|
|
Line 20: |
Line 20: |
| ==Dear Sir:== | | ==Dear Sir:== |
|
| |
|
| SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-024-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a} (2) (iv) and 50.73(a) (2) (i) (B}. This report is required to be issued within thirty (30) days of event discovery. | | SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-024-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a} (2) (iv) and 50.73(a) (2) (i) (B}. This report is required to be issued within thirty (30) days of event discovery. |
| Sincerely yours, C. A Vondra General Manager - | | Sincerely yours, C. A Vondra General Manager - |
| Salem Operations MJP:pc Distribution | | Salem Operations MJP:pc Distribution |
Line 116: |
Line 116: |
| At the time of the event a severe thunderstorm was in progress. | | At the time of the event a severe thunderstorm was in progress. |
| Investigation revealed that lightning had struck in the vicinity of the phase B Generator Step-Up (GSU) transformer {EL}. Evidence of the lightning strike included carbonization of the high voltage bushing, damage to the corona rings and lightning arrestor and eyewitness accounts. | | Investigation revealed that lightning had struck in the vicinity of the phase B Generator Step-Up (GSU) transformer {EL}. Evidence of the lightning strike included carbonization of the high voltage bushing, damage to the corona rings and lightning arrestor and eyewitness accounts. |
| The Nuclear Regulatory Commission (NRC) was notified of the actuation of the Reactor Protection System (RPS) {JC} at 2037 hours on June 16, 1991 in accordance with Code of Federal Regulations lOCFR | | The Nuclear Regulatory Commission (NRC) was notified of the actuation of the Reactor Protection System (RPS) {JC} at 2037 hours on June 16, 1991 in accordance with Code of Federal Regulations 10CFR |
| : 50. 72 (b) (2) (ii). | | : 50. 72 (b) (2) (ii). |
| APPARENT CAUSE OF OCCURRENCE: | | APPARENT CAUSE OF OCCURRENCE: |
Line 157: |
Line 157: |
| Technical Specific~tion 3.8.1.1 Action "a" states: | | Technical Specific~tion 3.8.1.1 Action "a" states: |
| "With either an offsite circuit or diesel generator of the above required A.C. electrical power sources inoperable, demonstrate the OPERABILITY of the remaining A.C. sources by performing Surveillance Requirements 4.8.1.1.1.a and 4.8.1.1.2.a2 within one hour and at least once per 8 hours thereafter; restore at least two offsite circuits and three diesel generators to OPERABLE status within 72 hours or be in at least HOT STANDBY within the next 6 hours and in COLD SHUTDOWN within the following 30 hours." | | "With either an offsite circuit or diesel generator of the above required A.C. electrical power sources inoperable, demonstrate the OPERABILITY of the remaining A.C. sources by performing Surveillance Requirements 4.8.1.1.1.a and 4.8.1.1.2.a2 within one hour and at least once per 8 hours thereafter; restore at least two offsite circuits and three diesel generators to OPERABLE status within 72 hours or be in at least HOT STANDBY within the next 6 hours and in COLD SHUTDOWN within the following 30 hours." |
| Due to plant conditions, the Unit 1 Diesel Generators were successfully tested within one hour of Unit stabilization following the loss of the No. 2 Station Power Transformer {i.e., one of the two sources of offsite power) as per the Action Statement (on June 16, 1991 at 2154, 2155, and 2156 hours respectively). Preparations for testing the Diesel Generators was initiated approximately one hour and twenty minutes after the loss of the No. 2 Station Power Transformer. The delay in the testing of the Unit 1 diesel generators was therefore due to the time required to stabilize the Unit. However, it does constitute a noncompliance which is reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations lOCFR 50.73(a) (2) (i) (B). | | Due to plant conditions, the Unit 1 Diesel Generators were successfully tested within one hour of Unit stabilization following the loss of the No. 2 Station Power Transformer {i.e., one of the two sources of offsite power) as per the Action Statement (on June 16, 1991 at 2154, 2155, and 2156 hours respectively). Preparations for testing the Diesel Generators was initiated approximately one hour and twenty minutes after the loss of the No. 2 Station Power Transformer. The delay in the testing of the Unit 1 diesel generators was therefore due to the time required to stabilize the Unit. However, it does constitute a noncompliance which is reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (i) (B). |
| Early in the Unit 1 event, the SNSS did initiate actions to perform an operability check of the Salem Unit 2 diesel generators. This was required, per Technical Specifications (identical to the Unit 1 Action requirements), due to the loss of the offsite power source (i.e., No. 2 Station Power Transformer). The Unit 2 Diesel Generators were successfully tested within one hour. | | Early in the Unit 1 event, the SNSS did initiate actions to perform an operability check of the Salem Unit 2 diesel generators. This was required, per Technical Specifications (identical to the Unit 1 Action requirements), due to the loss of the offsite power source (i.e., No. 2 Station Power Transformer). The Unit 2 Diesel Generators were successfully tested within one hour. |
| Also, following the loss of No. 2 SPT and the subsequent transfer of the No. 2B Vital Bus from the No. 22 SPT to the No. 21 SPT, a Containment Purge/Pressure Vacuum Relief {CP/P-VR) isolation signal from the 2R41C Radiation Monitoring System (RMS) {IL} Plant Vent noble gas monitor actuated. At the time of this event, the CP/P-VR valves were closed. The root cause of the CP/P-VRS actuation is attributed to equipment design. As indicated in prior LERs (e.g., | | Also, following the loss of No. 2 SPT and the subsequent transfer of the No. 2B Vital Bus from the No. 22 SPT to the No. 21 SPT, a Containment Purge/Pressure Vacuum Relief {CP/P-VR) isolation signal from the 2R41C Radiation Monitoring System (RMS) {IL} Plant Vent noble gas monitor actuated. At the time of this event, the CP/P-VR valves were closed. The root cause of the CP/P-VRS actuation is attributed to equipment design. As indicated in prior LERs (e.g., |
Line 166: |
Line 166: |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 7 of 8 ANALYSIS OF OCCURRENCE: (cont'd) | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 7 of 8 ANALYSIS OF OCCURRENCE: (cont'd) |
| ~~~~~~~~ | | ~~~~~~~~ |
| corrective maintenance. The building includes the power for transmission (i.e., microwave) for the Emergency Notification System (ENS) telephone system~ With the loss of the Group Bus, the house power supply was lost. Subsequently, the ENS phone system was made inoperable. Emergency notifications, required by the Code of Federal Regulations lOCFR 50.72, were made over the PSE&G private CENTREX microwave system. | | corrective maintenance. The building includes the power for transmission (i.e., microwave) for the Emergency Notification System (ENS) telephone system~ With the loss of the Group Bus, the house power supply was lost. Subsequently, the ENS phone system was made inoperable. Emergency notifications, required by the Code of Federal Regulations 10CFR 50.72, were made over the PSE&G private CENTREX microwave system. |
| Phone 'systems lost in addition to the ENS, due to the power loss to the Di!t)erisi:on Building Telephone House, included the "DID" system, the.Nuclear Emergency Telephone System {NETS) to all on-site Emergency Response Facilities, the NAWAS (Delaware Backup) system and the U.S. Coast Guard Repeater. | | Phone 'systems lost in addition to the ENS, due to the power loss to the Di!t)erisi:on Building Telephone House, included the "DID" system, the.Nuclear Emergency Telephone System {NETS) to all on-site Emergency Response Facilities, the NAWAS (Delaware Backup) system and the U.S. Coast Guard Repeater. |
| As stated above, the ENS phone lines were disabled due to unavailability of the Dimension Building Telephone House power supply and the diesel generator. This supply had been cleared and tagged in support of corrective maintenance. | | As stated above, the ENS phone lines were disabled due to unavailability of the Dimension Building Telephone House power supply and the diesel generator. This supply had been cleared and tagged in support of corrective maintenance. |
| In conclusion, the Salem Unit 1 reactor trip of June 16, 1991, caused by an act of nature, resulted in limited consequence. The health and safety of the public was not affect~d. Once the event occurred the plant protective design features and operator performance were adequate. However, due to the actuation of the RPS and actuation of an ESF signal (CP/P-VR isolation}, this report has been prepared in accordance with Code of Federal Regulations lOCFR 50.73(a) (2) (iv) requirements. | | In conclusion, the Salem Unit 1 reactor trip of June 16, 1991, caused by an act of nature, resulted in limited consequence. The health and safety of the public was not affect~d. Once the event occurred the plant protective design features and operator performance were adequate. However, due to the actuation of the RPS and actuation of an ESF signal (CP/P-VR isolation}, this report has been prepared in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (iv) requirements. |
| CORRECTIVE ACTION: | | CORRECTIVE ACTION: |
| The damage to the Phase B GSU transformer was repaired. | | The damage to the Phase B GSU transformer was repaired. |
Similar Documents at Salem |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station July 15, 1991 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-024-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a} (2) (iv) and 50.73(a) (2) (i) (B}. This report is required to be issued within thirty (30) days of event discovery.
Sincerely yours, C. A Vondra General Manager -
Salem Operations MJP:pc Distribution
. ~ :: - : : c* *-' . r&~
j_ .. 95* 2189 I 1OM I 12-ec
NRC F.ORM 366 (6.ari LICENSEE EVENT REPORT (LER)
- U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PEA RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE I
OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) I PAGE (31 Salem Generating Station - Unit 1 015101010121 71 2 1 OF 018 TITLE (41 Reactor Trip From 100% Power Due To Lightning Strike EVENT DATE 151 LER NUMBER 161 REPORT DATE (7) OTl;tER FACILITIES INVOLVED 18)
~f~t~
SEQUENTIAL REVISION MONTH DAY YEAR YEAR NUMBER \\ NUMBER MONTH DAY YEAR FAC1 LITY NAMES DOCKET NUMBERIS)
Salem Unit 2 o I 5 Io Io I o I 31l11 o I 6 ii - oi - olo ol 6 9 1 911 21 4 7 ii 5 911 0151010101 I I THIS REPORT IS SUBMITTED PURSUANT TO THE RloQUl_REMENTS OF 10 CFR §:(Chock one or more of th* following} (111 OPERATING POWER LEVEL MODE (8)
I 110 10 -
1 20.402(b) 20 ..C05(o)(1 )(i)
~
..__
20.405(c) 50.36(cll1l
,_x
.....__
50.731*112Hivl 50.731*112)(v) -
,__
73.71(b) 73.71(c)
- -:.:-:-:-:-:
- -:-:-:-::-:-
.;.:.:-:.:-:-
(10)
- :*:*:*:*:*:*:*:*
- -:* -:::::*
20.405(1)(1 )(iii 20.405(0111 )(iii)
.___
x
.___
50.38lc)(2) 50.731*)(2)(1)
-- 50.73(*112llvii) 50.73loll2)(viiillAI
..__ OTHER (S~cify in Abstroct below and in Text, NRC Form 366A}
.:.:-:-:-:-:-
- -:-::.:-:-:
-:-::*:-:-:-:-:
- -:-:-:-:-:
~,:,::::::::::::::::::::::::::::::::::::
-:-:-:
~
20 ..C06(o)(1 )(iv) 20.405(01(1 )Iv)
,____ 50.73(o)(2llii) 50.73(e)(211iiil - 50.73(o)(2)(viiil (Bl 50.73lo)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE M. J. Pollack - LER Coordinator 6 I 019 I 3 19 t- I 2 I 0 I 2 12 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113)
- :::::::::::::::: :::::::: :-:-:*::::*:: :-:-:.*--:-: -:-:::-
MANUFAC- REPORTABLE :-:::*:-::-:- :::::::::-:-:-:: :-:- :::::::: MANUFAC* REPORTABLE 1:::-::*::::::
- -
- -
CAUSE SYSTEM COMPONENT TO NPRDS -:-:-:-:-:-:- :;:;:::::::::::: .;.::-:.:-:- CAUSE SYSTEM COMPONENT TUA ER -:-::.;.:. -:*:" -:-:
TUA ER TO NPRDS ,:-::-:-:-:- :::::::::-:*
,:,:-:::::::: :::::::::::::::: :,:::::: :;:::
- }/:': '//:/: ::::":) :;:,::::::: ( /)) *::::
- -:- :::::::::::: :-:--:-: -::::: ::::*:*:
- -: :::.;.;..:-: 1-:-: :-:-::::::::::::: *:*::*:*:
I I I I I I I *'.*'.
- -:-:-: I I I I I I I :*:*:-:-:-: ::::.::::
- -:-:::::,::::: -'.:::::::::::-:- ;::::-:- '.-'.*:;:::::::::::::*:*:*:*:
I I I I I I I
- -:::-:- :::::::::::::: :::::::
- -:-: -:-:-::::::::::: -:-:-:-:-: ::::::::
- ::::::::::::::: ::--::::::::: :;:::::: I I I I I I I
>' :\::i:i:}!:'*mrn:,:,:;:fi::i:
1:-::*:-
SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED
_n ~
SUBMISSION DATE 1151 YES (If yes, comp/ere EXPECTED SUBMISSION DATE! NO I I I ABSTRACT (Limit ro 1400 spaces, i.e., soproximately fifreen single-space typewritten lines) 1161 On June 16, 1991, at 1940 hours0.0225 days <br />0.539 hours <br />0.00321 weeks <br />7.3817e-4 months <br />, during normal full power operation, Salem Unit 1 experienced a Reactor Trip/Turbine Trip. The first out overhead annunciation was "4KV Group Bus Undervoltage". At the time of the event a severe thunderstorm was in progress. Investigation revealed that lightning had struck in the vicinity of the phase B Generator Step-Up (GSU) transformer {EL}
- Evidence of the lightning strike included carbonization of the high voltage bushing, damage to the corona rings and lightning arrestor and eyewitness accounts. The root cause of the reactor trip event is attributed to an act of nature; i
- e *I a lightning strike in the vicinity of the phase B GSU transformer, resulted in a 4KV Group Bus Undervoltage and subsequent reactor trip. Lightning protection was assessed by engineering and found to be appropriate. The damage to the Phase B GSU transf orrner was repaired. Subsequently, on June 24, 1991r the Unit 1 was returned to service. Also as a result of the lightning strike, 500 KV breaker flashover protection was initiated due to sufficient current through the transformer neutral. This resulted in the loss of the No. 2 Station Power Transformer and subsequent de-energization of the 1F and lG Group Busses. An engineering review has been initiated to prevent flashover protection actuation from a coasting generator. Design changes will be implemented as appropriate.
NRC Form 366 (6.891
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
..
Salem Generating Station DOCKET NUMBER LER NUMBER PAGE U~n_i_t_1_ _ _ _ _ _ _ _ _ _ _ _ _ _~5~0:~0~0~2~7~2:::___ _ _ _~9~1~-~0=.--=2fl-00_ _ _ _=2--'0.of 8 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xxl IDENTIFICATION OF OCCURRENCE:
Reactor Trip from 100% power due to lightning strike Event Date: 6/16/91 Report Date: 7/15/91 This report was initiated by Incident Report Nos.91-441, 91-442,91-443, 91-444, and 91-479.
CONDITIONS
- - - - - - - - - -PRIOR
- - - - -TO--- OCCURRENCE:
Mode 1 Reactor Power 100% - Unit Load 1142 MWe DESCRIPTION OF- - -OCCURRENCE:
- - - * * - - - -- --- ~-
On June 16, 1991 at 1940 hours0.0225 days <br />0.539 hours <br />0.00321 weeks <br />7.3817e-4 months <br />, during normal full power operation, Salem Unit 1 experienced a Reactor Trip/Turbine Trip. The first out overhead annunciation was "4KV G:roup Bus Undervoltage".
At the time of the event a severe thunderstorm was in progress.
Investigation revealed that lightning had struck in the vicinity of the phase B Generator Step-Up (GSU) transformer {EL}. Evidence of the lightning strike included carbonization of the high voltage bushing, damage to the corona rings and lightning arrestor and eyewitness accounts.
The Nuclear Regulatory Commission (NRC) was notified of the actuation of the Reactor Protection System (RPS) {JC} at 2037 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.750785e-4 months <br /> on June 16, 1991 in accordance with Code of Federal Regulations 10CFR
- 50. 72 (b) (2) (ii).
APPARENT CAUSE OF OCCURRENCE:
The root cause of the Salem Unit 1 June 16, 1991 reactor trip event is attributed to an act of nature. At 1940 hours0.0225 days <br />0.539 hours <br />0.00321 weeks <br />7.3817e-4 months <br />, a lightning strike in the vicinity of the phase B GSU transformer, resulted in a 4KV Group Bus Undervoltage and subsequent reactor trip. Lightning protection was assessed by engineering and was found to be appropriate.
Refer to the attached schematic, for additional details, when reviewing this section and the Analysis of Occurrence section.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 3 of 8 SEQUENCE OF EVENTS: (cont'd)
Date/Time Event 7-16/1940 Lightning strike in vicinity of Phase B of the Main Power Transformer (i.e., GST}
Electrical fault on 500 KV Main Power Transformer Unit 1 Generator Differential Regular and Backup Trip Relays actuate 500 KV Breakers open (lOX and 12X); Generator Field Breaker opens and Turbine Trip signal initiated 4KV Group Busses transfer initiates; from the Auxiliary Power Transformer to the Nos. 11 and 12 Station Power Transformers Rx Trip Breakers open 4KV Group Bus transfer complete and Bus voltage returns to normal Flashover protection relays and alarms (Salem Units 1 and 2) actuate (to + 4 seconds) 12 and 22 Station Power Transformers trip 18 Vital Bus Transfers.to 11 SPT 2B Vital Bus Transfers to 21 SPT lF and lG Group Busses deenergize and alarm in Control Room ANALYSIS OF OCCURRENCE:
Following the GSU transformer lightning strike, the resultant phase to ground fault operated the generator differential regular and backup instantaneous trip relays on Phases B and C GSU transformers opening the lOX and 12X 500 KV breakers, opening the generator field breaker and causing a Unit 1 turbine trip (Unit Isolation Trip). The Unit Isolation Trip subsequently initiated a Group Bus transfer (i.e., fast transfer scheme) from the Auxiliary Power Transformer to the Nos. 11 and 12 Station Power Transformers, respectively.
It is not uncommon, when you have single phase to ground faults, for only two (2) of the three (3) phases to pick-up the instantaneous relays initiating the Unit Isolation Trip (i.e., Phase A instantaneous relays did not pick-up) .
At the time of the Phase B phase to ground fault, voltages on the
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 4 of 8 ANALYSIS OF OCCURRENCE: (cont'd) electric distribution system for the four (4) 4KV Group Busses and the three (3) 4KV Vital Busses decayed. All 4KV Vital Bus voltages recovered within 4 cycles while the Group Bus voltages recovered after completion of the fast transfer (in approximately 12 cycles). This degraded Group Bus voltage (below 70% rated voltage) lasted sufficiently long to initiate a Reactor Trip signal via the Group Bus undervoltage relays.
Also as a result of the lightning strike, 500 KV breaker (lOX and 12X) flashover protection initiated due to sufficient current through the transformer neu"tral. The flashover protection occurred four (4) seconds following the fault, on the phase B GSU transformer, causing:
- 1) all adjacent 500 KV breakers to open; 2) loss of half of the 13 KV ring bus (13 KV 4-5 and 3-4 breakers opened); 3) lockout of the Unit 3 (Gas Turbine) 13 KV breaker; 4) the New Freedom Line was remote tripped to the New Freedom Substation; and 5) i~olation of the Salem New Freedom Line from Section 2 (of the 500 KV Switchyard) .
Flashover protection actuation should have occurred approximately 13 cycles after fault occurrence. It could not be determined why flashover protection was delayed; however, the delay did not have an impact on this event. Testing was performed but the circuits timed correctly and the event could not be duplicated.
The loss of 500 KV power to Section 1' (of the 500 KV Switchyard) resulted in the loss of the No. 2 Station Power Transformer {SPT).
With the loss of the No. 2 SPT, 13 KV power to the Nos. 12 and 22 SPTs was lost.
After the loss of the No: 12 SPT, the lF and lG Group Busses de-energized (i.e., the Auxiliary Power Transformer was already de-energized due to the Unit Isolation Tri~ signal) and the lB Vital Bus s~ccessfully transferred from the No. 12 SPT to the No. 11 SPT.
Due to the loss of the No. 22 SPT, the 2B Vital Bus successfully transferred from No. 22 SPT to the No. 21 SPT.
An extensive analysis provided by oscillograph, digital fault recordeJ*
and sequence of events recorder records indicated that the relay operations were correct for the conditions. Although the breaker flashover scheme is designed to protect against the flashover of either 500 KV generator breaker, it also operates for a fault between the 500 KV generator breakers and the main transformer when the fault current is supplied by the generator. There was no evidence, either oscillographic or physical, of the flashover of either 500 KV generator breaker. Therefore it is concluded that the flashover relay scheme was operated by the current contributed by the coasting generator. An Engineering review, along with appropriate modifications, has been initiated.
After the loss of the "lF" and "lG" Group Busses, the following
--
LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 5 of 8 ANALYSIS OF OCCURRENCE: (cont'd) significant equipment was de-~nergized:
- 1. Nos. 13 and 14 Reactor Coolant Pumps {RCPs); The loss of No. 13 RCP resulted in limited pressurizer spray capability; however, the No. 11 RCP was available for pressurizer spray and was successfully used.
- 2. Control Pressurizer Heaters and pne set of Backup Pressurizer Heaters
- 3. Plant Vent composite sample pump; this pump is required to remain operable as per Technical Specification 3.3.3.9 Table 3.3-13. Chemistry was notified and alternate sampling was initiated. The pump was returned to service when lF Group Bus was restored {at 0041 hours4.74537e-4 days <br />0.0114 hours <br />6.779101e-5 weeks <br />1.56005e-5 months <br /> on June 17, 1991)
An excessive cooldown occurred following the reactor trip. This was due to Auxiliary Feedwater making up for Steam Generator shrink from the trip and loss of Nos. 13 and 14 Reactor Coolant Pumps. In accordance with the guidance provided by the EOPs, closure of the main steam isolation valves was successfully performed. Excessive cooldown is a concern identified from prior plant trips. Engineering has assessed this phenomenon and concluded that it does not pose a safety concern; however, corrective actions are being pursued (reference LER 311/91-029-00).
The 11MS10 atmospheric relief valve (SB} changed operational modes from automatic to manual and then went full open while reducing its setpoint (to 1005 psig) to control Stearn Generator pressure. A work order was initiated to investigate and correct this concern.
Operator actions following the automatic actuation of the reactor trip began with the NCO initiating a manual trip. Procedure EOP-TRIP-1 was then entered followed by entry into EOP-TRIP-2. Actions required by these procedures were complied with including closure of the main steam isolation valves due to Tavg excessive cooldown. Operators compensated for the inadvertent full opening of the 11MS10 valve (following its setpoint adjustment}, and subsequent lower level in No.
11 Steam Generator, by adjusting the Auxiliary Feedwater flow to the No. 11 Steam Generator. With the loss of the 1F and 1G Group Busses, the Control Pressurizer Heaters and one set of Backup Pressurizer Heaters were unavailable. Also, as stated above, the No. 13 RCP became unavailable. Using the available Backup Pressurizer Heaters and the No. 11 RCP Pressurizer spray capability Operators were abJ.e to to maintain RCS pressure control.
After completing the actions required by EOP-TRIP-1 and EOP-TRIP-2, IOP-8 was entered. Using this procedure, the plant was stabilized (in Mode 3) with the twc (2) operating Reactor Coolant Pumps (i.e., Nos.
13 and 14 RCPs were not operating due to the loss of the 1F and 1G Group Busses). After stabilization of the plant, Technical Specifications were reviewed and required actions performed due to the loss of an off-site power source (Technical Specification 3.8.1.1 Action "a").
DOCKET NUMBER
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station LER NUMBER PAGE Unit 1 5000272 91-024-00 6 of 8 ANALYSIS OF OCCURRENCE: (cont'd)
Technical Specific~tion 3.8.1.1 Action "a" states:
"With either an offsite circuit or diesel generator of the above required A.C. electrical power sources inoperable, demonstrate the OPERABILITY of the remaining A.C. sources by performing Surveillance Requirements 4.8.1.1.1.a and 4.8.1.1.2.a2 within one hour and at least once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> thereafter; restore at least two offsite circuits and three diesel generators to OPERABLE status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
Due to plant conditions, the Unit 1 Diesel Generators were successfully tested within one hour of Unit stabilization following the loss of the No. 2 Station Power Transformer {i.e., one of the two sources of offsite power) as per the Action Statement (on June 16, 1991 at 2154, 2155, and 2156 hours0.025 days <br />0.599 hours <br />0.00356 weeks <br />8.20358e-4 months <br /> respectively). Preparations for testing the Diesel Generators was initiated approximately one hour and twenty minutes after the loss of the No. 2 Station Power Transformer. The delay in the testing of the Unit 1 diesel generators was therefore due to the time required to stabilize the Unit. However, it does constitute a noncompliance which is reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (i) (B).
Early in the Unit 1 event, the SNSS did initiate actions to perform an operability check of the Salem Unit 2 diesel generators. This was required, per Technical Specifications (identical to the Unit 1 Action requirements), due to the loss of the offsite power source (i.e., No. 2 Station Power Transformer). The Unit 2 Diesel Generators were successfully tested within one hour.
Also, following the loss of No. 2 SPT and the subsequent transfer of the No. 2B Vital Bus from the No. 22 SPT to the No. 21 SPT, a Containment Purge/Pressure Vacuum Relief {CP/P-VR) isolation signal from the 2R41C Radiation Monitoring System (RMS) {IL} Plant Vent noble gas monitor actuated. At the time of this event, the CP/P-VR valves were closed. The root cause of the CP/P-VRS actuation is attributed to equipment design. As indicated in prior LERs (e.g.,
311/90-033-00), the Salem Unit 2 RMS Victoreen equipment is prone to failure on voltage transients. CP/P-VR isolation is an Engineered Safety Feature; therefore, the NRC was notified of this actuation at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br /> on June 16, 1991 in accordance with Code of Federal Regulations 10CFR 50. 72 (b} (2} (ii).
Following the CP/P-VR isolation signal, the channel was reset and returned to service.
At the time of the lightning strike, the lF Group Bus was supplying power to the Dimension Building Telephone House due to the normal UPS and di~sel generator being cleared and tagged in support of
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-024-00 7 of 8 ANALYSIS OF OCCURRENCE: (cont'd)
~~~~~~~~
corrective maintenance. The building includes the power for transmission (i.e., microwave) for the Emergency Notification System (ENS) telephone system~ With the loss of the Group Bus, the house power supply was lost. Subsequently, the ENS phone system was made inoperable. Emergency notifications, required by the Code of Federal Regulations 10CFR 50.72, were made over the PSE&G private CENTREX microwave system.
Phone 'systems lost in addition to the ENS, due to the power loss to the Di!t)erisi:on Building Telephone House, included the "DID" system, the.Nuclear Emergency Telephone System {NETS) to all on-site Emergency Response Facilities, the NAWAS (Delaware Backup) system and the U.S. Coast Guard Repeater.
As stated above, the ENS phone lines were disabled due to unavailability of the Dimension Building Telephone House power supply and the diesel generator. This supply had been cleared and tagged in support of corrective maintenance.
In conclusion, the Salem Unit 1 reactor trip of June 16, 1991, caused by an act of nature, resulted in limited consequence. The health and safety of the public was not affect~d. Once the event occurred the plant protective design features and operator performance were adequate. However, due to the actuation of the RPS and actuation of an ESF signal (CP/P-VR isolation}, this report has been prepared in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (iv) requirements.
CORRECTIVE ACTION:
The damage to the Phase B GSU transformer was repaired.
Subsequently, on June 24, 1991, the Unit 1 was returned to service ..
A review of the lightning protection features, in use at Salem Station, was conducted by Engineering & Plant Betterment. It was found that these features are appropriate for transformer protection.
An Engineering review has been initiated to assess the prevention of flashover protection actuation for a fault between the 500 KV generator breakers and the main transformer when the fault current is supplied by the generator. Design changes will be implemented as appropriate.
The Procedure Upgrade Project (PUP) effort will restructure the system operating procedures for the electrical system to provide necessary guidance for energizing dead busses including all necessary relays (with reset and prerequisite condition requirements).
Investigation of the inadvertent llMSlO valve opening (fulJ.), when changing its setpoint, revealed that the manual/auto controller" had failed. It was subsequently replaced.
~~~~4 *~~~
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 91-02_4-90 8 of 8 ijJ EM NJ 1l Z LH"S ATTACHMENT - ?CHEMAT~C sm~\ko .....
. um ll um SEC'T., **
r--~----~----:..;r-r--~-------J"\--Jr~-~---------~--i l X ~ SEc1.s.-*:-;--------:;--*******--. .__a
- ) . )i) . .) -) i II ~
....,......,,. I I ..., I I I I . . . 1' I . -
~"'~SECT.I""" -J
'-""' !IX -
.. *T. r***-.J'"\.----.......-r.,.-~-------~----**-*--*--***-----~
20ll
.r**I
~r))
ol
- ) ~_.
f
)) !I lie I ,..,. -I I _, .
. I
~--***-t-************************************1 glI I . I ~ 1 sm sm.
I t- -~w:-- - -
JX
.J"'\. - -
JO
-~........-,.-r-'=--
-
......."='-"r wA'-~~ - - - - - - - -~:('- -
-1I _) ) I~- I
. \+ . ) iI I ~--************~*********************~*-*******
I IC.IJ.It6ln. t.~PWR. I I ,
- ,---.,----- : :!
111.
I ~'t. ~::,. I I
~,,. l*~."'
~ '-.-"".t' ~\..
i ----*,----
...~
IC NO IC I
,_..+..,
M IM. !M
- NJ.I Gtll.llAM TIUJ6F ORl.U sm.2 SEtT.3 -*
...
- lll.IGtll.~ ~.
!RAHS/"...,_,, ., !N. IM. /N.-
I 'Wiµ W Wi" ,.,.,~.....
~- ..... ~-...,_
_..,_ 6 ~
f:a. I
. ---
NO.~Plll.
..,..,_...,*n l.--IAT ll'J.&Plll.
- z~:- ** ..Jl
............. " I
.I "'" *!IP I
21.l~ IASI)
NO llO
= = ;t
""
~
.
$""
If
""5
i
"1 ~
?2"50 IC
~~mo=(~
II: NO NO
~i!!irr-L~..,
t:::i\ ll n-&.~ .. ~n~r:o
\e) ,l1'u.~
lrl.lfR~.Plff.
,.,..,.,,_
- U,.Ua' Salem MJP:pc SORC Mtg.91-077