              l
            June, 85        l
                              l
            July, 85        l
                            l
            August, 85      l
                            l
            September, 85    l
                            I
            October, 85      I                  i 13 Days Shut Down Cycle XVII-XVIII Refueling Outage
                            i
            November, 85    1 30 Days Shut Down                  l  Cycle XVII-XVIII Refueling Outage
                            i
            December, 85    l              l 9 Days Shut Down        Cycle XVII-XVIII Refueling Outage
                            l
            January, 86    l
                            1
            February, 86    l
                            l
            March, 86      l
                            l
            April, 86      l
                            l
l          May, 86        l
                            1
            June, 86        I                    i 13 Days Shut Down
                          1_
            July, 86      l_I 1 Day Shutdown
                            i
            August, 86      l
                            l
            September, 86 l
                          1_
            October, 86    1_l I Day Shutdown
              .        .,      .    . . .      .        .,                  __  _  -            ._, -
}}

Latest revision as of 17:07, 19 December 2021

SALP Rept 50-029/85-98 for Feb 1985 - Oct 1986
ML20207F622
Person / Time
Site: Yankee Rowe
Issue date: 12/30/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20207F617 List:
References
50-029-85-98, 50-29-85-98, NUDOCS 8701060160
Download: ML20207F622 (57)


See also: IR 05000029/1985098

Text

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ENCLOSURE

SALP BOARD REPORT

U.S. NUCLEAR REGULATORY COMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT 50-29/85-98

YANKEE ATOMIC ELECTRIC COMPANY

YANKEE NUCLEAR POWER STATION

ASSESSMENT PERIOD: FEBRUARY 1, 1985 - OCTOBER 6, 1986

BOARD MEETING DATE: DECEMBER 4, 1986

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8701060160 861230 9

PDR ADOCK 0500

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TABLE OF CONTENTS

PAGE

I. INTR 000CTION......................................................... 1

A. Purpose and 0verview............................................ 1

B. SALP Board Members.............................................. 1

C. Background...................................................... 2

II. CRITERIA............................................................. 6

III. SUMMARY OF RESULTS................................................... 7

A. Facility Performance............................................ 7

B. Overall Facility Evaluation..................................... 8

IV. PERFORMANCE ANALYSIS................................................. 9

A. Plant Operations................................................ 9

B. Radiological Controls........................................... 13

C. Maintenance and Modifications................................... 17

D. Survei11ance.................................................... 21

E. Fire Protection and Housekeeping................................ 24

F. Emergency Preparedness.. ....................................... 26

G. Security and Safeguards................ ........ . ... ... 28

H. Refueling and Outage Management................................. 31

I. Assurance of Quality............................................ 34

J. Training and Qualification Effectiveness........................ 37

K. Licensing Activities............................. ...... . 40

V. SUPPORTING DATA AND SUMMARIES........................................ 43

A. Investigation and Allegation Review............................. 43

B. Escalated Enforcement Action.................................... 43

C. Management Conferences.......................................... 43

D. Licensee Event Reports.......................................... 43

E. Operating Reactors Licensing Actions............................ 44

TABLES

Table 1 - Tabular Listing of LERs by Functional Area

Table 2 - LER Synopsis

Table 3 - Inspection Hours SuTT.sr3

Table 4 - Enforcement Summary

Table 5 - Enforcement Data

Table 6 - Inspection Report Activities

Table 7 - Reactor Trips and Unplanned Shutdowns

FIGURES

Figure 1 - Number of Days Shutdown

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I. INTRODUCTION

A. Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an integrated

NRC staff effort to collect the available observations and data on a peri-

odic basis and to evaluate licensee performance based upon this informa-

tion. SALP is supplemental to normal regulatory processes used to ensure

compliance to NRC rules and regulations. SALP is intended to be suffi-

ciently diagnostic to provide a rational basis for allocating NRC re-

sources and to provide me?.ningful guidance to the licensee's management

to promote quality and safety of plant operation.

The NRC SALP Board, composed of the staff members listed below, met on

December 4, 1986 to review the collection of performance observations

and data to assess license. performance in accordance with guidance in

NRC Manual Chapter 0516, " Systematic Assessment of Licensee Performance."

A summary of the guidance and evaluation criteria is provided in Section

II of this report.

This report is the SALP Board's assessment of the licensee's safety per-

formance at the Yankee Nuclear Power Plant for the period February 1,

1985 through October 6, 1986. It is noted that the summary findings and

totals reflect a 20 month assessment period.

B. SALP Board Members

Board

S. J. Collins, Deputy Director, Division of Reactor Projects (DRP) and

Chairman

  • W. F. Kane, Director, DRP

E. C. Wenzinger, Chief, Projects Branch No. 3, DRP

T. C. Elsasser, Chief, Reactor Projects Section 3C, DRP

H. Eichenholz, Senior Resident Inspector, Yankee Nuclear Power Station

T. T. Martin, Director, Division of Radiation Safety and Safeguards

(DRSS)

Branch, DRSS

i *W. V. Johnston, Deputy Director, Division of Reactor Safety (DRS)

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  • L. H. Bettenhausen, Chief, Operations Branch, DRS

G. E. Lear, Director, PWR Project Directorate No. 1, NRR

E. M. McKenna, Project Manager, PWR Project Directorate No. 1, NRR

Attendees

G. R. Klingler, Reactor Operations Engineer, Office of Inspection and

Enforcement

W. J. Lazarus. Chief, Emergency Preparedness Section, DRSS

M. M. Shanbaky, Chief, Facilities Radiation Protection Section, DRSS

T. F. Dragoun, Senior Radiation Specialist, DRSS

l * Indicates part-time Board members.

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C. Background

1. Licensee Activities

The facility operated at or near full power from February 1, 1985

.until April 26, 1985. On April 27, 1985 a load reduction to 15 MWe

was initiated to repair an extraction steam line leak. A second leak

was discovered and repaired during power ascension on April 29, 1985.

From April 30, 1985 until June 30, 1985 the plant was at essentially

full power, other than periods of minor power restrictions that re-

sulted from increased cooling pond water temperature.

The licensee determined on May 13, 1985 that a control rod movement

restriction was required to comply with Section I.A of Appendix K

to 10 CFR 50.46, that pertained to axial power distribution assump-

tions for the Loss of Coolant Accident analysis. Operation of the

core in a rodded condition (i.e., control rod Group C inserted below

83 inches withdrawn) continued until September 23, 1985, when the

restriction was removed in response to a licensee analysis that

provided an acceptable basis for unrodded core operations. The power

coastdown to the Core XVII-XVIII refueling outage began in August

3, 1985. Two plant milestones involving the 25th anniversary of

initial criticality and exceeding the previous operating record of

289 continuous days of operation occurred on August 19, 1985 and

September 1, 1985, respectively. On September 23, 1985 licensee

protective measures in response to Hurricane Gloria were implemented.

There was no impact on the facility and operations continued.

On October 19, 1985, with the plant in its 336th day of continuous

operation, the facility was shut down until December 10, 1985 for

its scheduled refueling and maintenance outage. Major activities

during the outage included refueling, steam generator tube inspec-

tions, installation of a new solid state reactor protection system,

main generator overhaul, and implementation of Systematic Evaluation

Program modifications (SEP). During the refueling period, the lic-

ensee identified degradation of a total of four fuel rods in three

fuel assemblies. These occurrences were partially attributed to

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baffle spacer flow jetting that induced fretting of the fuel clad-

ding. Higher than normal coolant activity levels resulted during

Cycle XVII operation.

The facility started up from the refueling outage on December 5,

1985, with the plant remaining in Mode 2 to facilitate contractor

work on turbine-related problems. A reactor scram from low power

occurred on December 9, 1985 as a result of a contractor employee

bumping a relay during post modification cleanup in the control room.

The plant achieved Mode 1 operation and was phased to the grid on

December 10, 19S5, but a nitrogen leak in the No. I station service

transformer required that the generator be taken offline for a

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period of time on December 11, 1985. The plant returned to the grid

with power escalation being halted on December 17, 1985 due to ex-

cessive leakage from the No. I heater drain pump. A subsequent

problem with a stuck closed No. 3 turbine control valve limited the

plant to 97% of rated power, which was achieved on December 23, 1985.

A plant shutdown to Mode 2 was initiated on December 28, 1985 for

repair of the No. 3 turbine control valve, with an unplanned auto-

matic scram occurring from a false high startup rate condition re-

sulting from maintenance being performed on the nuclear instrumen-

tation system. A failure of the No. 3 boiler feedwater pump (BFP)

and motor occurred while plant operators were preparing to return

the plant to operation from Mode 2 on December 29, 1985. The plant

returned to the grid on December 30, 1985 and, while undergoing a

reactor power increase, the main coolant Dose Equivalent Iodine

(DEI) level reached 74% of the Technical Specification (TS) limit.

Operator actions resulted in reduction of DEI levels to approxi-

mately 5% of the TS limit. Following the return to operation of the

failed BFP on January 4, 1986, the plant achieved full power on

January 7, 1986 and remained at that level until January 25, 1986.

On this date, a planned load reduction to 65% of rated power oc-

curred for repairs to the No. 2 heater drain pump due to excess

packing leakage and turbine valve testing. The plant returned to

full power on January 26, 1986.

The facility operated at or near full power from January 26, 1986

until the end of the assessment period on October 6, 1986, with the

exception of the following load reductions or outages. On January

31, 1986 an unplanned load reduction to 76% of rated power occurred

due to a leaking pump seal on the No. 3 BFP; a planned reduction

to 70% of rated power occurred on March 22, 1986 to perform main-

tenance on the Nos. 1 and 3 BFPs and turbine valve testing; and an

emergency load reduction to 78% of rated power was initiated by

plant operators when a loss of cooling water to th* generator hydro-

! gen cooler occurred. A low steam generator level automatic scram

occurred on June 1, 1986 due to a loss of both heater drain pumps

during a severe lightning storm. An unplanned load reduction to 75%

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' of rated power occurred cn June 13, 1986 in response to a leak in

l tne packing gland of the No. 1 BFP. The licensee proceeded to cold

shutdown on June 18, 1986 for an outage to effect repairs to a

leaking weld in a coupling located in containment on the No. 2 steam

generator's blowdown line.

, During this outage that lasted until July 1, 1986, the licensee

l identified the following anomalous conditions: 1) a main coolant

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hot leg isolation valve (MC-MOV-325) was found to have a failed

valve stem, and 2) four valves in the reactor coolant vent and

emergency feedwater systems had incorrect overload trip coils in-

stalled in their respective power supply circuit breakers. Also

, during this outage a valving error by a plant auxiliary operator

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resulted in the potential for a loss of shutdown cooling and severe

damage of the main coolant pump internals. A planned load reduction

to 50% of rated power occurred on September 20, 1986 to perform

maintenance on BFPs, to conduct condenser tube leak checks, and to

conduct turbine control valve testing. On October 4,1986 a low

control cir pressure condition occurred that subsequently resulted

in a reactor automatic scram on low steam generator levels. During

the plant startup later the same day, an operator error resulted

in a reactor automatic scram occurring when a main steam line non-

return valve trip / reset switch was inadvertently placed in the trip

position. The plant was at 75% of rated power at the end of the

assessment period on October 6, 1986.

During this assessment period the plant availability factor was 88%.

2. Inspection Activities

One NRC resident inspector was assigned to the site during the en-

tire assessment period. The total NRC resident and region-based in-

spection hours for this 20 month assessment period was 3057 hours0.0354 days <br />0.849 hours <br />0.00505 weeks <br />0.00116 months <br />

(1,834 hours0.00965 days <br />0.232 hours <br />0.00138 weeks <br />3.17337e-4 months <br /> on an annual basis) with a distribution in the ap-

praisal functional areas as shown in Table 3.

The resident inspector conducted one event-related special inspec-

tion that involved the review of the circumstances and licensee

corrective actions related to the discovery of inoperable motor

operated valves in the reactor coolant vent and emergency feedwater

systens.

During the period, NRC team inspections were conducted of the fol-

lowing areas:

a. Implementation of various items required by NUREG 0737 includ-

ing post-accident sampling and monitoring capabilities.

b. Evaluation of the annual emergency preparedness exercises con-

ducted May 15, 1985 and June 11, 1986.

c. Licensee's action to address the concerns identified in NRC

Generic Letter 83-28, in the areas of Equiprent Classification,

Post-Maintenance Testing, and Vendor Interface.

d. Compliance with 10 CFR 50, Appendix R safe shutdown capability.

e. An operational QA effectiveness inspection.

In this period five violations, including one Severity Level III,

were issued. Tabulations of Violations and Inspection Activities

are presented in Tables 5 and 6, respectively.

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This report also assessed " Training and Qualification Effectiveness"

and " Assurance of Quality" as separate functional areas. Although these

topics, in themselves, are assessed in the other functional areas through

their use as avaluation criteria, the two areas provide a synopsis. For

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example, quality assurance effectiveness has been assessed on a day-to-

day basis by the resident inspector and as an integral aspect of special-

ist inspections. Although quality work is the responsibility of every

employee, one of the management tools to measure this effectiveness is

reliance on quality assurance inspections and audits. Other major factors

that influence quality, such as involvement of first-line supervision,

safety committees, and worker attitudes, are discussed in each functional

area.

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II. CRITERIA

Licensee performance is assessed in selected functional areas. Each functional

area represents areas significant to nuclear safety and the environment, and

are normal programmatic areas. The following evaluation criteria were used

as appropriate to assess each functional area.

1. Management involvement and control in assuring quality.

2. Approach to resolution of technical issues from a safety standpoint.

3. Responsiveness to NRC initiatives.

4. Enforcement history.

5. Reporting and analysis of reportable events.

6. Staffing (including management).

7. Training effectiveness and qualification.

However, the SALP Board is not limited to these criteria and others may have

been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is clas-

sified into one of three performance categories. The definitions of these

performance categories are:

Category 1: Reduced NRC attention may be approprinte. Licensee management

attention and involvement are aggressive and oriented toward nuclear sz %ty;

licensee resources are ample and effectively used such that a high level of

performance with respect te operational safety is being achieved.

Category 2: NRC attention should be maintained at normal levels. Licensee

management attention anc involvement are evident and concerned with nuclear

safety; licensee resources are adequate and reasonably effective such that

satisfactory performance with respect to operational safety is being achieved.

Category 3: Both NRC and licensee attention should be increased. Licensee

management attention or involvement is acceptable and considers nuclear safety,

but weaknesses are evident; licensee resources appear strained or not effec-

tively used such that minimal satisfactory performance with respect to opera-

tional safety is being achieved.

The SALP trend categories are as follows.

Ircroving: Licensee performance has generally improved over the last part of

the SALF assessment period.

Declinino: Licensee performance has generally declined over the last part of

the SALP assessment period.

A trend is assigned only when, in the opinion of the SALP Board, the trend

is significant enough to be considered a precursor to a change in performance

category in the near future.

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III. SUPMARY OF RESULTS

A. Facility Performance

Last Period This Period

(11/1/83 - (2/1/85 -

Functional Area 1/31/85) 10/6/86) Trend

A. Plant Operations 1 1

B. Radiological Controls 2 1

C. Maintenance and Modifications 1 1

D. Surveillance 1 1

E. Fire Protection and Housekeeping 1 1

F. Emergency Preparedness 1 2

G. Security and Safeguards 2 2

H. Refueling and Outage Management 1 1

1. Assurance of Quality 2# 1

J. Training and Qualification

Effectiveness ## 2

K. Licensing Activities 1 1

  1. Previously assessed as Design Control / Quality Assurance
    1. Not Previously addressed as separate area

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B. Overall Facility Evaluation

Our assessment confirms your strong orientation towards plant safety,

technical strength, and staff experience which are considered

licensee attributes. Additionally, we acknowledge your initiatives

to address plant aging concerns and to increase the oversight and

effectiveness of your quality programs.

Management attention has resulted in your continued high level of

performance in eight of the eleven rated functional areas, as

illustrated by your successful initiatives to upgrade performance in

the Radiological Controls area. Our evaluation indicates that this

aggressive approach and high level of management involvement have not

been evident ~in the oversight of the security program, the effective-

ness of the licensed operator training program, and recent implemen-

tation of emergency plan actions.

As a result of this assessment, NRC activities in Category 1 functional

areas are eligible for reduced inspection effort. We will consider your

high level of performance and initiatives to address identified short-

comings in our prioritization of the inspection program for your

facility.

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IV. PERFORMANCE ANALYSIS

A. Plant Operations (655 hours0.00758 days <br />0.182 hours <br />0.00108 weeks <br />2.492275e-4 months <br />, 22%)

1. Analysis

The previous SALP rated plant operations as Category 1, with a con-

clusion that the licensee continued to demonstrate a strong and

effective commitment to safety in this area.

This functional area includes plant operations as well as opera-

tional support activities. During the current SALP period, there

was one region-based inspection of this area. Plant operations were

observed by the resident inspector throughout the period.

Plant operators and licensee management response to plant events

and conditions have generally demonstrated a strong and effective

approach to resolution of technical issues. The team effort, which

includes Yankee Nuclear Services Division (YNSD) project and engi-

neering personnel, demonstrates a clear understanding of the issues,

and exhibits a conservative, technically sound approach to safety

issues. Abnormal events during which these characteristics were

demonstrated included: 1) plant operations with degraded fuel clad-

ding, 2) the identification of a LOCA analysis deficiency, and

3) the discovery of an electrical loading problem. Plant staff

corrective actions were noted as aggressive in resolving the opera-

tional concerns. However, the YNSD Projects staff has at times de-

layed identification of impending operational problems, which has

resulted in unnecessary reactive conditions being imposed upon the

operating organization. A notable example of this was compensatory

measures required during 480V A-C bus cross-tie operations while

the plant was in a startup and shutdown condition. Management at-

tention to improve YNSD Projects response timeliness is warranted.

The general performance of the operations department reflects a

commitment to quality operation as evidenced by few personnel

errors and a low reactor scram (trip) rate of 0.15 scrams per 1000

critical hours while at power. This scram rate is significantly

belc,w the national average of about one per 1000 critical hours.

Consistent evidence of prior planning and assignment of priorities

were apparent. When personnel errors occur they are isolated in-

stances that are not reflective of a programmatic breakdown. The

performance level of plant operators during routine and transient

plant operations reflects a conscientious attitude and concern for

plant safety. However, one event involving the opening of all four

main coolant loop bypass valves by the operators in an attempt to

mitigate decreasing main coolant temperature was a deviation from

their normally conservative manner in which they respond to opera-

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tional problems. Although their actions were contrary to Technical

Specifications (TS), an NRC-requested safety evaluation demonstrated

that the event was of minimal safety significance.

Continued improvement in licensed operator knowledge of equipment

status has been evident. Events involving failure to document equip-

ment malfunctions and failure to initiate corrective maintenance

have been essentially eliminated due to responsive management at-

tention to the prior SALP concerns in this area. Increased on-line.

maintenance to assess the consequences of off-normal indications

is occurring.

The licensee maintains a professional atmosphere in the control room

by prohibiting radios, television, and unrelated reading material,

which tends to minimize disruptive activities. In response to NRC-

initiatives, the licensee has developed formal administrative means

i for 1) effectively limiting control room access, and 2) specifying

expected conduct and performance policies for operational personnel.

A noted licensee strength is the nearly " blackboard" status for

control room overhead annunciators that is routinely maintained.

The licensee has established well-stated administrative controls ,

to provide notification and event reporting as required by 10 CFR

50.72 and 50.73. Licensec Event Reports (LERs) are, in general, pre-

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perly identified, analyzed, and reported in a timely manner. The .

NRC review of the licensee's LERs determined that they were of

above-average quality. Prior SALP concerns involving incorrect and

insufficient information in LERs have not recurred. The licensee

utilizes Flent Information Reports (PIRs) for addressinc non report-

able concerns. Quality is evident in the areas of causal analysis

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and corrective actions; however, report issuance timeliness rou-

tinely exceeds the licensee's established administrative controls.

The overall good quality of LERs is attributable to the increased

involvement and thorough reviews conducted by the Plant Operations

Review Committee (PORC) and management. Numerous meetings of the

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PORC were observed by the resident inspector, with proper question-

ing attitudes consistently observed that resulted in active and

probing discussions on items of concern and plant events. However,

, the PORC meeting minutes tend to lack an adequate level of detaii

to reflect the details of the discussions that occur. Station man-

agement instituted training for the PORC members to improve their

sensitivity to responsibilities associated with procedural matters

and 10 CFR 50.59 evaluation adequacy.

Some of the initiatives undertaken in this assessment period by the

i Nuclear Safety Audit and Review Committee include 1) ensuring that

safety evaluations are performed in an adequate manner, and 2) im-

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proving committee-cognizance over the In-Plant Audit Program by

having members participate or monitor at least one audit to provide

a better understanding of the program.

A January 1986 NRC review of the licensee's initial operator lic-

ensing program found the administrative control systems to be ade-

quate. However, the training program and its administrative con-

trol systems have not effectively prepared large classes of candi-

dates to operate the facility as demonstrated by the low success

rate on NRC licensing examinations. During this assessment period

one class of operator candidates consisting of four reactor opera-

tors (R0s) and tnree senior reactor cperators (SR0s) were trained

to operate the facility, but only three of the candidates (43%)

were issued operating licenses.

Presently, station staffing is adequate. A five-shift rotation

schedule is used. Early in the assessment period the licensee as-

signed a spare shift supervisor and a senior control room operator

to facilitate operational flexibility. However, the current number

of licensed reactor operators requires reliance on overtime, at a

level that is presently in compliance with NRC requirements, to meet

watchstanding needs. The current class for R0 and SR0 licenses is

cocprised of five and three candidates, respectively. It appears

that even if all of the licensee's candidates are fully successful,

the overall depth of licensed operator staffing levels may not sig-

nificantly change because of the potential for attrition of current

operators.

The use of Special Orders in lieu of approved procedures was a prior

SALP concern. Recurrence of this issue has been identified in this

assessment period, which suggests insufficient management attention.

A plant procedures programmatic inspection, with specific emphasis

placed on plant operations, was conducted. This review, in conjunc-

tion with routine observations, identified issues that involve:

1) difficulties in determining that independent verification for

certain systems has been performed, 2) the need to increase the

emphasis on attention to detail as part of the procedure review

program, and 3) the need to insure that procedures are developed

for all planned operations. Over-reliance on special orders and

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'

weaknesses in procedural content may be due to the demands placed

on the operations department support staff that is currently being

relied upon to perform this important function, as that staff at

times appears to be taxed by a heavy workload.

During this assessment period, the licensee accomplished notable

milestones related to plant performance that involved reaching the

25th anniversary of initial criticality, the setting of a new plant

continuous operation record of 336 days without a shutdown, and

maintaining the olant in an on-line status for 539 out of the 613

days contained within the period. This represents a plant availa-

l

I

, - - -. -. --

.

_

.

.

12 *

.

bility of 88 percent and is significantly above the national average

of 69 percent. These accomplishments are indicative of the operat-

ing and support staff's overall quality performance.

2. Conclusion

Category 1.

3. Board Recommendation

None.

. .

.

13

.

8. Radiological Controls (507 hours0.00587 days <br />0.141 hours <br />8.382936e-4 weeks <br />1.929135e-4 months <br />, 14%)

1. Analysis

In the previous SALP report the licensee's performance in Chemistry

and Radiological Controls was rated as Category 2. Weaknesses were

identified in the areas of staff development, oversight of radwaste,

control of work in radiation areas, recordkeeping, and respiratory

protection programs. Three minor violations were cited. SALP Board

recommendations were made regarding: 1) supervisory staffing,

2) staff development, 3) self evaluation, and 4) radiological pro-

cedure review and compliance.

During this SALP period, region-based radiation specialists conducted

seven inspections in the following areas: radiation protection (3);

environmental monitoring (1); radiological chemistry (1); non-radio-

logical chemistry (1); and waste management (1). The resident in-

spector also reviewed selected program areas. No violations were

identified.

Site and corporate management directed a high level of attention

and resources towards resolving Radiological Protection (RP) program

weakness during this period. Substantial progress was made in the

area cf self-identification and resolution of problems. Management

has revised existing policies and established new policies that

firmly support a conservative approach to radiation protection. For

example, the Radiological Work Policy requires all personnel to

comply with all RP requirements and delineates disciplinary action

for noncompliance.

A major project was undertaken to replace the outdated RP procedures

by using assistance from the corporate technical staff with input

and review by the small highly experienced site staff. This re-

sulted in clear, well written draft RP procedures. Management de-

cided to enhance this effort by id ng en innovative approach of two

tiers of procedures - one simplified ievel for use by plant workers

with the second level providing detailed instructions for the radi-

ation department staff. This project is nearly complete.

Ir;wovements in planning were noted during this period. The ALARA

reviews for all dose intensive Design Change Request work was com-

pleted prior to the start of the refueling outage. An infrequent

spent resin shipment was thoroughly preplanned and controlled re-

sulting in minimal personnel exposure and no site contamination.

Additionally, the impact of temporary changes to the radiologically

controlled area boundary was minimized through good planning.

Records are complete and well-maintained for routine radiation sur-

veys, routine chemistry surveillance, radioactive liquid waste pro-

cessing, radiological environmental monitoring and meteorological

, .

.

14

,

monitoring. A large main frame computer and record keeping system

dedicated to RP and chemistry has recently been installed on site

that will enhance recordkeeping capabilities.

The licensee routinely exhibits technical thoroughness in the resolu-

tion of radiation safety issues. A new on-site QC function was estab-

lished to oversee all phases of radwaste processing and radioactive

materials shipments. The QC personnel were specifically trained and

qualified for this dJty. Personnel exiting the radiological control

area on site are required to self-frisk, use an automatic hand and

foot monitor, and then pass through a sensitive portal monitor exit.

This multistep process provides a high degree of radioactive con-

tamination control. The Environmental Lab has conducted exhaustive

technical studies of the behavior characteristics of the Harshaw

TLD system used for personnel dosimetry. This approach results in

a high confidence in the reported personnel exposures.

Responsiveness to NRC initiatives in almost all cases has been timely,

technically sound and thorough. Previous NRC concerns regarding RP

department staffing levels and lines of authority have been resolved.

The need for procedural compliance was addressed by strong management

disciplinary action with contractor and permanent site personnel.

The RP prooram was understaffed and lacking experience at the begin-

ning of this period due to loss of the radiation protection manager

and two of four supervisory personnel. The impact of this loss of

key personnel from this small staff was aggravated by the lack of

a staff development program and cross-training of supervisors. A

systematic program was implemented to correct this situation, and

by the midpoint of this assessment period, all positions had been

refilled. New job descriptions with clearly assigned primary and

backup responsibilities were promulgated and a staff development

program was put in place. In addition, a permanent supervisory posi-

tion was added to coordinate various program improvements that are

uncerway and planned for the future such as the expanded use of com-

puters. The increased staff size and depth resolve the concerns

stated in the previous SALP.

A defined but informal training program is provided to RP supervisors

and technicians, which makes a positive contribution to understand-

ing of the work as evidenced by adherence to procedures with few

personnel errors. A policy change now permits only fully ANSI quali-

fied RP technicians to implement the RP program. The trainee posi-

tion called " tester" was abolished in a licensee initiative to

strengthen the technician performance level. The qualification pro-

gram for radwaste QC inspectors made a positive contribution to the

inspection activities and adherence to procedures.

The licensee has improved its chemistry and radiochemistry programs.

The licensee has a strong program to insure compliance with Techni-

cal Specification requirements for inplant and effluent sampling

._-

__ .

. .

.

, 15

and analysis. In particular, the licensee has paid particular atten-

tion to meeting its Radiological Environmental Technical Specifica-

tions (RETS), which were effectively implemented during this assess-

ment period. The review of the licensee's implementation of the RETS

indicated that procedures for control and monitoring of effluents

were very effectively stated and thoroughly carried out.

Initiatives to improve management oversight and to improve labora-

tory instrumentation and chemistry facilities were implemented. A

surveillance matrix, which is reviewed by two levels of management,

tracks the required sampling of radioactive and non-radioactive sys-

tems. However, for the nonradioactive systems that have a potential

for an unmonitored, unplanned release, there are no action statements

to provide guidance, if a priori criteria are exceeded. This is a

minor discrepancy associated with an otherwise excellent program.

Procedures for gaseous and liquid effluent controls and offsite dose

calculations are generally implemented properly. However, an un-

planned, unauthorized gasecus release occurred subsequent to purging

of a main coolant icop when the activated charcoal filter failed

to retain the gaseous iodine. Management took aggressive actions

to prevent a similar release including: lowering the alarm setpoint,

replacing the charcoal, and periodically determining the removal

efficiency for the charcoal. A timely and technically sound resolu-

tion to this issue was implemented. Previously, periodic in place

testing of charcoal filters had not been performed with the excep-

tion of the Control Room Emergency Ventilation System. Although not

required by Technical Specifications, such testing is considered

standard industry practice.

Procedures for chemistry surveillances have been implemented and

analyses performed as required. Technical Specifications require

analysis of main coolant and gaseous effluents following a 15 per-

cent per hour power change. The operators are aware of this require-

ment, and normally take action to insure compliance. However, in

one instance, the analyses were performed but results were not re-

ported to the control room. The licensee implemented a timely re-

sponse to this concern, including issuance of a written instruction

l to chemistry technicians to report these results to the control roo~

!

and revision to procedures to indicate appropriate notification

requirements. This is another indication of increased management

attention to the follow up and correction of identified problerts.

The licensee improved its chemistry staffing and qualification pro-

I gram during this assessment. This was demonstrated by documentation

of on-the-job training and retraining of chemistry personnel, in-

creased staff, and clearly defined position descriptions to address

major responsibilities. A number of these improvements were in re-

i sponse to industry and NRC initiatives. However, on its own initi-

l

ative, the licensee recognized the need and initiated action, to

develop managerial depth within the chemistry department.

. .

.

16

.

The licensee's ability to accurately measure radioactivity in ef-

fluents was confirmed by intercomparisons with the NRC using the

NRC Mobile Radiological Measurements Laboratory.

Weaknesses in the nonradiological chemistry program, identified dur-

ing the previous assessment period, included lack of a measurement

control program, lack of a retraining program for chemistry techni-

cians, and an unreliable and insensitive method for determination

of chloride in water. A new Chemistry Department Manager was assigned

to the facility in August 1984. During the current assessment period,

it was noted that significant improvements have been made. These

include: the use of control charts for chemical analyses, testing

of technicians by requiring them to analyze samples containing un-

knowns, and an improvement in laboratory facilities through the pur-

chase of new equipment that will provide for greater reliability

and sensitivity.

The licensee maintains well-stated, controlled and explicit proce-

dures for control of radiological environmental monitoring program

(REMP) activities and for the calibration of meteorological moni-

toring instrumentation. Records of REMP and meteorological monitor-

ing were complete, well-maintained and available. Procedures are

consistently followed. REMP sainpling stations were located as stated

by procedure, required sampling frequencies were met, and equipment

was calibrated as required. Positions and responsibilities are well-

defined for management of the REMP. Calibrations of meteorological

monitoring instruments are performed more frequently than required,

and reviewed calibration data have been satisfactory.

During the last SALP, the NRC made several recommendations in this

functional area to aid improvement in licensee performance. These

recommendations, promptly implemented by the licensee, were a blue-

print to improve radiological controls performance from consistently

average to exceptional. By the midpoin'. of the assessment period,

all recommendations had been fully implemented. This resulted in

a continuous improvement in licensee performance throughout the as-

sessment period. In the latter part of the period, the licensee also

implemented additional programmatic improvements on their own initi-

ative which even further improved performance in this functional

area. Significant programmatic improvement, coupled with a lack of

deficiencies and consistently strong performance in all associated

activitiu , indicates a strong licensee commitment to achieve and

sustain a high level of performance in this diverse functional area.

2. Conclusion

Category 1.

3. Board Recommendation

None.

.. __

. .

.

17

.

C. Maintenance and Modifications (601 hours0.00696 days <br />0.167 hours <br />9.937169e-4 weeks <br />2.286805e-4 months <br />, 20%)

1. Analysis

The previous SALP rated the licensee's performance as Category 1.

Positive findings were made in the areas of management involvement,

plant reliability, improved analysis of maintenance related events,

training and qualification, responsiveness to NRC initiatives, and

prioritization of safety-related maintenance. The licensee continues

to demonstrate responsiveness to NRC concerns in this functional

area by providing effective, timely corrective actions which pre-

vented recurrence of 10 CFR 50.59 and technical specification re-

lated problems in performing jumper and lifted lead activities.

During the current SALP period maintenance and modification activi-

ties were reviewed in four region-based inspections. The resident

inspector also examined activities in this functional area as part

of the routine inspection program.

The maintenance program inspections conducted during this period

identified no programmatic deficiencies and detected no trends of

maintenance problems. Active licensee management involvement in

the maintenance program is evident on all levels, with maintenance

-

practices being conducive to early detection of developing equiprent

problems In the process of planning maintenance work, the foreman

automatically reviews the maintenance history cards for the item

being repaired, thus detecting any developing trends. The mainten-

ance department, instrument and control department, and maintenance

support department continue to be staffed by experienced, qualified

craft and supervisory personnel. The attitude that maintenance per-

sonnel exhibit, and the generally good housekeeping conditions in-

volved while performing their work, are indications of good main-

tenance attitudes and practices.

The licensee is in the process of increasing the training program

effectiveness for I&C, mechanical and electrical maintenance per-

sonnel, as part of obtaining INPO accreditation. Training and quali-

fication of maintenance personnel is a noted strength, as evidenced

by the few personnel errors that occur.

The licensee continues to demonstrate concern for plant reliability

and safety. Appropriate equipment upgrading is being considered and

implemented for systems and components proving to be difficult to

maintain either due to age, inadequate performance or unavailability

of spare parts. A ten year plan, reviewed annually and updated or

modified as needed, was developed to identify these licensee con-

cerns. The licensee's initiative in this regard was evidenced by

the installation of a new solid state Reactor Protection Systerr and

the replacement or addition of core exit and reactor head thermo-

couples.

.-. - . _ _ _

. .

.

.

18

During this assessment period, the licensee performed some difficult

maintenance work. A main coolant pump suction valve stem failure

was identified during an unplanned maintenance outage that occurred

to perform repairs for a leak in a steam generator (SG) blowdown

line. The NRC viewed the licensee's corrective actions in response

to the stem failure as being representative of a conservative,

technically sound and thorough approach to resolving conditions

where the potential for adverse safety conditions exist.

Nine LER's were submitted in this functional area. A review of the

event details indicates that the corrective action implemented by

the maintenance organization was effective in that recurrent events

were not prevalent. No adverse trends were identified that would

contribute to equipment unavailability or improper performance as

a result of maintenance activities. The licensee's event analyses,

using PIRs, provided thorough reviews involving the PORC, and de-

scribed proper corrective actions to prevent the recurrence of non-

reportable events.

.

The NRC issued a Severity Level III violation in response to the

licensee's identification of the existence of incorrect overload

devices that resulted in the inoperability of four motor operated

valves utilized in the reactor coolant vent and emergency feedwater

systems. These incorrect devices were installed in October, 1985

during the refueling outage as part of implementing a design modi-

fication installed to address current regulatory issues and plant

betterment efforts. The licensee assembled a task force to determine

the root causes of the event and identify corrective actions. The

root cauce of this event was attributed to the ambiguous description

contained within the design and procurement documents provided by

YNSD project engineering personnel, with contributing causes in-

volving inadequate receipt inspection and insufficient post instal-

lation testing of the installed equipment. A civil penalty was not

proposed by the NRC because: 1) licensee identification and prompt

reporting occurred; 2) the corrective actions were prompt and com-

prehensive; and 3) good prior performance was evident.

The prior SALP recommended that the licensee ensure that sufficient

maintenance engineering resources in the Maintenance Support Depart-

l ment (MSD) are available with a formalized training program estab-

!

'

lished for these engineers. This recommendation emanated from NRC

concerns for the need to assure that complete and timely reviews

of quality related documentation are performed, and in recognition

of the important functions served by this resource in maintenance

! and modification activities. No additional resources, however, have

'

been allocated to the MSD during the assessment period. Currently,

the formalized training program for attaining, maintaining, and

upgrading MSD personnel oualifications includes attendance at formal

schools and seminars. However, the program does not appear to be

effectively implemented. The weaknesses regarding receipt inspection

,

1

- . - _-- ___ - _. - --

.

.

.

19

.

and post-modification testing of the above event involved both MSD

engineering and an apparent unfamiliarity with motor control center

equipment. The licensee's task force assigned to investigate the

Level III Violation has called for management review of the adequacy

of resources for implementation of design change modifications. Man-

agement attention is warranted to complete the MSD review and ad-

dress recommendations to assure its effectiveness.

The licensee's preventive maintenance (PM) program has been viewed

as a licensee strength. Initiating additional PM activity in areas

exhibited by industry experience, such as feedwater system check

valves, should be considered.

In general, the licensee continues to be responsive to NRC initi-

atives involving maintenance and modifications. Replacement of

Agastat GP series relays due to service life concerns was imple-

mented in a timely fashion in safety-related applications in re-

sponse to IE Information Notice 84-20. Commitments and implemented

activity by the licensee in areas of NRC concern have involved 10

CFR 50 Appendix R, post-accident sampling, grid undervoltage pro-

tection, Systematic Evaluation Program, EQ program, and Generic

Letter 83-28 modifications. The licensee also completed modifica-

tions to centainment isolation valves resulting from leak rate

testing identified deficiencies.

The program for control of technical manuals, as required by Generic

Letter 83-28, has been slow in developing. The technical information

program formalized by the licensee's programmatic procedure has

neither established the applicability and accuracy of manuals in

use nor ensured their control. Management attention to fulfill com-

mitments in this area is warranted.

Audits performed by the YNSD Quality Audit and Engineering Group

involving procurement, preventive and corrective maintenance, and

post-maintenance testing were conducted on a yearly basis, with the

use of comprehensive checklists noted. Deficiencies and observations

were documented, with responses reflecting timely and appropriate

corrective actions. QA/QC involvement in safety related activities

regarding design change processes and material procurement appears

( to be adequate. The recently established Quality Control (QC) group's

j responsibilities include a review of all maintenance requests (MR).

l

'

However, this QC review is performed prior to detailed planning of

the work which limits the usefulness of the review. QC inserts hold

points only for notification prior to the start of the work. During

the team inspection that reviewed QA/QC effectiveness, it was de-

! termined that proper documenting of maintenance was not being ac-

complished, with the QC function observed not to be aggressive in

identifying tnese deficiencies.

..

.- . _ _ _ _ . _ _ _ - _ . _ _

I

... ..

.

,

20

In response to recurrent fuel failure problems, a task force, which

was formed to investigate the situation during Cycle XVII operation,

has developed plans and programs necessary to eliminate future

failures. Initiatives included: 1) design and implementation of

baffle spacer plugs to preclude flow-induced fretting from occurring,

2) use of ultrasonic fuel inspection techniques to replace tradi-

tional fuel sipping methods to identify failures in second cycle

fuel bundles, and 3) factoring design features into future fuel to

strengthen the resistance of the fuel bundles to previously identi-

fled failure mechanisms. The licensee is currently monitoring Cycle

XVIII operation indications of cladding failure (which appear to

be second cycle fuel related) and will be assessing the need for

additional corrective measures.

In summary, maintenance and modification activities are observed

to be implemented in an outstanding manner. The plant, particularly

avith regard to equipment important to safety, performs with high

reliability. Forced entries into TS action statements because of

safety related equipment problems are rare. Proper regard for

equipment concerns, such as aging, poor performance, or maintain-

ability, and responsiveness to NRC concerns has been effectively

demonstrated. The modification-related breakdown associated with

the installation of incorrect overload devices for four valves was

determined to be an isolated occurrence that was not representative

of the normally observed high standard of licensee performance.

Improvements are needed to: 1) provide more effective integration

and involvement of QC in routine maintenance activities, 2) provide

a proper level of documentation for maintenance activities being

perforced, and 3) address resource and training issues in the MSD.

2. Conclusion

Category 1.

3. Board Recommendation

None.

.

21

.

D. Surveillance (284 hours0.00329 days <br />0.0789 hours <br />4.695767e-4 weeks <br />1.08062e-4 months <br />, 10%)

1. Anal: *is

Surveielance was rated Category 1 during the last SALP. Weaknesses

in the management control and attention in the chemistry area were

specific NRC concerns. This issue was resolved during this assess-

ment period by continued improvements in chemistry department per-

formance that resulted from strong management involvement at cor-

porate, plant, and department levels. Further discussion on this

item is contained in the Radiological Controls functional area. The

licensee's perceived incompatibility between current steam generator

in-service inspection sample size and Technical Specification ac-

ceptance criteria has been the subject of their continued efforts

in this assessment period, with the development of a Technical

Specification amendment request nearing completion that should aid

in resolving the issue.

During this assessment period, operational and refueling surveil-

lance activities were reviewed by the resident inspector during

routine inspections. Two inspe:tions were conducted by region-based

inspectors in the areas of surveillance testing and calibration con-

trol program and main coolant syr, tem structural integrity surveil-

lance requirements. NRC concerns were raised because of the opera-

tions department failure to conduct meaningful daily required chan-

nel checks for meteorological monitoring and steam generator blow-

down radiation monitoring instruments, as well as a failure to im-

plement a requirement to verify the position of the in-service main

coolant loop bypass valve (s) while in Mode 3. Two violations were

issued in response to the observed inadequacies. The licensee is

conducting a review of surveillance procedures in comparison to the

Technical Specifications to ensure that appropriate surveillance

requirements have been addressed and are properly incorporated into

procedures.

The QA/QC programs appear to be well-managed in this functional area.

The Quality Coatrol Group and the Operational Quality Group have

defined their areas of responsibility and they have actively pur-

sued an NRC-identified weakness that involved management review of

l QC inspection reports.

Management involvement and control in assuring quality was evident.

Department managers are responsible for the performance of surveil-

lance activities within their assigned areas. This ensures a high

level of management involvement by dedicated individuals. When

Technical Specifications changes occur, the plant superintendent

'

directs the implementing activity to ensure correct incorporation

of requirements into the program. Prior planning was consistently

y ,

.

22

'

evident, records were complete, well-maintained and available. Sur-

veillance testing activities are consistently performed according

to test procedures.

Technical personnel involved with preparing changes to Technical

Specification surveillance requirements were fully knowledgeable-

of the engineering aspects of what was viewed by the NRC as somewhat

unique existing surveillance requirements. The licensee has been

aggressive in obtaining an appropriate technical approach to re-

solving an examination problem with eddy current inspection of steam

generator (SG) tubes. During the routine reviews by the resident

and specialist inspectors the licensee's technical staff was found

to be well trained and knowledgeable, in almost all cases, of ap-

plicable surveillance and testing requirements. Staffing is ample,

with training and qualification programs making a positive contri-

bution to properly controlled and documented testing activities.

Surveillance test results continue to be evaluated in a thorough

and accurate manner. In many cases, the maintenance department pro-

vides ongoing performance trending of as-found equipment performance.

Almost without exception, technically sound and acceptable rEsolu-

tions to NRC and licensee-identified concerns are provided by the

licensee in a timely manner.

The nutter of reportable events for this functional area (four) is

not considered to be high. One LER described a missed surveillance

test on two containment isolation valves because of failure to in-

corporate the testing requirement into an appropriate procedure.

Another LER involved an inadequacy in the testing method for a valve

that is tested per the IST program. The remaining LERs identifiec

equipment inoperabilities due to component failures. In all cases

the licensee's corrective action was prompt and effective.

Licensee initiatives to identify problems are frequent, and reflect

a conservative approach whenever the potential for safety signific-

ance exists. Biweekly containment inspections, although not required,

are conducted in a thorough manner to provide early detection of

potentially adverse conditions involving main coolant system integ-

rity and equipment performance. This is of particular significance

in light of degraded fuel performance exhibited during this assess-

ment period. Equipment failures identified during surveillance

testing are aggressively reviewed for root cause, and if situations

warrant, thc licensee will increase the frequency of testing or

perform additional types of tests to isolate the problem. The lic-

ensee consistently performs eddy current testing on more than the

minimum number of SG tubes required by Technical Specifications.

The licensee continues to exhibit strong overall performance in this

functional area. Management attention to resolve identified weak-

ness involving operations department surveillances have resulted

in a positive trend toward the end of the assessment period. Sur-

,

, --..,mw.. ..w-...-- , , . . - - - , , - - , - - - - , - . , .y, , m . - - . , ,.. , . , . ,._ . - - , , . - . . .

_ _ _ . . .-. .

.. n

.

1

.

23

veillance testing control and performance trending used by the

various maintenance departments are considered a significant licen-

see strength.

2. Conclusion

Category 1.

3. Board Recommendation

None.

'I

k

i

e

!

r

I

i

',

l

. ,

,

24

.

E. Fire Protection and Housekeeping (162 hours0.00188 days <br />0.045 hours <br />2.678571e-4 weeks <br />6.1641e-5 months <br />, 5%)

1. Analysis

.

The previous SALP rated fire protection and housekeeping as Cate-

gory 1. That SALP identified the need for the licensee to provide

continued or additional direct management attention: 1) to encourage

and assure adherence to established procedures; 2) to increase first

line supervision in the field to direct and control work activities

to prevent fires; and 3) to remove non-fire protection duties from

the plant fire protection coordinator during refueling and major

maintenance outages.

During this assessment period, frequent observations of fire pro-

tection and housekeeping activities were conducted by the resident

inspector, with one region-based inspection performed. The licensee

continued to demonstrate its responsiveness to NRC concerns by pro-

viding effective, timely corrective actions to previous issues which,

with minor exceptions, prevented recurrence of the above concerns

during the current assessmant period. The licensee has demonstrated

initiative, as well as a strong and effective approach to the

resolution of technical issues, by instituting at the inception of

the 1985 refueling outage, a fire protection tour at the end of each

shift. The tours, which were conducted by refueling outage co-

ordinators or shift supervisors, were designed to identify inade-

quacies in the control of combustibles. This was in addition to

the observed high level of involvement by the Fire Protection Co-

ordinator in the ongoing outage activities.

Throughout this assessment period, housekeeping and plant cleanli-

ness were maintained at an excellent level. This was the result

of aggressive management involvement that was evident in their

routine station tours, identification of areas needing attention,

and the allocation of resources to both maintain and upgrade the

site facilities. Interdepartmental cooperation on a working level

has resulted in a number of previously contaminated areas becoming

recovered.

Fire brigade training in the area of tactics and hands-on equipment

use was viewed by the resident inspector as aggressive and well

defined. Backshift brigade drills were routinely conducted by the

Fire Protection Coordinator (FPC), with written performance ap-

praisal of the drill disseminated to the brigade members. A

training weakness in fire protection system knowledge that involves

the plant operators was identified on two occasions by the NRC.

Minimal involvement of the training department was noted regarding

assessment of the overall effectiveness of fire protection systems

training. The licensee provided timely resolution of NRC concerns

involving the qualification program for fire watch personnel.

. - - - - - - - - . .-. - . , - . - _ -

._.

o ,

,

25

.

During the current assessment period, an NRC team inspection took

place to determine compliance with the 10 CFR 50 Appendix R require-

ments with respect to the plant's ability to safely shutdown in the

event of a fire. During this inspection, the plant's corporate and

site management exhibited aggressiveness to the resolution of fire

protection issues. It was evident that priority was given to prob-

lems requiring hardware fixes.

The licensee made several modifications to achieve compliance with

Appendix R separation requirements, and the licensee incorporated

several diverse means of achieving a plant safe shutdown in the

event of a fire, including a new dedicated Safe Shutdown System.

The licensee also had developed adequate procedures, including de-

tailed repair procedures for cold shutdown equipment, and had

demonstrated competence in the use of these procedures. Good

planning and training were evident with respect to these procedures.

The inspection team's conclusion was that the licensce's fire pro-

tection program is adequate and a major contributing factor is the

rapport maintained by the fire protection staff and management and

the increased awareness of the plant's personnel of fire protection

Concerns.

In summary, the fire protection and housekeeping programs continue

to receive aggressive management attention, as evidenced by: 1) the

implementation of effective and timely corrective actions to arrest

the declining trend in the fire protection area at the end of the

last SALP period, and 2) the excellent level of housekeeping condi-

tions found throughout the facility. This area remains a licensee

strength.

2. Conclusion

Category 1.

3. Board Recommendation

Licensee: Provide increased involvement by the training department

in fire protection system training.

NRC: None.

t

. . _ _ _ . _ _ _ . _ _

_ . . . _ _ _ _ _ _ . _ _ _ . _ _ . _ _ _ . - _ _ _ . . _ . _ . _ ,______ , -_. - ,. -

_ _ - -

3 -

,

26

s

F. Emergency Preparedness (445 hours0.00515 days <br />0.124 hours <br />7.357804e-4 weeks <br />1.693225e-4 months <br />, 15%)

1. Analysis

During the previous assessment period licensee performance in this

area was rated as Category 1 (consistent), based upon performance

during the annual exercise, and a high degree of management involve-

ment in emergency preparedness, as evidenced by training, respon-

siveness to identifying and correcting program deficiencies, and

in response to actual events.

During the current assessment period, one partial-scale exercise

and one full-scale exercise were observed, a routine safety inspec-

tion specifically related to follow-up of previous deficiancies was -

conducted, and changes to on-site and off-site emergency plans were

reviewed. In addition, a new Emergency Operations Facility was com-

pleted and fully operational ahead of schedule. Licensee management

undertook a rigorous training program, including drills, to ensure

all required personnel were familiar with facility operation.

For the majority of the assessment period there has not been a per-

manently assigned site Emergency Preparedness Coordinator (EPC) for

the Yankee Nuclear Power Station. On-site duties have been performed

by an individual detailed from the Yankee Atomic Electric Company

corporate office in Framingham, Massachusetts, for the purpose of

upgrading emergency planning capabilities. A permanent site Emer-

gency Preparedness Coordinator was assigned as of August 25, 1986.

One LER was submitted by the licensee in this area, which involved

a failure of PORC to review a change to the Emergency Plan. This

item was identified during an in plant QA audit, with prompt and

effective corrective actions taken in response to the root cause

involving a lack of adequate corporate level administrative controls.

During the partial-scale exercise conducted on May 15, 1985, the

licensee demonstrated a good emergency response capability. Person-

nel were generally well-trained and qualified in their emergency

response roles. Command and control at each emergency response

facility were effective. Protective action recommendations for the

general population were accurate. No significant deficiencies were

identified.

A review by the resident inspector of a medical emergency drill

conducted in September 1985 to assess the emergency medical team

response to on-site medical emergencies, radiation protection con-

siderations, security requirements, and interfaces with off-site

support services (i.e., ambulance and hospital) determined that the

activities reflected a properly planned, executed and audited drill.

The emergency medical response capability remains a licensee

strength.

_ _ _ . _ _ - _ - . _ _ _ _ - . - - _ . . - -

. - - -- - _ _ . _ . -.

O *

.

27

e

During the full-scale exercise conducted on June 11, 1986, the lic-

ensee demonstrated an adequate emergency response capability. How-

ever, some significant deficiencies were identified. As the emer-

gency escalated, turnover of authority was not clear. Protective

action recommendations made to Vermont and Massachusetts were pri-

marily based upon dose projection data without consideration of

potential degradation of plant and core conditions. The licensee's

post-exercise critique was noted to be somewhat superficial and did

not cover the significant deficiencies identified by the NRC in-

spection team. Following clarification of the NRC concerns, more

, aggressive licensee managem?nt attention was focused on issues the

NRC believed would result in improvement of the licensee's emergency

response capabilities. However, the above previously mentioned

deficiencies suggest the need for continued management involvement

to assure that resolution is provided via the licensee's established

corrective action plan.

2. Conclusion

Category 2.

3. Board Recommendation

Nont.

.

.----.-.a . -,---_ - -- - - -- - - -.- , - , - . , , .


*e .. - - - -. , - - - . . - - , , , , y - ---, - - - .- - - --.-- ..--- . ~ , -,,-.,n ---.

a u

.

28

4

G. Security and Safeguards (154 hours0.00178 days <br />0.0428 hours <br />2.546296e-4 weeks <br />5.8597e-5 months <br />, 5%)

1. Analysis

During the previous SALP period, the licensee's performance in this

area was Category 2 (improving). An area in need of improvement was

identified as developing a better understanding of NRC performance

objectives in the implementation of co:spensatory measures.

During this assessment period, two rmannounced inspections were

performed by a region-based inspectcr. Routine resident inspections

continued throughout the assessment period. No violations were

identified.

An NRC Regulatory Effectiveness Review (RER) of the security program

was conducted on July 28 - August 1,1986. The preliminary findings

presented to the licensee at the completion of the review included

weaknesses in barrier features, assessment aids and detection aids

that required the immediate implementation of compensatory actions

by the licensee. During the RER followup inspection, a programmatic

weakness was found in the area of security recordkeeping practices.

Records were determined not to be readily available or easily re-

trievable, and were not centrally stored. The majority of the

weaknesses further derronstrated a continuing need for a better

understanding of NRC security program objectives by licensee and

contractor security management. The licensee should have identified

and corrected many of the deficiencies found by the RER team and

during' inspections (such as the records problem discussed above).

While no violations of NRC requirements were identified during this

assessment period, and several program improvements were implemented

to respond to NRC-identified weaknesses, there is still room for

additional improvement.

The licensee's responses to NRC findings were generally prompt and

effective. There was evidence of continuing management attention,

both corporate and plant, to program needs in terms of facility,

equipment, and program upgrades. While these largely involved the

expenditure of capital resources, the program upgrades included an

increase in maintenance support for security equipment and the de-

velopment and implementation of a more comprehensive audit and sur-

veillance program. The prior upgrading of some systems, and the

continuin; in:rease in maintenance support for the systems, have

resulted in a substantial reduction in the need for compensatory

measures. However, management attention to overall program effec-

tiveness was still not tiufficient, as evidenced by the large number

of access control area door alarms. The licensee has identified the

necessary long term hardware fixes, but plant management has not

been aggressive in obtaining plant personnel cooperation in pre-

cluding the need for security force response to compensate for

equipment inadequacies.

__ _ _ - _.

. .

.

29

,

The recently developed (June 1985) licensee audit and surveillance

program represents a substantial improvement over the previous audit

program, in that it focusas on compliance with the licensee's com-

mitments contained in the NRC-approved security program plans and

the licensee's implementing procedures. Improvements in the detec-

tion, identification, and implementation of audit deficiencies was

observed by the NRC. However, the compliance-oriented nature of

the audit program places insufficient emphasis on overall improve-

ment by not measuring program effectiveness.

The licensee submitted three security event reports during the

assessment period, in accordance with 10 CFR 73.71. For one event,

which involved a loss of certain systems due to a power surge, an

amended report was requested (and received) by NRC to understand

better the circumstances and impact of the event. Another event,

which involved servicing systems that had been properly compensated,

did not require reporting. The third event involved the loss of a

portion of a document that had been categorized as Safeguards In-

formation. It 'was later determined that the document was erroneously

categorized. While each event was promptly reported, each report

indicated deficiencies in licensee management's understanding in

regard to the NRC requirements. Enhanced performance by site lic-

ensee management is required.

The security contractor has an adequate number of supervisory per-

sonnel on shift who appear to be well qualified. Staffing of the

security force appears to be adequate for normal conditions. However,

the use of overtime was required in August when it became necessary

to man several compensatory posts unexpectedly. The security force

was not up to its full complement, and the required working of

overtime had a noticeably deleterious effect on the existing poor

morale, caused by extended labor negotiations between the security

contractor and the force. An NRC inspection at that time found that,

despite the generally low morale condition, the force remained

dedicated to its duties and responsibilities. Licensee management

attention should be directed toward maintaining the force at its

full complement to avoid complications when unexpected circumstances

stress the security organization.

l The training and qualification program for the security force is

i carried out in accordance with the NRC-approved plan. The program

l includes on-the-job evaluations of security force members by the

I

contractor's supervisors and effective feedback to the training

function. Members of the security force are knowledgeable of their

[

1

duties and responsibilities and carry them out in a professional

manner. In response to an NRC recommendation, increased emphasis

on armed response drills was noted during this assessment period.

!

'

These training experiences should continue in order to further en-

hance the capabilities of the security organization.

l

t ._ __ -. _

. _. . -- -_ - - - --- - - - - - - -

._ _

q

. .

.

30

,

During the assessment period, the licensee submitted five revisions

to security program plans to NRC, under the provisions of 10 CFR

50.54(p). Some requested changes reflected a lack of understanding

of the provisions of the regulations; however, prompt resolution

was provided by the licensee upon NRC identification of unacceptable

conditions. Although latter submittals have shown improvement,

continued management attention is necessary to provide complete and

accurate descriptions and summaries of changes to ensure that there

is no decrease in the effectiveness of previous NRC-approved plans.

Although the security program is adequate, program implementation

and oversight is compliance oriented. Neither licensee nor security

contractor management has demonstrated understanding of program ob-

jectives. As a result, program improvements have been minimal and

management oversight is not fully effective.

2. Conclusion

J

Category 2.

3. Board Recommendation

i None.

!

l

l

l

i

- _ . _ - .. . _ _ _ . . _ _ _ _ _ _ _ __ _ _ _ _ _ . . ~ _ _ . _ . _ _ _ . _ . _ , _ _ _ . _ _ _ _ _ _ ______ _ _ _ ._ _ _ _ _ _

_

,

e 4

0

31

,

H. Refueling and Outage Management (142 hours0.00164 days <br />0.0394 hours <br />2.347884e-4 weeks <br />5.4031e-5 months <br />, 5%)

1. Analysis

The previot.; SALP rated refueling and outage management as Category

1, with thir functional area considered to be a notable licensee

strength.

During this assessment period, a refueling outage began on October

19, 1985. Preparations for refueling were reviewed by the resident

inspector and included outage planning and procedural preparations.

Post refueling physics testing was the subject of two region-based

inspections.

One unscheduled extended maintenance outage occurred between June

18 and July 1, due to a leak on a steam generator blowdown line and

the failure of a valve stem on a loop isolation valve. These acti-

vities were reviewed by the resident inspector.

Management involvement and control in this functional area continues

to be a licensee strength. A high level of attention by both senior

corporate and site management is provided in scheduling, planning,

and controlling activities associated with plant outages. During

the current refueling outage, the assistant operations manager (SRO

licensed) was detailed to act as the refueling outage coordinator.

A senior control room operator and a reactor engineer were assigned

to provide back shift coordinator coverage. Proper and detailed

shift turnovers were observed to occur. The outage planning and

coordination organization resulted in decision making consister.tiy

at a level that ensured adequate manapn ent review of activities.

Daily planning meetings, held twice per day, were effective in co-

ordinating work accomplished and identifying mechanisms to improve

schedules.

Activities related to refueling and outage activities were verified

to be performed in accordance with approved procedures, with records

being complete, well maintained and available. The assistant plant

superintendent continues to be charged with overall outage planning

responsibility. His high level of dedication, attention to detail,

and proper concern for adherence to administrative policies place

a priority on plant and personnel safety. This is a notable

strength that contributed significantly to the licensee's excellent

performance in this functional area.

The license's response to unexpected problems during the outage is

viewed as a continuing strength. Thoroughness and conservatism,

with an ongoing attention to safety, characterized the licensee's

approach to resolving technical issues. Identified oeficiencies in

controlling work activities resulted in prompt corrective action.

Problems and issues encountered during the outage were diverse. In

. - . ,

a .

.

,. 32

handling these problems, the inplace corrective action systems

promptly identified the non-reportable concerns. Plant ir. formation

reports have been utilized to assess the events with the onsite

safety committee ensuring appropriate corrective action was identi-

fled to prevent recurrence. During the refueling, the NRC observed

that further-licensee action is needed to strengthen procedural

controls associated with maintenance, surveillance and operational

activities used to ensure that containment integrity is maintained

when required.

Licensee staffing levels were ample to perform the refueling acti-

vities, with supervisory involvement in field operations evident.

Augmentation of the station staff with appropriate contractor help

and assistance from the Yankee Nuclear Service Division staff was

implemented by the licensee. Effective integration occurred between

plant and contractor personnel, especially within containment where

aggressive supervision of contractor radiation protection techni-

cians was provided. The training and qualification efforts of the

licensee in preparing and conducting refueling outage activities

made a positive contribution to the safe conduct of the refueling

outage. Pre-refueling reviews of guidelines and procedures involving

normal and abnormal or emergency conditions, with the use of train-

ing check off sheets, was implemented well in advance of the initi-

ation of the refueling outage. A general plant safety meeting was

used to review previous refueling incidents by plant managers to

prevent recurrence. Personnel errors were minimal, reflecting an

understanding of the work and adherence to procedures. Effective

feedback was provided to operating personnel when it was observed

that nen- fuel could be lifted with only a partial latching of the

lifting tool. Proper attention to detail and recovery operations

by the licensed operators controlling the activity is credited with

preventing the occurrence of a dropped fuel bundle event.

At the completion of the refueling outage, updated drawings and

procedures that reflect facility modifications are made available

to support startup and subsequent plant operations. A Pre-startup

Training manual was developed and utilized to qualify licensed plant

operators on the various design changes and modifications made

during the ref.aling outage.

In summary, the licensee's performance in this area continues to

be a noteworthy strength. Active involvement of corporate and site

managers, with quality performance of personnel involved in outage

i

I

activities, has resulted in safe and timely completion of outage

activities.

2. ' Conclusion

Category 1.

, o

C

33

.

3. Board Recommendation

None.

!

i

l

l

l

r

!

. .

.

34

,

I. Assurance of Quality

1. Analysis

During this assessmer,t period, management involvement and control

in assuring quality is being considered as a separate functional

area in addition to being one of the evaluation criteria for the

other functional areas. Consequently, this discussion is a synopsis

of the assessments relating to quality work conducted in other areas.

In addition, the prior assessment period included as a separate area

the topic of Design Control / Quality Assurance (QA), which was as-

signed a Category 2 performance rating. The licensee has adequately

addressed previous NRC concerns which included: 1) adequacy of de-

sign control and safety evaluation review; 2) evaluation of training

effectiveness for non-licensed training; and 3) performance of the

Operations Quality Group (0QG). However, prior NRC concerns with

the licensee's implementation of their quality control (QC) inspec-

tion program, did not result in effective corrective measures.

The emphasis for the performance of quality resides with the indi-

viduals performing the work activities involved in operating, main-

taining, and modifying the plant. Licensee management efforts appear

to be directed towards QA/QC involvement that enhances quality by

feeding bad VM related observations without removing the primary

responsibilities of the workers in ensuring quality. To this end,

the licensee's programs have been very effective in most areas, as

evidenced by plant and personnel performance factors. Programmatic

deficiencies have not been identified by the licensee or the NRC

that have adversely impacted on the safe operation of the plant.

Performance of onsite and offsite review committees continues to

be viewed as a licensee strength in performing their assigned func-

tions. The licensee uses PIRs and LERs as effective corrective

action systems to address licensee identified deficiencies and aid

in preventing future loss of quality performance.

The QC group has been in existence for ten months and consists of

a supervisor and three inspectors with plans for an additional in-

spector by 1987. The responsibilities of the QC group include moni-

toring of various plant maintenance, modification, surveillance,

administrative and radwaste activities to verify adherence to qual-

ity assurance requirements. In addition, inspectors occasionally

accompany equipm nt shipped offsite for repairs to insure quality

care and work are maintained at the repair facility. The licensee's

QC group has also established provisions to in:.rease the QC staff

during outage periods with personnel from the corporate office.

The QC group has exhibited strong performance in the radwaste ship-

ping area by providing 100% coverage. Another positive initiative

was the cross-certification of permanent QC personnel on at least

two inspection disciplines (most actually have three areas of ex-

pertise).

e

O s

O

35

.

In the previous SALP report the NRC recommended that the licensee

review the existing quality control inspection program and proce-

dures to identify areas of disagreement, and formally document and

implement the desired program with appropriate controls. An opera-

tionally oriented QA effectiveness team inspection conducted at the

end of this assessment period found that the corrective action for

previously identified deficiencies was not effective in some areas.

The licensee's QC inspection of maintenance and surveillance acti-

vities was not implemented in accordance with procedures that es-

tablish requirements, provide acceptance' limits, and include in-

spection responsibilities. Weaknesses in supervisory reviews for

quality control inspection reports and establishment of hold points

were also identified.

The QA effectiveness team inspection had further findings which are

indicative of a potential weakness in QA/QC management involvement.

These included: 1) the lack of management review of all Quality

Control Inspection Reports (QCIRs); 2) the lack of understanding

the significance and method of completing the final review section

of the QCIRs; 3) the excessive delay in revising procedures; 4) the

failure to identify that inspection procedures were not implemented

as written; and 5) management's position that the QA program did

not apply to certain consumables. The findings of the QA team as-

sessment are not indicative of a programmatic breakdown, but do in-

'

dicate that more intensive management involvement in this area is

warranted.

The audit program is conducted in accordance with the licensee's

procedure and published schedule. Licensee initiatives to improve

effectiveness of the program have included: 1) improved offsite

review committee cognizance of the audits; 2) increased staffing

and use of plant related expertise for the audits; 3) incorporation

of audit findings in trending reports; and 4) reports of audit de-

ficiencies and observations that have gone uncorrected for more the-

six months, highlight items which require management attention. The

licensee's station staff has remarked positively about audit program

improvements, and considers that they are providing a more meaning-

ful self-evaluation process.

The licensee's Quality Audit and Engineering Group has been success-

ful in establishing a program to track, trend and evaluate NRC

findings, LERs, nonconformance reports, PIRs, audit observations

and deficiencies, and QA surveillance deficiencies. As of July, 1986,

QC group inspection deficiencies were incorporated into the Quality

Assurance Department's Trending program. Semi-annual trending re-

ports are issued to all levels of licensee management. Other indi-

cations of related improvements in management involvement and con-

trol in assuring quality include the following licensee initiatives:

1) utilization of yearly performance-oriented corporate goals in

i

. .. .

.

36

,

all areas of operations; 2) development and use of plant quarterly

.

performance statistical trends; and 3) comparing industry-wide plant

performance.

To more clearly define the fitness for duty program, the licensee

has issued a revised drug and alcohol policy effective October 1,

1986. This policy incorporates drug and alcohol testing of.all

employees at annual physicals and a strict prohibition against the

sale, use, or possession of drugs or alcohol on licensee property.

Also, licensee employees are not to report for work under the in-

fluence of either drugs or alcohol. The policies also cover both

visitors and contractors requiring unescorted access to the plant

site. In a related matter, the licensee's plant management, super-

visory and senior technical personnel attend fitness for duty and

behavior observation training given by a behavior observation pro-

fessional on a once per year basis.

In summary, management involvement and control in assuring quality

continues to be aggressive in providing the proper level of over-

sight. On an overall basis, the QA and QC staffs were monitoring

all licensee activities at a high degree of involvement and con-

tinued positive performance trends were generally noted. The fol-

lowup of identified deficiencies exhibited thoroughness as well as

exceeding the frequency required by their program. The trending

analysis is used to identify those areas where performance improve-

ment is needed and as such it is proving to be a valuable management

4

tool. Also, QA audits have gained wider worker acceptance as the

type of auditing technique becomes more meaningful with respect to

the evaluation of quality and performance. The only exception tc

an otherwise exemplary performance is the one inadequate corrective

action associated with the concerns expressed in the previous SALP

'

period. In this area, focused management attention is warranted

in developing and implementing program procedures for the QC in-

spection activities that are responsive to NRC requirements with

respect to proper documentation of inspection activities.

2. Conclusion

Category 1.

3: Board Recommendation

None.

.

--n.., , . n . . - . - - - - , . -, - , . , -o -y ,.c - --- , .--- --a , , . - - - _ - - , . _ . - . - , _ . - . - , - - - - - - -

-

.

-.

_

,-

37

J. Training and Qualification Effectiveness

1. Analysis

During this assessment period, Training and Qualification Effective-

ness is being considered as a separate functional area for the first

time. Training and qualification effectiveness continues to be an

evaluation criterion for each functional area.

The various aspects of this functional area hate 1een considered

and discussed as an integral part of other functional areas and the

respective inspection hours have been included in each one. Conse-

quently, this discussion is a synopsis of the assessments related

to training conducted in other areas. Training effectiveness has

been measured primarily by the observed performance of licensee

personnel,-and to a lesser degree, as a review of program adequacy.

The discussion below addresses three principal areas: licensed

operator training, non-licensed staff training, and the status of

INPO training accreditation.

'

l

In the area of licensed operator training, the licensee maintains

a relatively small training staff and relies on^ contractor support

to perform a large portion of initial operator instruction, all

simulator training and most of the candidate evaluations conducted

prior to NRC examinations. The review cf the licensed operator

training program detected significant weaknesses that have nega-

tively impacted on the ability of the licensee to successfully

prepare candidates for NRC examinations. Continued and additional

management attention is warranted to provjde corrective measures

to: 1) improve training effectiveness upon identification of can-

'didate weaknesses during all evaluation phases of the training

program, and 2) provide aggressive training department oversight

of training programs, including contractor involvement, to insure

,

adequate standards of instruction are maintained.

l I

!

The licensee ha:, taken actions to improve the quality of candidates

entering the licensing program and to improve the screening of can-

didates during the training program., Candidates will be required

to become more involved with plant evolutions as part of their

training. An additional licensee initiative involves the implementa-

i tion of a new hiring policy that requires a Bachelor riegree in en-

gineering or engineering technology for an individual to be eligible

for vacant auxiliary operator positions. The first hire under this

policy occurred in August, 1986. ,

,

Training material was identified as a training weak' ness in the prior

SALP and no significant improvement has been noted during the as-

sessment period. Some recently prepared training material has become

out-of-date due to plant modifications. The licensee has committed

to have a complete and accurate set of training mateffal by March

!

l

I

l

!

, - - _ - - . _ _

, .-

_ _ .

ee' e

.

.

38

1987. The training programs for non-licensed operator, licensed

operator, and licensed operator requalification received INPO ac-

creditation in March 1986. Since accreditation is relatively recent,

no candidates have completed the approved program. However, a lic-

ensing class entered the accredited program in the summer of 1986

and will complete the program in April, 1987.

During this assessment period, non-licensed training proved to be

effective as evidenced by very few personnel errors. The licensee

relies heavily on department on-the-job training to establish and

maintain personnel technical qualification. Notable training and

qualification effectiveness strengths were: 1) use of department

managers as GET/Requalification training leaders to cover those

areas of their expertise; 2) strong performance by plant operators

in procedural implementation of safe shutdown system use in accord-

ance with 10 CFR 50 Appendix R; 3) quality control inspector knowl-

edge of radwaste transportation requirements

program to familiarize all emergency response;personnel

and 4) a vigorous

in effective

use of the new E0F.

Weaknesses in training and qualification effectiveness were identi-

fled in some areas; e.g., 1) maintenance support engineers' under-

standing of equipment performance and receipt inspection require-

ments, as well as ineffective implementation of their training pro-

grams; 2) inadequate training and its effectiveness assessments for

fire protection systems knowledge; and, 3) inattentiveness of the

maintenance staff to completion of documentation requirements of

MRs, in conjuction with insufficient identification by QC inspectors

that program requirements were not being met.

The licensee continues to aggressively pursue the training program

accreditation with INPO. On October 17, 1986, just subsequent to

the end of this assessment period, the licensee had submitted and

INP0 had accepted the Self Evaluation Reports for: maintenance (I&C,

mechanical, electrical), chemistry, radiation protection, shift

technical advisor, and technical staff and managers. The INP0 site

accreditation team visit is scheduled for June,1987.

!

l

In summary, problems persist in preparing personnel for NRC license

' examinations. The overall program for the candidates as well as the

quality of training material continues to be marginal. In contrast.

i

'

the training of licensee personnel to perform a variety of assignec

responsibilities appears to be very effective. There is a low in-

,

cidence of personnel errors, few of which could be directly attri-

i

butable to shortcomings in the training program. A number of lic-

! ensee initiative > during this assessment period indicated managerial

interest in various aspects of training at many levels. The short-

comings in preparing licensed operators for NRC examinations appears

to be a notable exception to an otherwise effective overall training

program.

-.

.

-- .

.

39

..

2. Conclusions

,' Category 2.

3. Board Recommendation

Licensee:

-

Closely monitor trainee progress in the licensing program and

provide for an assessment of the quality of instruction and

evaluation provided by contractors.

-

Complete and update training material.

,

, -

'__ _ , _ , . . , _ _ _ _ _ _ _ _ _ ... .- - --

~ ,

.

40

K. Licensing Activities (107 hours0.00124 days <br />0.0297 hours <br />1.76918e-4 weeks <br />4.07135e-5 months <br />, 4%)

1. Analysis

This evaluation represents the combined inputs of the Operating

Reactor Project Manager, technical reviewers, and the resident in-

spector.

During the SALP evaluation period, YAEC continued to show excellent

management overview in the area of licensing activities. The licen-

see does not have a formal integrated implementation schedule plan.

However, the licensee has a system for establishing priorities on

issues such that both licen:ee and NRC resources are focused on the

most significant issues. Also, the licensee has a system for co-

ordinating manpower requirements, equipment procurement and engi-

neering changes for outage planning. The licensee has been ogen in

discussing their priorities for both completion of licensing issues

and for their implementation with NRC and has been receptive to NRC

comments. The NRC has noted evidence of prior planning, in particu-

lar, timely submission of the incore detector operability TS pro-

posed change and also the early submittal of a proposed change to

the TS relating to the next reload (Spring 1987).

Licensee management has taken an aggressive role in an effort to

achieve resolution of long-standing issues such as the SEP reviews. '

Upper management involvement in establishing priorities and in

reaching technical resolution has been evident.

Early in the reviec perioc, some problems were experienced with

respect to providing sufficient information to support the no sig-

nificant hazards considerations determination and, on occasion (such

as proposed change 192), for the proposed changes themselves. Im-

provement has been noted in this area over the period.

The Yankee plant is unique in many aspects and the licensee often

relies on the long operating experience and simplicity of design

to justify alternative approaches to resolution. Because of the age

and size of the plant many generic resolutions of issues are not

appropriate and thus more work is required by both the NRC and YAEC

to complete the reviews. In general the licensee has been able to

satisfy the intent of NRC requirements in plant-specific applica-

tions. For example, the licensee has installed a safety parameter

display system (SPDS) which is relatively simple, acceptable to the

NRC and effectively used by the plant staff.

l The licensee has developed an approach for resolution of SEP exter-

! nal event reviews which relies on the recently installed dedicated

l shutdown capability and on the results of their probabilistic safety

l study. This approach should result in efficient use of resources

to obtain maximum safety benefit.

l

l

l.

l

l

l

!

.-_ . - .

.

.

41

->

Clear understanding of the issues and sound technical approaches for

resolution have been evident in the areas of fire protection, re-

sponse to GL83-28 concerns (Salem ATWS) and for the many proposed

changes to the Technical Specifications.

In the detailed control room design review, the licensee did not

initially perform a sufficiently detailed function / task analysis

particularly of instrumentation and control requirements. The lic-

ensee did not appear to recognize the importance of this analysis

in.the overall review and was reluctant to implement remedial ac-

tions. While progress has been made recently through meetings and

licensee submittals, this aspect is not yet resolved.

.The issue of bus undervoltage protection has been prolonged. The

NRC safety evaluations have clearly indicated the staff's position

regarding testing of both the first and second level of protection.

The licensee did not resolve the safety issues dealing with the

first level of protection, even after they were identified by the

staff. Several rounds of correspondence have occurred and the issue

is still not settlec.

A problem regarding adequacy of minimum starting voltages in the

electrical distribution system for safety-related equipment was

reported by the licensee some time after this generic issue had been

originally resolved. One of the underlying reasons for this prciblem

was an assumption by the YNSD engineering staff regarding pump motor

rating which had not been adequately verified on site.

Some of the issues mentioned above originated prior to the rating

period and may have been complicated by turnover of licensing per-

sonnel both at YAEC and the NRR organization. However, more atten-

tion to detail, improved communication within YAEC, and enhanced

verification activities by the licensee may be appropriate.

In April, 1985, the licensee implemented a plant level organiza-

tional change that impacted on existing Technical Specifications.

,

As of the end of the current assessment period an appropriate lic-

ensing action has not been submitted. Additionally, as indicated

in Section G, Security and Safeguards, the licensee has not been

fully responsive to the prior SALP's concern involving changes sub-

mitted under Section 10 CFR 50.54 (p). Additional management atten-

tion in these areas is warranted to prevent future inadequacies from

developing.

The licensee continues to respond promptly to NRC staff initiatives.

During this performance period, the licensee worked with NRC to

resolve a substantial number of multiplant, TMI and plant specific

issues. Actions completed included environmental qualification of

electrical equipment, GL83-28 issues, as well as a large backlog

of TS changes. In addition, significant progress has been made in

!  !

!

. _ _ . , __.

w .

.

42

o

the areas of SPDS, Regulatory Guide 1.97 (Post Accident Monitoring),

e

and SEP issues. All issues on fire protection are essentially re-

solved and implemented.

The licensee has been cooperative in providing information through

conference calls, meetings, and submittals. In addition, periodic

meetings are held between the NRC Project Manager and the YAEC

licensing representative to discuss licensing issues. Generally,

issues have been resolved in a timely manner.

The licensee performs most of their engineering, including the re-

load analysis, in-house. Staffing levels seem satisfactory for the

level of work required.

The analysis of the licensee's reportable events is contained in

the plant operations section of this report. Only a single event

(LER 85-01) was identified by the licensee where plant operations

could have potentially been in deviation with the safety analysis.

This event involved the identification of a LOCA analysis deficiency

which was compensated for by the insertion of selected control rods.

The licensee provided timely resolution of this issue in a technic-

ally sound and thorough manner that reflects their conservative

approach whenever the potential for safety significance exists. Re-

views of licenset responses required by NRC I&E Bulletins have

improved in response to management attention to previously-identi-

fled weaknesses in this area.

In sur. mary, the YAEC organization has performed well in the licens-

ing area during the report period as evidenced by the large number

of completed actions. Strong management involvement has been noted;

however, continued management attention should be focused on the

areas noted above to maintain the high performance level.

l

2. Conclusion

Category 1.

3. Board Recommendation

l

None.

i

,

l

,,

.

43

.

V. SUPPORTING DATA AND SUMMARIES

A. Investigation and Allegation Review

There was one allegation during this SALP period. It involved the licen-

see's policy on use of prescription narcotic medicine by members of the

contract guardforce while on duty. Currently, the licensee's contracted

security force has appropriate policies covering the use of prescription

medicines. No violation of NRC requirements was identified.

B. Escalated Enforcement Action

1. Civil Penalties

There were no civil penalties issued during this assessment period.

2. Orders

There were no orders involving escalated enforcement action during

this assessment period.

3. Confirmatory Action Letters

There were no confirmatory action letters issued during this as-

sessment period.

C. Management Conferences

On July 22, 1986, an enforcement conference was held at the NRC Region

I office to discuss the installation of undersized trip coils in the

circuit breakers for motor-operated valves located in the reactor coolant

system vents and emergency feedwater system.

D. Licensee Event Reports

1. Tabular Listing

Type of Events:

A. Personnel Errors 11

B. Design / Man./Const./ Install 3

C. External Cause 0

D. Defective Procedure 2

E. Component Failure 7

X. Other 0

Totals 23

LERs Reviewed

LER No. 85-01 to 86-13

1

l

-

44

2. Causal Analysis

The following sets of common mode events were identified;

a. LERs 85-02 and 86-11 reported missed or incorrectly performed

surveillances.

b. LERs 85-09, 85-10, 86-04, 86-12, and 86-13 reported a total

of five reactor trips (two at power and three while in startup).

Of these, three reactor trips (all while in startup) involved

personnel error.

c. LERs 85-08 and 86-06 involved inoperabilities of steam genera-

tor blowdown monitors

d. LERs 85-04, 85-06, 85-07, 85-08, 86-04. 86-06, and 86-08 are

events due to component failures.

E. Operatino Reactors Licensino Actions

1. Schedular Extensions Granted

None.

2. Reliefs Granted

None.

3. Fva-" inns Gre.ted

October 2, 1986 Exemptions to Section III.G of 10 CFR Part 50 Ap-

pendix R (Fire Protection)

4. Orders

A confirmatory order was issued on July 5,1985, modifying the

license regarding additional licensee commitments on emergency

response capability (Supplement 1 to NUREG-0737)

5. License Amend ents Issued

Amendment E3 issued on July 1,1985, Technical Specifications on:

a) typographical corrections / clarifications, b) removal of references

to 3 loop operation, c) NUREG-0737 clarification items, d) Inte-

grated Plant Safety Assessment Report items, and e) Radiological

,

Effluent TS clarifications.

Amendment 84 issued on October 1, 1985, Technical Specifications

on a) pressurizer code safety valve capacity / snubbers, b) degraded

grid voltage, and c) main coolant vents.

o

,

45

Amendment 85 issued on October 31, 1985, Technical Specifications

on pressurizer safety valve setpoint tolerance.

Amendment 86 issued on November 8, 1985, Technical Specifications

on containment isolation surveillance.

Amendment 87 issued on November 18, 1985, Technical Specifications

on ECCS surveillance intervals.

Amendment 88 issued on November 27, 1985, Technical Specifications

on refueling.

Amendment 89 issued on November 30, 1985, Technical Specifications

on degraded grid voltage (second level).

Amendment 90 issued on December 16, 1985, Technical Specifications

on ECCS leakage.

Amendment 91 issued on January 15, 1986, Technical Specifications

for train coolant system inspections.

Amendment 92 issued on May 14, 1986, Technical Specifications for

SIT, steam generator blowdown monitors, etc.

On May 14, 1986, notice of denial of changes on: 1) isolated loop

charging, 2) reference to TS 4.0.5, 3) control room ventilation TS,

4) use of temporary door in airlock, and 5) removal of tritium

sample requirements.

Amenament 93 issued on May 20, 1986, Technical Specifications for

spent fuel pit movements.

Amendment 94 issued on May 28, 1986, Technical Specifications for

main steam line low pressure isolation trip.

Amendment 95 issued on June 5,1986, Technical Specifications for:

a) containment high range radiation monitors, core exit and vessel

head thermocouples, containment pressure and water level monitors,

and b) containment hydrogen monitor.

Amendment 96 issued on June 9, 1986, Technical Specifications on

blank flange.

Amendment 97 issued on June 17, 1986, Technical Specifications on

containment breathing air system isolation.

Amendment 98 issued on August 20, 1986, Technical Specifications

on RETS Reporting Requirements.

Amendment 99 issued on September 23, 1986, Technical Specifications

on changes to RETS.

A .

.

TABLE 1

TABULAR LISTING OF LERS BY FUNCTIONAL AREA

YANKEE NUCLEAR POWER STATION

CAUSE CODES *

Area A B C D E Total

A. Plant Operations 2 1 2 5

B. Radiological Controls 1 1

C. Maintenance and Modifications 4 1 1 3 9

D. Surveillance 1 1 2 4

E. Fire Protection and Housekeeping 1 1

F. Emergency Preparedness 1 1

G. Security and Safeguards 0

H. Refueling and Outage Management 0

I. Assurance of Quality

J. Training and Qualification Effectiveness 0

K. Licensing Activities 2 _ _ _ _

2

TOTALS: 11 3 0 2 7 23

  • LER Cause Codes (Assignea during NRC review.)

A - Personnel Error

B - Design, Manufacturing, Construction, or Installation Error

C - External

D - Defective Procedure

l E'- Equipment Malfunction

!

,

!

.

1 e. 9 k.'

6-

TABLE 2

LER SYNOPSIS (2/1/85 - 10/6/86)

YANKEE NUCLEAR POWER STATION

LER NUMBER SUMMARY DESCRIPTION

85-01 Determination of Inappropriate LOCA Methodology Assumption

-85-02 CS-V-621 Not Tested in Accordance With The ISI Program

85-03 Fuel Degradation (Assemblies B-696I, B-688 and A-679 In Core Posi-

tions ,,-9, H-8, and K-5)

85-04 Pressurizer Safety Valve PR-SV-181 (S/N BW 07972) Setpoint Greater

Than TS

,

85-05 Switchgear Room Fire Barrier Inadequacy

85-06 Condensate Pump Trip Circuit Inoperable

85-07 Nuclear Instrumentation Channels 7 & 8 Low Power Set Points In-

operable

85-08 No. 4 Steam Generator Blowdown Monitor Inoperative

85-09 Reactor Scram During Startup due to Maintenance Personnel Error.

85-10 Inadvertent Reactor Scram During Maintenance Activity

86-01 Technical Specification Violation Concerning the Yankee Emergency

Plan

86-02 Insufficient Implementation Procedures For the Offsite Dose Calcu-

lation Manual

4

86-03 Failure to Comply with a Technical Specification Action Statement

86-04 Reactor Scram - Loss of Heater Drain Pumps

. 86-05 Dose Equivalent I-131 >1.0 Microcuries Per Gram

.

86-06 Inoperable No. 3 Steam Generator Blowdown Monitor

86-07 480 VAC Busses Cross-Tie Electrical Loading Problem

86-08 No. 1 Main Coolant Pump Suction Valve Stem Failure

86-09 Incorrect Overload Devices for Four Motor-0perated Valves

._ - .- . -. ,

_ _ - _ _ _ - _ _ _ _ _ _ _

= M

i

T-2-2

.

LER NUMBER SlM4ARY DESCRIPTION

86-10 Potential Loss Of Shutdown Cooling

86-11 Containment Isolation Valves Missed Surveillance

86-12 Plant Trip on Low SG Level Due to Loss of Control Air

86-13 Reactor Scram due to Operator Error

l

l

t

t

. _ _ _ . _ .

_

< -k

.

4

TABLE 3

INSPECTION HOURS SUMMARY (2/1/85 - 10/6/86)

YANKEE NUCLEAR POWER STATION

HOURS  % OF TIME

A. Plant Operations 655 22%

B. Radiological Controls 507 14%

C. Maintenance and Modifications 601 20%

D. Surveillance 284 10%

E. Fire Protection and Housekeeping 162 5%

F. Emergency Preparedness 445 15%

G. Security and Safeguaras 154 5%

H. Refueling and Outage Management 142 5%

I. Assurance of Quality NA NA

J. Training and Qualification Effectiveness NA NA

K. Licensing Activities * 107 4%

Total 3057 100%

  • Inspection effort only.

l

t

_ _ __ _ . _ . _ . - -

- - - - _ _ _ _ _ _ _ _ _ _ _ _

< (' k

.

6

TABLE 4

ed

ENFORCEMENT SUMMARY

YANKEE NUCLEAR POWER STATION

Severity Levels

FUNCTIONAL AREAS I II III IV V DEV Total

A. Plant Operations 1 1

B. Radiological Controls

C. Maintenance and Modifications 1 1

D. Surveillance 2 2

E. Fire Protection and Housekeeping

F. Emergency Preparedness

G. Security and Safeguards

H. Refueling and Outage Management

I. Assurance of Quality 1 1

J .' Training and Qualification Effectiveness

K. Licensing Activities

1 2 2 5

_-

..

r

-

7

%

.

'-

TABLE 5

ENFORCEMENT DATA

YANKEE NUCLEAR POWER STATION

Inspection Inspection Severity Functional

Report No. Date Level Area Violation

85-07 3/21-4/26/85 V D Failure to establish a

written procedure that pre-

-

scribes the required quali-

tative assessment for in-

strumentation channel checks

required by the Technical

Specifications for meteoro-

logical monitoring system.

86-02 1/7-2/14/86 V D Failure to establish a

written procedure that prc-

scribes the required quali-

tative assessment for in-

strumentation channel checks

required by the Technical

Specifications for steam

generator blowdown monitors.

86-08 6/10-10/8/86 IV A Failure to maintain at least

one main coolant loop bypass

valve closed while in Mode

3 and failure to conduct

a required surveillance test

on these valves.

86-09 6/26-7/2/86 III C Installation of undersized

trip coils in circuit

breakers for motor-operated

valves located in the reac-

tor coolant system and

emergency feedwater system.

.

86-17 9/29-10/3/86 IV H Failure to follow procedures

requiring quality control

for maintenance activities.

!

.- - -_ ___ . ._ ,_ ._ -

- g

6

i

u

TABLE 6

INSPECTION REPORT ACTIVITIES

YANKEE NUCLEAR POWER STATION

Inspection Inspection Areas

Report No. Hours Inspected

85-04- 110 Routine Resident

85-05 160 Post-Accident Sampling System

85-06 30 Startup Physics Testing

85-07 114 Routine Resident

85-08 163 Emergency Preparedness Exercise

F5-09 72 Radiation Protection Prorrr,

'

85-10 40 Radiological Environmental Monitoring Program

85-11 141 Routine Resident

85-12 135 Generic Letter 83-28, Salem-ATWS Concerns

85-13 34 Safe Shutdown System Building Construction

85-14 181 Routine Resident

85-15 137 Routine Resident

85-16 7. Radiation Protection Program

85-17 31 Physical Security

85-18 156 Routine Resident

85-19 12 Licensing Review (on-site) of P.C. 186

85-20 37 Maintenance Program

85-21 27 Nonradiological Chemistry Program

85-22 --

Operator Examination

85-23 74 Radiation Protection Program

85-24 126 Routine Resident

l

f

, . - - - . - - - -e. , , . - - - c. < -

-, . --.. ., - - . , -,,

.

i :o

e

  • f. T-6-2

Inspection Inspection Areas

Report No. Hours Inspected

85-25 135 Appendix R

86-01 42 Refueling and Startup Testing

86-02 99 Routine Resident

86-03 18 Licensed Operator Training Program

86-04 37 Radioactive Waste Management

86-05 196 Routine Resident

86-06 83 Emergency Preparedness Exercise

66-07 --

Operator Examination

86-08 200 Routine Resident

86-09 49 Reactor Coolant System Vents-Special Inspection

86-10 19 Emergency Preparedness

86-11 32 Surveillance Testing and Calibration Control Program

86-12 74 Radiation Protection Program

86-13 --

Not Used

86-14 35 Physical Security

86-15 --

Not Used

86-16 58 Radiological and Chemical Confirmatory Measurements

, 86-17 124 Operational QA Effectiveness

,

l

- _ _ _ . - _ _ .

. . . _ _

r

t" 'h

I

c

TABLE 7

REACTOR TRIPS AND UNPLANNED SHUTDOWNS

YANKEE NUCLEAR POWER STATION

Power Proximate Root

Date Level Cause Cause

12/9/85 <2% Unit Trip Personnel error maintenance. Contractor

employee inadvertenly bumped an RPS relay

while cleaning within the control room's

main control board.

12/28/85 <2% Unit Trip Personnel error - maintenance and opera-

tions. False high startup rate trip caused

when maintenance personnel performed a

functional test in conjunction with

troubleshooting. The root cause was per-

sonnel failure to recognize performance

of the test while at <15% power will resuit

in a plant scram.

6/1/86 100% Unit Trip Equipment failure - random cause. Loss

of both heater drain pumps resulted in a

low steam generator level reactor scram.

The pumps were damaged in a lightning storm.

6/18/86 100% Shutdown Equipment failure - mechanical defect

(under review). Shutdown to repair a

leaking weld in a coupling on the No. 2

steam gerator's blowdown line.

10/4/86 100% Unit Trip Equipment failure - random cause. Low

control air pressure condition caused by

a component failure subsequently resulted

in a plant scram on low steam generator

levels. A contributing cause was inade-

quacies in guidance in a recovery procedure

involving feedwater control valve lock-up.

10/4/86 <2%' Unit Trip Personnel error - operations. Control

room operator error resulted in RPS trip

, when the non-return valve trip / reset switch

'

was inadvertantly placed in the trip posi-

tion during a plant startup.

I

. . . , _ - - . _ . . . _ . , _

_ _ _ - . .-

( 1

c: :o

I

c

FIGURE 1

NUMBER OF DAYS SHUT DOWN

YANKEE NUCLEAR POWER STATION

I

February, 85 l

l

March, 85 l

l

April, 85 l

l

May, 85 l

l

June, 85 l

l

July, 85 l

l

August, 85 l

l

September, 85 l

I

October, 85 I i 13 Days Shut Down Cycle XVII-XVIII Refueling Outage

i

November, 85 1 30 Days Shut Down l Cycle XVII-XVIII Refueling Outage

i

December, 85 l l 9 Days Shut Down Cycle XVII-XVIII Refueling Outage

l

January, 86 l

1

February, 86 l

l

March, 86 l

l

April, 86 l

l

l May, 86 l

1

June, 86 I i 13 Days Shut Down

1_

July, 86 l_I 1 Day Shutdown

i

August, 86 l

l

September, 86 l

1_

October, 86 1_l I Day Shutdown

. ., . . . . . ., __ _ - ._, -