Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs| ML18106A578 |
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| Site: |
Salem  |
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| Issue date: |
03/20/1998 |
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| From: |
Knieriem B Public Service Enterprise Group |
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| To: |
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| Shared Package |
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| ML18106A576 |
List: |
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| References |
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| LER-98-005-02, LER-98-5-2, NUDOCS 9805050346 |
| Download: ML18106A578 (6) |
|
Similar Documents at Salem |
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LER-1998-005, Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs |
| Event date: |
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| Report date: |
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| Reporting criterion: |
10 CFR 50.73(a)(2) |
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| 2721998005R00 - NRC Website |
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text
J..
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 COMMISSION E;>CPIRES 04/30/98 14-951 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY LICENSEE EVENT REPORT (LER)
INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (See reverse for required number of
!T-6 F33J, U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150*
digits/characters for each block) 01041. OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
FACILITY NAME 11 I DOCKET NUMBER (2)
PAGE 131 SALEM UNIT 1 05000272 1 OF 6 TITLE 141 Inoperability Of The 12 'Fuel Oil Transfer Pump Due To Installation Of Incorrect Control Switch EVENT DATE 151 LER NUMBER 161 REPORT DATE 171 OTHER FACILITIES INVOLVED 181 I
I REVISION FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL MONTH DAY YEAR NUMBER NUMBER 02 19 98 98 005 00 03 20 98 FACILITY NAME DOCKET NUMBER OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or morel 1111 MODE 191 4
20.2201lbl 20.2203(a)(2)(v) x 50. 731a112llil
- 50. 73(a)(2)(viiil POW.ER 20.2203(a)(1) 20.2203(a)(3)(i)
- 50. 73(a)(2lliil
- 50. 73(a)(2)(x)
LEVEL (101 000 20.2203(all211il 20.22031all311iil
- 50. 731all2lliiil 73.71 20.2203(a)(2)(ii) 20.2203(a)(4)
- 50. 73(a)(2)(iv)
OTHER 20.22031all211iiil 50.36(cll 1 I
- 50. 73(a)(2)(v)
Specify in Abstract below
- 50. 73(a)(2)(vii) or in NRC Form 366A 20.2203(a)(2)(iv) 50.36(c)(21 LICENSEE CONTACT FOR THIS LER 1121 NAME TELEPHONE NUMBER (Include Area Code)
Brooke Knieriem, Licensing Engineer
( 609) 339-1782 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE I
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED 114)
EXPECTED MONTH DAY YEAR
'YES x INO SUBMISSION llf yes. complete EXPECTED SUBMISSION DATE).
DATE 1151 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) 116)
This LER documents the inoperability of the Salem Unit 1, 12 Emergency Diesel Generator Fuel Oil Transfer pump (FOTP) due to the installation of an incorrect control switch.
The incorrect control switch was configured in a way that did not allow automatic operation of the FOTP.
This event is reportable under 10CFR50.73(a) (2) ( i) (B) I any operation or condition prohibited by the plant's Technical Specifications.
Specifically, contrary to Technical Specification (TS) 3.8.1.1, A. c.
Sources, and TS 3.0.4, entry into an operational mode or other condition, Salem Unit 1 entered (from Mode 5) and operated in Mode 4 with the 12 inoperable, and without the knowledge of the operators.
The apparent cause of the inoperability of the 12 FOTP was the failure of planning and maintenance personnel to eh sure that the proper configuration the 12 FOTP was maintained by installation of the correct control switch.
Additionally, station personnel failed to ensure that an adequate post maintenance retest was performed to verify that the 12 FOTP was restored to operable condition following 9805050346 980427 PDR ADOCK 05000272 S
PDR the maintenance.
FOTP of an
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LEA NUMBER 161 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM UNIT 1 05000272 98 -- 005 --
00 TEXT llf more space is required, use additional copies of NRC Form 366A) ( 171
PLANT AND SYSTEM IDENTIFICATION
Westinghouse - Pressurized Water Reactor Emergency Diesel Generator
{EK/DG}
- Energy Industry Identification System (EIIS) codes and component function identifier codes appear as {ss/cc}
CONDITIONS PRIOR TO OCCURRENCE Hot Shutdown, Mode 4 DESCRIPTION OF OCCURRENCE PAGE 131 2
OF 6
During Emergency Diesel Generator (EDG) operation, two FOTPs ~or each unit are used to automatically transfer fuel oil from the Fuel Oil Storage tanks to the Fuel Oil Day Tank (FODT) for each engine.
Each of the FOTPs is controlled through a Regular-Backup selector switch and an Off-Auto-Manual selector switch.
By alignment of the two switches~ *one FOTP is aligned to start at the Regular FODT start level of 33 inches (Regular-Backup switch in the Regular position, Off-Auto-Manual selector switch in the Auto position) to refill the FODT.
The other-FOTP is aligned as the Backup pump (Regular-Backup switch in the Backup position, Off-Auto-Manual selector switch in the Auto position).
In the event that the Regular FOTP fails to start or fails to deliver adequate flow to maintain FODT level, the Backup pump will start when level reaches the FODT low level alarm setpoint.
On February 18, 1998 Salem Unit 1 entered Mode 4.
On the following day, Salem personnel began a 31 day surveillance test of the Auto start feature of the 12 FOTP to verify its operability.
This test is performed under procedure Sl.OP-ST.DG-OOOS(Q), "12 Fuel Oil Transfer System Operability Test".
During the test, the 12 FOTP was aligned to start at the Regular FODT start level but failed to start.
The pump was then declared inoperable.
At the time of the unsatisfactory surveillance, Salem Unit 1 was in Hot Shutdown (Mode 4).
TS 3.8.1.1.b.2 requires that in Modes 1-4, two FOTPs be operable.
With one of the above required FOTPs inoperable, the action statement requires that the inoperable FOTP be restored to an operable status within seventy-two hours or the unit must be placed in Hot Standby (Mode 3) within the next six hours and in Cold Shutdown (Mode 5) within the following thirty hours.
Additionally, contrary to TS 3.. 0.4, Unit 1 entered Mode 4 from Mode 5 during the time that the 12 FOTP was inoperable, without the knowledge of the operators.
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME 111 SALEM UNIT 1 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER 121 LER NUMBER 161 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 05000272 98 --
005 --
00 TEXT (If more space is required. use additional copies of NRC Form 366AI 1171 Description (Cont.)
PAGE 131 3
OF 6
An inspection of the 12 FOTP Off-Auto-Manual selector switch was performed and it was determined that an incorrect switch was installed for the Off-Auto-Manual selector switch.
The incorrect switch (part number 910PDD511) was configured in a manner that did not permit automatic operation.
The correct switch for this application (part number 910PGC513) was identified and installed.
Operability of the 12 FOTP was then verified through satisfactory performance of Sl.OP-ST.DG-OOOS(Q}, and the action statement was exited.
In November 1997, station personnel identified that the 12 FOTP Off-Auto-Manual switch would not spring return from the Manual to the Auto position.
A work order was written to replace the switch.
During the planning process for this work order an incorrect switch (part number 910PDD511) was staged and issued for installation.
This part was not adequately verified to be correct by planning and maintenance personnel prior to installation.
Upon completion of the maintenance in January 1998, the post-maintenance retest was performed as specified by the work package.
The retest required verification that equipment and components disturbed during the performance of the maintenance had been returned to the proper plant configuration.
Since the incorrect switch installation was not discovered, the specified retest was not adequately accomplished.
Additionally, the post-maintenance retest only required verification that the configuration be verified.
It did not require that testing be performed to verify that the 12 FOTP was operable.
A field inspection was performed to verify the configuration of the switches for the 11, 21, and 22 FOTPs.
The installed Off-Auto-Manual selector switch for the 21 FOTP was also found to be incorrect (also a part number 910PDD511).
However, up to the time of discovery, the 21 FOTP had been operating satisfactorily as verified by surveillance testing.
It appears that this switch was modified to function as an Off-Auto-Manual selector switch.
Specifically, a cam roller from part 910PGC513 switch appears to have been installed in a part 910PDD511 switch to make it function as an Off-Auto-Manual switch.
The acceptability of this configuration was evaluated and determined to be acceptable.
However, the 21 FOTP Off-Auto-Manual switch will be replaced with the correct switch at the earliest opportunity.
APPARENT CAUSE OF OCCURRENCE The apparent cause of this event was the failure of planning and maintenance personnel to verify that the correct replacement switch was identified, staged, and installed for the 12 FOTP Off-Auto-Manual selector switch.
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER 16)
YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM UNIT 1 05000272 98 --
005 --
00 TEXT (If more space is required, use additional copies of NRC Form 366A) ( 17)
APPARENT CAUSE OF OCCURRENCE(cont.)
PAGE 13) 4 OF 6
Additionally, the post-maintenance retest that was specified to.verify that equipment and components disturbed during the performance of the maintenance were returned to the proper plant configuration was not adequately performed because the installation of an incorrect switch was not identified.
The post-maintenance retest also was not adequate in that it did not verify the operability of the FOTP following maintenance.
PRIOR SIMILAR OCCURRENCES A review of LERs ~or Salem Units 1 and 2 issued in the last two years identified one LER which discussed a similar occurrence.
LER 311/97-002-00 reported the installation of non-seismically qualified pressure switches in the Auxiliary Building Ventilation system.
The cause of this event was not determined.
SAFETY CONSEQUENCES AND IMPLICATIONS
During EDG operation, each FOTP has sufficient capacity to ensure that the Fuel Oil Day tanks are kept at the level required to support EDG operation.
Normally, one FOTP is arranged to supply the Fuel Oil Day tanks for each EDG.
Its operation is controlled by a level switch in the Day Tank.
The other FOTP is lined up as the backup, also operating in response to a level switch in the Day Tank.
The level switch controlling the backup FOTP also activates the Day Tank low level alarm.
Should the regular pump fail to start, the backup pump will start and is capable of supplying sufficient flow to maintain Day Tank levels for all three EDGs.
At the time the backup pump starts, the low level alarm is received and will alert operators to the condition.
The Day Tank low tank level setpoint is based upon maintaining no less than a sixty minute fuel oil reserve.
This would provide operators with adequate time to take manual control of a FOTP and restore Day Tank level should both FOTPs fail to automatically start.
Should a single failure of a FOTP (the backup FOTP) occur with the other FOTP inoperable, no means would be available to maintain level in the FODTs during EDG operation.
Under this condition, and in the event of a postulated event (Loss of Coolant Accident coincident with a Loss of Offsite Power), power would not be available to equipment necessary to remove decay heat and to mitigate the consequences of the accident once the FODTs were emptied.
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME ( 1 l LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6)
YEAR I SEQUENTIAL I REVISION NUMBER NUMBER PAGE 131 SALEM UNIT 1 05000272 98 --
005 --
00 5
OF 6
TEXT (If more space is required. use additional copies of NRC Form 366Al ( 17 I Safety Consequences (Cont.)
TS 3.8.1.1.b.2 requires that in Modes 1-4, two.FOTPs be operable.
With one FOTP inoperable, the action statement requires that the inoperable FOTP be restored to an operable status wfthin seventy-two hours or the unit must be placed in Hot Standby (Mode 3) within the next six hours _and in Cold Shutdown (Mode 5) within the following thirty hours.
Because the inoperability of the 12 FOTP was identified, corrected and the FOTP restored to operability within the time specified by TS, Unit 1 was not in a condition that would impact the health and safety of the general public.
CORRECTIVE ACTIONS
- 1. A field inspection was performed to verify the configuration of_ the switches for the 11, 21, and 22 FOTPs.
The Off-Auto-Manual switch for the 21 FOTP was found to have an incorrect part number.
However, this pump was operable based on surveillance test performance since the switch was installed.
This configuration was evaluated by the Operations Department through the performance of an Operability Determination and was found to be acceptable for contin.ued operation.
- 2. The correct Off-Auto-Manual switch (part number 910PGC513) was installed and the operability of the 12 FOTP was verified (WO 00980219074).
- 3. The correct Off-Auto-Manual switch (part number 910PGC513) will be installed for the 21 FOTP at the next available opportunity.
(WO 00980227082).
- 4. The requirement to review drawings to verify that parts being staged are correct has been reinforced with planning personnel.
Planning personnel have also been reminded of their responsibility to specify the appropriate testing requirements on work orders in accordance with; NC.NA-AP.ZZ-0050(Q), "Station Testing Program", NC.NA-TS.ZZ-0050(Q),
"Station Testing Program Matrix".
- 5. All personnel involved have been held accountable in accordance with PSE&G 1 s procedures and policies.
- 6. An inspection will be performed of a random sampling of thirty switches in safety related applications to determine if any other instances of incorrect switch configuration exist.
The results of this sampling will serve as the basis for further inspection.
(PIR 00980219131, CRCA 02)
- 7. As a part of second quarter In-service Day training, Maintenance department personnel will receive a rollout discussion on the importance of (i) ensuring that replacement parts are correct by comparing them to
- (4-951 U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1 l DOCKET NUMBER (2)
LER NUMBER (6)
YEAR I SEQUENTIAL I REVISION NUMBER NUMBBI SALEM UNIT 1 05000272 98 --
005 --
00 TEXT (If more space is required, use additional copies of NRC Form 366AI ( 171 CORRECTIVE ACTIONS{Cont.)
PAGE (3) 6 OF *5 the Bill Of Materials and by comparison to the removed parts, (2) verifying the correct contact switch configuration on new contacts, (3) performing modifications to replacement parts only in accordance with approved procedures. (PIR 00980219131, CRCA 01)
- 8. Operations department personnel will receive a rollout discussion to emphasize the importance of reviewing completed work against planned work to ensure that adequate retests are performed in accordance with procedure NC.NA-AP.ZZ-0009{Q}, "Work Control Process". (PIR 00980219131, CRCA 03)
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| 05000272/LER-1998-001, :on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124 |
- on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124
| | | 05000311/LER-1998-001-01, :on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5 |
- on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5
| | | 05000311/LER-1998-002-01, :on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions |
- on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-002, :on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys |
- on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003-02, :on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged |
- on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003, Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | | | 05000272/LER-1998-003, :on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps |
- on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-004, :on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted |
- on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-004, Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | | | 05000272/LER-1998-004-01, :on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors |
- on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors
| 10 CFR 50.73(a)(2) | | 05000272/LER-1998-005-01, :on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP |
- on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-005, :on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger |
- on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-005, Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | 10 CFR 50.73(a)(2) | | 05000311/LER-1998-006-01, :on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters |
- on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-006, :on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels |
- on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-006, :on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info |
- on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1998-007, :on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified |
- on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000311/LER-1998-007, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-007-01, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-008, :on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected |
- on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected
| 10 CFR 50.73(a)(2) | | 05000311/LER-1998-008-01, :on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure |
- on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure
| 10 CFR 50.73(a)(2)(i) | | 05000272/LER-1998-009, :on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed |
- on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-009-01, :on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors |
- on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors
| | | 05000272/LER-1998-010, :on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2 |
- on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000311/LER-1998-010-01, :on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired |
- on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-011, :on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold |
- on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) | | 05000311/LER-1998-011-01, :on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure |
- on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure
| | | 05000272/LER-1998-012, :on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised |
- on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-012, :on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With |
- on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With
| 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-012-01, :on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc |
- on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-013-01, :on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With |
- on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-013, :on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With |
- on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-014, :on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With |
- on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With
| | | 05000272/LER-1998-014-01, :on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With |
- on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-015-01, :on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With |
- on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-015, Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | | | 05000311/LER-1998-016, :on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With |
- on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
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