Similar Documents at Ginna |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
e!
'CCELERATED DEMONRATION SYSTEM DISTRIBUTION INFORMATION DISTRIBUTION SYSTEM (RIDS) 'EGULATORY ACCESSION NBR:9112170532 DOC.DATE: 91/12/11 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME 'AUTHOR AFFILIATION BACKUS,W.H. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp..
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 91-009-00:on 911111,steam generator feedwater on both steam generators. Caused by perturbations of isolations'ccurred
~
advanced digital feedwater control sys.Feedwater regulating D valves manually controlled.W/911211 ltr.
i(7 (LER), gIncidentg Rpt, etc.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 AEOD/ROAB/DS P 2 2
.NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB 7E 1 . 1 NRR/DLPQ/LHFB10 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB8H3 1 1 NRR~ST/S PLB8 Dl 1 1 NRR/DST/SRXB 8E 1 1 1 1 RES/DSIR/EIB 1 1 N1 LE 01 1 '1 EXTERNAL: EG&G BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 D
D D
NOTE TO ALL "RIDS'ECIPIENTS:
PLEASE HELP US TO REDUCE i'i'ASTE! CONTACT THE DOCUlii!EiiTCONTROL DESK, ROOli I Pl-37 (EXT. 2M79) TQ LILIih!INAl'E YOUR NAiIF. FROii1 DISTRIBUTION LISTS FOR DOCUiiIENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED'TTR 31 ENCL 31
a ke 0
~ ~ ' w ~~
ns ~
st
, ss@ss ROCHESTER GAS AND ELECTRIC CORPORATION e e9 EAST AVENUE, ROCHESTER N. K 14649-0001 ",
ROBERT C MECREDY TELEPiSONE Vice Psesidens AREA CUE 7 s 6 546 2700 Cfnnn s'ueiess PsodueBun December 11, 1991 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 91-009, Automatic Feedwater Control Perturbations, Due To'lectromagnetic Noise Spikes From Unrelated Relay Actuation, Caused Steam Generator Feedwater Isolation on High Level R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item .(a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Event Report LER 91-009 is hereby submitted.
This event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy xco U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector
I 0
NAC tera 000 ISAS I U*NUOLCAR RICULATQR'v coeal~
At<<IIOVIDOMS NO,SIM OIOrr UCENSEE EVENT REPORT (LER) lxSIRIS I/Sr/tt fACILITYNA<
~ erie rrre 4 Tr<<L NRC fare SS.IM 4 I II I IMI M.TSUIQII4 M.TSNIQIIHXIIAI M.TI le IQI I II M.TSNIQ)lralltl
~ i>rio,. W)Wi$~g'.
+ SIACI 4 I III IHI SO.IMle) llllrl M.TSNIQIIX4 LICINSII CONTACT tO1 THIS LIR lltl M.TSIIIQllel NAMt TILltHONINVMSIR ARIA COOt Wesley H. Backus Technical Assistant to the rations Mana er 31 5524- 4446 f
COM<<LITC ONI LINC f01 IACH COM<<ONINT AILURC OtICRIIIO IN THIS RltORT llll CAVSt SYSTSM COMtO HINT MANVfAO TO A
NtROI Prr """ ~"> ""+ CAVSI
. 5":ij> S.<~,~86:
SYSTSM COMtONCNT MANVfAO TURIN ltORTASL TO NtROS TURIR
'jjpQ%. (@~kg e~rg~@4~@
MOHTH CAY YIAR IVtfLtMINTALRtt01T IXtlCTIO IIII CXflCTIO Lvll<<I SCION OATI I'III Y Ct lllfer, reer<<rra IX<</CTIO SVS MISSION OATII NO LIITAAOTII<<err a Irof ireea, I ~ .. rterer<<errNf INaee r<<vrre<<rrr trteerarre <<ew ll ~I On November 11, 1991 at approximately 1214 EST, with the reactor at approximately 98% full power, steam generator feedwater isolations occurred on both steam generators. These feedwater isolations were caused by perturbations of the advanced digital feedwater control system which increased feedwater flow to t1 generators. 'team Immediate operator action was to manually control the feedwater regulating valves to reduce steam generator levels and stabilize the plant.
The underlying cause of the event was determined to be electro-magnetic noise spikes affecting the advanced digital feedwater control system.
Corrective action taken was to modify specific relay circuits that were causing these spikes.
NAC faa SM IIAS I
I l IIAC See I000 I M V.I. IIVCLCAA AlOVLATOAV<<OMMHNISI
/M ll%0&I04 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AtPAOV KO OMA a>>tiACS ll)IWS I'ACILITY IIAMC III OOCKET IIVM~ EA l11 Llll IIVMOIIIIII ~ AOI III
'NOVINT<Al, 'ttV4%8 U A R.E. Ginna Nuclear Power Plant TQTT III~ ~%M A ~. ~ y480OAV NAC Anil ~'il 2 4491 009 00 02or0 I ITI PRE-EVENT PLANT CONDITIONS The plant was at approximately 98% steady state reactor power with no major activities in progress. The Maintenance Department was performing troubleshooting, to determine the source of electromagnetic noise, spikes in the Advanced Digital Feedwater Control System (ADFCS). The troubleshoot-ing was being performed under the guidance of Work Order package f9122181. Unexplained electromagnetic 'noise spike problems were identified previously as coinciding with the start of the diesel fire pump, and which had minor effect on the ADFCS control functions.
The ADFCS was installed during the 1991 "Annual Refueling and Maintenance Outage. These electromagnetic noise spikes were first noticed on June 4, 1991, when a minor feedwater perturbation occurred, following a diesel fire pump start.
Since June 4, spikes have occurred almost every time the diesel 'fire pump has started. The ADFCS .has handled spikes with no noticeable feedwater perturbations, except for two (2) occasions. These occasions, the first on June 4, 1991 and the second on September 13, 1991, were handled by the ADFCS in automatic and no operator action was required.
There has been an ongoing search for the possible source of this electromagnetic noise spike so that corrected. As part of this ongoing search, the Electrical it could be Engineering Department evaluated their cable tray database and identified circuit E174 as a possible source. Circuit E174 is the 125 Volt DC power feed to the fire relay panel and shares some cable trays with ADFCS input cables, most notably, the feedwater header pressure inputs to and P502).
ADFCS'P501
'IAC AOAM AAA ital
NIIC Pe<<<<1 044 I
~ I.'ICENSEE EVENT REPORT ILER) TEXT CONTINUATION
<<U.S. NUCLIAA AIOULAT01T COMMITeION
/
AAAAOV%0 OMI NO TISOWIOA T)eAt1%$ ~ III 1$
I'ACILITYNAMI III DOC%IT NUNMtN ITI Llll NUMOl1 III ~ AOI IS NOMIC v TAA, '
AQVANT<<AL 4 1 1(V4<<O<<<<
<<<<4 1 R.E. Ginna Nuclear Power Plant TQ(T IA'<<<<44 NMCO 4 ~. <<<<M MM41<<<<M /Oral ~ T I II TI osooo244 91 0 09 0 0 0 30' 9 Westinghouse Electric Corporation (the manufacturer of the ADFCS) was contacted and could not explain the ADFCS excursions based on, data available. In conjunction with the Electrical Engineering Department, Westinghouse had previously recommended that the shielding and grounding schemes for all ADFCS inputs be checked. These inputs were checked in August, 1991. This check indicated that all ADFCS inputs are correctly shielded and grounded.
DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAZOR OCCURRENCES:
0 November 11, 1991, 1214 EST: Event Date and Approximate Time.
0 November 11, 1991, 1214 EST: Discovery Date and Approximate Time.
o November 15, 1991: Cause of EMP noise spike identified and suppressed to acceptable levels.
WGBFZ:
On November 11, 1991, at approximately 1214 EST, with the reactor at approximately 98% full power, the diesel fire pump was started, as required for ADFCS troubleshooting per Work. Order f9122181.
Approximately thirty (30) seconds after the diesel fire pump was started an "ADFCS System Trouble" alarm (G-22) was received.
The Control Room operator responsible for feedwater control had pre-positioned himself in front of the "A" and "B" S/G Main Feedwater Regulating Valves (FRV) control panel prior to the start of the diesel fire pump.
~ <<1C ADAM TQAA
<<tel
1IIC Seam I$4$ l
~ LICENSEE EVENT REPORT ILER) TEXT CONTINUATION V.S. IIVCLCA1 AIOVLATOAYCOSSSSt%IOII r
ASSAOYCO OU ~ IIO SI$ 0&IOS TIIAI1$$ ~ ITI %$
AACILITYNASIS I 1 I- OOCKST IIVIAOIAIll L$ 1 NLAN$1 I~ I ~ A4$ ISI SSOUS>S<AL ' ASYCK)U U 1 U A R.E. Ginna Nuclear Power Plant o2 44 0 09 0004 or0 TQ(T /IT mew AIASS 1 ~. ~ e4004HV JYAC AMID ~ Yl I Ill o s o o 9 1 9 At this time, the Control Room operator noticed that both the "A" and "B" Steam Generator (S/G) main feedwater flows were pegged high .with both "A" and "B" S/G Main Feedwater Regulating Valves continuing to open further.
The condensate low pressure heater . bypass valve opened automatically and the standby condensate pump started automa'tically (to increase main feedwater pump suction pressure). Main Feedwater pump suction pressure was decreasing due to the increased feedwater flow to the S/Gs. The "A" and "B" S/G levels continued to increase and before the Control Room operator could shift 'the FRVs to manual, ADFCS automatically shifted the FRVs to manual. While the Control Room operator was manually lowering the setpoints for the FRV controllers, to control S/G level, the following alarms annunciated and feedwater isolation o'ccurred on both S/Gs; G-4 (S/G A HI LEVEL CHANNEL ALERT 67%)
and G-6 (S/G B HI LEVEL CHANNEL,ALERT 67%).
Immediately following the feedwater isolation, the condensate booster pumps tripped on high* pressure. A load de'crease was initiated at 10%/hour to lessen the impact of unstable S/G levels. Main feedwater to the S/Gs was controlled in manual in order to stop secondary system oscillations that were occurring due to the event. During the S/G level stabile.zation, S/G feedwater isolation occurred several times. The S/G levels were subsequently stabilized and main feedwater control was returned to automatic.
After main feedwater control was returned to automatic the load decrease was terminated. Total load decrease was approximately 0.54 full power during the event.
Subsequently, the condensate low pressure heater bypass valve was closed, the condensate booster pumps were restored, and the standby condensate pump was secured and realigned for automatic standby.
~ ~
VAC SOAV SSAA i $ 4$ l
II1C I<e<ws l043 I
~ LICENSEE EVENT REPORT ILER1 TEXT CONTINUATION V S. 1VCLSA1 1SOVLATO1Y COMMISSION ATT1DVCO OVS <<O SISO&10l S>et<1%$ ~ IS I SS 1ACILITT IIAMt III DOC%ST IIVMOS1 lll LSII IIVMOI1 ISI ~ AOI ISI r r SSOVT<<T<AL TuT nr <<r<r r<Aee r <rr<rrr, ~ ~
R.E. Ginna Nuclear Power Plant A<rc I<<r<<< ~ Lv I I TI o 5 o o o 2 4491 0 Q9 0005 o>0 9 C INOPERABLE STRUCTURES, COMPONENTS', OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
None.'.
OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
E. METHOD OF DISCOVERY:
The event was immediately apparent due to alarms and indications in the Control Room.
OPERATOR. ACTION:
The Control Room operators took immediate manual actions to control S/G levels, reduce power level, and stabilize the plant. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10 CFR 50.72, non-emergency, 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.
G. SAFETY SYSTEM RESPONSES:
The "A" and "B" FRVs closed automatically from the feedwater isolation signal.
III. CAUSE OF >wryly A. IMMEDIATE CAUSE:
The feedwater isolation of the "A" and "B" S/G was due to the "A" and "B" S/G narrow range levels being
)/ = 67%.
~ <AC 101M
)00A
<040<
IIAC Pere l044l M V.5. IIVCLTAW 150VLATOAT CISPAII55IISI LICENSEE EVENT REPORT (LER) TEXT CONTINUATION P APPAOv50 Ov5 rrO IITC~IOA TlrprA55 5ITI,55 PACILITT rIAAI5 III OOCIIKT IIVAIOCA Ill L5A IILAPCIA I5! PAO5 I5I TTarrarrTrAL eg V Ie IO rr e e R.E. Ginna Nuclear Power Plant 2 4 4 1 0 0 9 0 0 06 av0 9 TSCT np rrrere ~ r reereep. ~ oeeoaw rTAC rrerrrr ~ VV I I TI o s o o o INTERMEDIATE CAUSES:
The "A" and "B". S/G narrow range levels were >/= 67%
due to increased feedwater flow to both S/Gs caused by a perturbation of the ADFCS.
The perturbation of th'e ADFCS was apparently due to electromagnetic noise spikes affecting the feedwater header pressure inputs to ADFCS, (i.e. P501 and P502).
C. ROOT CAUSE:
After extensive troubleshooting, it was determined that the spikes that affected the ADFCS feedwater header pressure inputs were caused by the de-energiza-tion of Relay ARSO, located in the fire relay panel.
This relay, which lights the diesel fire pump trouble light, de-energizes approximately 10 to 15 seconds after a diesel fire pump start. During this de-energization, inductive "kickback" causes an electro-magnetic noise spike to be generated and induced into the feedwater header pressure inputs. The signal cables carrying the feedwater header pressure transmitter (PT-.501 and PT-502) inputs share some common cable trays with the 'DC power source for the ARSO relay, and a noise spike was induced from the ARSO relay cable to the feedwater header pressure input cables.
ANALYSIS OF &TENT This event. is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires reporting of, "any event or condition that resulted in manual cr automatic actuation of any Engineered Safety Feature (ESF) including the Reactor Protection System (RPS)". The feedwater isolation of the "A" and "B" S/Gs was an automatic actuation of an ESF system.
~ r A C ~ O 1 re r TATI
'I MAC Pere 19441 M V.l. IIVCLCAA 1lQULATOAY COMMI5OQM LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPAOYlO OMl rrQ P
)IlQ~IQA l>ceIAlS lrll 1$
I'ACILITYNAlllIII QOCKlT HU%%$ 1 lll LIII MVeell1 Ill ~ AOl lll j ~ Ovlrrer AL rrlv le Io rr A
R.E. Ginna Nuclear Power Plant 24 49 0- 07 os0 TlxT IA' ~ ~. r ~ ereereMI eIAC Perrrr ~'llI I TI o s o o o 1 9 0 9 An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the feedwater isolations because:
o The feedwater isolations occurred at the required S/G levels.
o The plant was quickly stabilized and manual control of the FRVs was accomplished to mitigate the transient.
o As the feedwater 'solation occurred as designed, the assumptions of the FSAR for steam line break were met.
Based on the above, -it can be concluded that the public's health and safety were assured at all times.
V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVIBFZ NORMAL STATUS:
0 The Diesel Fire Pump was temporarily removed from service pending the outcome of root cause troubleshooting and determination. (The pump was returned to service after a noise suppression diode was installed across relay AR80).
0 When S/G levels were stabilized, subsequent to the ADFCS perturbation termination, the FRVs were placed in automatic control.
0 After the plant had been stabilized and the FRVs returned to automatic control, the condensate low pressure heater bypass valve was closed, the condensate booster pumps were restored and the standby condensate pump was secured and realigned for automatic standby.
rrAC POAM el4ll
(~ 1vv ~
NAC I
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION-U,S, NUCLTAA AIOULATOAVCOMAIITSION A>>AOVlO OUI NO )1$ 0&I04 T Ict<A CS ~ IlI 'l$
FACILITY NAIAC III OOCAtT NU~tA Ill LtA NLAA4IAIII ~ AOI IlI T~ OVINTIAL AAV IS lO N v 1 A R.E. Ginna Nuclear Power Plant o'o 24 491 00 00 08 Terr IA ~ >>A>> A ~. ~>>>>VV>>VNAC AV>> ~ SU I I TI o 5 o 9 DFO 9 B. ACTION TAKEN OR PLANNED TO PREVENT RECURE&NCE:
o
- A reverse-biased diode was temporarily installed across the coil of AR80 on November 15, 1991 and subsequent testing determined that the spikes from the AR80 circuit, affecting ADFCS feedwater pressure inputs following diesel fire pump
, starts, were eliminated. This noise suppression diode 'was permanently installed on November 18, 1991.
After reviewing the results of troubleshooting and the discussion with Westinghouse, the following is an outline of the corrective actions being taken or planned in response to the ADFCS noise spiking events:
o Short Term Response a) Operations personnel were made aware that one source of spikes on ADFCS was eliminated, but that spikes from other sources, while reduced in frequency. and magnitude, might occur. Operations will identify any new spikes on the ADFCS by submitting a Work Request/Trouble Report (WR/TR).
b) A WR/TR was submitted for installation of a diode for the fire booster pump relay AR85 (which also produces small spikes on ADFCS). However, these spikes are not of the same magnitude as the noise spikes that were caused by the Diesel Fire Pump starts.
o Intermediate Term Response Electrical Engineering will consult with Westinghouse concerning a database change to increase the ADFCS slew rate filter constant.
This filter is used to dampen any abrupt changes to feedwater regulating valve demand in the event that feedwater header pressure input values are rejected due to noise spikes. It is thought NAC IOAV TAAA
~T4ll
NIIC form SOSA U.E, NUCLEA(l AECULATOAYCOSSSIIS3(ON (04S I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION ASSAOYEO OUI fNO TI SOW(04 Exs(RES 'S(SI 'ES SACILITY NASIE Ill COCKET NUIAOEII (El LE(i NUIAOEA I~ I ~ ACE (j(
$ SCUSNTrAL osvrsrorr N O Nvm O R.E. Ginna Nuclear Power Plant o s o o o 24 491 009 00 09 OF 0 9 TExT (rf moro A(sos rs rosrrsos, om sNsooonor (Y(lc form ~'ll(ill that this filter can also "Lock In" an erroneous value following a feedwater headei pressure spike. Increasing this constant will more quickly restore a correct value for feedwater header pressure, after a spike has decayed. The spikes last less than five (5) seconds.
o Long Term Response a) Electrical Engineering will check with Westinghouse for the results of their review of ADFCS arbitration error checking software. This review will determine if the error checking routine for the switching to arbitration values instead of feedwater header pressure field input values is substituting erroneous values for feedwater header pressure used in FRV demand calculations.
b) Electrical Engineering will evaluate the routing of feedwater header pressure input circuits (to the- ADFCS), and will identify any additional modifications that may be required to eliminate the electromagnetic noise spike concern.
VX. ADDITXONAL NFORMATION A. FAILED COMPONENTS:
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: . No documentation of imilar LER events with the same root cause could be
.identified.
C. SPECIAL CO~BFZS:
None.
NAC s01lo SSOA rS4TI