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{{#Wiki_filter:NRCForn366U.S.NUCLEARREGULATORYCOMMiSSION(6-1998)LICENSEEEYENTREPORT(LER)(Seereverseforrequirednumberofdigits/charactersforeachblock)APPROVEOBYOMBNo.31600104EXP(RES06130I2001fSTSIIATEDBURDENPERRESPONSETOCOMPLYWITHT)SSMANDATORYWfORMATIONCOLLECTIONREOUESTI500HRS.REPORTEDLESSONSLEARNEDAREWCORPORATEDWTOTHELICENSINGPROCESSJJIOFEOBACKTOeeUSTRY.fORWARDCOMMENTSREGA)CINGBURDENESTIMATETOTHESP'ORMATIONANORECORDSMANAGEMENTBRANCHITSF55).U.S.NUCLEARREGIAATORYCOMMISSION.WAS)eNGTON.DC205554ool.AtTOTHEPAPERWORKRECUCTIONPROJECT(M500101),CFFCEOfMANAGEMENTANDBUDGET.WASHINGTON.DC205OSFACILITYNAME(1)TITLE(4)CookNuclearPlantUnit2DOCKETNUMBER(2)05000-316PAGE(3)1of1DegradedComponentCoolingWaterFlowtoContainmentMainSteamLinePenetrationsEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIESINVOLVED(8)MONTH06DAY10YEARYEARSEQUENTIALNUMBER1996,1999-001'EVISIONNUMBER00MONTHDAYYEAR03291999AILINAMCookPlantUnit1AILIYHAM05000-315KNUMOPERATINGMODE(9)POWERLEVEL(10)10020.2201(b)20.2203(a)(1)20.2203(a)(2)(i)20.2203(a)(2)(ii)20.2203(a)(2)(iii)20.2203(a)(2)(iv)20,2203(a)(2)(v}20.2203(a)(3)(i)20.2203(a)(3)(ii)20.2203(a)(4)50.36(c)(1}50.36(c)(2)LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(i)50.73(a)(2)(ii)50.73(a)(2)(iii)50.73(a)(2)(iv)50.73(a)(2)(v)50.73(a)(2)(vii)50.73(a}(2)(viii)50.73(a)(2)(x)73.71OTHERSpeorryinAberrso(belowornNRCForm366ATELEPHONENUMBER(Inc@deAreeCode)THISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTSOF10CFR():(Checkoneormore)(11)LyleR.Berry,RegulatoryComplianceEngineer(616)465-5901x2637COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETOEPIXPP,,d.SCAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETOEPIXSUPPLEMENTALREPORTEXPECTED(14)XYES(IfYes,completeEXPECTEDSUBMISSIONDATE)NOEXPECTEDSUBMISSIONDATE(15MONTHDAY06251999Abstract(Limitto1400spaces,i.e.,approximately15single-spacedtypewrittenlines)(18)OnFebruary26,1999,duringanengineeringreviewoftheUnit2ComponentCoolingWaterSystem(CCW),itwasidentifiedthatpoweroperationwaspermittedinJune1996withdegradedCCWflowtothecoolersforcontainmentpenetrations2-CPN-3and2-CPN-4.Themainsteamheadersforsteamgenerators22and23passthroughthesepenetrations.OperatingwiththedegradedCCWtothesecoolersmayhaveresultedinexcessivethermalstressonthepenetrationsleeves/liners.TheUpdatedFinalSafetyAnalysisReport(UFSAR)creditsthepenetrationcoolersformaintainingthetemperatureofadjacentconcretelessthan150degreesF.Atthetimeoftheevent,containmentexteriorsurfaceconcretetemperaturesweremeasuredatamaximumof155degreesF.Operabilitydeterminationsperformedatthetimeoftheevent,tojustifycontinuedoperationwithdegradedCCWflowtothemainsteamlinepenetrations,havebeenre-evaluatedandfoundtobe,inadequate.Thiseventwasreportedviaa4'hournon-emergencyEmergencyNotificationSystem(ENS)reportonFebruary27,1999,pursuanttotherequirementsof10CFR50.72(b)(2)(i).ThisLERisbeingsubmittedpursuanttotherequirementsof10CFR50.73(a)(2)(ii)(B)asaneventorconditionthatresultedinthenuclearpowerplantbeinginaconditionthatwasoutsidethedesignbasisoftheplant.Initialinvestigationsindicatethatthecauseforthiseventwasaninadequateunderstandingofthedesignbasisforthecontainmentpenetrationcoolers.Additionalinvestigationstoassesspotentialdegradationtotheconcrete,linersandsleevesatthesepenetrationsareongoing.Theresultsofthoseinvestigations,includingidentifiedrootcause(s),preventiveactionsandsafetysignificancewillbeprovidedwhencompleted.9'T)04090c)04'))903c)9PDRADOCIJL050003i68PDR}}
{{#Wiki_filter:NRCForn366U.S.NUCLEARREGULATORY COMMiSSION (6-1998)LICENSEEEYENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEOBYOMBNo.31600104EXP(RES06130I2001 fSTSIIATED BURDENPERRESPONSETOCOMPLYWITHT)SSMANDATORY WfORMATION COLLECTION REOUESTI500HRS.REPORTEDLESSONSLEARNEDAREWCORPORATED WTOTHELICENSING PROCESSJJIOFEOBACKTOeeUSTRY.fORWARDCOMMENTSREGA)CING BURDENESTIMATETOTHESP'ORMATION ANORECORDSMANAGEMENT BRANCHITSF55).U.S.NUCLEARREGIAATORY COMMISSION.
WAS)eNGTON.
DC205554ool.
AtTOTHEPAPERWORK RECUCTION PROJECT(M500101),
CFFCEOfMANAGEMENT ANDBUDGET.WASHINGTON.
DC205OSFACILITYNAME(1)TITLE(4)CookNuclearPlantUnit2DOCKETNUMBER(2)05000-316 PAGE(3)1of1DegradedComponent CoolingWaterFlowtoContainment MainSteamLinePenetrations EVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MONTH06DAY10YEARYEARSEQUENTIAL NUMBER1996,1999-001'EVISIONNUMBER00MONTHDAYYEAR03291999AILINAMCookPlantUnit1AILIYHAM05000-315 KNUMOPERATING MODE(9)POWERLEVEL(10)10020.2201(b)20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20,2203(a)(2)(v}
20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1
}50.36(c)(2)
LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a}(2)(viii) 50.73(a)(2)(x) 73.71OTHERSpeorryinAberrso(belowornNRCForm366ATELEPHONE NUMBER(Inc@deAreeCode)THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFR():(Checkoneormore)(11)LyleR.Berry,Regulatory Compliance Engineer(616)465-5901x2637COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXPP,,d.SCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(14)XYES(IfYes,completeEXPECTEDSUBMISSION DATE)NOEXPECTEDSUBMISSION DATE(15MONTHDAY06251999Abstract(Limitto1400spaces,i.e.,approximately 15single-spaced typewritten lines)(18)OnFebruary26,1999,duringanengineering reviewoftheUnit2Component CoolingWaterSystem(CCW),itwasidentified thatpoweroperation waspermitted inJune1996withdegradedCCWflowtothecoolersforcontainment penetrations 2-CPN-3and2-CPN-4.Themainsteamheadersforsteamgenerators 22and23passthroughthesepenetrations.
Operating withthedegradedCCWtothesecoolersmayhaveresultedinexcessive thermalstressonthepenetration sleeves/liners.
TheUpdatedFinalSafetyAnalysisReport(UFSAR)creditsthepenetration coolersformaintaining thetemperature ofadjacentconcretelessthan150degreesF.Atthetimeoftheevent,containment exteriorsurfaceconcretetemperatures weremeasuredatamaximumof155degreesF.Operability determinations performed atthetimeoftheevent,tojustifycontinued operation withdegradedCCWflowtothemainsteamlinepenetrations, havebeenre-evaluated andfoundtobe,inadequate.
Thiseventwasreportedviaa4'hournon-emergency Emergency Notification System(ENS)reportonFebruary27,1999,pursuanttotherequirements of10CFR50.72(b)(2)(i).
ThisLERisbeingsubmitted pursuanttotherequirements of10CFR50.73(a)(2)(ii)(B) asaneventorcondition thatresultedinthenuclearpowerplantbeinginacondition thatwasoutsidethedesignbasisoftheplant.Initialinvestigations indicatethatthecauseforthiseventwasaninadequate understanding ofthedesignbasisforthecontainment penetration coolers.Additional investigations toassesspotential degradation totheconcrete, linersandsleevesatthesepenetrations areongoing.Theresultsofthoseinvestigations, including identified rootcause(s),
preventive actionsandsafetysignificance willbeprovidedwhencompleted.
9'T)04090c)04
'))903c)9 PDRADOCIJL050003i68PDR}}

Revision as of 09:15, 29 June 2018

LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing
ML17325B522
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/29/1999
From: BERRY L R
INDIANA MICHIGAN POWER CO.
To:
Shared Package
ML17325B521 List:
References
LER-99-001, LER-99-1, NUDOCS 9904090204
Download: ML17325B522 (1)


Text

NRCForn366U.S.NUCLEARREGULATORY COMMiSSION (6-1998)LICENSEEEYENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEOBYOMBNo.31600104EXP(RES06130I2001 fSTSIIATED BURDENPERRESPONSETOCOMPLYWITHT)SSMANDATORY WfORMATION COLLECTION REOUESTI500HRS.REPORTEDLESSONSLEARNEDAREWCORPORATED WTOTHELICENSING PROCESSJJIOFEOBACKTOeeUSTRY.fORWARDCOMMENTSREGA)CING BURDENESTIMATETOTHESP'ORMATION ANORECORDSMANAGEMENT BRANCHITSF55).U.S.NUCLEARREGIAATORY COMMISSION.

WAS)eNGTON.

DC205554ool.

AtTOTHEPAPERWORK RECUCTION PROJECT(M500101),

CFFCEOfMANAGEMENT ANDBUDGET.WASHINGTON.

DC205OSFACILITYNAME(1)TITLE(4)CookNuclearPlantUnit2DOCKETNUMBER(2)05000-316 PAGE(3)1of1DegradedComponent CoolingWaterFlowtoContainment MainSteamLinePenetrations EVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MONTH06DAY10YEARYEARSEQUENTIAL NUMBER1996,1999-001'EVISIONNUMBER00MONTHDAYYEAR03291999AILINAMCookPlantUnit1AILIYHAM05000-315 KNUMOPERATING MODE(9)POWERLEVEL(10)10020.2201(b)20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20,2203(a)(2)(v}

20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1

}50.36(c)(2)

LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a}(2)(viii) 50.73(a)(2)(x) 73.71OTHERSpeorryinAberrso(belowornNRCForm366ATELEPHONE NUMBER(Inc@deAreeCode)THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFR():(Checkoneormore)(11)LyleR.Berry,Regulatory Compliance Engineer(616)465-5901x2637COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXPP,,d.SCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(14)XYES(IfYes,completeEXPECTEDSUBMISSION DATE)NOEXPECTEDSUBMISSION DATE(15MONTHDAY06251999Abstract(Limitto1400spaces,i.e.,approximately 15single-spaced typewritten lines)(18)OnFebruary26,1999,duringanengineering reviewoftheUnit2Component CoolingWaterSystem(CCW),itwasidentified thatpoweroperation waspermitted inJune1996withdegradedCCWflowtothecoolersforcontainment penetrations 2-CPN-3and2-CPN-4.Themainsteamheadersforsteamgenerators 22and23passthroughthesepenetrations.

Operating withthedegradedCCWtothesecoolersmayhaveresultedinexcessive thermalstressonthepenetration sleeves/liners.

TheUpdatedFinalSafetyAnalysisReport(UFSAR)creditsthepenetration coolersformaintaining thetemperature ofadjacentconcretelessthan150degreesF.Atthetimeoftheevent,containment exteriorsurfaceconcretetemperatures weremeasuredatamaximumof155degreesF.Operability determinations performed atthetimeoftheevent,tojustifycontinued operation withdegradedCCWflowtothemainsteamlinepenetrations, havebeenre-evaluated andfoundtobe,inadequate.

Thiseventwasreportedviaa4'hournon-emergency Emergency Notification System(ENS)reportonFebruary27,1999,pursuanttotherequirements of10CFR50.72(b)(2)(i).

ThisLERisbeingsubmitted pursuanttotherequirements of10CFR50.73(a)(2)(ii)(B) asaneventorcondition thatresultedinthenuclearpowerplantbeinginacondition thatwasoutsidethedesignbasisoftheplant.Initialinvestigations indicatethatthecauseforthiseventwasaninadequate understanding ofthedesignbasisforthecontainment penetration coolers.Additional investigations toassesspotential degradation totheconcrete, linersandsleevesatthesepenetrations areongoing.Theresultsofthoseinvestigations, including identified rootcause(s),

preventive actionsandsafetysignificance willbeprovidedwhencompleted.

9'T)04090c)04

'))903c)9 PDRADOCIJL050003i68PDR