ML17331A469: Difference between revisions

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| issue date = 10/03/1980
| issue date = 10/03/1980
| title = LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
| title = LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
| author name = MURPHY C E
| author name = Murphy C
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name =  
| addressee name =  

Revision as of 15:40, 18 June 2019

LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
ML17331A469
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 10/03/1980
From: Murphy C
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A467 List:
References
LER-80-032-03L, LER-80-32-3L, NUDOCS 8010090368
Download: ML17331A469 (4)


Text

NRC FORM 366 P.77)Ll CENSE E EV EN T R E PORT U.S.NUCLEAR REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 03 Q4~Qs 25 26 LICENSE TYPE 30 57 CAT 58 9 0 8 Q9 Q EVENT DATE 74 75 REPORT DATE 80 CONTROL BLOCK: Q1 I 6 M I D C C 2Q2 0 0 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER CON'T soURGE~LQB 0 5 0 0 0 3 1 6 Q7 0 7 8 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10~02 WHI E PERFORMING A SURVEI A E EST TO~0 3 MAINTENANCE THE PUMP WAS UNSTABLE AND DECLARED INOPERABLE.

THE REDUNDANT RH~04 WAS OPERABLE.THIS IS THE FIRST EVENT OF THIS TYPE.~06~06~07~08 7 8 9 80~09 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE F QTT L~LQ LZJQ>>Z'Z Z Z Z QE4~ZQTE~Z QTR 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER]RP EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPORT~3Q 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.COMPONENT TAKEN ACTION'N PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~0QTR~ZQ15~ZQ25~ZQ21 0 0 0 0~N Q22~NQ24~Z Q25 Z 9 9 9 Q>>33 34 35 36 , 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE TEST PROCEDURE DID"P VI F THE PRO EOURE WAS H G RWST WHICH SWEEPS THE AIR OUT OF THE HEAT EXCHA G 3 THE RHR SYSTEM HAS BEEN DRAINED ANO REFILLED TWICE S I E~14 CHANGED PROCEDURE RETURNED THE SYSTEM TO SERVICE WITH 0 DIFF I.ULTY.7 8 9 FACILITY STATUS 99 POWER OTHER STATUS Q I 5 E 28 1 0 0 29 44 7 8 o 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z P42 9 10 PUBLICITY ISSIIEP DESCRIPTION

~+NQnn 9'0 NAME PF PREPARER~E~MURPHY NA CCI MQ~Q ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY~s~Z Qss~ZQ54 NA 7 8 9 10 11 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 Lo¹0JQET z Q>>NA 7 8 9 11 12 13 PERSONNEL, INJURIES NUMBER DESCRIPTION 41 5~00 0 Q45 NA DISCOVERY DESCRIPTION Q32 OPERATOR OBSERVATION NA LOCATION OF RELEASE Q goioopo34 g'RC USE ONLY 68 69 P)IONA,616-465-5901 X-1305 80 80 80 80 80 80 c4 ER 80~TR 0 a 49 a f!

ATTACHMENT P1 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS: NO FURTHER ACTION IS REQUIRED AS A RESULT OF THIS EVENT.

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