ML17266A145: Difference between revisions

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| issue date = 02/11/1980
| issue date = 02/11/1980
| title = Updated LER 79-028/01X-1:on 790903,in Cold Shutdown During Hurricane,Cable Fell Into Startup Transformer B.Ac Electrical Sys B de-energized & Diesel Generator Failed to Start.Caused by Delay in B Diesel Binding
| title = Updated LER 79-028/01X-1:on 790903,in Cold Shutdown During Hurricane,Cable Fell Into Startup Transformer B.Ac Electrical Sys B de-energized & Diesel Generator Failed to Start.Caused by Delay in B Diesel Binding
| author name = JAMES D K
| author name = James D
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  

Revision as of 02:52, 19 June 2019

Updated LER 79-028/01X-1:on 790903,in Cold Shutdown During Hurricane,Cable Fell Into Startup Transformer B.Ac Electrical Sys B de-energized & Diesel Generator Failed to Start.Caused by Delay in B Diesel Binding
ML17266A145
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 02/11/1980
From: James D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17207A841 List:
References
LER-79-028-01X, LER-79-28-1X, NUDOCS 8002220334
Download: ML17266A145 (3)


Text

Initial Report-Se ember 17, 1979 NRC PORI0 260 P TTt LlCENSEE EYENT REPORT U S.NUCLEAR REGULATORY COMAtISSIOI+

CONTROl BL,CCIC: I l l l t Ol=(PLEASE PAINT OR YPE ALL REQUIRED INPORAtATIONI O.9 LICCySEE CODE O.16 I.ECca St~YPC 10 S~CAF St UCMc 5'aIcac SEA 2 CON'T 9 OR 71 IQE.1 lll l O9 EVCKA O*T 15 AEPDAT OATS 50'.;;LL ca 0 51 0 0 3 I 5 QLAAA 60 6I OOCaI~NuaFaSSA 61 cEI EV ENT 0 ESCR IPTION~O PR 0 9 4SLE COaI5 ECU B4CES+Io While in the cold shutdown con%Cion during Hurricane David, a cable fell 0 2 across lines jnto the"B" S/U transformer, causing a lockout on the~0 East Bus and de-energizing the"B" S/U transformer.

The"B" A.C.electri-cal system was de-energized, and the"B" Diesel Generator (.DG)failed to start.Following an electrical check-out, the"B" DG was manually started QQIFILI 1115111*1 I-I I.I I I-l 3\I I I Q~Q'Adequate core cooling was maintained at all times.This is the fifth occurrence of this'type (See LERs 335-76-21, 76-44, 77-3 and 77-]5).STSTEu CAVSE , CAVSS COMP..VAIVc CODE CODE SVSCDDS'CMIOKCKTCDOS SVS 005 SVSCDOc aac~EE Q LEJQ EAJQ~ll E L 11 Yl 3 Q LAJQ~2Q 1 6': 9 IO tl, Il!2'IS 19 10 ScDVCKTIAL OCCVAAEIICE REPORT REVISIOK~LcAIEIO EV EAT YEAA'AcroAT KO, CODE TYPE.PIO.QYE>>-Fa 0~79'+~02 8+~~01 2I 11 26'6 ll 15 29 20 SI IOK PVTVA c Clr EC.Sy VTDDEEa ATT*Caa&SIaT NPR~PRIME CI>>MI, COMPOK cKT TA)CSN AiTIOac CK>LrLK~SIETAOO IIOVAS 2'1 SVScaI~~ao PCAM 1 VS, SV PPLI EA MAIIVSA~VAEA LAaa~ZQ cZQ~ZQ'~00 0~YQ~AQ 13 IQ 3 3 4 51'c SS 26.2I 40 41 42 40 44 47 CAUSE OESCRIPTION ANO CORRM'PIV ACTiONS O2l An investighti on revealed that a rela in the auto-start circuitr of the~"B" DG was mechanically binding.This relay was.replaced.An operational test was then satisfactorily completed whereby the"B" S/U transformer (which had been repaired and tested)was intentionally de-energized.

The"B" DG was observed to auto-start an 0'2 9 P*CIU.Y.Sa ATVS!~POWSA 5~~QEZ~00 D Qc l 2 t0 ll 12*CttVITY CoaITS."IT

~ACLSA&0 OIa ASLEASE AMOV KTora ACTIV ITY OSS 9~Z Q22~ZQ24 NA l 5 9 I0 I~P A505>>Ecii cXrOSVAES~D>>(P 0 QZF~ZQza NA l 5'I I 11 Il PcASOaaaa tl.IHJVAI ES a~+5 0 Qa'II LOCATION oP ASLEASS OSE NA~4, 45 METIIOO OC CTKEA sTA'555~olscov EAT olscovcAY 05$cAI pTIDK'Q~2 NA IRAQI 0 erator Observation

!AI 45 20 50 1 5 0 9 I'I 12 5 LOSS OC CA OCaICCE TO PCCILtTY 2 TTTc OES Aactloaa LIB 2 l0 PVSLIr.t Y tSSVEO OCSCA:PT:Oy 9 LlLIO44~0'AAIA OP PREPARER D-K.James EOOSNIQ+Q NRC US=ONLY (3051 552-3813 REPORTABLE OCCURRENCE 335-79-.28, Update 81 LICENSEE EVENT REPORT PAGE TWO Additional Event Descri tion and Probable Conseouences 4 While in the cold shutdown condition (Mode 5)during the passage of Hurricane David, a support cable for the tower crane in th ,Unit 2 construction area fell across'lines'into the"B" Start-up'Trans=ormer.

A lockout occurred on the East Bus and.the"B" Start-up Tra.sform r was de-energized.

The"B" side of the electrical system de-energized with the exception of the"B" DC Bus which was carried by the"8" battery.The"B" Inverter failed to respond but the"D" Inverter remained in service.A blown fuse was discovered later in the"B" Inverter circuit.Tne"AB" A.C.Busses were lost as they were tied to the"B" side.The"AB" D.C.Bus was lost as it was tied to"B" D.C.Bus, which is assumed to have de-energized as a result of the current transient produced by the event.The SUPS (including instrumentation, annunciation, lighting, communications

[except PAX and BELL], NAMAS and Sequence of Events Recorder)was also lost.At this tim i-: was discovered that"B" Diesel Generator was not supplying loads (failed to start).Follovong a visual and electrical check-out of'he"B" Diesel Generator,'it was manua'}ly started.Adequate core cooling was maintained and verified>y starting the"A" IPSI pump and manually controlling Shutdown Cooling flow.Additional Cause D sc.i~t'.on and Corrective'Action The"A" Diesel Generator was yepified OPERABLE.All of the electrjca]

busses and components lost during event were re-energiz d.Since the reason fop the"B" Diesel Generator not starting autorqatjc~lly on vndervoltage was not.known, and the potential for a faulted bus or ground was suspected, a thorough check-out was conducted prior to manually starting and loading the"B" Diesel Generator.

Two days following the event, a plant staff review and investigation revealed that the K22 relay in the auto-start circuitry of the"B" Diesel'enerator was mechanically binding.This relay was replaced.'Subsequently, an operational test was.satisfactorily completed whereby the"8" Start-up Transformer (which was repaired and tested)was intentionally de-ener g'ized, and auto-start and loading of the"B" Diesel Generator was verified to occup, 0 0