Information Notice 1993-95, Storm-Related Loss of Offsite Power Events Due to Salt Buildup on Switchyard Insulators: Difference between revisions
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{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:UNITED STATES | ||
COMMISSION | NUCLEAR REGULATORY COMMISSION | ||
OFFICE OF NUCLEAR REACTOR REGULATION | |||
NOTICE 93-95: STORM-RELATED | WASHINGTON, D.C. 20555 December 13, 1993 NRC INFORMATION NOTICE 93-95: STORM-RELATED LOSS OF OFFSITE POWER EVENTS | ||
DUE TO SALT BUILDUP ON SWITCHYARD INSULATORS | |||
INSULATORS | |||
==Addressees== | ==Addressees== | ||
All holders of operating | All holders of operating licensees or construction permits for nuclear power | ||
reactors located close to a large body of salt water. | |||
PurDose | |||
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information | |||
notice to alert addressees to the potential for loss of offsite power due to | |||
salt contamination of switchyard insulators. It is expected that recipients | |||
to | will review the information for applicability to their facilities and consider | ||
actions, as appropriate, to avoid similar problems. However, no specific | |||
action or written response is required. | |||
==Description of Circumstances== | |||
On March 17, 1993, the Florida Power Corporation Crystal River Unit 3 experienced a loss of the 230 kV switchyard (normal offsite power to safety- related busses) when a light rain caused arcing across salt-laden 230 kV | |||
insulators and opened breakers in the switchyard. At the time, the unit was | |||
in cold shutdown during a maintenance outage. The 'Al emergency diesel | |||
to | generator was used to power safety-related loads including shutdown cooling | ||
until the 230 kV switchyard was restored. The ABE emergency diesel generator | |||
was unavailable due to maintenance. The 500 kV switchyard supplied nonvital | |||
loads throughout the event. | |||
On March | On March 16 through 18, 1993, Carolina Power and Light Company's Brunswick | ||
Units 1 and 2 experienced a loss of the 230 kV switchyards (all offsite power) | |||
when light rain caused arcing across salt-laden insulators and opened breakers | |||
in the switchyard. At the time, both units were in cold shutdown during an | |||
extended outage. Emergency diesel generators were used to power safety- related loads including shutdown cooling until the offsite power was restored. | |||
Since 1982, the Boston Edison Company Pilgrim station has also experienced | |||
several loss of offsite power events when heavy ocean storms deposited salt on | |||
the 345 kV switchyard causing the insulators to arc to ground. | |||
9312070298 LAe~ffL.A~1241{3/f3P | |||
tE | |||
X1P4 N4 e, 93-95* 777 | |||
k IN 93-95 K> | |||
December 13, 1993 Discussion | |||
Intense and unusual storms on March 13 and 14, 1993, produced high tides and | |||
high winds (average of 80 to 97 kilometers/hour high winds (50 to 60 | |||
miles/hour], with gusts up to 160 kilometers/hour [100 miles/hour] blowing | |||
ashore from the ocean i.e., Gulf of Mexico and Atlantic Ocean. These storms | |||
caused an unusual buildup of salt on the switchyard insulators at | |||
The | Crystal River Unit 3 and Brunswick Units 1 and 2. The storms were unusual in | ||
that they included high winds but little or no precipitation. As a result, salt from ocean spray built up on the switchyard insulators and was not washed | |||
away by rain. | |||
Days later, light rain increased the electrical conductivity of the salt, resulting in arcing across the insulators at both sites. To remove the salt | |||
from the insulators, Florida Power Corporation and Carolina Power and Light | |||
insulators | Company deenergized the affected switchyards, washed the insulators with high | ||
pressure demineralized water, then returned the switchyards to service. The | |||
washing stopped the electrical arcing across the insulators. | |||
The 500 kV switchyard for Crystal River Unit 3 is located adjacent to the | |||
230 kV switchyard. It was relatively unaffected. The 500 kV switchyard is | |||
used for main generator output when Unit 3 is operating and is used for an | |||
alternate source of offsite power (i.e., backfeeding of nonvital loads) during | |||
Unit 3 outages. The 500 kV switchyard experienced less arcing across the | |||
insulators than the 230 kV switchyard and no tripped breakers. As a | |||
precautionary measure, the licensee also deenergized and washed the 500 kV | |||
switchyard insulators. Factors that may have reduced the storm inpact on the | |||
500 kV switchyard included location (farther away from the shore) and higher | |||
insulation level (the 500 kV insulators were designed for up to 700 kV | |||
operation while the 230 kV insulators were designed for up to 242 kV | |||
operation). In addition, the licensee observed that, of the two types of | |||
230 kV insulators installed, the newer post type had less arcing than the | |||
older cap and pin type. | |||
Licensee followup action in response to these events, to improve the future | |||
performance of non-safety switchyard equipment, included: investigating | |||
available salt buildup monitoring systems, evaluating insulator washing | |||
the | methods/capabilities, considering the use of room temperature vulcanized (RTV) | ||
silicon rubber coatings, installing newer metal oxide gapless surge arrestors | |||
to replace older silicon carbide gap type surge arrestors, and replacing | |||
cellon-treated wood transmission towers. | |||
The 345 kV switchyard insulators at Pilgrim were coated with RTV silicon | |||
rubber (Sylgard) in 1987. It was expected that the RTV coating, when applied | |||
in 1987, would be effective for a period of 15 years. However, actual | |||
the | experience at Pilgrim indicates that the coating is effective for a much | ||
`- IN 93-95 December 13, 1993 shorter period of time. Consequently, the Insulators at Pilgrim were cleaned | |||
and coated with RTV again during the spring 1993 refueling outage. As a long- term option, the licensee is considering a replacement of the existing 345 kV | |||
switchyard with a modern compactly designed switchyard which would be more | |||
resistant to the coastal environment. | |||
These events illustrate the significance of maintaining reliable offsite and | |||
onsite power sources during outages as well as during operation. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Bran . Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII P. Fillion, RII | |||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR | |||
(904) 795-7677 (301) 504-2779 R. Prevatte, RII | |||
(919) 457-9531 Attachment: | |||
===List of Recently Issued NRC Information Notices=== | |||
Attachment | |||
IN 93-95 December 13, 1993 LIST OF RECENTLY ISSUED | |||
NRC INFORMATION NOTICES | |||
Informati on Date of | |||
Notice No. Subject Issuance Issued to | |||
93-94 Unauthorized Forced 12/09/93 All holders of OLs or CPs | |||
Entry into the Pro- for nuclear power reactors. | |||
tected Area at Three | |||
Mile Island Unit 1 on | |||
February 7, 1993 | |||
93-93 Inadequate Control of 12/08/93 All holders of OLs or CPs | |||
Reactor Coolant System for nuclear power reactors. | |||
Conditions During Shutdown | |||
93-92 Plant Improvements to 12/07/93 All holders of OLs or CPs | |||
Mitigate Common Depend- for nuclear power reactors. | |||
encies in Component | |||
Cooling Water Systems | |||
91-21, Inadequate Quality 12/07/93 All holders of OLs or CPs | |||
for | Supp. 1 Assurance Program of for nuclear power reactors | ||
Vendor Supplying and all recipients of | |||
Safety-Related Equipment NUREG-0040, "License Con- tractor and Vendor Inspec- tion Status Report" (White | |||
Book). | |||
89-77, Debris in Containment 12/03/93 All holders of OLs or CPs | |||
Supp. 1 Emergency Sumps and for nuclear power reactors. | |||
Incorrect Screen | |||
Configurations | |||
93-91 Misadjustment Between 12/03/93 All holders of OLs or CPs | |||
General Electric 4.16-KV for nuclear power reactors. | |||
Circuit Breakers and Their | |||
Associated Cubicles | |||
93-90 Unisolatable Reactor 12/01/93 All holders of OLs or CPs | |||
Coolant System Leak for nuclear power reactors. | |||
Following Repeated | |||
Applications of Leak | |||
Sealant | |||
OL - Operating License | |||
CP - Construction Permit | |||
IN 93-95 December 13, 1993 shorter period of time. Consequently, the Insulators at Pilgrim were cleaned | |||
and coated with RTV again during the spring 1993 refueling outage. As a long- term option, the licensee is considering a replacement of the existing 345 kV | |||
switchyard with a modern compactly designed switchyard which would be more | |||
resistant to the coastal environment. | |||
These events Illustrate the significance of maintaining reliable offsite and | |||
onsite power sources during outages as well as during operation. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
of | one of the technical contacts listed below or the appropriate Office of | ||
Nuclear Regulation (NRR) project manager. | |||
OgItf Ognefw 5 Brian K. Grimeg | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII P. Fillion, RII | |||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR | |||
(904) 795-7677 (301) 504-2779 R. Prevatte, RII | |||
(919) 457-9531 Attachment: | |||
===List of Recently Issued NRC Information Notices=== | |||
*SEE PREVIOUS CONCURRENCE | |||
OFFICE *RII *TECH ED *EELB *C:EELB:NRR | |||
NAME RSchin JBeeson PKang CBerlinger | |||
DATE _07/13/93 08/09/93 11/03/93 /03/93 I_ 1077 1 nlnr *OGCB!DORS *C:OGCB:DORS | |||
JTWiggins NECampbell GHMarcus / /IIIl | |||
11/04/93 11/18/93 11/23/93 12/1'5/93 | |||
1LOUMtNi NAIt: Ns-V*.zN | |||
IN 93-XX | |||
December xx, 1993 shorter period of time. Consequently, the insulators at Pilgrim were cleaned | |||
and coated with protective RTV coating again during the spring 1993 refueling | |||
outage. As an alternate long term option, the licensee is considering a | |||
replacement of the existing 345 kV switchyard with a modern compactly designed | |||
switchyard which would be more resistant to the coastal environment. | |||
These events illustrate the significance of maintaining reliable offsite and | |||
onsite power sources during outages as well as during operation. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII P. Fillion, R11 | |||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR | |||
(904) 795-7677 (301) 504-2779 R. Prevatte, RII | |||
(919) 457-9531 Attachment: | |||
List of Recently Issued NRC Information Notices | |||
*SEE PREVIOUS CONCURRENCE | |||
OFFICE *RII *TECH ED *EELB *C:EELB:NRR | |||
NAME RSchin JBeeson PKang CBerlinger | |||
DATE 07/13/93 -08/09/93 ,11/03/93 11/03/93 D: DE I *OGCB:DORS *C:OGCB:DORS D: DORS | |||
JTWiggins NECampbell l GHMarcus BKGrimes l | |||
11/04/93 11/18/93 11/23/93 112/ /93 | |||
-J | |||
r | |||
UCLUMNI NAMt: bWIl1H1N.NMC /Wr PD | |||
IN 93-XX | |||
the | November xx, 1993 NRC review of these events concluded that the safety-related equipment at the | ||
affected units performed as designed and there were no increased risks to the | |||
public. | |||
This information | This information notice requires no specific action or written response. If | ||
notice | you have any questions about the information in this notice, please contact | ||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: R. Schin, RII P. Fillion, RII | |||
Technical | |||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR | |||
(904) 795-7677 (301) 504-2779 R. Prevatte, R11 | |||
(919) 457-9531 Attachment: | |||
===List of Recently Issued NRC Information Notices=== | |||
*SEE PREVIOUS CONCURRENCE | |||
OFFICE *RII *TECH ED *EELB *C:EELB:NRR | |||
NAME RSchin JBeeson PKang CBerlinger | |||
DATE J07/13/93 o08/09/93 i11/03/930, 11/03/93 | |||
1I | |||
~1* | |||
D: DE *OGCB:DORS C:OGCB:DORS D: DORS | |||
JTWiggins NECampbell GHMarcus BKGrimes L | |||
/ | 11/04/93 111/18/93 11/Z/93 11/ /93 | ||
- - -- -- - - - -- - - | |||
DOCUMENT NAME: SWITCHIN.NEC | |||
IN 93-XX | IN 93-XX | ||
that the safety-related | November xx, 1993 NRC review of these events concluded that the safety-related equipment at the | ||
affected units performed as designed and there were no increased risks to the | |||
public. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII P. Fillion, RII P. Kang, NRR | |||
(404) 331-5561 (404) 331-7288 (301) 504-2779 P. Holmes-Ray, SRI, Crystal River | |||
(904) 795-7677 R. Prevatte, SRI, Brunswick | |||
Notices | (919) 457-9531 Attachment: | ||
List of Recently Issued NRC Information Notices | |||
- | |||
*SEE PREVIOUS CANCUIRRFNCr | |||
OFFICE *RII *TECH ED *EELB *C:EELB:NRR | |||
NAME RSchin JBeeson PKang CBerlinger | |||
D: DORS | DATE 07/13/93 08/09/93 11/03/93 11/03/93 D: DE OGCB:DORS c:OGCB:RSfl n-nnl* z | ||
NECampbell | JTWiggins NECampbell GHMacus BKGrimes | ||
11/04/93 11/1!/93 'f I II/ /93 II/ /93 n 1flPkrilIT ,k*IAr- tLI .- | |||
UUvUtICNI MIAMEi: 3Wl1tlnrN.NLLv | |||
7Vt C , I,/-? d2., ~z Pe | |||
no,& AAW&WetfA. 7 | |||
IN 93-XX | |||
November xx, 1993 This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
contacts | Technical contacts: R. Schin, RII P. Fillion, RII | ||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, SRI, Crystal River | |||
(904) 795-7677 R. Prevatte, SRI, Brunswick | |||
(919) 457-9531 Attachment: | |||
Notices*SEE PREVIOUS | ===List of Recently Issued NRC Information Notices=== | ||
*SEE PREVIOUS CONCURRENCE | |||
OFFICE *RII *TECH ED *EELB *C:EELB:NRR | |||
NAME RSchin JBeeson PKang CBerlinger | |||
DATE 1 07/13/93 - 08/09/93 11/03/93 ,11/03/93 D:DE OGCB:DORS C:OGCB:DORS D:DORS | |||
JTWiggins l NECampbell GHMarcus BKGrimes | |||
A /f/9/ /93 -9I/ /93 U/ /93 DOCUME 3E: SWITCHIN.NEC | |||
IN 93-XX | |||
August xx, 1993 This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII | |||
(404) 331-5561 P. Fillion, RII | |||
(404) 331-7288 di | |||
P. Holmes-Ray, SRI, Crystal River | |||
(904) 795-7677 | |||
6 4' | |||
R. Prevatte, SRI, Brunswick | |||
(919) 457-9531 Attachment: | |||
List of Recently Issued NRC Information Notices | |||
*SFF PREVIOUS CONCURRENCE | |||
--- | |||
OFFICE | |||
- I____ | |||
*RII | |||
I- | |||
W' | |||
IttLLx | |||
I | |||
__ I_ .,-n | |||
LLL;V, | |||
e | |||
"Ir | |||
I o..erg BUD. | |||
II | |||
NAME RSchin JBeeson VS/ PKang CBerlinger | |||
DATE 07/13/ 93 093 ________ __# | |||
__93 _ _/93 | |||
-- 39 nffF Io Onrr FtlORS C!OGCR :DORS D: DORS | |||
vI . -. ____ | |||
__ ._ | |||
JTWiggins NECampbell GHMarcus BKGrimes | |||
08/ /93 08/ /93 08/ /93 08/ /93 DOCUMENT NAML: SMILHIN.iLL | |||
* w | |||
- IN 93-XX | |||
August xx, 1993 This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Regulation (NRR) project manager. | |||
Brian K. Grimes, Director | |||
Division of Operating Reactor Support | |||
Office of Nuclear Reactor Regulation | |||
Technical contacts: R. Schin, RII P. Fillion, RII | |||
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, SRI, Crystal River | |||
(904) 795-7677 R. Prevatte, SRI, Brunswick | |||
Notices | (919) 457-9531 Attachment: | ||
List of Recently Issued NRC Information Notices | |||
*SFF PREVIOUS CONCURRENCE | |||
OFFICE RII *TECH ED EELB C:EELB:NRR | |||
NAME . RSchin JBeeson SSaba (I. ¢ CBerlinger | |||
D: DORS | DATE /93 | ||
______08/7 08/ /93 08/ /93 | |||
-~.1 D: DE OGCB:DORS C:OGCB:DORS D: DORS | |||
NECampbell | JTWiggins NECampbell GHMarcus BKGrimes | ||
08/ /93 08/ /93 08/ /93 1 08/ /93 DOCUMENT NAME: SWITCHIN.NEC}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} | ||
Revision as of 03:23, 24 November 2019
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555 December 13, 1993 NRC INFORMATION NOTICE 93-95: STORM-RELATED LOSS OF OFFSITE POWER EVENTS
DUE TO SALT BUILDUP ON SWITCHYARD INSULATORS
Addressees
All holders of operating licensees or construction permits for nuclear power
reactors located close to a large body of salt water.
PurDose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to the potential for loss of offsite power due to
salt contamination of switchyard insulators. It is expected that recipients
will review the information for applicability to their facilities and consider
actions, as appropriate, to avoid similar problems. However, no specific
action or written response is required.
Description of Circumstances
On March 17, 1993, the Florida Power Corporation Crystal River Unit 3 experienced a loss of the 230 kV switchyard (normal offsite power to safety- related busses) when a light rain caused arcing across salt-laden 230 kV
insulators and opened breakers in the switchyard. At the time, the unit was
in cold shutdown during a maintenance outage. The 'Al emergency diesel
generator was used to power safety-related loads including shutdown cooling
until the 230 kV switchyard was restored. The ABE emergency diesel generator
was unavailable due to maintenance. The 500 kV switchyard supplied nonvital
loads throughout the event.
On March 16 through 18, 1993, Carolina Power and Light Company's Brunswick
Units 1 and 2 experienced a loss of the 230 kV switchyards (all offsite power)
when light rain caused arcing across salt-laden insulators and opened breakers
in the switchyard. At the time, both units were in cold shutdown during an
extended outage. Emergency diesel generators were used to power safety- related loads including shutdown cooling until the offsite power was restored.
Since 1982, the Boston Edison Company Pilgrim station has also experienced
several loss of offsite power events when heavy ocean storms deposited salt on
the 345 kV switchyard causing the insulators to arc to ground.
9312070298 LAe~ffL.A~1241{3/f3P
tE
X1P4 N4 e, 93-95* 777
k IN 93-95 K>
December 13, 1993 Discussion
Intense and unusual storms on March 13 and 14, 1993, produced high tides and
high winds (average of 80 to 97 kilometers/hour high winds (50 to 60
miles/hour], with gusts up to 160 kilometers/hour [100 miles/hour] blowing
ashore from the ocean i.e., Gulf of Mexico and Atlantic Ocean. These storms
caused an unusual buildup of salt on the switchyard insulators at
Crystal River Unit 3 and Brunswick Units 1 and 2. The storms were unusual in
that they included high winds but little or no precipitation. As a result, salt from ocean spray built up on the switchyard insulators and was not washed
away by rain.
Days later, light rain increased the electrical conductivity of the salt, resulting in arcing across the insulators at both sites. To remove the salt
from the insulators, Florida Power Corporation and Carolina Power and Light
Company deenergized the affected switchyards, washed the insulators with high
pressure demineralized water, then returned the switchyards to service. The
washing stopped the electrical arcing across the insulators.
The 500 kV switchyard for Crystal River Unit 3 is located adjacent to the
230 kV switchyard. It was relatively unaffected. The 500 kV switchyard is
used for main generator output when Unit 3 is operating and is used for an
alternate source of offsite power (i.e., backfeeding of nonvital loads) during
Unit 3 outages. The 500 kV switchyard experienced less arcing across the
insulators than the 230 kV switchyard and no tripped breakers. As a
precautionary measure, the licensee also deenergized and washed the 500 kV
switchyard insulators. Factors that may have reduced the storm inpact on the
500 kV switchyard included location (farther away from the shore) and higher
insulation level (the 500 kV insulators were designed for up to 700 kV
operation while the 230 kV insulators were designed for up to 242 kV
operation). In addition, the licensee observed that, of the two types of
230 kV insulators installed, the newer post type had less arcing than the
older cap and pin type.
Licensee followup action in response to these events, to improve the future
performance of non-safety switchyard equipment, included: investigating
available salt buildup monitoring systems, evaluating insulator washing
methods/capabilities, considering the use of room temperature vulcanized (RTV)
silicon rubber coatings, installing newer metal oxide gapless surge arrestors
to replace older silicon carbide gap type surge arrestors, and replacing
cellon-treated wood transmission towers.
The 345 kV switchyard insulators at Pilgrim were coated with RTV silicon
rubber (Sylgard) in 1987. It was expected that the RTV coating, when applied
in 1987, would be effective for a period of 15 years. However, actual
experience at Pilgrim indicates that the coating is effective for a much
`- IN 93-95 December 13, 1993 shorter period of time. Consequently, the Insulators at Pilgrim were cleaned
and coated with RTV again during the spring 1993 refueling outage. As a long- term option, the licensee is considering a replacement of the existing 345 kV
switchyard with a modern compactly designed switchyard which would be more
resistant to the coastal environment.
These events illustrate the significance of maintaining reliable offsite and
onsite power sources during outages as well as during operation.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Bran . Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR
(904) 795-7677 (301) 504-2779 R. Prevatte, RII
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
Attachment
IN 93-95 December 13, 1993 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Informati on Date of
Notice No. Subject Issuance Issued to
93-94 Unauthorized Forced 12/09/93 All holders of OLs or CPs
Entry into the Pro- for nuclear power reactors.
tected Area at Three
Mile Island Unit 1 on
February 7, 1993
93-93 Inadequate Control of 12/08/93 All holders of OLs or CPs
Reactor Coolant System for nuclear power reactors.
Conditions During Shutdown
93-92 Plant Improvements to 12/07/93 All holders of OLs or CPs
Mitigate Common Depend- for nuclear power reactors.
encies in Component
Cooling Water Systems
91-21, Inadequate Quality 12/07/93 All holders of OLs or CPs
Supp. 1 Assurance Program of for nuclear power reactors
Vendor Supplying and all recipients of
Safety-Related Equipment NUREG-0040, "License Con- tractor and Vendor Inspec- tion Status Report" (White
Book).
89-77, Debris in Containment 12/03/93 All holders of OLs or CPs
Supp. 1 Emergency Sumps and for nuclear power reactors.
Incorrect Screen
Configurations
93-91 Misadjustment Between 12/03/93 All holders of OLs or CPs
General Electric 4.16-KV for nuclear power reactors.
Circuit Breakers and Their
Associated Cubicles
93-90 Unisolatable Reactor 12/01/93 All holders of OLs or CPs
Coolant System Leak for nuclear power reactors.
Following Repeated
Applications of Leak
Sealant
OL - Operating License
CP - Construction Permit
IN 93-95 December 13, 1993 shorter period of time. Consequently, the Insulators at Pilgrim were cleaned
and coated with RTV again during the spring 1993 refueling outage. As a long- term option, the licensee is considering a replacement of the existing 345 kV
switchyard with a modern compactly designed switchyard which would be more
resistant to the coastal environment.
These events Illustrate the significance of maintaining reliable offsite and
onsite power sources during outages as well as during operation.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
OgItf Ognefw 5 Brian K. Grimeg
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR
(904) 795-7677 (301) 504-2779 R. Prevatte, RII
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SEE PREVIOUS CONCURRENCE
OFFICE *RII *TECH ED *EELB *C:EELB:NRR
NAME RSchin JBeeson PKang CBerlinger
DATE _07/13/93 08/09/93 11/03/93 /03/93 I_ 1077 1 nlnr *OGCB!DORS *C:OGCB:DORS
JTWiggins NECampbell GHMarcus / /IIIl
11/04/93 11/18/93 11/23/93 12/1'5/93
1LOUMtNi NAIt: Ns-V*.zN
IN 93-XX
December xx, 1993 shorter period of time. Consequently, the insulators at Pilgrim were cleaned
and coated with protective RTV coating again during the spring 1993 refueling
outage. As an alternate long term option, the licensee is considering a
replacement of the existing 345 kV switchyard with a modern compactly designed
switchyard which would be more resistant to the coastal environment.
These events illustrate the significance of maintaining reliable offsite and
onsite power sources during outages as well as during operation.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, R11
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR
(904) 795-7677 (301) 504-2779 R. Prevatte, RII
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SEE PREVIOUS CONCURRENCE
OFFICE *RII *TECH ED *EELB *C:EELB:NRR
NAME RSchin JBeeson PKang CBerlinger
DATE 07/13/93 -08/09/93 ,11/03/93 11/03/93 D: DE I *OGCB:DORS *C:OGCB:DORS D: DORS
JTWiggins NECampbell l GHMarcus BKGrimes l
11/04/93 11/18/93 11/23/93 112/ /93
-J
r
UCLUMNI NAMt: bWIl1H1N.NMC /Wr PD
IN 93-XX
November xx, 1993 NRC review of these events concluded that the safety-related equipment at the
affected units performed as designed and there were no increased risks to the
public.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, RII P. Kang, NRR
(904) 795-7677 (301) 504-2779 R. Prevatte, R11
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SEE PREVIOUS CONCURRENCE
OFFICE *RII *TECH ED *EELB *C:EELB:NRR
NAME RSchin JBeeson PKang CBerlinger
DATE J07/13/93 o08/09/93 i11/03/930, 11/03/93
1I
~1*
D: DE *OGCB:DORS C:OGCB:DORS D: DORS
JTWiggins NECampbell GHMarcus BKGrimes L
11/04/93 111/18/93 11/Z/93 11/ /93
- - -- -- - - - -- - -
DOCUMENT NAME: SWITCHIN.NEC
IN 93-XX
November xx, 1993 NRC review of these events concluded that the safety-related equipment at the
affected units performed as designed and there were no increased risks to the
public.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII P. Kang, NRR
(404) 331-5561 (404) 331-7288 (301) 504-2779 P. Holmes-Ray, SRI, Crystal River
(904) 795-7677 R. Prevatte, SRI, Brunswick
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
-
- SEE PREVIOUS CANCUIRRFNCr
OFFICE *RII *TECH ED *EELB *C:EELB:NRR
NAME RSchin JBeeson PKang CBerlinger
DATE 07/13/93 08/09/93 11/03/93 11/03/93 D: DE OGCB:DORS c:OGCB:RSfl n-nnl* z
JTWiggins NECampbell GHMacus BKGrimes
11/04/93 11/1!/93 'f I II/ /93 II/ /93 n 1flPkrilIT ,k*IAr- tLI .-
UUvUtICNI MIAMEi: 3Wl1tlnrN.NLLv
7Vt C , I,/-? d2., ~z Pe
no,& AAW&WetfA. 7
IN 93-XX
November xx, 1993 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, SRI, Crystal River
(904) 795-7677 R. Prevatte, SRI, Brunswick
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SEE PREVIOUS CONCURRENCE
OFFICE *RII *TECH ED *EELB *C:EELB:NRR
NAME RSchin JBeeson PKang CBerlinger
DATE 1 07/13/93 - 08/09/93 11/03/93 ,11/03/93 D:DE OGCB:DORS C:OGCB:DORS D:DORS
JTWiggins l NECampbell GHMarcus BKGrimes
A /f/9/ /93 -9I/ /93 U/ /93 DOCUME 3E: SWITCHIN.NEC
IN 93-XX
August xx, 1993 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII
(404) 331-5561 P. Fillion, RII
(404) 331-7288 di
P. Holmes-Ray, SRI, Crystal River
(904) 795-7677
6 4'
R. Prevatte, SRI, Brunswick
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SFF PREVIOUS CONCURRENCE
---
OFFICE
- I____
- RII
I-
W'
IttLLx
I
__ I_ .,-n
LLL;V,
e
"Ir
I o..erg BUD.
II
NAME RSchin JBeeson VS/ PKang CBerlinger
DATE 07/13/ 93 093 ________ __#
__93 _ _/93
-- 39 nffF Io Onrr FtlORS C!OGCR :DORS D: DORS
vI . -. ____
__ ._
JTWiggins NECampbell GHMarcus BKGrimes
08/ /93 08/ /93 08/ /93 08/ /93 DOCUMENT NAML: SMILHIN.iLL
- w
- IN 93-XX
August xx, 1993 This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contacts: R. Schin, RII P. Fillion, RII
(404) 331-5561 (404) 331-7288 P. Holmes-Ray, SRI, Crystal River
(904) 795-7677 R. Prevatte, SRI, Brunswick
(919) 457-9531 Attachment:
List of Recently Issued NRC Information Notices
- SFF PREVIOUS CONCURRENCE
OFFICE RII *TECH ED EELB C:EELB:NRR
NAME . RSchin JBeeson SSaba (I. ¢ CBerlinger
DATE /93
______08/7 08/ /93 08/ /93
-~.1 D: DE OGCB:DORS C:OGCB:DORS D: DORS
JTWiggins NECampbell GHMarcus BKGrimes
08/ /93 08/ /93 08/ /93 1 08/ /93 DOCUMENT NAME: SWITCHIN.NEC