IR 05000354/2025003: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot insert
 
StriderTol Bot change
Line 84: Line 84:
Division of Operating Reactor Safety  
Division of Operating Reactor Safety  


=SUMMARY=
SUMMARY  
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Hope Creek Generating Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71111.2


===List of Findings and Violations===
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
No findings or violations of more than minor significance were identified.
performance by conducting an integrated inspection at Hope Creek Generating Station, in
accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs
program for overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified
non-cited violation is documented in report section: 71111.24.  


===Additional Tracking Items===
List of Findings and Violations
None.


=PLANT STATUS=
No findings or violations of more than minor significance were identified.


Hope Creek began the inspection period at rated thermal power. On July 7, 2025, Hope Creek was reduced to 75 percent power in response to a main condenser 'C' North circulating water outlet through-wall leak. The leak was plugged and the unit returned to 100 percent power the next day. On July 10, 2025, Hope Creek was reduced to 85 percent power for a control rod pattern adjustment and returned to 100 percent power the next day. On July 19, 2025, Hope Creek was reduced to 84 percent power for a control rod pattern adjustment and returned to 100 percent power the next day. Between July 12 and August 17, 2025, Hope Creek was periodically lowered a few percent due to condenser backpressure limitations. On August 19, 2025, Hope Creek was reduced to 81 percent power for main condenser 'C' North waterbox leak repairs as well as 'A' North and 'A' South waterbox tube leak searches. The unit returned to 100 percent rated thermal power on August 24, 2025. On August 25, 2025, Hope Creek commenced its end-of-cycle coastdown. On September 25, 2025, Hope Creek commenced a shutdown from 87 percent power for a refueling outage.
Additional Tracking Items


==INSPECTION SCOPES==
None.  
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.


==REACTOR SAFETY==
PLANT STATUS
==71111.04 - Equipment Alignment==
 
===Partial Walkdown Sample (IP Section 03.01) (3 Samples)===
Hope Creek began the inspection period at rated thermal power. On July 7, 2025, Hope Creek
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:  
was reduced to 75 percent power in response to a main condenser 'C' North circulating
water outlet through-wall leak. The leak was plugged and the unit returned to 100 percent power
the next day. On July 10, 2025, Hope Creek was reduced to 85 percent power for a control rod
pattern adjustment and returned to 100 percent power the next day. On July 19, 2025, Hope
Creek was reduced to 84 percent power for a control rod pattern adjustment and returned to
100 percent power the next day. Between July 12 and August 17, 2025, Hope Creek was
periodically lowered a few percent due to condenser backpressure limitations. On August 19,
2025, Hope Creek was reduced to 81 percent power for main condenser 'C' North waterbox
leak repairs as well as 'A' North and 'A' South waterbox tube leak searches. The unit returned to
100 percent rated thermal power on August 24, 2025. On August 25, 2025, Hope Creek
commenced its end-of-cycle coastdown. On September 25, 2025, Hope Creek commenced a
shutdown from 87 percent power for a refueling outage.
 
INSPECTION SCOPES
 
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed activities described in IMC 2515,
Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of
IPs. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel to assess licensee performance and compliance with Commission rules
and regulations, license conditions, site procedures, and standards.
 
REACTOR SAFETY  
 
71111.04 - Equipment Alignment  
 
Partial Walkdown Sample (IP Section 03.01) (3 Samples)  
 
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:  


(1)  
(1)  
'B' residual heat removal (RHR) division during 'A' RHR pump breaker replacement and motor inspection, July 31, 2025 (2)  
'B' residual heat removal (RHR) division during 'A' RHR pump breaker replacement
'B' core spray division post-maintenance walkdown, September 5, 2025 (3)  
and motor inspection, July 31, 2025  
'A RHR as alternate decay heat removal method with 'B' RHR in shutdown cooling and reactor water level at the vessel flange, September 28, 2025
(2)  
'B' core spray division post-maintenance walkdown, September 5, 2025  
(3)  
'A RHR as alternate decay heat removal method with 'B' RHR in shutdown cooling
and reactor water level at the vessel flange, September 28, 2025  
 
71111.05 - Fire Protection
 
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)
 
The inspectors evaluated the implementation of the fire protection program by conducting a
walkdown and performing a review to verify program compliance, equipment functionality,
material condition, and operational readiness of the following fire areas:
 
(1)
Electric access area and heating, ventilation, and air conditioning (HVAC) wing, Fire
Area 3543, July 3, 2025
(2)
Diesel generator rooms, Fire Area 3531, July 21, 2025
(3)
Electric access area, Fire Area 3533, during major loss of emergency assessment
capability (EN# 57878), August 20, 2025
(4)
Control rod drive hydraulic control unit area, Fire Area 3435, September 18, 2025
 
Fire Brigade Drill Performance Sample (IP Section 03.02) (2 Samples)
 
(1)
The inspectors evaluated the onsite fire brigade training and performance during an
announced fire drill on July 22, 2025.
(2)
The inspectors evaluated the onsite fire brigade training and performance during an
unannounced fire drill on September 9, 2025.
 
71111.06 - Flood Protection Measures
 
Flooding Sample (IP Section 03.01) (1 Sample)


==71111.05 - Fire Protection==
(1)
===Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)===
The inspectors evaluated internal flooding mitigation protections in the safety
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
auxiliaries cooling system (SACS) rooms on July 17, 2025.
: (1) Electric access area and heating, ventilation, and air conditioning (HVAC) wing, Fire Area 3543, July 3, 2025
: (2) Diesel generator rooms, Fire Area 3531, July 21, 2025
: (3) Electric access area, Fire Area 3533, during major loss of emergency assessment capability (EN# 57878), August 20, 2025
: (4) Control rod drive hydraulic control unit area, Fire Area 3435, September 18, 2025  


===Fire Brigade Drill Performance Sample (IP Section 03.02) (2 Samples)===
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
: (1) The inspectors evaluated the onsite fire brigade training and performance during an announced fire drill on July 22, 2025.
: (2) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on September 9, 2025.


==71111.06 - Flood Protection Measures==
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)  
===Flooding Sample (IP Section 03.01) (1 Sample)===
: (1) The inspectors evaluated internal flooding mitigation protections in the safety auxiliaries cooling system (SACS) rooms on July 17, 2025.


==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance==
(1)
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
The inspectors observed operations personnel during the reactor power reduction
: (1) The inspectors observed operations personnel during the reactor power reduction and trip for the refueling outage on September 25, 2025.
and trip for the refueling outage on September 25, 2025.  


===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)===
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)  
: (1) The inspectors observed and evaluated annual simulator examinations on July 10, 2025.
 
: (2) The inspectors observed and evaluated annual simulator examinations on July 24, 2025.
(1)
The inspectors observed and evaluated annual simulator examinations on
July 10, 2025.  
(2)
The inspectors observed and evaluated annual simulator examinations on
July 24, 2025.  
 
71111.12 - Maintenance Effectiveness


==71111.12 - Maintenance Effectiveness==
Maintenance Effectiveness (IP Section 03.01) (1 Sample 1 Partial)  
Maintenance Effectiveness (IP Section 03.01) (1 Sample 1 Partial)  


The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:  
The inspectors evaluated the effectiveness of maintenance to ensure the following
structures, systems, and components (SSCs) remain capable of performing their intended
function:  
 
(1)  
(1)  
(Partial)
(Partial)
Unresolved item (05000354/2025050-03) regarding the lantern ring and packing on emergency diesel generator lube oil heat exchanger floating heads, August 6, 2025
Unresolved item (05000354/2025050-03) regarding the lantern ring and packing on
: (2) B2 SACS heat exchanger flange leak, effectiveness review after temporary modification completion to address all SACS heat exchanger flanges, September 29, 2025
emergency diesel generator lube oil heat exchanger floating heads, August 6, 2025  
(2)
B2 SACS heat exchanger flange leak, effectiveness review after temporary
modification completion to address all SACS heat exchanger flanges,
September 29, 2025  


==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
71111.13 - Maintenance Risk Assessments and Emergent Work Control  
===Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)===
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
: (1) Elevated risk during scheduled activity on 'C' emergency diesel generator, July 7, 2025
: (2) Elevated risk during emergent trip of 'B' reactor protection system electrical protection assembly breakers, August 13, 2025


==71111.15 - Operability Determinations and Functionality Assessments==
Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)
===Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)===
 
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
The inspectors evaluated the accuracy and completeness of risk assessments for the
: (1) Oscillating power range monitor due to confirmation counts during power reduction, July 15, 2025
following planned and emergent work activities to ensure configuration changes and
: (2) Control room HVAC due to low differential pressure on control room supply fan, on July 15, 2025
appropriate work controls were addressed:
: (3) Final feedwater heating temperature reduction due to core end of life coastdown, July 29, 2025 (4)  
 
'A' emergency diesel generator due to noise from intercooler piping during monthly surveillance, July 31, 2025
(1)
: (5) No record of standby liquid control squib valve surveillance test, August 12, 2025
Elevated risk during scheduled activity on 'C' emergency diesel generator,
July 7, 2025
(2)
Elevated risk during emergent trip of 'B' reactor protection system electrical protection
assembly breakers, August 13, 2025
 
71111.15 - Operability Determinations and Functionality Assessments  
 
Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)  
 
The inspectors evaluated the licensee's justifications and actions associated with the
following operability determinations and functionality assessments:  
 
(1)
Oscillating power range monitor due to confirmation counts during power reduction,
July 15, 2025  
(2)
Control room HVAC due to low differential pressure on control room supply fan, on
July 15, 2025  
(3)
Final feedwater heating temperature reduction due to core end of life coastdown,
July 29, 2025  
(4)  
'A' emergency diesel generator due to noise from intercooler piping during monthly
surveillance, July 31, 2025  
(5)
No record of standby liquid control squib valve surveillance test, August 12, 2025  
 
71111.20 - Refueling and Other Outage Activities


==71111.20 - Refueling and Other Outage Activities==
Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)  
Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)  


(1)  
(1)  
(Partial) The inspectors evaluated refueling outage 26 activities from September 25 to 30, 2025
(Partial)
The inspectors evaluated refueling outage 26 activities from September 25
to 30, 2025  


==71111.24 - Testing and Maintenance of Equipment Important to Risk==
71111.24 - Testing and Maintenance of Equipment Important to Risk  
The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:


===Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)===
The inspectors evaluated the following testing and maintenance activities to verify system
: (1) Barrier breach of control room envelope, July 8, 2025
operability and/or functionality:
: (2) Channel calibration following high pressure coolant injection relay replacement, July 9, 2025 (3)  
 
'B' service water pump 4 kilovolt breaker replacement, July 14, 2025 (4)480 volt motor control center starter preventive maintenance on drywell nitrogen supply motor-operated valve 1GSHV-4984B, July 17, 2025
Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)  
: (5) Core spray division 2 channel discharge line flow (minimum flow bypass),
 
(1)
Barrier breach of control room envelope, July 8, 2025  
(2)
Channel calibration following high pressure coolant injection relay replacement,
July 9, 2025  
(3)  
'B' service water pump 4 kilovolt breaker replacement, July 14, 2025  
(4)
480 volt motor control center starter preventive maintenance on drywell nitrogen
supply motor-operated valve 1GSHV-4984B, July 17, 2025  
(5)
Core spray division 2 channel discharge line flow (minimum flow bypass),
August 18, 2025  
August 18, 2025  


===Surveillance Testing (IP Section 03.01) (3 Samples)===
Surveillance Testing (IP Section 03.01) (3 Samples)  
: (1) Refueling floor and reactor building exhaust process radiation monitoring channel time response testing, July 1, 2025 (2)  
 
'C' main steam line flow sensor B21-N687C calibration, July 11, 2025 (3)  
(1)
Refueling floor and reactor building exhaust process radiation monitoring channel
time response testing, July 1, 2025  
(2)  
'C' main steam line flow sensor B21-N687C calibration, July 11, 2025  
(3)  
'C' RHR pump surveillance test, September 3, 2025  
'C' RHR pump surveillance test, September 3, 2025  


===Inservice Testing (IST) (IP Section 03.01) (1 Sample)===
Inservice Testing (IST) (IP Section 03.01) (1 Sample)  
: (1) Reactor core isolation cooling surveillance test, September 8,


==RADIATION SAFETY==
(1)
==71124.07 - Radiological Environmental Monitoring Program (REMP)==
Reactor core isolation cooling surveillance test, September 8, 2025
===Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)===
: (1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples.


===Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)===
RADIATION SAFETY
: (1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program. Partial completed in second quarter and remaining part of sample completed in third quarter.


===GPI Implementation (IP Section 03.03) (1 Sample)===
71124.07 - Radiological Environmental Monitoring Program (REMP)  
: (1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative (GPI) program to identify incomplete or discontinued program elements.


==OTHER ACTIVITIES - BASELINE==
Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)
===71151 - Performance Indicator Verification  
 
(1)
The inspectors evaluated environmental monitoring equipment and observed
collection of environmental samples.
 
Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)
 
(1)
The inspectors evaluated the implementation of the licensees radiological
environmental monitoring program. Partial completed in second quarter and
remaining part of sample completed in third quarter.
 
GPI Implementation (IP Section 03.03) (1 Sample)
 
(1)
The inspectors evaluated the licensees implementation of the Groundwater
Protection Initiative (GPI) program to identify incomplete or discontinued program
elements.
 
OTHER ACTIVITIES - BASELINE  
 
71151 - Performance Indicator Verification  


The inspectors verified licensee performance indicators submittals listed below:  
The inspectors verified licensee performance indicators submittals listed below:  


MS09: Residual Heat Removal Systems (IP Section 02.08)===
MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)
{{IP sample|IP=IP 71151|count=1}}
 
: (1) July 1, 2024 through June 30, 2025  
(1)
July 1, 2024 through June 30, 2025  
 
71153 - Follow-Up of Events and Notices of Enforcement Discretion
 
Personnel Performance (IP Section 03.03) (2 Samples)


===71153 - Follow-Up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)===
(1)
{{IP sample|IP=IP 71153|count=2}}
The inspectors evaluated the failure of the main control room master fire control panel
: (1) The inspectors evaluated the failure of the main control room master fire control panel and PSEG's performance on August 20, 2025 (EN# 57878).
and PSEG's performance on August 20, 2025 (EN# 57878).  
: (2) The inspectors evaluated the B2 SACS heat exchanger leak and emergency operating procedure entry, September 10,
(2)
The inspectors evaluated the B2 SACS heat exchanger leak and emergency
operating procedure entry, September 10, 2025.


==INSPECTION RESULTS==
INSPECTION RESULTS  
Licensee-Identified Non-Cited Violation 71111.24 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.


Violation: Hope Creek Technical Specification 6.8.1 requires that written procedures shall be implemented covering the activities referenced in Regulatory Guide 1.33, Revision 2, Appendix A which includes procedures for operation of safety-related boiling water reactor systems such as emergency core cooling systems in section 4.H. Procedure HC.IC-FT.BE-0004, "Core Spray Division 2 Channel E21-N651B Discharge Line Flow (Minimum Flow Bypass)," Revision 11, step 4.3.9 directed the technicians to notify the reactor operator that the core spray loop B minimum flow bypass valve may be positioned as required by plant conditions. Contrary to this, following notification by the technician, the reactor operator subsequently did not return the minimum flow bypass valve to an open position as required by plant conditions to restore the core spray system to an operable status. As a result, PSEG identified that from 9:41 p.m. on August 14, 2025, to 4:42 p.m. on August 15, 2025, control room operators had not returned the Division 2 core spray minimum flow valve to an open position following completion of an instrumentation and control surveillance test and was therefore inoperable until restored to an open position.
Licensee-Identified Non-Cited Violation
71111.24
This violation of very low safety significance was identified by the licensee and has been
entered into the licensee corrective action program and is being treated as a non-cited
violation, consistent with Section 2.3.2 of the Enforcement Policy.
Violation: Hope Creek Technical Specification 6.8.1 requires that written procedures shall be
implemented covering the activities referenced in Regulatory Guide 1.33, Revision 2,
Appendix A which includes procedures for operation of safety-related boiling water reactor
systems such as emergency core cooling systems in section 4.H. Procedure HC.IC-FT.BE-
0004, "Core Spray Division 2 Channel E21-N651B Discharge Line Flow (Minimum Flow
Bypass)," Revision 11, step 4.3.9 directed the technicians to notify the reactor operator that
the core spray loop B minimum flow bypass valve may be positioned as required by plant
conditions. Contrary to this, following notification by the technician, the reactor operator
subsequently did not return the minimum flow bypass valve to an open position as required
by plant conditions to restore the core spray system to an operable status. As a result, PSEG
identified that from 9:41 p.m. on August 14, 2025, to 4:42 p.m. on August 15, 2025, control
room operators had not returned the Division 2 core spray minimum flow valve to an open
position following completion of an instrumentation and control surveillance test and was
therefore inoperable until restored to an open position.  


Significance/Severity: Green. The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding screened to very low safety significance (Green), by answering No to all the questions in Exhibit 2A.
Significance/Severity: Green. The inspectors assessed the significance of the finding using
IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-
Power. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors
determined the finding screened to very low safety significance (Green), by answering No to
all the questions in Exhibit 2A.  


Corrective Action References: Notifications 20999492 and
Corrective Action References: Notifications 20999492 and 21000111


==EXIT MEETINGS AND DEBRIEFS==
EXIT MEETINGS AND DEBRIEFS  
The inspectors verified that no proprietary information was retained or documented in this report.
* On November 19, 2025, the inspectors presented the integrated inspection results to Eric Larson, Site Vice President, and other members of the licensee staff.
* On July 17, 2025, the inspectors presented the REMP Exit/Debrief for Hope Creek and Salem inspection results to Eric Larson, Hope Creek Site Vice President, and David Sharbaugh, Salem Site Vice President, and other members of the licensee staff.


=DOCUMENTS REVIEWED=
The inspectors verified that no proprietary information was retained or documented in this
report.
* On November 19, 2025, the inspectors presented the integrated inspection results to
Eric Larson, Site Vice President, and other members of the licensee staff.
*
On July 17, 2025, the inspectors presented the REMP Exit/Debrief for Hope Creek and
Salem inspection results to Eric Larson, Hope Creek Site Vice President, and David
Sharbaugh, Salem Site Vice President, and other members of the licensee staff.
 
DOCUMENTS REVIEWED  


Inspection
Inspection
Line 307: Line 474:
HC.MD-PM.PB-
HC.MD-PM.PB-
0001
0001
4.16 KV Breaker Cleaning and P.M.
4.16 KV Breaker Cleaning and P.M.  
 
OP-HC-103-106
OP-HC-103-106
Control Room Envelope Integrity
Control Room Envelope Integrity  
 
Work Orders
Work Orders
30312533
30312533
226599
50226599


71152A
71152A

Revision as of 00:36, 21 February 2026

Integrated Inspection Report 05000354/2025003
ML25351A122
Person / Time
Site: Hope Creek 
Issue date: 12/17/2025
From: Nicole Warnek
Division of Operating Reactors
To: Mcfeaters C
Public Service Enterprise Group
References
IR 2025003
Download: ML25351A122 (0)


Text

December 17, 2025

SUBJECT:

HOPE CREEK GENERATING STATION - INTEGRATED INSPECTION REPORT 05000354/2025003

Dear Charles McFeaters:

On September 30, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station. On November 19, 2025, the NRC inspectors discussed the results of this inspection with Eric Larson, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

Due to the temporary cessation of government operations, which commenced on October 1, 2025, the NRC began operating under its Office of Management and Budget-approved plan for operations during a lapse in appropriations. Consistent with that plan, the NRC operated at reduced staffing levels throughout the duration of the shutdown. However, the NRC continued to perform critical health and safety functions and make progress on other high-priority activities associated with the ADVANCE Act and Executive Order 14300. On November 13, 2025, following the passage of a continuing resolution, the NRC resumed normal operations. However, due to the 43-day lapse in normal operations, the Office of Nuclear Reactor Regulation granted the Regional Offices an extension on the issuance of the calendar year 2025, 3rd quarter integrated inspection reports normally issued by November 15, 2025, to December 31, 2025. The NRC will resume the routine cycle of issuing inspection reports on a quarterly basis beginning with the calendar year 2025, 4th quarter integrated inspection reports, which will be issued 45 days after the 4th quarter ends on December 31, 2025.

No NRC-identified or self-revealing findings were identified during this inspection.

A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)

consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Hope Creek Generating Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Nicole S. Warnek, Chief Projects Branch 3 Division of Operating Reactor Safety

Docket No. 05000354 License No. NPF-57

Enclosure:

As stated

Inspection Report

Docket Number:

05000354

License Number:

NPF-57

Report Number:

05000354/2025003

Enterprise Identifier: I-2025-003-0037

Licensee:

PSEG Nuclear, LLC

Facility:

Hope Creek Generating Station

Location:

Hancocks Bridge, NJ

Inspection Dates:

July 1, 2025 to September 30, 2025

Inspectors:

J. Bresson, Project Engineer

P. Finney, Senior Resident Inspector

N. Harmon, Health Physicist

J. Morgan, Operations Engineer

R. Rolph, Senior Health Physicist

Approved By:

Nicole S. Warnek, Chief

Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Hope Creek Generating Station, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified

non-cited violation is documented in report section: 71111.24.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Hope Creek began the inspection period at rated thermal power. On July 7, 2025, Hope Creek

was reduced to 75 percent power in response to a main condenser 'C' North circulating

water outlet through-wall leak. The leak was plugged and the unit returned to 100 percent power

the next day. On July 10, 2025, Hope Creek was reduced to 85 percent power for a control rod

pattern adjustment and returned to 100 percent power the next day. On July 19, 2025, Hope

Creek was reduced to 84 percent power for a control rod pattern adjustment and returned to

100 percent power the next day. Between July 12 and August 17, 2025, Hope Creek was

periodically lowered a few percent due to condenser backpressure limitations. On August 19,

2025, Hope Creek was reduced to 81 percent power for main condenser 'C' North waterbox

leak repairs as well as 'A' North and 'A' South waterbox tube leak searches. The unit returned to

100 percent rated thermal power on August 24, 2025. On August 25, 2025, Hope Creek

commenced its end-of-cycle coastdown. On September 25, 2025, Hope Creek commenced a

shutdown from 87 percent power for a refueling outage.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix DProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 2515,</br></br>Appendix D" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

'B' residual heat removal (RHR) division during 'A' RHR pump breaker replacement

and motor inspection, July 31, 2025

(2)

'B' core spray division post-maintenance walkdown, September 5, 2025

(3)

'A RHR as alternate decay heat removal method with 'B' RHR in shutdown cooling

and reactor water level at the vessel flange, September 28, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Electric access area and heating, ventilation, and air conditioning (HVAC) wing, Fire

Area 3543, July 3, 2025

(2)

Diesel generator rooms, Fire Area 3531, July 21, 2025

(3)

Electric access area, Fire Area 3533, during major loss of emergency assessment

capability (EN 57878), August 20, 2025

(4)

Control rod drive hydraulic control unit area, Fire Area 3435, September 18, 2025

Fire Brigade Drill Performance Sample (IP Section 03.02) (2 Samples)

(1)

The inspectors evaluated the onsite fire brigade training and performance during an

announced fire drill on July 22, 2025.

(2)

The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill on September 9, 2025.

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated internal flooding mitigation protections in the safety

auxiliaries cooling system (SACS) rooms on July 17, 2025.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

The inspectors observed operations personnel during the reactor power reduction

and trip for the refueling outage on September 25, 2025.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1)

The inspectors observed and evaluated annual simulator examinations on

July 10, 2025.

(2)

The inspectors observed and evaluated annual simulator examinations on

July 24, 2025.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample 1 Partial)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

(Partial)

Unresolved item (05000354/2025050-03) regarding the lantern ring and packing on

emergency diesel generator lube oil heat exchanger floating heads, August 6, 2025

(2)

B2 SACS heat exchanger flange leak, effectiveness review after temporary

modification completion to address all SACS heat exchanger flanges,

September 29, 2025

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Elevated risk during scheduled activity on 'C' emergency diesel generator,

July 7, 2025

(2)

Elevated risk during emergent trip of 'B' reactor protection system electrical protection

assembly breakers, August 13, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Oscillating power range monitor due to confirmation counts during power reduction,

July 15, 2025

(2)

Control room HVAC due to low differential pressure on control room supply fan, on

July 15, 2025

(3)

Final feedwater heating temperature reduction due to core end of life coastdown,

July 29, 2025

(4)

'A' emergency diesel generator due to noise from intercooler piping during monthly

surveillance, July 31, 2025

(5)

No record of standby liquid control squib valve surveillance test, August 12, 2025

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors evaluated refueling outage 26 activities from September 25

to 30, 2025

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system

operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)

(1)

Barrier breach of control room envelope, July 8, 2025

(2)

Channel calibration following high pressure coolant injection relay replacement,

July 9, 2025

(3)

'B' service water pump 4 kilovolt breaker replacement, July 14, 2025

(4)

480 volt motor control center starter preventive maintenance on drywell nitrogen

supply motor-operated valve 1GSHV-4984B, July 17, 2025

(5)

Core spray division 2 channel discharge line flow (minimum flow bypass),

August 18, 2025

Surveillance Testing (IP Section 03.01) (3 Samples)

(1)

Refueling floor and reactor building exhaust process radiation monitoring channel

time response testing, July 1, 2025

(2)

'C' main steam line flow sensor B21-N687C calibration, July 11, 2025

(3)

'C' RHR pump surveillance test, September 3, 2025

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1)

Reactor core isolation cooling surveillance test, September 8, 2025

RADIATION SAFETY

71124.07 - Radiological Environmental Monitoring Program (REMP)

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated environmental monitoring equipment and observed

collection of environmental samples.

Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the implementation of the licensees radiological

environmental monitoring program. Partial completed in second quarter and

remaining part of sample completed in third quarter.

GPI Implementation (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees implementation of the Groundwater

Protection Initiative (GPI) program to identify incomplete or discontinued program

elements.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)

(1)

July 1, 2024 through June 30, 2025

71153 - Follow-Up of Events and Notices of Enforcement Discretion

Personnel Performance (IP Section 03.03) (2 Samples)

(1)

The inspectors evaluated the failure of the main control room master fire control panel

and PSEG's performance on August 20, 2025 (EN 57878).

(2)

The inspectors evaluated the B2 SACS heat exchanger leak and emergency

operating procedure entry, September 10, 2025.

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation

71111.24

This violation of very low safety significance was identified by the licensee and has been

entered into the licensee corrective action program and is being treated as a non-cited

violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Hope Creek Technical Specification 6.8.1 requires that written procedures shall be

implemented covering the activities referenced in Regulatory Guide 1.33, Revision 2,

Appendix A which includes procedures for operation of safety-related boiling water reactor

systems such as emergency core cooling systems in section 4.H. Procedure HC.IC-FT.BE-

0004, "Core Spray Division 2 Channel E21-N651B Discharge Line Flow (Minimum Flow

Bypass)," Revision 11, step 4.3.9 directed the technicians to notify the reactor operator that

the core spray loop B minimum flow bypass valve may be positioned as required by plant

conditions. Contrary to this, following notification by the technician, the reactor operator

subsequently did not return the minimum flow bypass valve to an open position as required

by plant conditions to restore the core spray system to an operable status. As a result, PSEG

identified that from 9:41 p.m. on August 14, 2025, to 4:42 p.m. on August 15, 2025, control

room operators had not returned the Division 2 core spray minimum flow valve to an open

position following completion of an instrumentation and control surveillance test and was

therefore inoperable until restored to an open position.

Significance/Severity: Green. The inspectors assessed the significance of the finding using

IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-

Power. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors

determined the finding screened to very low safety significance (Green), by answering No to

all the questions in Exhibit 2A.

Corrective Action References: Notifications 20999492 and 21000111

EXIT MEETINGS AND DEBRIEFS

The inspectors verified that no proprietary information was retained or documented in this

report.

  • On November 19, 2025, the inspectors presented the integrated inspection results to

Eric Larson, Site Vice President, and other members of the licensee staff.

On July 17, 2025, the inspectors presented the REMP Exit/Debrief for Hope Creek and

Salem inspection results to Eric Larson, Hope Creek Site Vice President, and David

Sharbaugh, Salem Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

Resulting from

Inspection

20997508

71111.05

Corrective Action

Documents

Resulting from

Inspection

20997021

71111.11Q Corrective Action

Documents

Resulting from

Inspection

20997872

21002528

71111.12

Corrective Action

Documents

Resulting from

Inspection

20997578

20999301

71111.13

Corrective Action

Documents

Resulting from

Inspection

20999638

20999469

71111.15

Corrective Action

Documents

20996525

20997306

20998326

71111.20

Corrective Action

Documents

Resulting from

Inspection

21001545

21001544

21001677

21003422

71111.24

Corrective Action

Documents

Resulting from

Inspection

20997725

20997742

20997892

20997457

20997306

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20999022

21001138

Procedures

HC.MD-PM.PB-

0001

4.16 KV Breaker Cleaning and P.M.

OP-HC-103-106

Control Room Envelope Integrity

Work Orders

30312533

50226599

71152A

Corrective Action

Documents

Resulting from

Inspection

20997262

20997594

20998461

20998853

20999085

20999084

20999652

20999594

20999693

21000269

21000208

21000318

21000317

21000933

21000932

20998155

21000855

21000974

21000973

21000931

21001259

21001515

21003541

21003540

21003308

71153

Corrective Action

Documents

21000840

21000838

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

21000794

21000795

21000796

20999815

20999816

20999817

20999818

20999819

20999820

21000793

21000794

21000795

21000796