:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged| ML18106A693 |
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Salem  |
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| Issue date: |
06/29/1998 |
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| From: |
Knieriem B Public Service Enterprise Group |
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| To: |
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| Shared Package |
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| ML18106A692 |
List: |
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| References |
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| LER-98-003-02, LER-98-3-2, NUDOCS 9807140090 |
| Download: ML18106A693 (4) |
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Similar Documents at Salem |
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text
I '.,
I NRC FORM 366 U.S. NUCLEAR LATORY COMMISSION ROVED BY OMB NO. 3150-0104 (4-95)
EXPIRES 04/30/98 ESTIMATED BURDEN PER
RESPONSE
TO COMPLY WITH THIS LICENSEE EVENT REPORT (LER)
MANDATORY INFORMATION COLLECTION REQUEST:
50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE (See reverse for required number of LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND digits/characters for each block)
RECORDS MANAGEMENT BRANCH (T*6
- F33J, U.S.
NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 205 5-0001, AND TO THE PAPERWORK REDUCTION PROJECT
~150-0104),
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, C 20503.
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE(3)
SALEM UNIT 2 05000311 1 OF 4 TITLE (4)
Inappropriate Plugging Of Tubes R9C60 And RlOC60 In The Salem Unit 2, 24 Steam Generator EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER 01 22 98 98 003 00 06 29 98 FACILITY NAME DOCKET NUMBER OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE (9) 1 20.2201(b) 20.2203(a)(2)(v)
- 50. 73(a)(2)(i)(B) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i)
- 50. 73(a)(2)(ii)
- 50. 73(a)(2)(x)
LEVEL (10) 100 20.2203(a)(2)(i) 20.2203(a)(3)(ii)
- 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv) x OTHER I
20.2203(a)(2)(iii) 50.36(c)(1)
- 50. 73(a)(2)(v)
Spec~ in Abstract below or in RC Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
Brooke Knieriem, Licensing Engineer
( 6 09) 339-1782 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR IYES x INO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).
DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
This voluntary LER reports an inappropriate repair that was performed on two tube plugs in the Salem Unit 2, 24 Steam Generator.
In 1996, an inappropriate repair of the cold leg sentinel plugs for tubes R9C60 and RlOC60 in the Salem Unit 2 I 24 Steam Generator was performed.
The repair installed a Plug-a-Plug (PAP) behind each of the existing sentinel plugs.
This repair eliminated the ability of the sentinel plugs to allow a small amount of primary-to-secondary leakage as an indication of tube fatigue cracking.
The apparent cause of this occurrence was the incorrect identification of tubes R9C60 and RlOC60 as tubes requiring installation of PAPs.
Continued operation of Unit 2 in this configuration was determined to be acceptable until the PAP behind the next refueling outage.
9807140090 980629 PDR ADOCK 05000311 S
PDR affected sentinel plugs can be removed during the (4-95)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
SALEM UNIT 2 05000311 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
PLANT AND SYSTEM IDENTIFICATION
Westinghouse - Pressurized Water Reactor Steam Generator
{SB/SG}
Westinghouse Model 51 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 98 -
003 -
00
- Energy Industry Identification System (EIIS) codes and component function identifier codes appear as {ss/cc}
CONDITIONS PRIOR TO OCCURRENCE PAGE(3) 2 OF 4
At the time of identification, Salem Unit 2 was operating at 100% power.
(Mode 1).
DESCRIPTION OF OCCURRENCE In 1988 tubes R9C60 and RlOC60 in the Salem Unit 2 24 Steam Generator (SG) were removed from service and stabilized using a Westinghouse stabilizer.
This action was taken in response to NRC Generic Letter 88-02 "Rapidly Propagating Fatigue Cracks In Steam Generator Tubes", and addressed steam generato~ tubes that were determined to be susceptible to circumferential failure above the SG top tube support plate due to secondary side flow induced vibration.
The Westinghouse stabilizer is installed inside the tube and consists of a stainless steel cable, approximately 31 feet long, with swaged sleeves.
The stabilizer functions to prevent a failed tube from contacting adjacent tubes.
In addition to the installation of the stabilizers, each tube was removed from service by plugging the hot and cold leg ends with Inconel 600 (I-600) plugs.
In 1991 (after two cycles of operation), the hot leg plugs in tubes R9C60 and RlOC60 were repaired to address potential corrosion induced failure of the I-600 plugs.
This repair was performed in response to NRC Bulletin 89-01, "Failure Of Westinghouse Steam Generator Mechanical Plugs".
At that time, the cold leg mechanical plug in each of these tubes was removed and an Inconel 690 (I-690) sentinel plug was installed to address Westinghouse SECL 91-439, "Salem Unit 2 Steam Generator Tube Stabilizers Safety Evaluation".
SECL 91-439 determined that the installed stabilizer design was not qualified to dampen vibration in the tube U-bend area presenting the potential for tube fatigue in that area.
The replacement sentinel plugs were designed with a
leak-limiting orifice and were installed to provide indication of tube fatigue cracking.
This cracking would be detectable via primary-to-secondary leakage monitoring.
The source of the leakage would be determined, and the separation would be repaired at the next outage.
l '" (4-95)
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6)
YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM UNIT 2 05000311 98 -
003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE(Cont.)
PAGE (3) 3 OF 4
In February of 1996, Frarnatorne Technologies (FTI) was authorized to repair all previously unrepaired or unreplaced I-600 plugs in the Unit 2 Stearn Generators.
The repair method that was used was the Plug-A-Plug (PAP) method.
This method installs a redundant I-690 plug behind the existing plug.
The work scope for the plug repair was based upon a repair list provided to FTI by the Public Service Electric and Gas Stearn.Generator Group.
This list was developed using information contained on the existing Plugging Tabulation Sh~ets.
The Tube Plugging Tabulation Sheets contained two entries for tubes R9C60 and RlOC60 located in different locations on the sheet.
The first entry for R9C60 and RlOC60 did not identify the tube plug type for the installed cold leg plugs.
The second entry listed the sentinel plug information for the installed cold leg plugs.
Only the first entry for R9C60 and RlOC60 was noted when preparing the plug repair list thus PSE&G personnel decided to repair those plugs by installing the PAP in the cold leg.
This decision was thought to be conservative at the time.
However, the change negated the leak limiting functionality of the sentinel plug as the PAP did not contain an orifice.
Therefore the sentinel plug's ability to provide indication of tube cracking was eliminated.
APPARENT CAUSE OF OCCURRENCE The apparent cause of this event was a failure of the Qualification, Verification, and Validation (QV&V) process.
This process was not properly implemented when the Tube Plugging Tabulation Sheet for the 24 Stearn Generator was updated, resulting in duplicate entries for tubes R9C60 and RlOC60.
In addition, a QV&V process for authorizing steam generator tube/tube plug repairs was not established.
Both factors contributed to the inadvertent repair to the cold leg sentinel plugs installed in R9C60 and RlOC60.
PRIOR SIMILAR OCCURRENCES A review of LERs for Salem Units 1 and 2 issued in the last two years identified no LERs that reported similar occurrences.
SAFETY SIGNIFICANCE
There are no safety consequences as a result of this event.
Because of the incorrect repair, tubes R9C60 and RlOC60 are plugged at both ends and are isolated from primary system pressure.
In this condition the sentinel plugs are unable to carry out their leak limiting function.
This condition does not significantly impact safety because if a circumferential crack were to develop in one of these tubes, the
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)
SALEM UNIT 2 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6)
YEAR l SEQUENTIAL l REVISION NUMBER NUMBER 05000311 98 -
003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
SAFETY SIGNIFICANCE(Cont.)
PAGE(3) 4 OF 4
stabilizer would restrain the failed tube and prevent damage to adjacent tubes.
In the event that the stabilizer did not function, and damage occurred to an adjacent tube, the resultant leakage from fretting through an in-service tube by the severed tube would be bounded by the existing tube rupture analysis.
CORRECTIVE ACTIONS
- 1.
All Salem Unit 2 steam generator tubes containing sentinel plugs were reviewed to verify that no other tubes were inappropriately plugged.
This condition is limited to Unit 2, as there are no sentinel plugs installed in the Salem Unit 1 steam generators.
- 2.
The inappropriate plugging of tubes R9C60 and RlOC60 was reviewed in accordance with 10CFRS0.59.
This review determined that the loss of functionality of the sentinel plugs in did not constitute an unreviewed safety question and that operation could continue until functionality.
is restored during the next Unit 2 refueling outage.
- 3.
The I-690 PAPS that were installed in tube R9C60 and R10C60 cold legs will be removed during the next Unit 2 refueling outage. (Problem Identification Report 980122241, Deficiency Report, Job Supervisor Notification 01)
- 4.
The tubes adjacent to tubes R9C60 and R10C60 will be inspected for wear during the next Unit 2 refueling outage.
(Problem Identification Report 980122241, Condition Resolution Corrective Action 01)
- 5.
The 24 Steam Generator Tube Plugging Tabulation sheet was updated to correct duplicate tube entries for tubes R9C60 and R10C60.
- 6.
A review process for authorizing steam generator tube plug repairs will be developed for future steam generator work.
(Problem Identification Report 980122241, Condition Resolution Corrective Action 03)
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| 05000272/LER-1998-001, :on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124 |
- on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124
| | | 05000311/LER-1998-001-01, :on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5 |
- on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5
| | | 05000311/LER-1998-002-01, :on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions |
- on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-002, :on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys |
- on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003-02, :on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged |
- on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003, Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | | | 05000272/LER-1998-003, :on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps |
- on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-004, :on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted |
- on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-004, Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | | | 05000272/LER-1998-004-01, :on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors |
- on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors
| 10 CFR 50.73(a)(2) | | 05000272/LER-1998-005-01, :on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP |
- on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-005, :on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger |
- on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-005, Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | 10 CFR 50.73(a)(2) | | 05000311/LER-1998-006-01, :on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters |
- on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-006, :on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels |
- on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-006, :on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info |
- on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1998-007, :on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified |
- on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000311/LER-1998-007, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-007-01, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-008, :on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected |
- on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected
| 10 CFR 50.73(a)(2) | | 05000311/LER-1998-008-01, :on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure |
- on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure
| 10 CFR 50.73(a)(2)(i) | | 05000272/LER-1998-009, :on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed |
- on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-009-01, :on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors |
- on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors
| | | 05000272/LER-1998-010, :on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2 |
- on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000311/LER-1998-010-01, :on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired |
- on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-011, :on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold |
- on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) | | 05000311/LER-1998-011-01, :on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure |
- on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure
| | | 05000272/LER-1998-012, :on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised |
- on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-012, :on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With |
- on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With
| 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-012-01, :on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc |
- on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-013-01, :on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With |
- on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-013, :on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With |
- on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-014, :on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With |
- on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With
| | | 05000272/LER-1998-014-01, :on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With |
- on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-015-01, :on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With |
- on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-015, Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | | | 05000311/LER-1998-016, :on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With |
- on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
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