Weschler Instruments Model 252 Switchboard MetersML031080024 |
Person / Time |
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Site: |
Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Issue date: |
03/31/1993 |
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From: |
Grimes B Office of Nuclear Reactor Regulation |
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To: |
|
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References |
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IN-93-023, NUDOCS 9303240274 |
Download: ML031080024 (23) |
|
Similar Documents at Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination 2020-09-03 The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>.
[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>. |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555 March 31, 1993 NRC INFORMATION NOTICE NO. 93-23: WESCHLER INSTRUMENTS MODEL 252 SWITCHBOARD METERS
Addressees
All holders of operating licenses or construction permits for nuclear power
reactors. 7
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to possible problems with Weschler Instruments
(Weschler) Model 252 commercial grade switchboard meters. It is expected that
recipients will review the information for applicability to their facilities
and consider actions, as appropriate, to avoid similar problems. However, suggestions contained in this information notice are not NRC requirements;
therefore, no specific action or written response is required.
Description of Circumstances
On November 9, 1992, Weschler informed the NRC of sticking meter movements in
some Model 252 meters manufactured and supplied as commercial grade items.
Although Weschler reported having no evidence that meters manufactured
specifically for safety-related service are affected, Weschler was concerned
that affected commercial grade meters could have been dedicated for use in
nuclear safety-related applications.
Discussion
Weschler determined that some of the commercial grade meters returned for
repair or calibration were inaccurate and erratic. The vendor engineering
report attributed this problem to sticking of the meter movement because of an
off-center torsion spring. Weschler determined that this condition resulted
from a deviation in the dimensions associated with the torsion head screws
combined with several coincidental factors that included (1) degradation of
clip-to-torsion screw lubrication, (2) low initial force from the spring- retaining clip or fatigue of the spring-retaining clip, (3) variations in the
alignment of the meter movement during initial assembly, and (4) the effect of
the summation of the dimensional tolerances in the assembly of the
subcomponents.
9303240274 P P 5tC C* i\ 9I _X3 C9c
IN 93-23 March 31, 1993 To prevent this deficiency in future products, Weschler revised its production
inspection procedures to specifically require checking the dimensions in
question. Weschler also revised its nuclear quality assurance procedures to.
require specific checks of torsion head screw dimensions, although the vendor
has not detected a problem with meters manufactured specifically for safety- related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned for repair and recalibration is to replace the faulty torsion
head screws because they can't be repaired. Upon request, Weschler will give
licensees information about the problem and the recommended corrective
measures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale, NRR
(301) 504-2974 Attachment:
List of Recently Issued NRC Information Notices
K-I
Attachment
IN 93-23 March 31, 1993 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date of
Notice No. Subject Issuance Issued to
93-22 Tripping of Klockner- 03/26/93 All holders of OLs or CPs
Moeller Molded-Case for nuclear power reactors.
Circuit Breakers due to
Support Level Failure
93-21 Summary of NRC Staff 03/25/93 All holders of OLs or CPs
Observations Compiled for light water nuclear
during Engineering Audits power reactors.
or Inspections of Licen- see Erosion/Corrosion
Programs
93-20 Thermal Fatigue Cracking 03/24/93 All holders of OLs or CPs
of Feedwater Piping to for PWRs supplied by
Steam Generators Westinghouse or Combustion
Engineering.
93-19 Slab Hopper Bulging 03/17/92 All nuclear fuel cycle
licensees.
93-18 Portable Moisture-Density 03/10/93 All U.S. Nuclear Regulatory
Gauge User Responsibilities Commission licensees that
during Field Operations possess moisture-density
gauges.
93-17 Safety Systems Response 03/08/93 All holders of OLs or CPs
to Loss of Coolant and for nuclear power reactors.
Loss of Offsite Power
93-16 Failures of Nut-Locking 02/19/93 All holders of OLs or CPs
Devices in Check Valves for nuclear power reactors.
93-15 Failure to Verify the 02/18/93 All holders of OLs or CPs
Continuity of Shunt Trip for nuclear power reactors.
Attachment Contacts in
Manual Safety Injection
and Reactor Trip Switches
93-14 Clarification of 02/18/93 All licensees who possess
10 CFR 40.22, Small source material.
Quantities of Source
Material
OL = Operating License
CP - Construction Permit
~'-2 IN 93-23 March 31, 1993 To prevent this deficiency in future products, Weschler revised its production
inspection procedures to specifically require checking the dimensions in
question. Weschler also revised its nuclear quality assurance procedures to
require specific checks of torsion head screw dimensions, although the vendor
has not detected a problem with meters manufactured specifically for safety- related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned for repair and recalibration is to replace the faulty torsion
head screws because they can't be repaired. Upon request, Weschler will give
licensees information about the problem and the recommended corrective
measures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
orig /s/'d by BKGrimes
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale, NRR
(301) 504-2974 Attachment: % L *
List of Receitly Issudd NRC Information Notices
DOCUMENT NAME: 93-2IN
- D/DRIL:NRR *D/DRCH:NRR *C/OGCB: DORS:NRR
CERossi BABoger GHMarcus
3 03/11/93 02/11/93 03/15/93
- OGCB:DORS:NRR*HICB:DRCH:NRR*SC/HICB:DRCH:NRR*C/HICB:DRCH:NRR*RPB:ADM
AJKugler SVAthavale JMauck JWermiel TechEd
02/08/93 02/08/93 02/10/93 02/10/93 02/08/93
IN 93-XX
March XX, 1993 To prevent this deficiency in future products, Weschler revised its production
inspection procedures to specifically require checking the dimensions in
question. Weschler also revised its nuclear quality assurance procedures to
require specific checks of torsion head screw dimensions, although the vendor
has not detected a problem with meters manufactured specifically for safety- related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned to it for repair and recalibration is to replace the faulty
torsion head screws because they can't be repaired. Upon request, Weschler
will give licensees information about the problem and the recommended
corrective measures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Suppprt
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale
(301) 504-2974 Attachment: List of Recently Issued NRC Information Notices
D/DORS:NRR *D/DRIL:NRR *D/DRCH:NRR C/OGCB:DORS:NRR
BKGrimes CERossi BABoger GHMarcu
03/ /93 03/11/93 02/11/93 / xi 9
- OGCB:DORS:NRR*HICB:DRCH:NRR*SC/HICB:DRCH:NRR*C/HICB:DRCH:NRR*RPB:ADM
AJKugler SVAthavale JMauck JWermiel TechEd
02/08/93 02/08/93 02/10/93 02/10/93 02/08/93
-C
K>~ 1 IN 93-XX
March XX, 1993 To prevent this deficiency in future products, Weschler revised its production
inspection procedures to specifically require checking the dimensions in
question. Weschler also revised its nuclear quality assurance procedures to
require specific checks of torsion head screw dimensions, although the vendor
has not detected a problem with meters manufactured specifically for safety- related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned to it for repair and recalibration is to replace the faulty
torsion head screws because they can't be repaired. Upon request, Weschler
will give licensees information about the problem and the recommended
corrective measures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale
(301) 504-2974 Attachment: List of Recently Issued NRC Information Notices
D/DORS:NRR C' *D/DRCH:NRR C/OGCB:DORS:NRR
BKGrimes BABoger GHMarcus
03/ /93 03//l/93 02/11/93 02/ /93
- OGCB:DORS:NRR*HICB:DRCH:NRR*SC/HICB:DRCH:NRR*C/HICB:DRCH:NRR*RPB:ADM MD:DRIL:NRR gtt
AJKugler SVAthavale JMauck JWermiel TechEd RZinmerman:ld
02/08/93 02/08/93 02/10/93 02/10/93 02/08/93 03/S/93
'S
K>
IN 93-XX
February XX, 1993 To prevent this deficiency in future products, Weschler revised its production
inspection procedures to specifically require checking the dimensions in
question. Weschler also revised its nuclear quality assurance procedures to
require specific checks of torsion head screw dimensions, although the vendor
has not detected a problem with meters manufactured specifically for safety- related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned to it for repair and recalibration is to replace the faulty
torsion head screws because they can not be repaired. Upon request, Weschler
will give licensees information about the problem and the recommended
corrective measures.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale
(301) 504-2974 Attachment: List of Recentl Issued NRC Information Notices
D/DORS:NRR /DRIL:NRR Di q C/OGCB:DORS:NRR
BKGrimes CERossi er +'% GHMarcus
02/ /93 02/ /93 U02/ 1/93 02/ /93
- OGCB:DORS:NRR*HICB:DRCH:NRR*SC/HICB:DRCH:NRR*C/H B:DRCH:NRR*RPB:ADM
AJKugler SVAthavale JMauck JWermiel TechEd
02/08/93 02/08/93 02/10/93 02/10/93 02/08/93 a&_ e P.. TVA
il C 0 "V C__ .1 ~o2 k2%~-m
C6Q
-
IN 93-XX
- -February XX, 1993 To prevent this deficiency in future products, Weschler has revised its
production inspection procedures to specifically require checking the
dimensions in question. In addition, Weschler has revised its nuclear quality
assurance procedures to require specific checks of torsion head screw
dimensions, although the vendor has not detected a problem with meters
manufactured specifically for safety-related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned to it for repair and recalibration is to replace the faulty
torsion head screws because they can not be repaired. Weschler will provide
information about the problem and the recommended corrective measures to
licensees upon request.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale
(301) 504-2974 Attachment: List of Recently Issued NRC Information Notices
D/DORS:NRR D/DRIL:NRR D/DRCH:NRR C/OGCB:DORS:NRR
BKGrimes CERossi BABoger GHMarcus
02/ /93 02/ /93 02/ /93 OGCB:DORS:NRR HICB:DRCH: RR &J .DRCH:NRR C/H RCH:NRR RPB:ADM
AJKugler.it SVAthavale JWe lel TechEd
02/ S/9?3U 02/8 /93 a-. 02/ /9< 02/10/93 02/ /93 Lif
IN 93-XX
February XX, 1993 To prevent this deficiency in future products, Weschler has revised its
production inspection procedures to specifically require checking the
dimensions in question. In addition, Weschler has revised its nuclear quality
assurance procedures to require specific checks of torsion head screw
dimensions, although the vendor has not detected a problem with meters
manufactured specifically for safety-related applications.
Weschler could not determine whether or not any Model 252 switchboard meters
sold as commercial grade items through the various distributors had been
dedicated for use in nuclear safety-related applications. Therefore, Weschler
has not directly notified any licensees about this problem.
Weschler stated that the principal corrective action it has taken for affected
meters returned to it for repair and recalibration is to replace the faulty
torsion head screws because they can not be repaired. Weschler will provide
information about the problem and the recommended corrective measures to
licensees upon request.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
the technical contact listed below or the appropriate Office of Nuclear
Reactor Regulation (NRR) project manager.
Brian K. Grimes, Director
Division of Operating Reactor Support
Office of Nuclear Reactor Regulation
Technical contact: S. V. Athavale
(301) 504-2974 Attachment: List of Recently Issued NRC Information Notices
D/DORS:NRR D/DRIL:NRR D/DRCH:NRR C/OGCB:DORS:NRR
BKGrimes CERossi BABoger GHMarcus
02/ /93 02/ /93 02/ /93 02/ /93 OGCB:DORS:NRR HICB:DRCH:NRR SC/HICB:DRCH:NRR C/HICB:DRCH:NRR RPB:ADM
AJKugler
02/ /93 SVAthavale
02/ /93 JMauck
02/ /93 JWermiel
02/ /93 TechEd 1&'a;n
02/1 /93 ap
a
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list | - Information Notice 1993-01, Accuracy of Motor-Operated Valve Diagnostic Equipment Manufactured by Liberty Technologies (4 January 1993)
- Information Notice 1993-02, Malfunction of a Pressurizer Code Safety Valve (4 January 1993, Topic: Loop seal)
- Information Notice 1993-04, Investigation and Reporting of Misadministrations by the Radiation Safety Officer (7 January 1993, Topic: Uranium Hexafluoride, Overexposure)
- Information Notice 1993-05, Locking of Radiography Exposure Devices (14 January 1993, Topic: Uranium Hexafluoride, Inattentive)
- Information Notice 1993-06, Potential Bypass Leakage Paths Around Filters Installed in Ventilation Systems (22 January 1993)
- Information Notice 1993-07, Classification of Transportation Emergencies (1 February 1993, Topic: Uranium Hexafluoride)
- Information Notice 1993-08, Failure of Residual Heat Removal Pump Bearings Due to High Thrust Loading (1 February 1993, Topic: Probabilistic Risk Assessment)
- Information Notice 1993-09, Failure of Undervoltage Trip Attachment on Westinghouse Model DB-50 Reactor Trip Breaker (2 February 1993, Topic: Commercial Grade)
- Information Notice 1993-10, Dose Calibrator Quality Control (2 February 1993, Topic: Uranium Hexafluoride)
- Information Notice 1993-11, Single Failure Vulnerability of Engineered Safety Features Actuation Systems (4 February 1993)
- Information Notice 1993-12, Off-Gassing in Auxiliary Feedwater System Raw Water Sources (11 February 1993)
- Information Notice 1993-13, Undetected Modification of Flow Characteristics in High Pressure Safety Injection System (16 February 1993)
- Information Notice 1993-14, Clarification of 10 CFR 40.22, Small Quantities of Source Material (18 February 1993)
- Information Notice 1993-15, Failure to Verify the Continuity of Shunt Trip Attachment Contacts in Manual Safety Injection and Reactor Trip Switches (18 February 1993)
- Information Notice 1993-16, Failures of Not-Locking Devices in Check Valves (19 February 1993, Topic: Anchor Darling, Flow Induced Vibration)
- Information Notice 1993-17, Safety Systems Response to Loss of Coolant and Loss of Offsite Power (25 March 1994, Topic: Fire Barrier, Backfit, Water hammer)
- Information Notice 1993-18, Portable Moisture-Density Gauge User Responsibilities During Field Operations (10 March 1993, Topic: Moisture Density Gauge, Moisture-Density Gauge, Stolen)
- Information Notice 1993-19, Slab Hopper Bulging (17 March 1993, Topic: Hydrostatic)
- Information Notice 1993-20, Thermal Fatigue Cracking of Feedwater Piping to Steam Generators (24 March 1993, Topic: Thermal fatigue)
- Information Notice 1993-21, Summary of NRC Staff Observations Compiled During Engineering Audits or Inspections of Licensee Erosion/Corrosion Programs (25 March 1993, Topic: Weld Overlay, Thermal fatigue, Reactive Inspection)
- Information Notice 1993-22, Tripping of Klockner-Moeller Molded-Case Circuit Breakers Due to Support Lever Failure (26 March 1993, Topic: Commercial Grade, Thermal fatigue)
- Information Notice 1993-23, Weschler Instruments Model 252 Switchboard Meters (31 March 1993, Topic: Commercial Grade, Thermal fatigue)
- Information Notice 1993-24, Distribution of Revision 7 of NUREG-1021, Operation Licensing Examiner Standards (31 March 1993, Topic: Job Performance Measure, Thermal fatigue)
- Information Notice 1993-25, Electrical Penetration Assembly Degradation (1 April 1993, Topic: Thermal fatigue)
- Information Notice 1993-26, Grease Soldification Causes Molded-Case Circuit Breaker Failure to Close (31 January 1994)
- Information Notice 1993-27, Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization (8 April 1993, Topic: Reactor Vessel Water Level, Thermal fatigue)
- Information Notice 1993-28, Failure to Consider Loss of DC Bus in the Emergency Core Cooling System Evaluation May Lead to Nonconservative Analysis (9 April 1993, Topic: Fuel cladding, Thermal fatigue)
- Information Notice 1993-29, Problems with the Use of Unshielded Test Leads in Reactor Protection System Circuitry (12 April 1993)
- Information Notice 1993-30, NRC Requirements for Evaluation of Wipe Test Results; Calibration of Count Rate Survey Instruments (12 April 1993)
- Information Notice 1993-31, Training of Nurses Responsible for the Care of Patients with Brachytherapy Implants (13 April 1993, Topic: Brachytherapy)
- Information Notice 1993-32, Nonconservative Inputs for Boron Dilution Events Analysis (21 April 1993, Topic: Shutdown Margin)
- Information Notice 1993-33, Potential Deficiency of Certain Class Ie Instrumental and Control Cables (28 April 1993)
- Information Notice 1993-33, Potential Deficiency of Certain Class IE Instrumental and Control Cables (28 April 1993, Topic: Brachytherapy)
- Information Notice 1993-34, Potential for Loss of Emergency Cooling Function Due to a Combination of Operational and Post-LOCA Debris in Containment (6 May 1993, Topic: Brachytherapy)
- Information Notice 1993-35, Insights from Common-Cause Failure Events (12 May 1993, Topic: Brachytherapy)
- Information Notice 1993-36, Notifications, Reports, and Records of Misadministrations (7 May 1993, Topic: Brachytherapy)
- Information Notice 1993-37, Eyebolts with Indeterminate Properties Installed in Limitorque Valve Operator Housing Covers (19 May 1993, Topic: Brachytherapy)
- Information Notice 1993-38, Inadequate Testing of Engineered Safety Features Actuation Systems (24 May 1993)
- Information Notice 1993-39, Radiation Beams From Power Reactor Biological Shields (25 May 1993)
- Information Notice 1993-39, Radiation Beams from Power Reactor Biological Shields (25 May 1993)
- Information Notice 1993-40, Fire Endurance Test Results for Thermal Ceramics FP-60 Fire Barrier Material (26 May 1993, Topic: Safe Shutdown, Fire Barrier, Fire Protection Program)
- Information Notice 1993-41, One Hour Fire Endurance Test Results for Thermal Ceramics Kaowool, 3M Company FS-195 and 3M Company Interam E-50 Fire Barrier Systems (28 May 1993, Topic: Safe Shutdown, Fire Barrier)
- Information Notice 1993-42, Failure of Anti-Rotation Keys in Motor-Operated Valves Manufactured by Yelan (9 June 1993)
- Information Notice 1993-43, Use of Inappropriate Lubrication Oils in Satety-Related Applications (10 June 1993, Topic: Commercial Grade)
- Information Notice 1993-44, Operational Challenges During a Dual-Unit Transient (15 June 1993)
- Information Notice 1993-45, Degradation of Shutdown Cooling System Performance (16 June 1993, Topic: Local Leak Rate Testing)
- Information Notice 1993-46, Potential Problem with Westinghouse Rod Control System and Inadvertent Withdrawal of Single Rod Control Cluster Assembly (10 June 1993)
- Information Notice 1993-47, Unrecognized Loss of Control Room Annunciators (18 June 1993)
- Information Notice 1993-48, Failure of Turbine-Driven Main Feedwater Pump to Trip Because of Contaminated Oil (6 July 1993, Topic: Water hammer)
- Information Notice 1993-49, Improper Integration of Software Into Operating Practices (8 July 1993)
... further results |
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