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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES
NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUITE 210 LISLE, IL 60532-4352  
                            NUCLEAR REGULATORY COMMISSION
February 10, 2015  
                                                REGION III
                                    2443 WARRENVILLE RD. SUITE 210
Mr. Larry Weber  
                                          LISLE, IL 60532-4352
Senior VP and Chief Nuclear Officer  
                                        February 10, 2015
Indiana Michigan Power Company  
Mr. Larry Weber
Nuclear Generation Group One Cook Place  
Senior VP and Chief Nuclear Officer
Indiana Michigan Power Company
Nuclear Generation Group
One Cook Place
Bridgman, MI 49106
SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2
              NRC INTEGRATED INSPECTION REPORT 05000315/2014005;
              05000316/2014005
Dear Mr. Weber:
On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2. The enclosed report
documents the results of this inspection, which were discussed on January 20, 2015, with
yourself and members of your staff.
Based on the results of this inspection, three NRC-identified and two self-revealed findings of
very low safety significance were identified. The findings involved violations of NRC
requirements. However, because of their very low safety significance, and because the issues
were entered into your corrective action program, the NRC is treating the issues as
non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy
If you contest the subject or severity of these NCVs, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the
cross-cutting aspect assigned to any finding in this report, you should provide a response within
30 days of the date of this inspection report, with the basis for your disagreement, to the
Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook
Nuclear Power Plant.


Bridgman, MI  49106
L. Weber                                      -2-
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy
of this letter, its enclosure, and your response (if any) will be available electronically for public
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
                                              Sincerely,
                                              /RA/
                                              Kenneth Riemer, Chief
                                              Branch 2
                                              Division of Reactor Projects
Docket Nos. 50-315; 50-316
License Nos. DPR-58; DPR-74
Enclosure:
IR 05000315/2014005; 05000316/2014005
  w/Attachment: Supplemental Information
cc w/encl: Distribution via LISTSERV


          U.S. NUCLEAR REGULATORY COMMISSION
SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000315/2014005;  
                          REGION III
05000316/2014005
Docket Nos:         05000315; 05000316
  Dear Mr. Weber: On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2.  The enclosed report
License Nos:       DPR-58; DPR-74
documents the results of this inspection, which were discussed on January 20, 2015, with
Report No:          05000315/2014005; 05000316/2014005
yourself and members of your staff. Based on the results of this inspection, three NRC-identified and two self-revealed findings of very low safety significance were identified.  The findings involved violations of NRC requirements.  However, because of their very low safety significance, and because the issues
Licensee:          Indiana Michigan Power Company
were entered into your corrective action program, the NRC is treating the issues as  non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy If you contest the subject or severity of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Facility:          Donald C. Cook Nuclear Power Plant, Units 1 and 2
Regulatory Commission, ATTN:  Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
Location:          Bridgman, MI
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
Dates:              October 1 through December 31, 2014
Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the
Inspectors:        J. Ellegood, Senior Resident Inspector
cross-cutting aspect assigned to any finding in this report, you should provide a response within
                    T. Taylor, Resident Inspector
30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook
                    J. Cassidy, Senior Health Physicist
Nuclear Power Plant.  
                    M. Garza, Emergency Response Specialist
  L. Weber -2-
                    T. Go, Health Physicist
                    J. Lennartz, Project Engineer
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public
                    M. Mitchell, Health Physicist
inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
                    M. Phalen, Senior Health Physicist
(the Public Electronic Reading Room).  
                    E. Sanchez Santiago, Reactor Inspector
Sincerely,  /RA/  Kenneth Riemer, Chief
Approved by:        Kenneth Riemer, Chief
Branch 2 Division of Reactor Projects
                    Branch 2
 
                    Division of Reactor Projects
Docket Nos. 50-315; 50-316 License Nos. DPR-58; DPR-74
                                                                  Enclosure
 
Enclosure: 
                                        TABLE OF CONTENTS
IR 05000315/2014005; 05000316/2014005 w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV
SUMMARY OF FINDINGS ........................................................................................................... 2
 
REPORT DETAILS ....................................................................................................................... 6
Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 05000315; 05000316 License Nos: DPR-58; DPR-74 Report No: 05000315/2014005; 05000316/2014005 Licensee: Indiana Michigan Power Company Facility: Donald C. Cook Nuclear Power Plant, Units 1 and 2 Location: Bridgman, MI Dates: October 1 through December 31, 2014 Inspectors: J. Ellegood, Senior Resident Inspector  T. Taylor, Resident Inspector  J. Cassidy, Senior Health Physicist
Summary of Plant Status ........................................................................................................... 6
M. Garza, Emergency Response Specialist
  1.     REACTOR SAFETY ................................................................................................. 6
T. Go, Health Physicist 
      1R01  Adverse Weather Protection (71111.01) ............................................................ 6
J. Lennartz, Project Engineer 
      1R04  Equipment Alignment (71111.04) ....................................................................... 7
M. Mitchell, Health Physicist  M. Phalen, Senior Health Physicist  E. Sanchez Santiago, Reactor Inspector Approved by: Kenneth Riemer, Chief
      1R05  Fire Protection (71111.05) .................................................................................. 8
Branch 2 Division of Reactor Projects
      1R06  Flooding (71111.06) ........................................................................................... 9
 
      1R07  Annual Heat Sink Performance (71111.07) ...................................................... 10
  TABLE OF CONTENTS SUMMARY OF FINDINGS ...........................................................................................................
      1R08  Inservice Inspection Activities (71111.08P) ...................................................... 10
2 REPORT DETAILS ................................................................................................................
      1R11  Licensed Operator Requalification Program (71111.11) .................................. 13
....... 6 Summary of Plant Status .......................................................................................................
      1R12  Maintenance Effectiveness (71111.12) ............................................................ 15
.... 6 1. REACTOR SAFETY ................................................................................................. 6
      1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15
1R01 Adverse Weather Protection (71111.01) ............................................................ 6
      1R15  Operability Determinations and Functional Assessments (71111.15) .............. 16
1R04 Equipment Alignment (71111.04) ....................................................................... 7
      1R18  Plant Modifications (71111.18) ......................................................................... 21
1R05 Fire Protection (71111.05) .................................................................................. 8
      1R19  Post-Maintenance Testing (71111.19) ............................................................. 24
1R06 Flooding (71111.06) ........................................................................................... 9
      1R20  Outage Activities (71111.20) ............................................................................ 27
1R07 Annual Heat Sink Performance (71111.07) ...................................................... 10
      1R22  Surveillance Testing (71111.22) ....................................................................... 28
1R08 Inservice Inspection Activities (71111.08P) ...................................................... 10
      1EP4  Emergency Action Level and Emergency Plan Changes (71114.04) ............... 29
1R11 Licensed Operator Requalification Program (71111.11) .................................. 13
  2.     RADIATION SAFETY ............................................................................................. 31
1R12 Maintenance Effectiveness (71111.12) ............................................................ 15
      2RS1  Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31
1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15
      2RS2  Occupational As-Low-As-Reasonably-Achievable Planning and Controls
1R15 Operability Determinations and Functional Assessments (71111.15) .............. 16
            (71124.02) ........................................................................................................ 37
1R18 Plant Modifications (71111.18) ......................................................................... 21
      2RS7  Radiological Environmental Monitoring Program (71124.07) ........................... 38
1R19 Post-Maintenance Testing (71111.19) ............................................................. 24
  4.     OTHER ACTIVITIES .............................................................................................. 40
1R20 Outage Activities (71111.20) ............................................................................ 27
      4OA1  Performance Indicator Verification (71151) ...................................................... 40
1R22 Surveillance Testing (71111.22) ....................................................................... 28
      4OA2  Identification and Resolution of Problems (71152) ........................................... 45
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
      4OA3  Followup of Events and Notices of Enforcement Discretion (71153) ............... 49
............... 29
      4OA6  Management Meetings ..................................................................................... 50
2. RADIATION SAFETY ............................................................................................. 31
SUPPLEMENTAL INFORMATION ............................................................................................... 1
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31
2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02) ........................................................................................................ 37
2RS7 Radiological Environmental Monitoring Program (71124.07) ........................... 38
4. OTHER ACTIVITIES .............................................................................................. 40
4OA1 Performance Indicator Verification (71151) ...................................................... 40
4OA2 Identification and Resolution of Problems (71152) ........................................... 45
4OA3  Followup of Events and Notices of Enforcement Discretion (71153) ............... 49
4OA6 Management Meetings ..................................................................................... 50
SUPPLEMENTAL INFORMATION ............................................................................................... 1
  KEY POINTS OF CONTACT..................................................................................................... 1
  KEY POINTS OF CONTACT..................................................................................................... 1
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2
  LIST OF DOCUMENTS REVIEWED  
  LIST OF DOCUMENTS REVIEWED......................................................................................... 3
......................................................................................... 3
  LIST OF ACRONYMS USED .................................................................................................. 13
  LIST OF ACRONYMS USED .................................................................................................. 13
 
2  SUMMARY OF FINDINGS Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;  Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional
Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment
and Exposure Controls. This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.
  Three Green findings were identified by the inspectors.  Additionally, there were two Green self-revealed findings. The findings were considered non-cited violations (NCVs) of NRC regulations.  The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and
determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process"
dated June 2, 2011.  Cross-cutting aspects are determined using IMC 0310, "Aspects Within the Cross-Cutting Areas" effective date December 4, 2014.  All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated July 9, 2013.  The NRC's
program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5, dated February 2014. Cornerstone:  Mitigating Systems
* Green.  A finding of very low safety significance, with an associated non-cited violation of 10 CFR Part 50, Appendix B, Criterion 16, "Corrective Actions," was identified by the inspectors for the licensee's failure to promptly identify and correct a condition adverse to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW) pump turbine bearing oil.  Specifically, the licensee failed to identify that water was entering the oil system after leakage had been identified directly above one of the
TDAFW pump turbine bearings.  On April 7, 2014, a cooling water leak was identified
above the outboard turbine bearing.  The leak was classified as about 1 drop-per-minute
(dpm).  On April 11, 2014, the licensee discovered the turbine bearing oil level was
above the maximum mark on an attached sight glass.  Several possible reasons were postulated for the high level (which had been steady in-band for over a year), such as rising turbine building temperatures and the fact that it was not uncommon for personnel
to do 'unnecessary' oil adds to the machine.  Oil was drained out until level returned to
the maximum mark.  On May 22, 2014, the licensee again noted oil level to be above the
maximum mark.  Oil was drained again, and similar reasons provided for the level increase.  Further, a statement was made that oil level had been steady for the past month, neglecting the previous high level condition.  In parallel, NRC inspectors had
questioned why level was being maintained at the maximum mark when the operator
logs and a sign stated level should be kept at the minimum mark.  On May 23, the
licensee decided to drain the oil system; 620 ml of water was found.  New oil was added,
and a temporary modification was installed which directed leakage away from the bearing.  The issue was entered into the Corrective Action Program (CAP), and an apparent cause evaluation later determined the leakage to be the primary intrusion pathway for the water. The issue was more-than-minor because it adversely affected the Configuration Control attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the
availability, reliability, and capability of systems that respond to initiating events to
prevent undesirable consequences.  Additionally, if left uncorrected, the issue could lead to a more significant safety concern.  The inspectors assessed the finding for 
3  significance using IMC 0609, "Significance Determination Process."  Per Appendix A, the finding screened as Green, or very low safety significance, in Exhibit 2.  Specifically, all questions were answered 'no' under Section A for findings related to Mitigating Structures, Systems and Components (SSCs) and Functionality.  The inspectors reviewed the licensee's past operability ev
aluation and concluded that given the projected amount of water that could be entrained in the oil during operation, along with
the duration of operation assumed in the safety analyses, that operability of the pump
would be maintained.  The finding had an associated cross-cutting aspect in the Human
Performance area, specifically, H.11, Challenge the Unknown.  Regarding the TDAFW oil system, the licensee rationalized why the level was increasing without sufficient investigation given the significance of the system, and did not seek further information that was readily available regarding appropriate oil levels.  (Section 1R15)
* Green.  A finding of very low safety significance, with an associated non-cited violation of Technical Specification (TS) 5.4, "Procedures," was self-revealed when a vacuum was inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for
surveillance activities.  The vacuum caused an indication of lowering level in the tank,
alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement
entry.  The licensee was performing work activities in preparation for a leak test of the FOST.  The general sequence of activities should have been a loosening of the vent filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator
(EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter
so test equipment could be connected to the tank.  Due to ambiguous work instruction
steps and activities not being adequately controlled to ensure the proper sequence occurred, workers first removed the vent filter completely and placed a Foreign Material Exclusion (FME) bag over the vent.  When operators later transferred fuel, a vacuum
was drawn in the tank and level appeared to be going down.  Utilizing a manual method


of level measurement (which had also been affected by the vacuum), operators
                                        SUMMARY OF FINDINGS
determined fuel was actually being lost from the tank to the environment. Shortly
Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;
thereafter, the bag was found and removed, and level restored to normal (there was no actual loss of fuel). Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the applicable
Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional
procedures recommended in Regulatory Guide 1.33.  Regulatory Guide 1.33 states, in
Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment
part, that maintenance that can affect the performance of safety-related equipment
and Exposure Controls.
should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.  Contrary to these requirements, the FOST surveillance was performed with inadequate instructions
This report covers a 3-month period of inspection by resident inspectors and announced
and was not coordinated appropriately.  The licensee entered the issue into the CAP and
baseline inspections by regional inspectors. Three Green findings were identified by the
performed a root cause analysis.  
inspectors. Additionally, there were two Green self-revealed findings. The findings were
The performance deficiency was more than minor because it adversely impacted the Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is
considered non-cited violations (NCVs) of NRC regulations. The significance of inspection
ensuring the availability, reliability, and capability of systems that respond to initiating
findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and
events to prevent undesirable consequences.  The finding screened as Green, or very
determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
low safety significance, utilizing IMC 0609, Appendix A, "The Significance Determination
dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects Within the
Process for Findings at Power."  Specifically, all questions were answered 'no' under Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag was installed, which rendered the AB FOST inoperable, for approximately
Cross-Cutting Areas effective date December 4, 2014. All violations of NRC requirements are
16 hours. This was less than the TS allowed outage time of 48 hours. The finding had
dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's
an associated cross-cutting aspect in the  
program for overseeing the safe operation of commercial nuclear power reactors is described in
human performance area, specifically, H.5, Work Management. Work activities should be planned, controlled, and executed with 
NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.
4  nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting aspect, the work was planned and executed with inadequate work instructions. Further,  
        Cornerstone: Mitigating Systems
there was a lack of coordination between a number of work groups and activities associated with the test.  (Section 1R15)  
    *  Green. A finding of very low safety significance, with an associated non-cited violation of
* Green.  A finding of very low safety significance, with an associated non- violation  of TS 5.4, "Procedures," was self-revealed on November 1, 2014, when the Unit 1 TDAFW pump tripped during an emergent dual-unit shutdown.  Both units were taken
        10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the
offline by operators due to debris intrusion from Lake Michigan into the cooling water
        inspectors for the licensees failure to promptly identify and correct a condition adverse
screenhouse. The TDAFW pump started as expected but shutdown after a few minutes
        to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW)
of operation. Investigation by the licensee revealed that a cover for the trip solenoid had been installed incorrectly. The cover was relatively loose and had been placed near components involved with the proper latching of the Trip and Throttle valve (TTV) (the  
        pump turbine bearing oil. Specifically, the licensee failed to identify that water was
valve which opens to let steam in to turn the pump on).  After refuting several possible
        entering the oil system after leakage had been identified directly above one of the
causes and running the pump several times for testing, the licensee determined the
        TDAFW pump turbine bearings. On April 7, 2014, a cooling water leak was identified
likely cause of the trip was the misplaced enclosure, which could have interfered with the proper latching of the TTV. Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the  
        above the outboard turbine bearing. The leak was classified as about 1 drop-per-minute
applicable procedures recommended in Regulatory Guide 1.33.  Regulatory Guide 1.33
        (dpm). On April 11, 2014, the licensee discovered the turbine bearing oil level was
states, in part, that maintenance that can affect the performance of safety-related
        above the maximum mark on an attached sight glass. Several possible reasons were
equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.  Contrary to these requirements, the cause of the misplaced enclosure was due to a lack
        postulated for the high level (which had been steady in-band for over a year), such as
of detailed instructions regarding the installation and removal of the enclosure. The  
        rising turbine building temperatures and the fact that it was not uncommon for personnel
enclosure was most recently affected by maintenance performed during the fall 2014
        to do unnecessary oil adds to the machine. Oil was drained out until level returned to
refueling outage. The licensee worked with the vendor and reinstalled the enclosure
        the maximum mark. On May 22, 2014, the licensee again noted oil level to be above the
correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of
        maximum mark. Oil was drained again, and similar reasons provided for the level
position and corrected.  The licensee entered the issue into the CAP. The performance deficiency was more than minor because it adversely impacted the Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is ensuring the availability, reliability, and capability of systems that respond to initiating
        increase. Further, a statement was made that oil level had been steady for the past
events to prevent undesirable consequences. The inspectors utilized IMC 0609
        month, neglecting the previous high level condition. In parallel, NRC inspectors had
Appendix A, "The Significance Determination Process for Findings at Power," to assess
        questioned why level was being maintained at the maximum mark when the operator
the significance of the finding. Per Exhibit 2, the finding represented a loss of function for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time. Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed
        logs and a sign stated level should be kept at the minimum mark. On May 23, the
risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since the last successful surveillance on October 23, 2014. Given the evidence available, this was the likely opportunity for the conditions to be established to set-up the improper engagement between the TTV and the trip hook.  In the detailed analysis, the finding screened as Green, or very low safety significanceThe finding had an associated
        licensee decided to drain the oil system; 620 ml of water was found. New oil was added,
cross-cutting aspect in the area of human performance, specifically, H.8, Procedure
        and a temporary modification was installed which directed leakage away from the
Adherence.  During maintenance, work proceeded on the trip enclosure despite a lack of detailed instructions on the removal/installation of the enclosure. (Section 1R19)  Cornerstone:  Barrier Integrity
        bearing. The issue was entered into the Corrective Action Program (CAP), and an
* Green.  The inspectors identified a non- violation of 10 CFR Part 50, Appendix B,  Criterion 3 "Design Control," for the licensee's inadequate radiological review of permanently removing the Auxiliary Missile Bl
        apparent cause evaluation later determined the leakage to be the primary intrusion
ocks (AMBs) from the Unit 1 and Unit 2 
        pathway for the water.
5  containment accident shields. The finding was determined to be more than minor because it was associated with the Barrier Integrity Cornerstone attribute of design
        The issue was more-than-minor because it adversely affected the Configuration Control
control; and adversely affected the cornerstone objective of maintaining radiological barrier functionality of the safety-related accident shield. Specifically, the failure to control plant design and adequately evaluate the radiological effects of permanently
        attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the
removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not
        availability, reliability, and capability of systems that respond to initiating events to
ensure that the accident shield will provide its design function to ensure safe radiation levels outside the containment building following a maximum design basis  accident. The inspectors evaluated the finding using the Significance Determination Process (SDP) in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," dated June 19, 2012.  Because the finding impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through
        prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead
IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power,"
        to a more significant safety concern. The inspectors assessed the finding for
dated June 19, 2012, using Exhibit 3, "Barrier Integrity Screening Questions."  The
                                                      2
finding screened as very-low safety significance (Green) because the finding only
 
represented a degradation of the radiological barrier function provided for the Auxiliary Building.  The inspectors determined the cause of this finding did not represent current licensee performance and, thus, no cross-cutting aspect was assigned.  (Section 1R18) Cornerstone:  Occupational Radiation Safety
  significance using IMC 0609, Significance Determination Process. Per Appendix A, the
* Green.  The inspectors identified a finding of very-low safety significance for inadequate procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with an associated non- violation of TS 5.4, "Procedures."  As a result, weekly, from November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the  
  finding screened as Green, or very low safety significance, in Exhibit 2. Specifically, all
Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area against unauthorized access. The inspectors determined that the performance deficiency was more than minor because if left uncorrected the performance deficiency could lead to a more significant  
  questions were answered no under Section A for findings related to Mitigating
  Structures, Systems and Components (SSCs) and Functionality. The inspectors
  reviewed the licensees past operability evaluation and concluded that given the
  projected amount of water that could be entrained in the oil during operation, along with
  the duration of operation assumed in the safety analyses, that operability of the pump
  would be maintained. The finding had an associated cross-cutting aspect in the Human
  Performance area, specifically, H.11, Challenge the Unknown. Regarding the TDAFW
  oil system, the licensee rationalized why the level was increasing without sufficient
  investigation given the significance of the system, and did not seek further information
  that was readily available regarding appropriate oil levels. (Section 1R15)
* Green. A finding of very low safety significance, with an associated non-cited violation
  of Technical Specification (TS) 5.4, Procedures, was self-revealed when a vacuum was
  inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for
  surveillance activities. The vacuum caused an indication of lowering level in the tank,
  alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement
  entry. The licensee was performing work activities in preparation for a leak test of the
  FOST. The general sequence of activities should have been a loosening of the vent
  filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator
  (EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter
  so test equipment could be connected to the tank. Due to ambiguous work instruction
  steps and activities not being adequately controlled to ensure the proper sequence
  occurred, workers first removed the vent filter completely and placed a Foreign Material
  Exclusion (FME) bag over the vent. When operators later transferred fuel, a vacuum
  was drawn in the tank and level appeared to be going down. Utilizing a manual method
  of level measurement (which had also been affected by the vacuum), operators
  determined fuel was actually being lost from the tank to the environment. Shortly
  thereafter, the bag was found and removed, and level restored to normal (there was no
  actual loss of fuel). Technical Specification 5.4, Procedures, states, in part, that written
  procedures shall be established, implemented, and maintained covering the applicable
  procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
  part, that maintenance that can affect the performance of safety-related equipment
  should be properly preplanned and performed in accordance with written procedures,
  documented instructions, or drawings appropriate to the circumstances. Contrary to
  these requirements, the FOST surveillance was performed with inadequate instructions
  and was not coordinated appropriately. The licensee entered the issue into the CAP and
  performed a root cause analysis.
  The performance deficiency was more than minor because it adversely impacted the
  Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is
  ensuring the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. The finding screened as Green, or very
  low safety significance, utilizing IMC 0609, Appendix A, The Significance Determination
  Process for Findings at Power. Specifically, all questions were answered no under
  Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.
  The FME bag was installed, which rendered the AB FOST inoperable, for approximately
  16 hours. This was less than the TS allowed outage time of 48 hours. The finding had
  an associated cross-cutting aspect in the human performance area, specifically, H.5,
  Work Management. Work activities should be planned, controlled, and executed with
                                                3
 
  nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting
  aspect, the work was planned and executed with inadequate work instructions. Further,
  there was a lack of coordination between a number of work groups and activities
  associated with the test. (Section 1R15)
* Green. A finding of very low safety significance, with an associated non- violation
  of TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1
  TDAFW pump tripped during an emergent dual-unit shutdown. Both units were taken
  offline by operators due to debris intrusion from Lake Michigan into the cooling water
  screenhouse. The TDAFW pump started as expected but shutdown after a few minutes
  of operation. Investigation by the licensee revealed that a cover for the trip solenoid had
  been installed incorrectly. The cover was relatively loose and had been placed near
  components involved with the proper latching of the Trip and Throttle valve (TTV) (the
  valve which opens to let steam in to turn the pump on). After refuting several possible
  causes and running the pump several times for testing, the licensee determined the
  likely cause of the trip was the misplaced enclosure, which could have interfered with the
  proper latching of the TTV. Technical Specification 5.4, Procedures, states, in part,
  that written procedures shall be established, implemented, and maintained covering the
  applicable procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33
  states, in part, that maintenance that can affect the performance of safety-related
  equipment should be properly preplanned and performed in accordance with written
  procedures, documented instructions, or drawings appropriate to the circumstances.
  Contrary to these requirements, the cause of the misplaced enclosure was due to a lack
  of detailed instructions regarding the installation and removal of the enclosure. The
  enclosure was most recently affected by maintenance performed during the fall 2014
  refueling outage. The licensee worked with the vendor and reinstalled the enclosure
  correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of
  position and corrected. The licensee entered the issue into the CAP.
  The performance deficiency was more than minor because it adversely impacted the
  Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is
  ensuring the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. The inspectors utilized IMC 0609
  Appendix A, The Significance Determination Process for Findings at Power, to assess
  the significance of the finding. Per Exhibit 2, the finding represented a loss of function
  for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time.
  Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed
  risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since
  the last successful surveillance on October 23, 2014. Given the evidence available, this
  was the likely opportunity for the conditions to be established to set-up the improper
  engagement between the TTV and the trip hook. In the detailed analysis, the finding
  screened as Green, or very low safety significance. The finding had an associated
  cross-cutting aspect in the area of human performance, specifically, H.8, Procedure
  Adherence. During maintenance, work proceeded on the trip enclosure despite a lack of
  detailed instructions on the removal/installation of the enclosure. (Section 1R19)
  Cornerstone: Barrier Integrity
* Green. The inspectors identified a non- violation of 10 CFR Part 50, Appendix B,
  Criterion 3 Design Control, for the licensees inadequate radiological review of
  permanently removing the Auxiliary Missile Blocks (AMBs) from the Unit 1 and Unit 2
                                              4
 
  containment accident shields. The finding was determined to be more than minor
  because it was associated with the Barrier Integrity Cornerstone attribute of design
  control; and adversely affected the cornerstone objective of maintaining radiological
  barrier functionality of the safety-related accident shield. Specifically, the failure to
  control plant design and adequately evaluate the radiological effects of permanently
  removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not
  ensure that the accident shield will provide its design function to ensure safe radiation
  levels outside the containment building following a maximum design basis accident.
  The inspectors evaluated the finding using the Significance Determination Process
  (SDP) in accordance with IMC 0609, Significance Determination Process, Attachment
  0609.04, Initial Characterization of Findings, dated June 19, 2012. Because the finding
  impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through
  IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
  dated June 19, 2012, using Exhibit 3, Barrier Integrity Screening Questions. The
  finding screened as very-low safety significance (Green) because the finding only
  represented a degradation of the radiological barrier function provided for the Auxiliary
  Building. The inspectors determined the cause of this finding did not represent current
  licensee performance and, thus, no cross-cutting aspect was assigned. (Section 1R18)
  Cornerstone: Occupational Radiation Safety
* Green. The inspectors identified a finding of very-low safety significance for inadequate
  procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with
  an associated non- violation of TS 5.4, Procedures. As a result, weekly, from
  November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the
  Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area
  against unauthorized access.
  The inspectors determined that the performance deficiency was more than minor
  because if left uncorrected the performance deficiency could lead to a more significant
  safety concern. Specifically, the failure to identify deficient Locked High Radiation Area
  (LHRA) controls could result in unintentional exposure to high levels of radiation. The
  finding was determined to be of very-low safety significance because the problem was
  not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no
  overexposure, nor substantial potential for an overexposure, and the licensees ability to
  assess dose was not compromised. The inspectors did not identify a corresponding
  cross-cutting aspect for this performance deficiency. The licensee entered the
  deficiency in their Corrective Action Program as Action Request (AR) 2014-9001
  immediately upon discovery and presentation by the inspectors. (Section 2RS1.1)
                                              5
 
                                        REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period in a refueling outage. On October 29, 2014, the plant was
restored to 100 percent power. On November 1, rough lake conditions generated substantial
amounts of debris that clogged trash racks and travelling screens. The licensee manually
tripped the reactor and maintained the plant in hot standby (Mode 3). On November 8, the
licensee restored the plant to 100 percent power.
Unit 2 began the inspection period at 100 percent power. On November 1, 2014, rough lake
conditions generated substantial amounts of debris that clogged trash racks and travelling
screens. The licensee reduced power to 50 percent to reduce circulating water flow.
Conditions continued to degrade; therefore the licensee manually tripped the reactor. The
licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.
On November 13, the plant was restored to 100 percent power.
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
  .1    Winter Seasonal Readiness Preparations
    a.  Inspection Scope
        The inspectors conducted a review of the licensees preparations for winter conditions to
        verify that the plants design features and implementation of procedures were sufficient
        to protect mitigating systems from the effects of adverse weather. Documentation for
        selected risk-significant systems was reviewed to ensure that these systems would
        remain functional when challenged by inclement weather. During the inspection, the
        inspectors focused on plant specific design features and the licensees procedures used
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
        requirements for systems selected for inspection, and verified that operator actions were
        appropriate as specified by plant specific procedures. Cold weather protection, such as
        heat tracing and area heaters, was verified to be in operation where applicable. The
        inspectors also reviewed CAP items to verify that the licensee was identifying adverse
        weather issues at an appropriate threshold and entering them into their CAP in
        accordance with station corrective action procedures. Documents reviewed are listed in
        the Attachment to this report. The inspectors reviews focused specifically on the
        following plant systems due to their risk significance or susceptibility to cold weather
        issues:
        This inspection constituted one winter seasonal readiness preparations sample as
        defined in Inspection Procedure (IP) 71111.01-05.
    b.  Findings
        No findings were identified.
                                                  6
 
.2  Readiness for Impending Adverse Weather ConditionHigh Wind Conditions
  a. Inspection Scope
      On November 6, 2014, the National Weather Service predicted high winds and rough
      lake conditions in the vicinity of the plant. Since debris intrusion during similar conditions
      the previous week had resulted in damage to equipment and a dual unit plant trip, the
      inspectors validated the sites readiness for the adverse weather. The inspectors
      reviewed the licensees overall preparations/protection for the expected weather
      conditions. The inspectors walked down the service water screen house to assess the
      licensee progress on repairing trash racks and traveling water screens. The inspectors
      evaluated the licensee staffs preparations against the sites procedures and determined
      that the staffs actions were adequate. During the inspection, the inspectors focused on
      actions taken to minimize debris intrusion and operators preparations to address
      degradation of raw water systems. The inspectors also reviewed a sample of CAP items
      to verify that the licensee identified adverse weather issues at an appropriate threshold
      and disposed them through the CAP in accordance with station corrective action
      procedures. Documents reviewed are listed in the Attachment to this report.
      This inspection constituted one readiness for impending adverse weather condition
      sample as defined in IP 71111.01-05.
  b. Findings
      No findings were identified.
1R04 Equipment Alignment (71111.04)
.1  Quarterly Partial System Walkdowns
  a. Inspection Scope
      The inspectors performed partial system walkdowns of the following risk-significant
      systems:
      *        Unit 2 Residual Heat Removal system after maintenance;
      *        Unit 2 Steam Generator (SG) power-operated relief valves during maintenance
              on other power-operated relief valves; and
      *        Unit 2 AFW during maintenance on a single train.
      The inspectors selected these systems based on their risk significance relative to the
      Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
      to identify any discrepancies that could impact the function of the system and, therefore,
      potentially increase risk. The inspectors reviewed applicable operating procedures,
      system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition
      reports, and the impact of ongoing work activities on redundant trains of equipment in
      order to identify conditions that could have rendered the systems incapable of
      performing their intended functions. The inspectors also walked down accessible
      portions of the systems to verify system components and support equipment were
      aligned correctly and operable. The inspectors examined the material condition of the
      components and observed operating parameters of equipment to verify that there were
      no obvious deficiencies. The inspectors also verified that the licensee had properly
                                                  7
 
      identified and resolved equipment alignment problems that could cause initiating events
      or impact the capability of mitigating systems or barriers and entered them into the CAP
      with the appropriate significance characterization. Documents reviewed are listed in the
      Attachment to this report.
      These activities constituted three partial system walkdown samples as defined in
      IP 71111.04-05.
  b. Findings
      No findings were identified.
.2  Semiannual Complete System Walkdown
  a. Inspection Scope
      On December 30, 2014, the inspectors completed a complete system alignment
      inspection of the Unit 1 Containment Spray system to verify the functional capability of
      the system. This system was selected because it was considered both safety significant
      and risk significant in the licensees probabilistic risk assessment. The inspectors
      walked down the system to review mechanical and electrical equipment lineups;
      electrical power availability; system pressure and temperature indications, as
      appropriate; component labeling; component lubrication; component and equipment
      cooling; hangers and supports; operability of support systems; and to ensure that
      ancillary equipment or debris did not interfere with equipment operation. A review of a
      sample of past and outstanding WOs was performed to determine whether any
      deficiencies significantly affected the system function. In addition, the inspectors
      reviewed the CAP database to ensure that system equipment alignment problems were
      being identified and appropriately resolved. Documents reviewed are listed in the
      Attachment to this report.
      These activities constituted one complete system walkdown sample as defined in
      IP 71111.04-05.
  b. Findings
      No findings were identified.
1R05 Fire Protection (71111.05)
.1  Routine Resident Inspector Tours (71111.05Q)
  a. Inspection Scope
      The inspectors conducted fire protection walkdowns which were focused on availability,
      accessibility, and the condition of firefighting equipment in the following risk-significant
      plant areas:
      *        Unit 2 AB EDG;
      *        Unit 2 CD EDG;
      *        Unit 2 Quadrant cable tunnels; and
      *        Unit 1 Essential Service Water Motor Control Center Room.
                                                  8
 
      The inspectors reviewed areas to assess if the licensee had implemented a fire
      protection program that adequately controlled combustibles and ignition sources
      within the plant, effectively maintained fire detection and suppression capability,
      maintained passive fire protection features in good material condition, and implemented
      adequate compensatory measures for out-of-service, degraded or inoperable fire
      protection equipment, systems, or features in accordance with the licensees fire plan.
      The inspectors selected fire areas based on their overall contribution to internal fire risk
      as documented in the plants Individual Plant Examination of External Events with later
      additional insights, their potential to impact equipment which could initiate or mitigate a
      plant transient, or their impact on the plants ability to respond to a security event.
      Using the documents listed in the Attachment to this report, the inspectors verified that
      fire hoses and extinguishers were in their designated locations and available for
      immediate use; that fire detectors and sprinklers were unobstructed; that transient
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
      seals appeared to be in satisfactory condition. The inspectors also verified that minor
      issues identified during the inspection were entered into the licensees CAP.
      Documents reviewed are listed in the Attachment to this report.
      These activities constituted four quarterly fire protection inspection samples as defined in
      IP 71111.05-05.
  b. Findings
      No findings were identified.
1R06 Flooding (71111.06)
.1  Underground Vaults
  a. Inspection Scope
      The inspectors selected underground bunkers/manholes subject to flooding that
      contained cables whose failure could disable risk-significant equipment. The inspectors
      determined that the cables were not submerged, that splices were intact, and that
      appropriate cable support structures were in place. In those areas where dewatering
      devices were used, such as a sump pump, the device was operable and level alarm
      circuits were set appropriately to ensure that the cables would not be submerged. In
      those areas without dewatering devices, the inspectors verified that drainage of the area
      was available, or that the cables were qualified for submergence conditions. The
      inspectors also reviewed the licensees corrective action documents with respect to past
      submerged cable issues identified in the corrective action program to verify the
      adequacy of the corrective actions. The inspectors performed a walkdown of the
      following underground bunkers/manholes subject to flooding:
      *        Bunkers/manholes containing security cabling; and
      *        Bunkers/manholes with safety-related cabling supporting technical specification
              offsite power sources
      Specific documents reviewed during this inspection are listed in the Attachment to this
      report. This inspection constituted one underground vaults sample as defined in
      IP 71111.06-05.
                                                9
 
  b. Findings
      No findings were identified.
1R07 Annual Heat Sink Performance (71111.07)
  a. Inspection Scope
      The inspectors reviewed the licensees inspection of Unit 1 CD EDG north air aftercooler
      to verify that potential deficiencies did not mask the licensees ability to detect degraded
      performance, to identify any common cause issues that had the potential to increase
      risk, and to ensure that the licensee was adequately addressing problems that could
      result in initiating events that would cause an increase in risk. The inspectors observed
      licensee visual observations of the internals of the heat exchanger to verify cleanliness
      of the heat exchanger. Additionally, the inspectors reviewed eddy current testing results
      and interviewed heat exchanger program engineers. Documents reviewed for this
      inspection are listed in the Attachment to this document.
      This annual heat sink performance inspection constituted one sample as defined in
      IP 71111.07-05.
  b. Findings
      No findings were identified.
1R08 Inservice Inspection Activities (71111.08P)
      From September 29, 2014, through October 10, 2014, the inspector conducted a review
      of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring
      degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,
      Emergency Feedwater Systems, Risk Significant Piping and Components, and
      Containment Systems.
      The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5
      below constituted one inservice inspection sample as defined in IP 71111.08-05.
.1  Piping Systems Inservice Inspection
  a. Inspection Scope
      The inspectors observed and reviewed records of the following non-destructive
      examinations (NDE) mandated by the American Society of Mechanical Engineers
      (ASME) Section XI Code to evaluate compliance with the ASME Code Section XI
      and Section V requirements, and if any indications and defects were detected, to
      determine whether these were dispositioned in accordance with the ASME Code or an
      NRC-approved alternative requirement:
      *        Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to
              elbow weld, 1-FW-12-02S;
      *        UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius;
              6-1-RC-7-IRS;
                                                10
 
    *      UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;
            4-1-RC-10-IRS; and
    *      Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel
            Support; 1-PRZ-26.
    There were no recordable indications identified during the previous refueling outage.
    The inspectors reviewed NDE records associated with the following pressure boundary
    welds completed for risk significant components during the current refueling outage to
    determine whether the licensee applied the pre-service NDE and acceptance criteria
    required by the Construction Code and ASME Code, Section XI. Additionally, the
    inspectors reviewed the welding procedure specification and supporting weld procedure
    qualification records to determine whether the weld procedure was qualified in
    accordance with the requirements of Construction Code and the ASME Code Section IX:
    *      Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314
            (Work Order 55440759-5); and
    *      Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work
            Order 55390312-01)
    The inspectors also reviewed NDE records associated with the following pressure
    boundary welds completed for risk significant systems since the beginning of the last
    refueling:
    *      Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve
            1-NFP-222-V2 (Work Order 55421212-10/13); and
    *      Welds OW-1 associated with the installation of pipe support 1-ARC-S4012
            (WO Order 55404504-06).
  b. Findings
    No findings were identified.
.2  Reactor Pressure Vessel Upper Head Penetration Inspection Activities
  a. Inspection Scope
    For the Unit 1 reactor vessel head, no examination was required pursuant to
    10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review
    was completed for this inspection procedure attribute.
  b. Findings
    No findings were identified.
.3    Boric Acid Corrosion Control (BACC)
  a. Inspection Scope
    The inspectors observed the licensees BACC visual examinations for portions of the
    RCS, connected systems, and verified whether these visual examinations emphasized
                                            11
 
      locations where boric acid leaks can cause degradation of safety significant
      components.
      The inspectors reviewed the following licensee evaluations of RCS components with
      Boric Acid deposits to determine whether degraded components were documented in
      the corrective action system. The inspectors also evaluated corrective actions for any
      degraded RCS components to determine whether they met the component Construction
      Code, ASME Section XI Code, and/or NRC approved alternative:
      *      AR 2013-4317; 1-QRV-114, body to bonnet leak;
      *      AR 2013-4625;1-CS-448-1 has a BA leak;
      *      AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;
      *      AR 2013-6839; U1C25 Refueling Cavity Leakage; and
      *      AR 2013-7061; 1-RH-147W has Boric Acid on Body to Bonnet.
      The inspectors reviewed the following corrective actions related to evidence of
      BA leakage to determine whether the corrective actions completed were consistent with
      the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,
      Criterion XVI:
      *      AR 2013-0534; 12-CS-185 has a body to bonnet leak;
      *      AR 2014-9459; 12-CS-185 has a ruptured diaphragm;
      *      AR 2013-7220; Reactor Head and Pressure Vent Piping Area;
      *      AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and
      *      AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min.
  b. Findings
      No findings were identified.
.4    Steam Generator Tube Inspection Activities
  a.  Inspection Scope
      The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data
      analysts, and reviewed documentation related to the SG ISI Program to determine
      whether:
      *      the numbers and sizes of SG tube flaws/degradation identified was consistent
              with the licensees previous outage Operational Assessment predictions;
      *      the SG tube ET examination scope and expansion criteria were sufficient to meet
              the Technical Specifications, and the Electric Power Research Institute (EPRI)
              Document 1013706, Pressurized Water Reactor Steam Generator Examination
              Guidelines;
      *      the SG tube ET examination scope included potential areas of tube degradation
              identified in prior outage SG tube inspections and/or as identified in NRC generic
              industry operating experience applicable to these SG tubes;
      *      the licensee-identified new tube degradation mechanisms and implemented
              adequate extent of condition inspection scope and repairs for the new tube
              degradation mechanism;
      *      the licensee implemented qualified depth sizing methods to degraded tubes
              accepted for continued service;
                                              12
 
      *        the ET probes and equipment configurations used to acquire data from the SG
                tubes were qualified to detect the known/expected types of SG tube degradation
                in accordance with Appendix H, Performance Demonstration for Eddy Current
                Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam
                Generator Examination Guidelines;
      *        the licensee performed secondary side SG inspections for location and removal
                of foreign materials;
      *        The licensee implemented repairs for SG tubes damaged by foreign material;
                and
      *        Foreign objects were left within the secondary side of the SGs, and if so, that the
                licensee implemented evaluations, which included the effects of foreign object
                migration and/or tube fretting damage.
  b.  Findings
      No findings were identified.
.5    Identification and Resolution of Problems
    a. Inspection Scope
      The inspectors performed a review of ISI-related problems entered into the licensees
      CAP and conducted interviews with licensee staff to determine whether:
      *        the licensee had established an appropriate threshold for identifying ISI-related
                problems;
      *        the licensee had performed a root cause (if applicable) and taken appropriate
                corrective actions; and
      *        the licensee had evaluated operating experience and industry generic issues
                related to ISI and pressure boundary integrity.
      The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,
      Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
      documents reviewed by the inspectors are listed in the Attachment to this report.
    b. Findings
      No findings were identified.
1R11 Licensed Operator Requalification Program (71111.11)
.1    Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)
  a.  Inspection Scope
      On November 19, 2014, the inspectors observed a crew of licensed operators in the
      plants simulator during licensed operator requalification training to verify that operator
      performance was adequate, evaluators were identifying and documenting crew
      performance problems and training was being conducted in accordance with licensee
      procedures. The inspectors evaluated the following areas:
      *        licensed operator performance;
                                                  13
 
    *        crews clarity and formality of communications;
    *        ability to take timely actions in the conservative direction;
    *        prioritization, interpretation, and verification of annunciator alarms;
    *        correct use and implementation of abnormal and emergency procedures;
    *        control board manipulations;
    *        oversight and direction from supervisors; and
    *        ability to identify and implement appropriate TS actions and Emergency Plan
              actions and notifications.
    The crews performance in these areas was compared to pre-established operator action
    expectations and successful critical task completion requirements. Documents reviewed
    are listed in the Attachment to this report.
    This inspection constituted one quarterly licensed operator requalification program
    simulator sample as defined in IP 71111.11
  b. Findings
    No findings were identified.
.2  Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)
  a. Inspection Scope
    On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the
    RCS during the Unit 1 refueling outage. This was a high-risk (Orange) activity planned
    during the outage. The inspectors evaluated the following areas:
    *        licensed operator performance;
    *        crews clarity and formality of communications;
    *        ability to take timely actions in the conservative direction;
    *        prioritization, interpretation, and verification of annunciator alarms (if applicable);
    *        correct use and implementation of procedures;
    *        control board (or equipment) manipulations;
    *        oversight and direction from supervisors; and
    *        ability to identify and implement appropriate TS actions and Emergency Plan
              actions and notifications (if applicable).
    The performance in these areas was compared to pre-established operator action
    expectations, procedural compliance and task completion requirements. Documents
    reviewed are listed in the Attachment to this report.
    This inspection constituted one quarterly licensed operator heightened activity/risk
    sample as defined in IP 71111.11, and was done in conjunction with the requirements of
    IP 71111.20.
                                                  14


safety concern.  Specifically, the failure to identify deficient Locked High Radiation Area (LHRA) controls could result in unintentional exposure to high levels of radiation. The finding was determined to be of very-low safety significance because the problem was not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no
1R12 Maintenance Effectiveness (71111.12)
overexposure, nor substantial potential for an overexposure, and the licensee's ability to assess dose was not compromised.  The inspectors did not identify a corresponding
   a. Inspection Scope
cross-cutting aspect for this performance deficiency.  The licensee entered the deficiency in their Corrective Action Program as Action Request (AR) 2014-9001 immediately upon discovery and presentation by the inspectors.  (Section 2RS1.1)  
    The inspectors evaluated degraded performance issues involving the following
    
    risk-significant systems:
6  REPORT DETAILS
    *        Nuclear Instrumentation;
Summary of Plant Status
    *        Main Steam;
Unit 1 began the inspection period in a refueling outage.  On October 29, 2014, the plant was restored to 100 percent power.  On November 1, rough lake conditions generated substantial
    *        Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and
amounts of debris that clogged trash racks and travelling screens.  The licensee manually tripped the reactor and maintained the plant in hot standby (Mode 3).  On November 8, the licensee restored the plant to 100 percent power.  Unit 2 began the inspection period at 100 percent power.  On November 1, 2014, rough lake conditions generated substantial amounts of debris that clogged trash racks and travelling screens.  The licensee reduced power to 50 percent to reduce circulating water flow.  Conditions continued to degrade; therefore the licensee manually tripped the reactor.  The licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.  On November 13, the plant was restored to 100 percent power.  1. REACTOR SAFETY Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01) .1 Winter Seasonal Readiness Preparations
    *        Rod Position Indication
a. Inspection Scope
    The inspectors reviewed events such as where ineffective equipment maintenance had
The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather.  Documentation for
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather.  During the inspection, the
    independently verified the licensee's actions to address system performance or condition
inspectors focused on plant specific design features and the licensee's procedures used
    problems in terms of the following:
to mitigate or respond to adverse weather conditions.  Additionally, the inspectors
    *       implementing appropriate work practices;
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were
    *       identifying and addressing common cause failures;
appropriate as specified by plant specific procedures.  Cold weather protection, such as
    *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
heat tracing and area heaters, was verified to be in operation where applicable.  The  
    *        characterizing system reliability issues for performance;
inspectors also reviewed CAP items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures.  Documents reviewed are listed in
    *        charging unavailability for performance;
the Attachment to this report.  The inspectors' reviews focused specifically on the
    *        trending key parameters for condition monitoring;
following plant systems due to their risk significance or susceptibility to cold weather issues: This inspection constituted one winter seasonal readiness preparations sample as defined in Inspection Procedure (IP) 71111.01-05. b. Findings
    *        ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
No findings were identified. 
    *       verifying appropriate performance criteria for SSCs/functions classified as (a)(2),
7  .2 Readiness for Impending Adverse Weather Condition-High Wind Conditions
              or appropriate and adequate goals and corrective actions for systems classified
a. Inspection Scope
              as (a)(1).
On November 6, 2014, the National Weather Service predicted high winds and rough lake conditions in the vicinity of the plant.  Since debris intrusion
    The inspectors assessed performance issues with respect to the reliability, availability,
during similar conditions the previous week had resulted in damage to equipment and a dual unit plant trip, the
    and condition monitoring of the system. In addition, the inspectors verified maintenance
inspectors validated the site's readiness for the adverse weather.  The inspectors
    effectiveness issues were entered into the CAP with the appropriate significance
reviewed the licensee's overall preparations/protection for the expected weather conditions.  The inspectors walked down the service water screen house to assess the licensee progress on repairing trash racks and traveling water screens.  The inspectors
    characterization. Documents reviewed are listed in the Attachment to this report.
evaluated the licensee staff's preparations against the site's procedures and determined
    This inspection constituted four quarterly maintenance effectiveness samples as defined
that the staff's actions were adequate.  During the inspection, the inspectors focused on
    in IP 71111.12-05.
actions taken to minimize debris intrusion and operators preparations to address degradation of raw water systems.  The inspectors also reviewed a sample of CAP items to verify that the licensee identified adverse weather issues at an appropriate threshold
  b. Findings
and disposed them through the CAP in accordance with station corrective action procedures.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one readiness for impending adverse weather condition sample as defined in IP 71111.01-05. b. Findings
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
No findings were identified. 1R04 Equipment Alignment (71111.04) .1 Quarterly Partial System Walkdowns
  a. Inspection Scope
a. Inspection Scope
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
The inspectors performed partial system walkdowns of the following risk-significant systems: * Unit 2 Residual Heat Removal system after maintenance;  
    maintenance and emergent work activities affecting risk-significant and safety-related
* Unit 2 Steam Generator (SG) power-operated relief valves during maintenance on other power-operated relief valves; and
    equipment listed below to verify that the appropriate risk assessments were performed
* Unit 2 AFW during maintenance on a single train. The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected.  The inspectors attempted
    prior to removing equipment for work:
to identify any discrepancies that could impact the function of the system and, therefore,
    *       Rough lake conditions during emergent trash rack work;
potentially increase risk.  The inspectors reviewed applicable operating procedures,
    *       Essential service water flow verification work concurrent with EDG testing; and
system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions.  The inspectors also walked down accessible
    *       Emergent repairs to the Unit 2 Motor-Driven Auxiliary Feedwater (MDAFW) pump
portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the
              room ventilation unit
components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly 
                                                15
8  identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP
with the appropriate significance characterization.  Documents reviewed are listed in the
Attachment to this report. These activities constituted three partial system walkdown samples as defined in
IP 71111.04-05. b. Findings
No findings were identified. .2 Semiannual Complete System Walkdown
a. Inspection Scope
On December 30, 2014, the inspectors completed a complete system alignment inspection of the Unit 1 Containment Spray system to verify the functional capability of
the system.  This system was selected because
it was considered both safety significant and risk significant in the licensee's probabilistic risk assessment.  The inspectors walked down the system to review mechanical and electrical equipment lineups; electrical power availability; system pressure and temperature indications, as
appropriate; component labeling; component lubrication; component and equipment
cooling; hangers and supports; operability of support systems; and to ensure that
ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding WOs was performed to determine whether any deficiencies significantly affected the system
function.  In addition, the inspectors reviewed the CAP database to ensure that system equipment alignment problems were being identified and appropriately resolved.  Documents reviewed are listed in the Attachment to this report. These activities constituted one complete system walkdown sample as defined in
IP 71111.04-05. b. Findings
No findings were identified. 1R05 Fire Protection (71111.05) .1 Routine Resident Inspector Tours (71111.05Q) a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
* Unit 2 AB EDG;
* Unit 2 CD EDG;
* Unit 2 Quadrant cable tunnels; and  
* Unit 1 Essential Service Water Motor Control Center Room. 
9  The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources
within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire
protection equipment, systems, or features in accordance with the licensee's fire plan. 
The inspectors selected fire areas based on their overall contribution to internal fire risk
as documented in the plant's Individual Plant Examination of External Events with later
additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment to this report, the inspectors verified that
fire hoses and extinguishers were in their designated locations and available for  
immediate use; that fire detectors and sprinklers were unobstructed; that transient
material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are listed in the Attachment to this report. These activities constituted four quarterly fire protection inspection samples as defined in
IP 71111.05-05. b. Findings
No findings were identified.
1R06 Flooding (71111.06) .1 Underground Vaults
a. Inspection Scope
The inspectors selected underground bunkers/manholes subject to flooding that contained cables whose failure could disable risk-significant equipment.  The inspectors
determined that the cables were not submerged, that splices were intact, and that appropriate cable support structures were in place.  In those areas where dewatering devices were used, such as a sump pump, the device was operable and level alarm
circuits were set appropriately to ensure that the cables would not be submerged. In  
those areas without dewatering devices, the inspectors verified that drainage of the area
was available, or that the cables were qualified for submergence conditions.  The inspectors also reviewed the licensee's corrective action documents with respect to past submerged cable issues identified in the corrective action program to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following underground bunkers/manholes subject to flooding:
* Bunkers/manholes containing security cabling; and
* Bunkers/manholes with safety-related cabling supporting technical specification offsite power sources Specific documents reviewed during this inspection are listed in the Attachment to this report. This inspection constituted one underground vaults sample as defined in  
IP 71111.06-05.
10  b. Findings
No findings were identified. 1R07 Annual Heat Sink Performance (71111.07) a. Inspection Scope
The inspectors reviewed the licensee's inspection of Unit 1 CD EDG north air aftercooler to verify that potential deficiencies did not mask the licensee's ability to detect degraded
performance, to identify any common cause issues that had the potential to increase risk, and to ensure that the licensee was adequately addressing problems that could result in initiating events that would cause an increase in risk.  The inspectors observed
licensee visual observations of the internals of the heat exchanger to verify cleanliness
of the heat exchanger.  Additionally, the inspectors reviewed eddy current testing results
and interviewed heat exchanger program engineers.  Documents reviewed for this
inspection are listed in the Attachment to this document. This annual heat sink performance inspection constituted one sample as defined in
IP 71111.07-05. b. Findings
No findings were identified. 1R08 Inservice Inspection Activities (71111.08P) From September 29, 2014, through October 10 , 2014 , the inspector conducted a review of the implementation of the licensee's Inservice Inspection (ISI) Program for monitoring degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,
Emergency Feedwater Systems, Risk Significant Piping and Components, and Containment Systems. The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5 below constituted one inservice inspection sample as defined in IP 71111.08-05.  .1 Piping Systems Inservice Inspection
a. Inspection Scope
The inspectors observed and reviewed records of the following non-destructive examinations (NDE) mandated by the American Society of Mechanical Engineers
(ASME) Section XI Code to evaluate compliance with the ASME Code Section XI
and Section V requirements, and if any indications and defects were detected, to  
determine whether these were dispositioned in accordance with the ASME Code or an
NRC-approved alternative requirement:  
* Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to
elbow weld, 1-FW-12-02S;  
* UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius; 6"-1-RC-7-IRS; 
11  * UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;
4"-1-RC-10-IRS; and
* Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel Support; 1-PRZ-26. There were no recordable indications identified during the previous refueling outage. The inspectors reviewed NDE records associated with the following pressure boundary welds completed for risk significant components during the current refueling outage to
determine whether the licensee applied the pre-service NDE and acceptance criteria


required by the Construction Code and ASME Code, Section XI. Additionally, the inspectors reviewed the welding procedure specification and supporting weld procedure qualification records to determine whether the weld procedure was qualified in accordance with the requirements of Construction Code and the ASME Code Section IX:
    These activities were selected based on their potential risk significance relative to the
* Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314 (Work Order 55440759-5); and  
    Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
* Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
Order 55390312-01) The inspectors also reviewed NDE records associated with the following pressure boundary welds completed for risk significant systems since the beginning of the last
    and complete. When emergent work was performed, the inspectors verified that the
refueling:
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
* Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve
    of maintenance work, discussed the results of the assessment with the licensee's
1-NFP-222-V2 (Work Order 55421212-10/13); and  
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
* Welds OW-1 associated with the installation of pipe support 1-ARC-S4012 (WO Order 55404504-06).  b. Findings
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
No findings were identified. .2 Reactor Pressure Vessel Upper Head Penetration Inspection Activities
    walked down portions of redundant safety systems, when applicable, to verify risk
a. Inspection Scope
    analysis assumptions were valid and applicable requirements were met.
For the Unit 1 reactor vessel head, no examination was required pursuant to 10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review was completed for this inspection procedure attribute. b. Findings
    Documents reviewed during this inspection are listed in the Attachment to this report.
No findings were identified. .3  Boric Acid Corrosion Control (BACC)
    These maintenance risk assessments and emergent work control activities constituted
a. Inspection Scope
    three samples as defined in IP 71111.13-05.
The inspectors observed the licensee's BACC visual examinations for portions of the
  b. Findings
RCS, connected systems, and verified whether these visual examinations emphasized 
    No findings were identified.
12  locations where boric acid leaks can cause degradation of safety significant
1R15 Operability Determinations and Functional Assessments (71111.15)
components. The inspectors reviewed the following licensee evaluations of RCS components with Boric Acid deposits to determine whether degraded components were documented in
  a. Inspection Scope
the corrective action system.  The inspectors also evaluated corrective actions for any degraded RCS components to determine whether they met the component Construction Code, ASME Section XI Code, and/or NRC approved alternative:  
    The inspectors reviewed the following issues:
* AR 2013-4317; 1-QRV-114, body to bonnet leak;  
    *       Main Steam Safety Valves lift during dual-unit trip;
* AR 2013-4625;1-CS-448-1 has a BA leak;  
    *        Water intrusion into the Unit 1 TDAFW turbine bearings;
* AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;  
    *       Question regarding TDAFW pump mission time;
* AR 2013-6839; U1C25 Refueling Cavity Leakage; and  
    *        Inability to make new ice during the Unit 1 refueling outage;
* AR 2013-7061; 1-RH-147W has Boric Acid on Body to Bonnet. The inspectors reviewed the following corrective actions related to evidence of BA leakage to determine whether the corrective actions completed were consistent with
    *       Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;
the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B, Criterion XVI:
    *       Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and
* AR 2013-0534; 12-CS-185 has a body to bonnet leak;
              failure of automatic generator trip during dual-unit trip; and
* AR 2014-9459; 12-CS-185 has a ruptured diaphragm;
    *       Leakby on a Unit 2 AFW flow control valve.
* AR 2013-7220; Reactor Head and Pressure Vent Piping Area;
    The inspectors selected these potential operability issues based on the risk significance
* AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and  
    of the associated components and systems. The inspectors evaluated the technical
* AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min. b. Findings
    adequacy of the evaluations to ensure that TS operability was properly justified and the
No findings were identified. .4 Steam Generator Tube Inspection Activities
    subject component or system remained available such that no unrecognized increase in
a. Inspection Scope
    risk occurred. The inspectors compared the operability and design criteria in the
The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data analysts, and reviewed documentation related to the SG ISI Program to determine
    appropriate sections of the TS and UFSAR to the licensees evaluations to determine
whether: * the numbers and sizes of SG tube flaws/degradation identified was consistent with the licensee's previous outage Operational Assessment predictions;
    whether the components or systems were operable. Where compensatory measures
* the SG tube ET examination scope and expansion criteria were sufficient to meet the Technical Specifications, and the Electric Power Research Institute (EPRI) Document 1013706, Pressurized Water Reactor Steam Generator Examination Guidelines;
    were required to maintain operability, the inspectors determined whether the measures
* the SG tube ET examination scope included potential areas of tube degradation identified in prior outage SG tube inspections and/or as identified in NRC generic
    in place would function as intended and were properly controlled. The inspectors
    determined, where appropriate, compliance with bounding limitations associated with the
    evaluations. Additionally, the inspectors reviewed a sampling of corrective action
    documents to verify that the licensee was identifying and correcting any deficiencies
    associated with operability evaluations. Documents reviewed are listed in the
    Attachment to this report.
    This operability inspection constituted seven samples as defined in IP 71111.15-05.
                                                16


industry operating experience applicable to these SG tubes;
b.  Findings
* the licensee-identified new tube degradation mechanisms and implemented adequate extent of condition inspection scope and repairs for the new tube
(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW
degradation mechanism;
    Pump Turbine Oil System
* the licensee implemented qualified depth sizing methods to degraded tubes accepted for continued service; 
    Introduction: A finding of very low safety significance (Green) with an associated NCV of
13  * the ET probes and equipment configurations used to acquire data from the SG tubes were qualified to detect the known/expected types of SG tube degradation
    10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the
in accordance with Appendix H, Performance Demonstration for Eddy Current Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam Generator Examination Guidelines; 
    inspectors for the licensees failure to promptly identify and correct a CAQ associated
* the licensee performed secondary side SG inspections for location and removal of foreign materials;
    with Unit 1 TDAFW pump turbine bearing oil. Specifically, the licensee failed to identify
* The licensee implemented repairs for SG tubes damaged by foreign material;
    that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage
and * Foreign objects were left within the secondary side of the SGs, and if so, that the licensee implemented evaluations, which included the effects of foreign object
    had been identified directly above one of the TDAFW pump turbine bearings.
    Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1
    TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.
    An AR was written (AR 2014-4473) which determined that due to the leak rate and the
    apparent lack of any equipment impacts, there were no operability concerns. On
    April 11, 2014, the licensee discovered that the turbine bearing oil level was
    approximately 0.5 inches above the MAXIMUM mark on the sight glass. Level had been
    recorded in the logs as being within band for over a year without any prior evidence of
    high level. Additionally, there were no evolutions that had been performed which would
    explain the high level. The licensee generated AR 2014-4684 to document this
    condition. The AR documented several possible reasons for the unexplained level rise.
    One was that turbine building temperature had gone up. Another was that it was not
    uncommon for personnel to unnecessarily add oil to the machine from time to time. No
    other information was provided to validate either potential cause. Additionally, there was
    no mention of the leak identified above one of the turbine bearings four days prior. No
    formal monitoring plan was established. An action was created to sample the oil for
    water, but as of six weeks later, a work order had not been finalized and scheduled.
    The only other action was a lessons-learned that was created for Mechanical
    Maintenance department regarding unnecessary oil adds. The response to the action
    from the group was that they dont typically do oil adds, but that they discussed the topic
    anyway. The inspectors reviewed reference information with respect to oil levels and
    their importance to machine operability. According to the vendor manual, EPRI
    guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is
    extremely critical in the turbine bearing pedestals. The references all concluded that oil
    level above the MAXIMUM mark could lead to oil frothing, which could affect stable
    operation of the turbine and loss of oil from the system. Further, the references, along
    with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM
    mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was
    over-filled to the MAXIMUM mark. No further information was provided on why this
    occurred or why it was acceptable to stay at the MAXIMUM mark. One quart of oil was
    drained from the turbine bearing pedestals, bringing the level back to near the
    MAXIMUM mark. Approximately five weeks later, an NRC inspector touring the plant
    questioned why level was near the MAXIMUM mark given a placard near the sight glass
    said to keep level at the MINIMUM mark (which aligned with the references above).
    The licensee generated an AR (2014-6315) about one week later on May 22 when the
    inspector asked about the condition again. In the AR, they documented the NRC
    observation and also the fact that an operator had noted level to be above the
    MAXIMUM mark by approximately 0.25 inches. Oil was again drained from the
    machine, this time to right above the MINIMUM mark. The operability assessment
    (which was not documented until the following day), stated that at time of discovery, the
                                                17


migration and/or tube fretting damage. b. Findings
machine was operable because of oil level not affecting operability of the turbine and a
No findings were identified. .5 Identification and Resolution of Problems
history of overfilling that sometimes required draining of the oil. Further, a statement
a. Inspection Scope
was made that there had been a consistent oil level trend for the past month. Again,
The inspectors performed a review of ISI-related problems entered into the licensee's CAP and conducted interviews with licensee staff to determine whether:
the leakage above the bearing was not discussed. There was no discussion of the
* the licensee had established an appropriate threshold for identifying ISI-related
previous high-level condition from April 11. On May 23, the licensee decided to
problems;
completely drain the oil and sample it for water; 620 ml of water was found in the 2.5
* the licensee had performed a root cause (if applicable) and taken appropriate corrective actions; and  
gallon system. New oil was added, and an apparent cause evaluation was performed.
* the licensee had evaluated operating experience and industry generic issues related to ISI and pressure boundary integrity. The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements.  The corrective action documents reviewed by the inspectors are listed in the Attachment to this report. b. Findings
The evaluation concluded that leakage above the bearing housing (documented
No findings were identified. 1R11 Licensed Operator Requalification Program (71111.11) .1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q) a. Inspection Scope
originally in AR 2014-4473), combined with a small casing steam leak that condensed
On November 19, 2014, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification training to verify that operator
above the housing while the machine was in operation, caused the water intrusion in the
bearing oil. Later evaluation determined the leak rate from the pipe had increased to
8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources
were diverted away from the bearing housing with a temporary modification pending
repairs (which were completed in the September-October 2014 refueling outage).
Based on the above, the inspectors concluded the licensee had sufficient information to
promptly identify and correct water intrusion into the TDAFW turbine bearing oil system
on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential
operability impacts (as described in the multiple references above) on April 11 and
May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-
related oil systems is a CAQ.
Analysis: The failure to promptly identify and correct a CAQ, as required by
10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the
TDAFW turbine oil system was an issue warranting further review in the SDP. Per
IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the issue was
more-than-minor because it adversely affected the Configuration Control attribute of the
Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences. Additionally, if left uncorrected, the issue could lead to a more significant
safety concern. Specifically, not recognizing water intrusion into safety-related oil
systems can impact operability and affect how safety equipment operates.
The inspectors assessed the finding for significance using IMC 0609, Significance
Determination Process, issued June 2, 2012. Per Appendix A, The Significance
Determination Process (SDP) for Findings-at-Power, issued June 19, 2012, the finding
screened as Green, or very low safety significance, in Exhibit 2. Specifically, all
questions were answered no under Section A for findings related to Mitigating SSCs
and Functionality. The inspectors reviewed the licensees past operability evaluation
and concluded that given the projected amount of water that could be entrained in the oil
during operation, along with the duration of operation assumed in the safety analyses,
that operability of the pump would be maintained.
The inspectors determined the finding had an associated cross-cutting aspect in the
Human Performance area, specifically, H.11, Challenge the Unknown. Some of the
tenets of H.11, as described in NUREG-2165, Safety Culture Common Language
Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency
and continuously challenge existing conditions in order to identify discrepancies that
might result in error or inappropriate action. Further, it states that individuals challenge
unanticipated results rather than rationalize them, and that abnormal indications are not
attributed to indication problems. Regarding the TDAFW oil system, the licensee
rationalized why the level was increasing without sufficient investigation given the
                                          18


performance was adequate, evaluators were identifying and documenting crew
    significance of the system, and did not seek further information that was readily available
performance problems and training was being conducted in accordance with licensee
    regarding appropriate oil levels.
procedures. The inspectors evaluated the following areas:  
    Enforcement: 10 CFR Part 50, Appendix B, Criterion 16, Corrective Action, requires, in
* licensed operator performance; 
    part, that conditions adverse to quality, such as deficiencies, defective material and
14  * crew's clarity and formality of communications;
    equipment, and nonconformances are promptly identified and corrected.
* ability to take timely actions in the conservative direction;
    Contrary to the above, between April 11 and May 23, 2014, the licensee failed to
* prioritization, interpretation, and verification of annunciator alarms;
    promptly identify and correct a CAQ. Specifically, the licensee failed to promptly identify
* correct use and implementation of abnormal and emergency procedures;
    and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system
* control board manipulations;
    despite multiple opportunities to do so. On April 7, the licensee became aware of a
* oversight and direction from supervisors; and
    water leak directly above the TDAFW pump turbine outboard bearing. On April 11, and
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly licensed operator requalification program simulator sample as defined in IP 71111.11 b. Findings
    May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark. The
No findings were identified. .2 Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q) a. Inspection Scope
    actions taken (draining the oil level) did not correct the condition adverse to quality in
On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the RCS during the Unit 1 refueling outage.  This was a high-risk (Orange) activity planned during the outage. The inspectors evaluated the following areas:
    that water continued to leak into the oil. On May 23, the licensee drained the oil system
* licensed operator performance;
    and discovered approximately 620 ml of water.
* crew's clarity and formality of communications;
    For immediate corrective actions, the licensee added new oil to the system and installed
* ability to take timely actions in the conservative direction;
    a temporary modification to prevent further water intrusion. Further corrective actions
* prioritization, interpretation, and verification of annunciator alarms (if applicable);
    included an apparent cause evaluation and past operability evaluation. Permanent
* correct use and implementation of procedures;
    repairs to the cooling water leak above the bearing were completed during the Fall 2014
* control board (or equipment) manipulations;
    refueling outage. The licensee initiated AR-2014-6315 to document the condition and
* oversight and direction from supervisors; and
    track corrective actions.
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications (if applicable). The performance in these areas was compared to pre-established operator action expectations, procedural compliance and task completion requirements.  Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly licensed operator heightened activity/risk sample as defined in IP 71111.11, and was done in conjunction with the requirements of  
    This violation is being treated as an NCV, consistent with Section 2.3.2 of the
IP 71111.20. 
    Enforcement Policy because it was of very low safety significance and was entered into
15  1R12 Maintenance Effectiveness (71111.12) a. Inspection Scope
    the licensees CAP. (NCV 05000315/2014005-01; Failure to Identify Conditions
The inspectors evaluated degraded performance issues involving the following risk-significant systems:
    Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System)
* Nuclear Instrumentation; 
(2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance
* Main Steam; 
    Introduction: A finding of very low safety significance (Green) with an associated NCV of
* Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and  
    TS 5.4, Procedures, was self-revealed when a vacuum was inadvertently drawn on the
* Rod Position Indication The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and
    AB FOST during preparations for surveillance activities. The vacuum caused an
independently verified the licensee's actions to address system performance or condition problems in terms of the following:
    indication of lowering level in the tank, alarms, and an unplanned TS LCO action
* implementing appropriate work practices;
    statement entry.
* identifying and addressing common cause failures;
    Description: On August 20, 2014, the licensee was performing work activities in
* scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
    preparation for an upcoming, routine leak-test of the AB FOST. The AB FOST is one of
* characterizing system reliability issues for performance;
    two underground tanks on site that supply fuel to the EDGs via the smaller day tanks
* charging unavailability for performance;
    (which are provided for each EDG and offer a more limited, immediate fuel supply). The
* trending key parameters for condition monitoring;
    test consists of establishing a vacuum in the tank and monitoring it for a period of time.
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
    Several support activities are required to be performed prior to the test, some of which
* verifying appropriate performance criteria for SSC's/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified
    include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the
as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system.  In addition, the inspectors verified maintenance
    FOST, and connection of vendor-supplied vacuum and test equipment to the vent. Per
effectiveness issues were entered into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the Attachment to this report. This inspection constituted four quarterly maintenance effectiveness samples as defined in IP 71111.12-05. b. Findings
    the overarching surveillance procedure, the basic order of activities should have been to
1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) a. Inspection Scope
    loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related
    from service, remove the vent cover, hook up the test equipment, and perform the test.
equipment listed below to verify that the appropriate risk assessments were performed
    During the day shift on August 20, workers went out to work on the vent cover. The
prior to removing equipment for work:
    associated work instruction did not provide adequate guidance on what exactly was to
* Rough lake conditions during emergent trash rack work;
    be done. While the intent was just to loosen the cover at that point, the Subject of the
* Essential service water flow verification work concurrent with EDG testing; and
                                              19
* Emergent repairs to the Unit 2 Motor-Driven Auxiliary Feedwater (MDAFW) pump room ventilation unit 
16  These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete.  When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope
of maintenance work, discussed the results of the assessment with the licensee's
probabilistic risk analyst or shift technical advisor, and verified plant conditions were
consistent with the risk assessment.  The inspectors also reviewed TS requirements and  
walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed during this inspection are listed in the Attachment to this report.  These maintenance risk assessments and emergent work control activities constituted three samples as defined in IP 71111.13-05. b. Findings
No findings were identified. 1R15 Operability Determinations and Functional Assessments (71111.15) a. Inspection Scope
The inspectors reviewed the following issues:
* Main Steam Safety Valves lift during dual-unit trip; 
* Water intrusion into the Unit 1 TDAFW turbine bearings;
* Question regarding TDAFW pump mission time;
* Inability to make new ice during the Unit 1 refueling outage;
* Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;
* Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and failure of automatic generator trip during dual-unit trip; and
* Leakby on a Unit 2 AFW flow control valve. The inspectors selected these potential operability issues based on the risk significance of the associated components and systems.  The inspectors evaluated the technical
adequacy of the evaluations to ensure that TS operability was properly justified and the  
subject component or system remained available such that no unrecognized increase in risk occurred.  The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensee's evaluations to determine
whether the components or systems were
operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures
in place would function as intended and were properly controlled.  The inspectors
determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies
associated with operability evaluations.  Documents reviewed are listed in the Attachment to this report. This operability inspection constituted seven samples as defined in IP 71111.15-05. 
17  b. Findings
(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW Pump Turbine Oil System
Introduction: A finding of very low safety significance (Green) with an associated NCV of 10 CFR Part 50, Appendix B, Criterion 16, "Corrective Actions," was identified by the  
inspectors for the licensee's failure to promptly identify and correct a CAQ associated
with Unit 1 TDAFW pump turbine bearing oil.  Specifically, the licensee failed to identify that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage had been identified directly above one of the TDAFW pump turbine bearings.  
Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1 TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.
An AR was written (AR 2014-4473) which determined that due to the leak rate and the  
apparent lack of any equipment impacts, there were no operability concerns. On 
April 11, 2014, the licensee discovered that the turbine bearing oil level was approximately 0.5 inches above the MAXIMUM mark on the sight glass.  Level had been recorded in the logs as being within band for over a year without any prior evidence of  
high level.  Additionally, there were no evolutions that had been performed which would
explain the high level.  The licensee generated AR 2014-4684 to document this
condition.  The AR documented several possible reasons for the unexplained level rise.  One was that turbine building temperature had gone up.  Another was that it was not uncommon for personnel to unnecessarily add oil to the machine from time to time.  No
other information was provided to validate either potential cause.  Additionally, there was
no mention of the leak identified above one of the turbine bearings four days prior. No
formal monitoring plan was established.  An action was created to sample the oil for
water, but as of six weeks later, a work order had not been finalized and scheduled.  The only other action was a 'lessons-learned' that was created for Mechanical Maintenance department regarding unnecessary oil adds.  The response to the action
from the group was that they don't typically do oil adds, but that they "discussed the topic
anyway."  The inspectors reviewed reference information with respect to oil levels and


their importance to machine operability.  
WO was Remove manway cover and vent cover. The instructions in the WO were
According to the vendor manual, EPRI guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is extremely critical in the turbine bearing pedestals. The references all concluded that oil
written as loosen/remove vent cover, and under the Precautions section the statement
level above the MAXIMUM mark could lead to oil frothing, which could affect stable
Per tank procedure, as a minimum, we only have to loosen vent filter. The workers
operation of the turbine and loss of oil from the system. Further, the references, along
ended up removing the cover instead of loosening it, and placed an FME bag over the
with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM
vent to prevent foreign material from entering the tank. Later on night shift, operations
mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was "over-filled" to the MAXIMUM mark. No fu
staff commenced the transfer of fuel to the day tanks. With the FME bag installed, a
rther information was provided on why this occurred or why it was acceptable to stay at the MAXIMUM mark.  One quart of oil was
vacuum was drawn on the tank. Based on the configuration of the level instruments and
drained from the turbine bearing pedestals, bringing the level back to near the
tank vent, the instruments indicated a lowering tank level and generated low level alarms
MAXIMUM mark.  Approximately five weeks later, an NRC inspector touring the plant
because of the vacuum. Operators performed a back-up measurement of tank level
questioned why level was near the MAXIMUM mark given a placard near the sight glass said to keep level at the MINIMUM mark (which aligned with the references  above). The licensee generated an AR (2014-6315) about one week later on May 22 when the
using a dip stick, however, again, based on the tank construction, this method also
inspector asked about the condition again.  In the AR, they documented the NRC observation and also the fact that an operator had noted level to be above the
showed what appeared to be a lowering tank level. With this information, operators
MAXIMUM mark by approximately 0.25 inches.  Oil was again drained from the
believed an actual loss of fuel from the tank had occurred. Absent any indications in the
machine, this time to right above the MINIMUM mark.  The operability assessment (which was not documented until the following day), stated that at time of discovery, the 
plant of fuel leaving the system, they concluded a release to the environment may have
18  machine was operable because of "oil level not affecting operability of the turbine" and a "history of overfilling that sometimes required draining of the oil."  Further, a statement
occurred. Appropriate reports were made to state, federal, and local agencies.
was made that there had been a consistent oil level trend for the past month. Again,  the leakage above the bearing was not discussed.  There was no discussion of the previous high-level condition from April 11.  On May 23, the licensee decided to  
Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed
completely drain the oil and sample it for water; 620 ml of water was found in the 2.5
level indications. During investigation soon after the abnormal level indications, the FME
gallon system. New oil was added, and an apparent cause evaluation was performed.
bag was found on the vent. Once removed, level in the tank returned to normal. There
The evaluation concluded that leakage above the bearing housing (documented
was no actual loss of fuel from the tank.
originally in AR 2014-4473), combined with a small casing steam leak that condensed above the housing while the machine was in operation, caused the water intrusion in the bearing oil. Later evaluation determined the leak rate from the pipe had increased to
Analysis: The failure to have adequate instructions for performing work on safety-related
8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources
equipment, as required by TS 5.4, Procedures, was a performance deficiency
were diverted away from the bearing housing with a temporary modification pending
warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued
repairs (which were completed in the September-October 2014 refueling outage). Based on the above, the inspectors concluded the licensee had sufficient information to promptly identify and correct water intrusion into the TDAFW turbine bearing oil system on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential
September 7, 2012. The performance deficiency was more than minor because it
operability impacts (as described in the multiple references above) on April 11 and 
adversely impacted the Configuration Control attribute of the Mitigating Systems
May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-
cornerstone, whose objective is ensuring the availability, reliability, and capability of
related oil systems is a CAQ. 
systems that respond to initiating events to prevent undesirable consequences.
Analysis: The failure to promptly identify and correct a CAQ, as required by 10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the TDAFW turbine oil system was an issue warranting further review in the SDP.  Per 
The finding screened as Green, or very low safety significance, utilizing IMC 0609
IMC 0612, Appendix B, "Issue Screening," dated September 7, 2012, the issue was  
Appendix A, The Significance Determination Process for Findings at Power, issued
more-than-minor because it adversely affected the Configuration Control attribute of the  
June 19, 2012. Specifically, all questions were answered no under Section A of
Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,  
Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag
and capability of systems that respond to initiating events to prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead to a more significant safety concern.  Specifically, not recognizing water intrusion into safety-related oil systems can impact operability and affect how safety equipment operates.  The inspectors assessed the finding for significance using IMC 0609, "Significance Determination Process," issued June 2, 2012. Per Appendix A, "The Significance
was installed, which rendered the AB FOST inoperable, for approximately 16 hours.
Determination Process (SDP) for Findings-at-Power," issued June 19, 2012, the finding
This was less than the TS allowed outage time of 48 hours.
The finding had an associated cross-cutting aspect in the human performance area,
specifically, H.5, Work Management. Work activities should be planned, controlled, and
executed with nuclear safety as the overriding priority. Contrary to the tenets of the
cross-cutting aspect, the work was planned and executed with inadequate work
instructions. Further, there was a lack of coordination between a number of work groups
and activities associated with the test.
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written
procedures shall be established, implemented, and maintained covering the applicable
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
part, that maintenance that can affect the performance of safety-related equipment
should be properly preplanned and performed in accordance with written procedures,
documented instructions, or drawings appropriate to the circumstances.
Contrary to those requirements, on August 20, 2014, the AB FOST leak test was
performed with inadequate procedures and with tasks done outside the proper
                                        20


screened as Green, or very low safety significance, in Exhibit 2.  Specifically, all questions were answered 'no' under Section A for findings related to Mitigating SSCs and Functionality.  The inspectors reviewed the licensee's past operability evaluation
    sequence. As a result, the AB FOST was rendered inoperable for approximately
and concluded that given the projected amount of water that could be entrained in the oil
    16 hours.
during operation, along with the duration of operation assumed in the safety analyses, that operability of the pump would be maintained. The inspectors determined the finding had an associated cross-cutting aspect in the Human Performance area, specifically, H.11, Challenge the Unknown.  Some of the tenets of H.11, as described in NUREG-2165, Safety Culture Common Language Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency
    Immediate corrective actions involved the removal of an FME bag which had been
and continuously challenge existing conditions in order to identify discrepancies that
    placed over the AB FOST vent. The licensee also generated AR-2014-9877, which
might result in error or inappropriate action.  Further, it states that individuals challenge
    included a root cause analysis. This violation is being treated as an NCV, consistent
unanticipated results rather than rationalize them, and that abnormal indications are not
    with Section 2.3.2 of the Enforcement Policy because it was of very low safety
attributed to 'indication problems.'  Regarding the TDAFW oil system, the licensee rationalized why the level was increasing without sufficient investigation given the 
    significance and was entered into the licensees CAP. (NCV 05000315/2014005-02;
19  significance of the system, and did not seek further information that was readily available regarding appropriate oil levels.
    05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank
Enforcement:  10 CFR Part 50, Appendix B, Criterion 16, "Corrective Action," requires, in part, that conditions adverse to quality, such as deficiencies, defective material and equipment, and nonconformances are promptly identified and corrected.  Contrary to the above, between April 11 and May 23, 2014, the licensee failed to promptly identify and correct a CAQ.  Specifically, the licensee failed to promptly identify and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system despite multiple opportunities to do so.  On April 7, the licensee became aware of a
    During Maintenance)
water leak directly above the TDAFW pump turbine outboard bearing.  On April 11, and
1R18 Plant Modifications (71111.18)
May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark.  The
  a. Inspection Scope
actions taken (draining the oil level) did not correct the condition adverse to quality in that water continued to leak into the oil.  On May 23, the licensee drained the oil system and discovered approximately 620 ml of water.  For immediate corrective actions, the licensee added new oil to the system and installed a temporary modification to prevent further water intrusion.  Further corrective actions
    The inspectors reviewed the following modification(s):
included an apparent cause evaluation and past operability evaluation.  Permanent
    *       Permanent removal of shield/missile blocks
repairs to the cooling water leak above the bearing were completed during the Fall 2014
    The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety
refueling outage.  The licensee initiated AR-2014-6315 to document the condition and
    evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to
track corrective actions. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety significance and was entered into the licensee's CAP.  (NCV 05000315/2014005-01; Failure to Identify Conditions Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System) (2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance
    verify that the modification did not affect the operability or availability of the affected
Introduction:  A finding of very low safety significance (Green) with an associated NCV of
    system(s). The inspectors, as applicable, observed ongoing and completed work
TS 5.4, "Procedures," was self-revealed when a vacuum was inadvertently drawn on the AB FOST during preparations for surveillance activities.  The vacuum caused an
    activities to ensure that the modifications were installed as directed and consistent with
indication of lowering level in the tank, alarms, and an unplanned TS LCO action statement entry.
    the design control documents; the modifications operated as expected; post-modification
Description:  On August 20, 2014, the licensee was performing work activities in preparation for an upcoming, routine leak-test of the AB FOST.  The AB FOST is one of two underground tanks on site that supply fuel to the EDG's via the smaller day tanks (which are provided for each EDG and offer a more limited, immediate fuel supply).  The
    testing adequately demonstrated continued system operability, availability, and reliability;
test consists of establishing a vacuum in the tank and monitoring it for a period of time. 
    and that operation of the modifications did not impact the operability of any interfacing
Several support activities are required to be performed prior to the test, some of which
    systems. As applicable, the inspectors verified that relevant procedure, design, and
include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the
    licensing documents were properly updated. Lastly, the inspectors discussed the plant
FOST, and connection of vendor-supplied vacuum and test equipment to the vent.  Per the overarching surveillance procedure, the basic order of activities should have been to loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST
    modification with operations, engineering, and training personnel to ensure that the
from service, remove the vent cover, hook up the test equipment, and perform the test. 
    individuals were aware of how the operation with the plant modification in place could
During the day shift on August 20, workers went out to work on the vent cover.  The
    impact overall plant performance. Documents reviewed are listed in the Attachment to
associated work instruction did not provide adequate guidance on what exactly was to be done.  While the intent was just to loosen the cover at that point, the 'Subject' of the 
    this report.
20  WO was "Remove manway cover and vent cover."  The instructions in the WO were written as "loosen/remove vent cover," and under the 'Precautions' section the statement
    This inspection constituted one permanent plant modification sample as defined in
"Per tank procedure, as a minimum, we only have to loosen vent filter."  The workers ended up removing the cover instead of loosening it, and placed an FME bag over the vent to prevent foreign material from entering the tank.  Later on night shift, operations
    IP 71111.18-05.
staff commenced the transfer of fuel to the day tanks.  With the FME bag installed, a
  b. Findings
vacuum was drawn on the tank.  Based on the configuration of the level instruments and
    Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks
tank vent, the instruments indicated a lowering tank level and generated low level alarms
    from the Containment Accident Shield
because of the vacuum.  Operators perform
    Introduction: A finding of very-low safety significance (Green) and associated NCV of
ed a back-up measurement of tank level using a dip stick, however, again, based on the tank construction, this method also showed what appeared to be a lowering tank level.  With this information, operators
    Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, was identified by the
believed an actual loss of fuel from the tank had occurred.  Absent any indications in the
    NRC inspectors for the licensees inadequate radiological review of permanently
plant of fuel leaving the system, they concluded a release to the environment may have occurred.  Appropriate reports were made to state, federal, and local agencies.  Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed level indications.  During investigation soon after the abnormal level indications, the FME
    removing the AMBs from the Unit 1 and Unit 2 containment accident shields.
bag was found on the vent.  Once removed, level in the tank returned to normal.  There was no actual loss of fuel from the tank.
    Description: In March 2014, the NRC reviewed a licensee modification
Analysis:  The failure to have adequate instructions for performing work on safety-related equipment, as required by TS 5.4, "Procedures," was a performance deficiency
    (EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The
warranting further review utilizing IMC 0612, Appendix B, "Issue Screening," issued September 7, 2012.  The performance deficiency was more than minor because it
    modification consisted of permanently removing the AMBs, located in front of the primary
adversely impacted the Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  The finding screened as Green, or very low safety significance, utilizing IMC 0609 Appendix A, "The Significance Determination Process for Findings at Power," issued
    containment equipment hatches on the 650 elevation of the Auxiliary Building. The
June 19, 2012.  Specifically, all questions were answered 'no' under Section A of  Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.  The FME bag was installed, which rendered the AB FOST inoperable, for approximately 16 hours.  This was less than the TS allowed outage time of 48 hours. The finding had an associated cross-cutting aspect in the human performance area, specifically, H.5, Work Management.  Work activities should be planned, controlled, and
    AMBs are portable and removable shield blocks and are a part of the safety-related
executed with nuclear safety as the overridi
                                              21
ng priority.  Contrary to the tenets of the cross-cutting aspect, the work was planned and executed with inadequate work
instructions.  Further, there was a lack of coordination between a number of work groups
and activities associated with the test.
Enforcement:  Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33.  Regulatory Guide 1.33 states, in
part, that maintenance that can affect the performance of safety-related equipment
should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to those requirements, on August 20, 2014, the AB FOST leak test was performed with inadequate procedures and with tasks done outside the proper 
21  sequence. As a result, the AB FOST was rendered inoperable for approximately 16 hours. Immediate corrective actions involved the removal of an FME bag which had been placed over the AB FOST vent. The licensee also generated AR-2014-9877, which  
included a root cause analysis. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety significance and was entered into the licensee's CAP. (NCV 05000315/2014005-02; 05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank  
During Maintenance) 1R18 Plant Modifications (71111.18) a. Inspection Scope
The inspectors reviewed the following modification(s):  
* Permanent removal of shield/missile blocks The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to  
verify that the modification did not affect the operability or availability of the affected system(s). The inspectors, as applicable, observed ongoing and completed work activities to ensure that the modifications were installed as directed and consistent with  
the design control documents; the modifications operated as expected; post-modification  
testing adequately demonstrated continued system operability, availability, and reliability;  
and that operation of the modifications did not impact the operability of any interfacing systems. As applicable, the inspectors verified that relevant procedure, design, and licensing documents were properly updated. Lastly, the inspectors discussed the plant  
modification with operations, engineering, and training personnel to ensure that the  
individuals were aware of how the operation with the plant modification in place could  
impact overall plant performance. Documents reviewed are listed in the Attachment to this report. This inspection constituted one permanent plant modification sample as defined in  
IP 71111.18-05. b. Findings
Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks from the Containment Accident Shield
Introduction: A finding of very-low safety significance (Green) and associated NCV of Title 10 CFR Part 50, Appendix B, Criterion 3, "Design Control," was identified by the  
NRC inspectors for the licensee's inadequate radiological review of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident shields.  
Description: In March 2014, the NRC reviewed a licensee modification (EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The  
modification consisted of permanently removing the AMBs, located in front of the primary  
containment equipment hatches on the 650' elevation of the Auxiliary Building. The  
AMBs are portable and removable shield blocks and are a part of the safety-related
22  containment accident shield. The AMBs are in place during power operations for shielding purposes.  The AMBs are removed during plant outages to permit containment access for equipment. The main purpose of the accident shield, as a part of original plant design and currently described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside the containment building following a maximum design-basis accident; specifically, a large break loss-of-coolant accident (LBLOCA).  The plant containment and the accident
shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and
the general public are protected by adequate containment shielding, post LBLOCA.  This
was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General Design Criteria 1 "Quality Standards and Records" of Appendix A "General Design Criteria for Nuclear Power Plants," 10 CFR Part 20 "Standards for Protection Against
Radiation," and 10 CFR Part 100 "Reactor Site Criteria."  The inspectors reviewed the
original and current plant design configuration and determined that, prior to plant
modification (EC-0000049191), the plant design met General Design Criteria 1 for
radiation safety.  Specifically, RG 1.69 "Concrete Radiation Shields for Nuclear Power Plants" was explicit in stating that General Design Criteria 1 for containment ensures reasonable assurance for compliance to 10 CFR Part 20 "Standards for Protection
Against Radiation" under post-accident conditions.  Additionally, initial plant design for
the containment accident shield was consistent with RG 1.69 "Concrete Radiation Shields for Nuclear Power Plants."  Using the licensee's design basis source term, licensee calculation number RS-C-0046 "Doses and Dose Rates from Post LOCA Airborne Sources" determined that with the
AMBs in place, the Post LBLOCA dose rates were:
* A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and 
* A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.  These dose rates provide for safe radiation levels outside the containment building following a maximum design-basis accident consistent with the UFSAR design
statements and in accordance with the requirements of 10 CFR Part 20, "Standards for Protection Against Radiation." The licensee provided no comparable post-modification dose rate calculations to the inspectors specific to AB 650' elevation once the AMBs were removed.  However, the licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates 
of 196.2 Rem/hr at 45 feet from the equipment hatch.  Additionally, the licensee had
analogous Post-LBLOCA dose rate calculations for the containment personnel hatch. 
These dose rates provide a frame of reference, in that, the calculations provide for no
AMB shielding.  However, the calculations did include shielding benefit from the inside containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources").  Specific calculated dose rates were:
* A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel hatch; and
* A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel
hatch. 
23  The inspectors determined that post-modification dose rates on the AB 650' elevation could result in lethal doses, as defined in NUREG/CR 6545 "Probabilistic Accident
Consequence Uncertainty Analysis:  Early Health Effects Uncertainty Assessment," to individuals in a very short period of time (from fractions of a second to minutes, depending on the location of personnel relative to the radiation source).  By permanently
removing the AMBs, the licensee failed to provide for safe radiation levels outside the
containment building following a maximum design-basis accident, contrary to the design bases and inconsistent with the requirements of 10 CFR Part 20. Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use, to the extent practical, engineering controls based upon sound radiation principles to achieve occupational doses and doses to members of the public that are as-low-as-reasonably-achievable (ALARA).  Original plant design and the plant's 40-year
operational history demonstrate that plant operation with the AMBs in place was both practical and ALARA. The licensee documented this issue in the CAP as AR 2014-13016.
  Corrective actions included licensee determination to achieve radiation attenuation analogous to original plant design of the AMBs in place.
Analysis:  The inspectors determined that the licensee's inadequate radiological review of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident shields was a performance deficiency.  The performance deficiency was determined to be more than minor (Green) because it was associated with the Barrier Integrity
Cornerstone attribute of design control; and adversely affected the cornerstone objective
of maintaining radiological barrier functionality of the safety-related containment accident shield.  Specifically, the failure to control plant design and adequately evaluate the
radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not ensure that the accident shield will provide its design function to ensure safe radiation levels outside the containment building following a maximum design basis accident. The inspectors evaluated the finding using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of
Findings," dated June 19, 2012.  Because the finding impacted the Barrier Integrity
Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," dated June 19, 2012, using Exhibit 3, "Barrier Integrity Screening Questions."  The finding screened as of very-low
safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the Auxiliary Building. The inspectors determined the cause of this finding did not represent current licensee performance and, thus, no cross-cutting aspect was assigned.
Enforcement:  Title 10 CFR Part 50, Appendix B, Criterion 3, "Design Control," requires, in part, that design changes be subject to design control measures commensurate with those applied to the original design. Contrary to the above, on February 6, 2009, the licensee performed a design change and failed to subject it to design control measures commensurate with those applied to the original design.  Specifically, the licensee modified the original plant design by 
24  removing the auxiliary missile blocks from the safety-related accident shield.  However, the design control measures applied to the modification failed to ensure safe radiation
levels outside the containment accident shield following a design basis loss-of-coolant
accident. Because this violation was of very-low safety significance and was entered into the licensee's CAP (AR 2014-13016), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.  (NCV 05000315/2014005-03; 05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield


Blocks on the Containment Accident Shield Post LBLOCA) 1R19 Post-Maintenance Testing (71111.19) a. Inspection Scope
containment accident shield. The AMBs are in place during power operations for
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
shielding purposes. The AMBs are removed during plant outages to permit containment
* Unit 1 AB EDG following governor replacement;
access for equipment.
* Unit 1 CRID III and IV maintenance;
The main purpose of the accident shield, as a part of original plant design and currently
* Unit 2 UAT breakers following failure to close;
described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside
* Unit 1 CD EDG governor replacement and aftercooler maintenance;
the containment building following a maximum design-basis accident; specifically, a
* Unit 1 TDAFW governor overhaul;
large break loss-of-coolant accident (LBLOCA). The plant containment and the accident
* Repair of Unit 2 AFW flow control valve flow retention issue;
shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and
* Repair of circuitry associated with failure of fast transfer and generator trip during dual-unit trip; and  
the general public are protected by adequate containment shielding, post LBLOCA. This
* Unit 1 TDAFW repairs following inadvertent trip. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate
was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General
for the maintenance performed; acceptance criteria were clear and demonstrated
Design Criteria 1 Quality Standards and Records of Appendix A General Design
operational readiness; test instrumentation was appropriate; tests were performed as
Criteria for Nuclear Power Plants, 10 CFR Part 20 Standards for Protection Against
Radiation, and 10 CFR Part 100 Reactor Site Criteria. The inspectors reviewed the
original and current plant design configuration and determined that, prior to plant
modification (EC-0000049191), the plant design met General Design Criteria 1 for
radiation safety. Specifically, RG 1.69 Concrete Radiation Shields for Nuclear Power
Plants was explicit in stating that General Design Criteria 1 for containment ensures
reasonable assurance for compliance to 10 CFR Part 20 Standards for Protection
Against Radiation under post-accident conditions. Additionally, initial plant design for
the containment accident shield was consistent with RG 1.69 Concrete Radiation
Shields for Nuclear Power Plants.
Using the licensees design basis source term, licensee calculation number RS-C-0046
Doses and Dose Rates from Post LOCA Airborne Sources determined that with the
AMBs in place, the Post LBLOCA dose rates were:
    * A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and
    * A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.
These dose rates provide for safe radiation levels outside the containment building
following a maximum design-basis accident consistent with the UFSAR design
statements and in accordance with the requirements of 10 CFR Part 20, Standards for
Protection Against Radiation.
The licensee provided no comparable post-modification dose rate calculations to the
inspectors specific to AB 650 elevation once the AMBs were removed. However, the
licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose
Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates
of 196.2 Rem/hr at 45 feet from the equipment hatch. Additionally, the licensee had
analogous Post-LBLOCA dose rate calculations for the containment personnel hatch.
These dose rates provide a frame of reference, in that, the calculations provide for no
AMB shielding. However, the calculations did include shielding benefit from the inside
containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from
Post LOCA Airborne Sources). Specific calculated dose rates were:
*    A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel
    hatch; and
*    A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel
    hatch.
                                        22


written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test
The inspectors determined that post-modification dose rates on the AB 650 elevation
could result in lethal doses, as defined in NUREG/CR 6545 Probabilistic Accident
Consequence Uncertainty Analysis: Early Health Effects Uncertainty Assessment, to
individuals in a very short period of time (from fractions of a second to minutes,
depending on the location of personnel relative to the radiation source). By permanently
removing the AMBs, the licensee failed to provide for safe radiation levels outside the
containment building following a maximum design-basis accident, contrary to the design
bases and inconsistent with the requirements of 10 CFR Part 20.
Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use,
to the extent practical, engineering controls based upon sound radiation principles to
achieve occupational doses and doses to members of the public that are
as-low-as-reasonably-achievable (ALARA). Original plant design and the plants 40-year
operational history demonstrate that plant operation with the AMBs in place was both
practical and ALARA.
The licensee documented this issue in the CAP as AR 2014-13016. Corrective actions
included licensee determination to achieve radiation attenuation analogous to original
plant design of the AMBs in place.
Analysis: The inspectors determined that the licensees inadequate radiological review
of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident
shields was a performance deficiency. The performance deficiency was determined to
be more than minor (Green) because it was associated with the Barrier Integrity
Cornerstone attribute of design control; and adversely affected the cornerstone objective
of maintaining radiological barrier functionality of the safety-related containment accident
shield. Specifically, the failure to control plant design and adequately evaluate the
radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2
containment accident shields did not ensure that the accident shield will provide its
design function to ensure safe radiation levels outside the containment building following
a maximum design basis accident.
The inspectors evaluated the finding using the SDP in accordance with IMC 0609,
Significance Determination Process, Attachment 0609.04, Initial Characterization of
Findings, dated June 19, 2012. Because the finding impacted the Barrier Integrity
Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, The
Significance Determination Process for Findings At-Power, dated June 19, 2012, using
Exhibit 3, Barrier Integrity Screening Questions. The finding screened as of very-low
safety significance (Green) because the finding only represented a degradation of the
radiological barrier function provided for the Auxiliary Building.
The inspectors determined the cause of this finding did not represent current licensee
performance and, thus, no cross-cutting aspect was assigned.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, requires,
in part, that design changes be subject to design control measures commensurate with
those applied to the original design.
Contrary to the above, on February 6, 2009, the licensee performed a design change
and failed to subject it to design control measures commensurate with those applied to
the original design. Specifically, the licensee modified the original plant design by
                                          23


documentation was properly evaluated.  The inspectors evaluated the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
    removing the auxiliary missile blocks from the safety-related accident shield. However,
NRC generic communications to ensure that the test results adequately ensured that the
    the design control measures applied to the modification failed to ensure safe radiation
equipment met the licensing basis and design requirements.  In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP
    levels outside the containment accident shield following a design basis loss-of-coolant
and that the problems were being corrected commensurate with their importance to safety.  Documents reviewed are listed in the Attachment to this report. This inspection constituted eight post-maintenance testing samples as defined in
    accident.
IP 71111.19-05. 
    Because this violation was of very-low safety significance and was entered into the
25  b. Findings
    licensees CAP (AR 2014-13016), this violation is being treated as an NCV, consistent
Introduction:  A finding of very low safety significance (Green) with an associated NCV of
    with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000315/2014005-03;
TS 5.4, "Procedures," was self-revealed on November 1, 2014, when the Unit 1 TDAFW
    05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield
pump tripped during an emergent dual-unit shutdown. Both units were taken offline by
    Blocks on the Containment Accident Shield Post LBLOCA)
operators due to debris intrusion from Lake Michigan into the cooling water screenhouse. The TDAFW pump started as expected but shutdown after a few minutes of operation. 
1R19 Post-Maintenance Testing (71111.19)
Description:  On November 1, 2014, operators removed both units from service in response to excessive debris intrusion into the cooling water screenhouse. Following the trip of both reactors, AFW pumps started as expected.  However, the Unit 1 TDAFW
  a. Inspection Scope
unexpectedly turned off after a few minutes of operation while operators were adjusting
    The inspectors reviewed the following post-maintenance activities to verify that
flow to the steam generators.  Adequate flow continued to be provided by the two other AFW pumps.  During the ensuing forced outage to address the debris intrusion issue, the licensee performed an investigation into why the pump tripped off.  The licensee
    procedures and test activities were adequate to ensure system operability and functional
explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry, and governor control problems.  The investigation included several test runs of the pump
    capability:
while rapidly changing demand in an effort to 'stress' the pump and replicate the trip
    *      Unit 1 AB EDG following governor replacement;
event. During continued troubleshooting, the licensee later discovered a protective enclosure around an electronic component (the trip solenoid) had been installed incorrectly.  The enclosure was relatively loose, and the licensee found by moving it
    *      Unit 1 CRID III and IV maintenance;
slightly, it could be placed in a position where a threaded rod on the enclosure could
    *      Unit 2 UAT breakers following failure to close;
interfere with the proper latching of the TTV for the pump. When the pump turns on, the
    *      Unit 1 CD EDG governor replacement and aftercooler maintenance;
TTV opens to admit steam to the turbine.  As the valve stem moves up, an attachment engages a trip hook.  The trip hook basically acts to hold the valve open.  On a trip condition, such as a pump overspeed, the hook would move out of the way, allowing the
    *      Unit 1 TDAFW governor overhaul;
valve to shut and the pump to turn off.  Precise engagement between the TTV and the
    *      Repair of Unit 2 AFW flow control valve flow retention issue;
trip hook is required for the pump to operate correctly.  In this case, the licensee's
    *      Repair of circuitry associated with failure of fast transfer and generator trip during
apparent cause evaluation determined the most likely cause was inadequate trip hook engagement as a result of the interference from the trip solenoid enclosure.  As part of the extent-of-condition, the licensee discovered the same potential issue on the Unit 2
            dual-unit trip; and
TDAFW pump.  Further investigation revealed that the enclosure was not captured in
    *      Unit 1 TDAFW repairs following inadvertent trip.
design diagrams, and that work instructions regarding its installation/removal were not
    These activities were selected based upon the structure, system, or component's ability
detailed.  Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been
    to impact risk. The inspectors evaluated these activities for the following (as applicable):
removed and reinstalled during the Fall 2014 refueling outage as part of planned maintenance.  Working with the pump vendor, the licensee identified the correct configuration of the enclosure and reinstalled them correctly on both pumps.  The
    the effect of testing on the plant had been adequately addressed; testing was adequate
licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW pump to operable status at the conclusion of the forced outage.
    for the maintenance performed; acceptance criteria were clear and demonstrated
Analysis:  The failure to have adequate instructions for performing work on safety-related equipment, as required by TS 5.4, "Procedures," was a performance deficiency
    operational readiness; test instrumentation was appropriate; tests were performed as
warranting further review utilizing IMC 0612, Appendix B, "Issue Screening," issued September 7, 2012.  The performance deficiency was more than minor because it
    written in accordance with properly reviewed and approved procedures; equipment was
adversely impacted the Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  The inspectors utilized IMC 0609 Appendix A, "The Significance Determination Process for Findings at Power," issued June 19, 2012, to assess the significance of the finding. 
    returned to its operational status following testing (temporary modifications or jumpers
26  Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater than the TS allowed outage time.  Therefore, the inspectors consulted the regional
    required for test performance were properly removed after test completion); and test
Senior Reactor Analyst (SRA) for a detailed risk evaluation.  The inspectors considered the Unit 1 TDAFW pump inoperable since the last successful surveillance on  October 23. Given the evidence available, this was the likely opportunity for the conditions to be established to set-up the improper engagement between the TTV and
    documentation was properly evaluated. The inspectors evaluated the activities against
the trip hook. The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook to perform a detailed risk evaluation.
    TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
The model has internal and external event initiators.  The SRA assumed an exposure period for the condition of 9 days.  The delta core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low safety significance (Green).  The dominant risk sequence was a fire in the turbine
    NRC generic communications to ensure that the test results adequately ensured that the
building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed. 
    equipment met the licensing basis and design requirements. In addition, the inspectors
Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the
    reviewed corrective action documents associated with post-maintenance tests to
potential impact of the finding on large early release frequency using IMC 0609
    determine whether the licensee was identifying problems and entering them in the CAP
Appendix H, "Containment Integrity Significance Determination Process."  The plant has an ice condenser containment and sequences important to large early release frequency are steam generator tube rupture, inter-system loss-of-coolant accident, and station
    and that the problems were being corrected commensurate with their importance to
blackout.  Some of the sequences that contributed to the change in CDF included station
    safety. Documents reviewed are listed in the Attachment to this report.
blackout sequences but their contribution was less than 1E-7/yr.  The SRA concluded that the risk of this finding should be characterized by the overall change in CDF. The finding had an associated cross-cutting aspect in the area of human performance, specifically, H.8, Procedure Adherence.  Safety Culture Common Language Initiative NUREG-2165 provides an example of the as
    This inspection constituted eight post-maintenance testing samples as defined in
pect as "individuals review procedures before work to validate they are appropriate for scope of work, and ensure required
    IP 71111.19-05.
changes are completed before implementation."  Contrary to this description, work
                                              24
proceeded on the trip enclosure despite a lack of detailed instructions on the removal/installation of the enclosure.
Enforcement:  Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33.  Regulatory Guide 1.33 states, in part, that maintenance that can affect the performance of safety-related equipment
should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip solenoid enclosure with inadequate work instructions.  As a result, an apparent cause
evaluation determined the misplaced enclosure was the likely cause of the pump 
failure during an actual demand following a dual-unit trip.  The violation existed from October 23, 2014, until troubleshooting and post-maintenance testing activities were completed on November 3, 2014, following the dual-unit trip. For immediate corrective actions, the licensee initiated AR-2014-13668 and began troubleshooting activities.  The licensee investigation revealed the misplaced trip
solenoid enclosure to be the likely cause of the pump trip.  Subsequently, the enclosures
were installed in the correct position.  This violation is being treated as an NCV,
consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety 
27  significance and was entered into the licensee's CAP.  (NCV 05000315/2014005-04;
Inadvertent Trip of the Unit 1 TDAFW Pump) 1R20 Outage Activities (71111.20) .1 Refueling Outage Activities
a. Inspection Scope
The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1 refueling outage, conducted September 24 - October 24, 2014, to confirm that the
licensee had appropriately considered risk, industry experience, and previous
site-specific problems in developing and implementing a plan that assured maintenance
of defense-in-depth. During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below:
* licensee configuration management, including maintenance of defense-in-depth commensurate with the Outage Safety Plan for key safety functions and compliance with the applicable TS when taking equipment out of service;
* implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing; * installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error;
* controls over the status and configuration of electrical systems to ensure that
TS and Outage Safety Plan requirements were met, and controls over switchyard activities;
* monitoring of decay heat removal processes, systems, and components;
* controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system;
* reactor water inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss;
* controls over activities that could affect reactivity;
* maintenance of secondary containment as required by TS;
* licensee fatigue management, as required by 10 CFR 26, Subpart I;
* refueling activities, including fuel handling and sipping to detect fuel assembly leakage; * startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing; and
* licensee identification and resolution of problems related to refueling outage activities.  
Documents reviewed are listed in the Attachment to this report. This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05. 
28  b. Findings
No findings were identified. .2 Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014
a. Inspection Scope
On November 1, rough lake conditions generated substantial amounts of debris that clogged trash racks and travelling screens.  The licensee manually tripped the Unit 1 reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce
circulating water flow.  Conditions continued to degrade; therefore the licensee
subsequently tripped the Unit 2 reactor.  Unit 1 remained in Mode 3 and returned to 
100 percent power on November 8.  Unit 2 was cooled down to Mode 5 to repair an intermediate range nuclear instrument.  Unit 2 was returned to 100 percent power on November 13.  The inspectors toured portions of containment, observed shutdown and startup activities, assessed plant risk, and observed maintenance activities. This inspection constituted one Forced Outage sample as defined in IP 71111.20-05. b. Findings
No findings were identified. 1R22 Surveillance Testing (71111.22) a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural


and TS requirements:  
b. Findings
* 1-OHP-4030-108-008R, Unit 1 ECCS Check Valve Test, (IST);
  Introduction: A finding of very low safety significance (Green) with an associated NCV of
* 1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);
  TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1 TDAFW
* 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, (Ice Condenser Surveillance);
  pump tripped during an emergent dual-unit shutdown. Both units were taken offline by
* Unit 1 Control Room Emergency Ventilation Surveillance, 1-EHP-4030-128-229 (Routine); and  
  operators due to debris intrusion from Lake Michigan into the cooling water
* Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine). The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following: 
  screenhouse. The TDAFW pump started as expected but shutdown after a few minutes
* did preconditioning occur; 
  of operation.
* the effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  Description: On November 1, 2014, operators removed both units from service in
* acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis;
  response to excessive debris intrusion into the cooling water screenhouse. Following
* plant equipment calibration was correct, accurate, and properly documented;
  the trip of both reactors, AFW pumps started as expected. However, the Unit 1 TDAFW
* as-left setpoints were within required ranges; and the calibration frequency was in accordance with TSs, the USAR, procedures, and applicable commitments; 
  unexpectedly turned off after a few minutes of operation while operators were adjusting
29  * measuring and test equipment calibration was current;
  flow to the steam generators. Adequate flow continued to be provided by the two other
* test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  AFW pumps. During the ensuing forced outage to address the debris intrusion issue,
* test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored
  the licensee performed an investigation into why the pump tripped off. The licensee
  explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry,
  and governor control problems. The investigation included several test runs of the pump
  while rapidly changing demand in an effort to stress the pump and replicate the trip
  event. During continued troubleshooting, the licensee later discovered a protective
  enclosure around an electronic component (the trip solenoid) had been installed
  incorrectly. The enclosure was relatively loose, and the licensee found by moving it
  slightly, it could be placed in a position where a threaded rod on the enclosure could
  interfere with the proper latching of the TTV for the pump. When the pump turns on, the
  TTV opens to admit steam to the turbine. As the valve stem moves up, an attachment
  engages a trip hook. The trip hook basically acts to hold the valve open. On a trip
  condition, such as a pump overspeed, the hook would move out of the way, allowing the
  valve to shut and the pump to turn off. Precise engagement between the TTV and the
  trip hook is required for the pump to operate correctly. In this case, the licensees
  apparent cause evaluation determined the most likely cause was inadequate trip hook
  engagement as a result of the interference from the trip solenoid enclosure. As part of
  the extent-of-condition, the licensee discovered the same potential issue on the Unit 2
  TDAFW pump. Further investigation revealed that the enclosure was not captured in
  design diagrams, and that work instructions regarding its installation/removal were not
  detailed. Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been
  removed and reinstalled during the Fall 2014 refueling outage as part of planned
  maintenance. Working with the pump vendor, the licensee identified the correct
  configuration of the enclosure and reinstalled them correctly on both pumps. The
  licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW
  pump to operable status at the conclusion of the forced outage.
  Analysis: The failure to have adequate instructions for performing work on safety-related
  equipment, as required by TS 5.4, Procedures, was a performance deficiency
  warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued
  September 7, 2012. The performance deficiency was more than minor because it
  adversely impacted the Configuration Control attribute of the Mitigating Systems
  cornerstone, whose objective is ensuring the availability, reliability, and capability of
  systems that respond to initiating events to prevent undesirable consequences.
  The inspectors utilized IMC 0609 Appendix A, The Significance Determination Process
  for Findings at Power, issued June 19, 2012, to assess the significance of the finding.
                                              25


where used;
Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater
* test data and results were accurate, complete, within limits, and valid;
than the TS allowed outage time. Therefore, the inspectors consulted the regional
* test equipment was removed after testing;
Senior Reactor Analyst (SRA) for a detailed risk evaluation. The inspectors considered
* where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the  
the Unit 1 TDAFW pump inoperable since the last successful surveillance on
system design basis;
October 23. Given the evidence available, this was the likely opportunity for the
* where applicable, test results not meeting acceptance criteria were addressed
conditions to be established to set-up the improper engagement between the TTV and
with an adequate operability evaluation or the system or component was declared inoperable;
the trip hook.
* where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook
* where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
to perform a detailed risk evaluation. The model has internal and external event
* prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
initiators. The SRA assumed an exposure period for the condition of 9 days. The delta
* equipment was returned to a position or status required to support the performance of its safety functions; and  
core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low
* all problems identified during the testing were appropriately documented and dispositioned in the CAP.   Documents reviewed are listed in the Attachment to this report. This inspection constituted two routine surveillance testing samples, one inservice testing sample, one ice condenser surveillance, and one containment isolation valve sample as defined in IP 71111.22, Sections-02 and-05. b. Findings
safety significance (Green). The dominant risk sequence was a fire in the turbine
No findings were identified. 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) a. Inspection Scope
building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed.
The regional inspectors performed an in-office review of the latest revisions to the Emergency Plan and Emergency Plan Implementing Procedures as listed in the Attachment to this report. The licensee transmitted the Emergency Plan and Emergency Action Level revisions to the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,
Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the
"Implementing Procedures.The NRC review was not documented in a safety
potential impact of the finding on large early release frequency using IMC 0609
evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.  The specific documents reviewed during this inspection are listed in the Attachment to this report. 
Appendix H, Containment Integrity Significance Determination Process. The plant has
30  This Emergency Action Level and Emergency Plan Change inspection constituted one sample as defined in IP 71114.04-06. b. Findings
an ice condenser containment and sequences important to large early release frequency
Introduction:  An Unresolved Item (URI) was identified because additional information is required to determine whether a performance deficiency that is more than minor exists
are steam generator tube rupture, inter-system loss-of-coolant accident, and station
and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of
blackout. Some of the sequences that contributed to the change in CDF included station
concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the number of Radiation Protection Technicians (RPTs) required to augment the on-shift emergency response organization in 60 minutes of a declared emergency and replaced
blackout sequences but their contribution was less than 1E-7/yr. The SRA concluded
them with a Radiological Assessment Coordinator (RAC) and an Environmental Assessment Coordinator (EAC).
that the risk of this finding should be characterized by the overall change in CDF.
Description.  During the review, the inspectors identified a change made in Table 1 of Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced
The finding had an associated cross-cutting aspect in the area of human performance,
the number of 60-minute response RPTs tasked with conducting offsite surveys from three RPTs to two RPTs and one EAC. The second change reduced the number of 60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one
specifically, H.8, Procedure Adherence. Safety Culture Common Language Initiative
RPT and one RAC.  According the licensee's 10 CFR 2014 50.54(q) screening
NUREG-2165 provides an example of the aspect as individuals review procedures
evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and
before work to validate they are appropriate for scope of work, and ensure required
B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute responders in Revision 19 of the plan in March of 2004. Inspectors' review of the  
changes are completed before implementation. Contrary to this description, work
10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had
proceeded on the trip enclosure despite a lack of detailed instructions on the
been done for this change.  The inspectors reviewed Revision 18 of the E-Plan and the  
removal/installation of the enclosure.
associated March 21, 2003 licensee request for prior approval for changes to the E-plan
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written
that was conducted, approved by the NRC, and implemented in this revision. The NRC approved change request included specific num
procedures shall be established, implemented, and maintained covering the applicable
bers of RPTs for 60-minute response tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.  The licensee indicated that the EAC and RAC were not currently qualified RPTs.  This suggests a performance deficiency, due to the appearance of a reduction in  
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
effectiveness to the licensee's E-plan, without prior NRC approval. However, in order to
part, that maintenance that can affect the performance of safety-related equipment
determine if this is a performance deficiency of more than minor significance, additional
should be properly preplanned and performed in accordance with written procedures,
information is required to understand if the RAC and EAC positions had equivalent capabilities as the qualified RPTs. The licensee has entered this issue in their Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory
documented instructions, or drawings appropriate to the circumstances.
actions were taken while their staff gathers additional information, which included
Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip
requiring two additional qualified RPTs to respond to the Operations Support Center
solenoid enclosure with inadequate work instructions. As a result, an apparent cause
within 60 minutes prior to activating the facility in the event of a declared emergency.  
evaluation determined the misplaced enclosure was the likely cause of the pump
The licensee stated that it will provide the inspectors with additional information within 
failure during an actual demand following a dual-unit trip. The violation existed from
30 days of the exit meeting.  Therefore, a URI was identified pending additional information. Specifically, documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC
October 23, 2014, until troubleshooting and post-maintenance testing activities were
are equivalent to the RPTs is necessary for the inspectors to determine whether the  
completed on November 3, 2014, following the dual-unit trip.
performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)
For immediate corrective actions, the licensee initiated AR-2014-13668 and began
troubleshooting activities. The licensee investigation revealed the misplaced trip
solenoid enclosure to be the likely cause of the pump trip. Subsequently, the enclosures
were installed in the correct position. This violation is being treated as an NCV,
consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety
                                          26


occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency Responder Staffing Without Prior Approval)  
      significance and was entered into the licensees CAP. (NCV 05000315/2014005-04;
31  2. RADIATION SAFETY 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) The inspection activities supplement t
      Inadvertent Trip of the Unit 1 TDAFW Pump)
hose documented in NRC Inspection Report 05000315-05000316/2014002 and constitute one complete sample as defined in Inspection Procedure 71124.01-05. .1 Radiological Hazard Assessment (02.02)  a. Inspection Scope
1R20 Outage Activities (71111.20)
The inspectors determined whether there have been changes to plant operations since the last inspection that may result in a significant new radiological hazard for onsite
.1   Refueling Outage Activities
workers or members of the public. The inspectors evaluated whether the licensee
  a. Inspection Scope
assessed the potential impact of these changes and has implemented periodic monitoring, as appropriate, to detect and quantify the radiological hazard. The inspectors reviewed the last two radiological surveys from selected plant areas and evaluated whether the thoroughness and frequency of the surveys where appropriate for the given radiological hazard. The inspectors selected the following radiologically risk significant work activities that involved exposure to radiation: 
      The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1
* Refuel Cavity Decontamination Activities;
      refueling outage, conducted September 24 - October 24, 2014, to confirm that the
* Steam Generator Platform Activities;
      licensee had appropriately considered risk, industry experience, and previous
* Valve Maintenance / Repair; 
      site-specific problems in developing and implementing a plan that assured maintenance
* Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted
      of defense-in-depth. During the refueling outage, the inspectors observed portions of
Areas; and  
      the shutdown and cooldown processes and monitored licensee controls over the outage
* Reactor Pit Very High Radiation Area (VHRA) Downpost Survey. For these work activities, the inspectors assessed whether the pre-work surveys performed were appropriate to identify and quantify the radiological hazard and to establish adequate protective measures.  The inspectors evaluated the radiological survey program to determine if hazards were properly identified, including the following: 
      activities listed below:
* identification of hot particles;  
      *        licensee configuration management, including maintenance of defense-in-depth
* the presence of alpha emitters;  
              commensurate with the Outage Safety Plan for key safety functions and
* the potential for airborne radioactive materials, including the potential presence of transuranics and/or other hard-to-detect radioactive materials (This evaluation may include licensee planned entry into non-routinely entered areas subject to previous contamination from failed fuel.);
              compliance with the applicable TS when taking equipment out of service;
* the hazards associated with work activities that could suddenly and severely increase radiological conditions and that the licensee has established a means to inform workers of changes that could significantly impact their occupational dose;
      *        implementation of clearance activities and confirmation that tags were properly
              hung and equipment appropriately configured to safely support the work or
              testing;
      *       installation and configuration of reactor coolant pressure, level, and temperature
              instruments to provide accurate indication, accounting for instrument error;
      *       controls over the status and configuration of electrical systems to ensure that
              TS and Outage Safety Plan requirements were met, and controls over switchyard
              activities;
      *        monitoring of decay heat removal processes, systems, and components;
      *       controls to ensure that outage work was not impacting the ability of the operators
              to operate the spent fuel pool cooling system;
      *        reactor water inventory controls including flow paths, configurations, and
              alternative means for inventory addition, and controls to prevent inventory loss;
      *        controls over activities that could affect reactivity;
      *       maintenance of secondary containment as required by TS;
      *       licensee fatigue management, as required by 10 CFR 26, Subpart I;
      *       refueling activities, including fuel handling and sipping to detect fuel assembly
              leakage;
      *       startup and ascension to full power operation, tracking of startup prerequisites,
              walkdown of the drywell (primary containment) to verify that debris had not been
              left which could block emergency core cooling system suction strainers, and
              reactor physics testing; and
      *        licensee identification and resolution of problems related to refueling outage
              activities.
      Documents reviewed are listed in the Attachment to this report.
      This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05.
                                                  27


and * severe radiation field dose gradients that can result in non-uniform exposures of
  b. Findings
the body. 
      No findings were identified.
32  The inspectors observed work in potential airborne areas and evaluated whether the air samples were representative of the breathing air zone.  The inspectors evaluated
.2   Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014
whether continuous air monitors were located in areas with low background to minimize false alarms and were representative of actual work areas.  The inspectors evaluated the licensee's program for monitoring levels of loose surface contamination in areas of the plant with the potential for the contamination to become airborne. b. Findings
  a. Inspection Scope
No findings were identified. .2 Instructions to Workers (02.03) a. Inspection Scope
      On November 1, rough lake conditions generated substantial amounts of debris that
The inspectors reviewed the following radiation work permits used to access high radiation areas and evaluated the specified work control instructions or control barriers:
      clogged trash racks and travelling screens. The licensee manually tripped the Unit 1
* RWP 141100; U1C26 - Refuel Cavity Decontamination Activities; 
      reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce
* RWP 141148; U1C26 - Steam Generator Platform Activities; 
      circulating water flow. Conditions continued to degrade; therefore the licensee
* RWP 141145; U1C26 - Valve Maintenance / Repair; 
      subsequently tripped the Unit 2 reactor. Unit 1 remained in Mode 3 and returned to
* RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant Restricted Areas; and  
      100 percent power on November 8. Unit 2 was cooled down to Mode 5 to repair an
* RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey. For these radiation work permits, the inspectors assessed whether allowable stay times or permissible dose (including from the intake of radioactive material) for radiologically
      intermediate range nuclear instrument. Unit 2 was returned to 100 percent power on
significant work under each radiation work permit were clearly identified. The inspectors  
      November 13. The inspectors toured portions of containment, observed shutdown and
evaluated whether electronic personal dosimeter alarm set-points were in conformance with survey indications and plant policy. For work activities that could suddenly and severely increase radiological conditions, the inspectors assessed the licensee's means to inform workers of changes that could
      startup activities, assessed plant risk, and observed maintenance activities.
significantly impact their occupational dose. b. Findings
      This inspection constituted one Forced Outage sample as defined in IP 71111.20-05.
No findings were identified. .3 Contamination and Radioactive Material Control (02.04) a. Inspection Scope
  b. Findings
The inspectors observed locations where the  
      No findings were identified.
licensee monitors potentially contaminated material leaving the radiological control area and inspected the methods used for control, survey, and release from these areas.  The inspectors observed the  
1R22 Surveillance Testing (71111.22)
performance of personnel surveying and releasing material for unrestricted use and
  a. Inspection Scope
evaluated whether the work was performed in accordance with plant procedures and  
      The inspectors reviewed the test results for the following activities to determine whether
whether the procedures were sufficient to control the spread of contamination and prevent unintended release of radioactive materials from the site.  The inspectors assessed whether the radiation monitoring instrumentation had appropriate sensitivity for the type(s) of radiation present.
      risk-significant systems and equipment were capable of performing their intended safety
33  The inspectors reviewed the licensee's criteria for the survey and release of potentially contaminated material.  The inspectors evaluated whether there was guidance on how to respond to an alarm that indicates the presence of licensed radioactive material. The inspectors reviewed the licensee's procedures and records to verify that the radiation detection instrumentation was used at its typical sensitivity level based on appropriate counting parameters.  The inspectors assessed whether or not the licensee
      function and to verify testing was conducted in accordance with applicable procedural
has established a
      and TS requirements:
de facto "release limit" by altering the instrument's typical sensitivity through such methods as raising the energy discriminator level or locating the instrument in a high-radiation background area. The inspectors selected several sealed sources from the licensee's inventory records and assessed whether the sources were accounted for and verified to be intact. The inspectors evaluated whether any transactions, since the last inspection, involving nationally tracked sources were reported in accordance with 10 CFR 20.2207. b. Findings
      *      1-OHP-4030-108-008R, Unit 1 ECCS Check Valve Test, (IST);
No findings were identified. .4 Radiological Hazards Control and Work Coverage (02.05) a. Inspection Scope
      *      1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);
The inspectors evaluated ambient radiological conditions (e.g., radiation levels or potential radiation levels) during tours of the facility.  The inspectors assessed whether the conditions were consistent with applicable posted surveys, radiation work permits, and worker briefings. The inspectors evaluated the adequacy of radiological controls, such as required surveys, radiation protection job coverage (including audio and visual surveillance for
      *      12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance,
remote job coverage), and contamination controls.  The inspectors evaluated the
              (Ice Condenser Surveillance);
licensee's use of electronic personal dosimeters in high noise areas as high radiation
      *      Unit 1 Control Room Emergency Ventilation Surveillance, 1-EHP-4030-128-229
              (Routine); and
      *      Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine).
      The inspectors observed in-plant activities and reviewed procedures and associated
      records to determine the following:
      *      did preconditioning occur;
      *      the effects of the testing were adequately addressed by control room personnel
              or engineers prior to the commencement of the testing;
      *      acceptance criteria were clearly stated, demonstrated operational readiness, and
              were consistent with the system design basis;
      *      plant equipment calibration was correct, accurate, and properly documented;
      *      as-left setpoints were within required ranges; and the calibration frequency was
              in accordance with TSs, the USAR, procedures, and applicable commitments;
                                                28


area monitoring devices. The inspectors reviewed the application of dosimetry to effectively monitor exposure to personnel in high-radiation work areas with significant dose rate gradients. The inspectors reviewed the following radiation work permits for work within airborne radioactivity areas with the potential for individual worker internal exposures:
    *       measuring and test equipment calibration was current;
* RWP 141100; U1C26 - Refuel Cavity Decontamination Activities; 
    *       test equipment was used within the required range and accuracy; applicable
* RWP 141148; U1C26 - Steam Generator Platform Activities; and
            prerequisites described in the test procedures were satisfied;
* RWP 141145; U1C26 - Valve Maintenance / Repair. For these radiation work permits, the inspectors evaluated airborne radioactive controls and monitoring, including potential for significant airborne levels (e.g., grinding, grit
    *       test frequencies met TS requirements to demonstrate operability and reliability;
blasting, system breaches, entry into tanks, cubicles, and reactor cavities).  The inspectors assessed barrier (e.g., tent or glove box) integrity and temporary high-efficiency particulate air ventilation system operation. 
            tests were performed in accordance with the test procedures and other
34  The inspectors examined the licensee's physical and programmatic controls for highly activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other
            applicable procedures; jumpers and lifted leads were controlled and restored
storage pools.  The inspectors assessed whether appropriate controls (i.e., administrative and physical controls) were in place to preclude inadvertent removal of  
            where used;
these materials from the pool. The inspectors examined the posting and physical controls for selected high radiation areas and very-high radiation areas to verify conformance with the occupational performance indicator. b. Findings
    *      test data and results were accurate, complete, within limits, and valid;
Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure
    *      test equipment was removed after testing;
Inadequacy
    *      where applicable for inservice testing activities, testing was performed in
Introduction:  An NRC identified Green NCV of TS 5.4.1, "Procedures," was identified for inadequate procedures used to verify Locked High Radiation Controls in the Unit 2 Containment.
            accordance with the applicable version of Section XI, American Society of
Description:  On July 24, 2014, the inspector walked down the Unit 2 containment cavity access ladder.  At the time of the walkdown, the access to the cavity was posted LHRA
            Mechanical Engineers code, and reference values were consistent with the
and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot
            system design basis;
high locked gate for access to the permanently installed cavity ladder.  Discussions with Radiation Protection staff had identified that the ladder lock device was not in place in March 2014.  Additionally, it was established that the locking cage was not placed back
    *      where applicable, test results not meeting acceptance criteria were addressed
on the ladder following the refueling outage in October 2013 when the area was  
            with an adequate operability evaluation or the system or component was
conservatively posted as a LHRA as the dose rates in the containment cavity were not in
            declared inoperable;
excess of 1000 millirem per hour at 30 centimeters.  The inspector reviewed Survey Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final Containment Cavity Survey following the last refueling outage.  This survey confirmed that the highest dose in the accessible areas of the cavity were nominally 2400 millirem
    *      where applicable for safety-related instrument control surveillance tests,
per hour on contact, and 500 millirem per hour at 30 centimeters from the source with
            reference setting data were accurately incorporated in the test procedure;
the highest readings in the cavity lift system pit area following the cavity decontamination. These dose rates would not constitute a LHRA (greater than  1000 millirem per hour at 30 centimeters.)  The survey showed that the gate to the cavity ladder was posted as a LHRA. Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access, Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure
    *      where applicable, actual conditions encountering high resistance electrical
guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation
            contacts were such that the intended safety function could still be accomplished;
Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional
    *      prior procedure changes had not provided an opportunity to identify problems
management expectations and a tracking tool for door/gate verifications while used as a field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified a substantial procedural weakness in this guidance in that the Data Sheet apparently did
            encountered during the performance of the surveillance or calibration test;
not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that
    *      equipment was returned to a position or status required to support the
the locked cage/ladder lock to the reactor cavity was in place and locked; a condition
            performance of its safety functions; and
which is necessary to provide reasonable assurance that the area is secured against unauthorized access and cannot be easily circumvented.  A review of the data verified that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity
    *      all problems identified during the testing were appropriately documented and
ladder during weekly LHRA verification from November 2013 through March 2014. The  
            dispositioned in the CAP.
NRC inspectors also reviewed the LHRA and VHRA verification documentation in the
    Documents reviewed are listed in the Attachment to this report.
35  RP station daily logs from November 2013 to March 2014 and the inspectors did not identify any discrepancies noted in the logs associated with in LHRA controls during their
    This inspection constituted two routine surveillance testing samples, one inservice
    testing sample, one ice condenser surveillance, and one containment isolation valve
    sample as defined in IP 71111.22, Sections-02 and-05.
  b. Findings
    No findings were identified.
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
  a. Inspection Scope
    The regional inspectors performed an in-office review of the latest revisions to the
    Emergency Plan and Emergency Plan Implementing Procedures as listed in the
    Attachment to this report.
    The licensee transmitted the Emergency Plan and Emergency Action Level revisions to
    the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,
    Implementing Procedures. The NRC review was not documented in a safety
    evaluation report and did not constitute approval of licensee-generated changes;
    therefore, this revision is subject to future inspection. The specific documents reviewed
    during this inspection are listed in the Attachment to this report.
                                                29


weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action Program documents did not identify a record of the missing ladder lock device or identification of an unlocked LHRA. Therefore the licensee was not aware of the
  This Emergency Action Level and Emergency Plan Change inspection constituted one
deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the
  sample as defined in IP 71114.04-06.
inspectors.  The failure to identify deficient LHRA controls could have the potential failure to identify and report a Performance Indicator (PI) occurrence.
b. Findings
Analysis:  The inspectors determined that there was an inadequacy in the licensee's procedure for identifying a deficient Locked High Radiation Area for the barrier in their weekly locked cage/ladder barrier to the cavity of Unit 2 containment.  The inspectors determined that the procedure did not provide clear directions to assure the Radiation
  Introduction: An Unresolved Item (URI) was identified because additional information is
Protection Technician would verify the required controls for LHRA is a performance  
  required to determine whether a performance deficiency that is more than minor exists
deficiency.  The inspectors determined that the cause of the performance deficiency was
  and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of
reasonably within the licensee's ability to foresee and correct and should have been
  concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the
prevented. The finding was not subject to traditional enforcement since the incident did not have a significant safety consequence, did not impact the NRC's ability to perform its regulatory
  number of Radiation Protection Technicians (RPTs) required to augment the on-shift
function, and was not willful. The inspectors determined that the performance deficiency was more than minor in accordance with IMC 0612, Appendix B, "Issue Screening," because if left uncorrected,
  emergency response organization in 60 minutes of a declared emergency and replaced
the performance deficiency could lead to a more significant safety concern. Specifically, the failure to identify deficient LHRA controls could result in unintentional exposure to high levels of radiation.   The finding was assessed using the Occupational Radiation Safety SDP and was determined to be of very-low safety significance because the problem was not an
  them with a Radiological Assessment Coordinator (RAC) and an Environmental
ALARA planning issue, there were no overexposures nor substantial potential for  
  Assessment Coordinator (EAC).
overexposures given the highest dose rates present in the room, the scope of work, and the licensee's ability to assess dose was not compromised. The inspectors did not identify a corresponding cross-cutting aspect for this performance deficiency.
  Description. During the review, the inspectors identified a change made in Table 1 of
Enforcement:  Technical Specification 5.4.1, "Procedures," requires that written procedures shall be established, implemented and maintained covering the activities
  Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced
referenced in Appendix A of Regulatory Guide 1.33, Revision 2.  Control of Radioactivity procedures, including limiting personnel exposure, are specified in Appendix A. Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate
  the number of 60-minute response RPTs tasked with conducting offsite surveys from
verification in conjunction with Procedural Guidance THG-026, Locked High Radiation Area, and Very-High Radiation Weekly Verification Process did not provide sufficient details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was
  three RPTs to two RPTs and one EAC. The second change reduced the number of
in place and locked; a condition which is necessary to provide reasonable assurance
  60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one
that the area is secured against unauthorized access and cannot be easily
  RPT and one RAC. According the licensees 10 CFR 2014 50.54(q) screening
circumvented. Consequently, weekly, from
  evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and
November 1, 2013, to March 2014 multiple 
  B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and
36  RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure the area against unauthorized access. Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, and the associated Procedural
  B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute
Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification.  Because this violation is of very-low safety significance and it was entered into the licensee's CAP as AR 2014-9001, this violation is being treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.  (NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient
  responders in Revision 19 of the plan in March of 2004. Inspectors review of the
Locked High Radiation Area Controls Due to Procedure Inadequacy) .5 Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06) a. Inspection Scope
  10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had
The inspectors discussed with the radiation protection manager the controls and procedures for high-risk, high radiation areas and very-high radiation areas. The  
  been done for this change. The inspectors reviewed Revision 18 of the E-Plan and the
inspectors discussed methods employed by the licensee to provide stricter control of  
  associated March 21, 2003 licensee request for prior approval for changes to the E-plan
very-high radiation area access as specified in 10 CFR 20.1602, "Control of Access to Very-High Radiation Areas," and Regulatory Guide 8.38, "Control of Access to High and Very-High Radiation Areas of Nuclear Plants."  The inspectors assessed whether any
  that was conducted, approved by the NRC, and implemented in this revision. The NRC
changes to licensee procedures substantially reduce the effectiveness and level of worker protection. The inspectors discussed the controls in place for special areas that have the potential to become very-high radiation areas during certain plant operations with first-line health
  approved change request included specific numbers of RPTs for 60-minute response
physics supervisors (or equivalent positions having backshift health physics oversight authority).  The inspectors assessed whether these plant operations require communication beforehand with the health physics group, so as to allow corresponding
  tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.
timely actions to properly post, control, and monitor the radiation hazards including re-access authorization. The inspectors evaluated licensee controls for very-high radiation areas and areas with the potential to become a very-high radiation areas to ensure that an individual was not able to gain unauthorized access to the very-high radiation areas. b. Findings
  The licensee indicated that the EAC and RAC were not currently qualified RPTs. This
No findings were identified. .6 Radiation Worker Performance (02.07) a. Inspection Scope
  suggests a performance deficiency, due to the appearance of a reduction in
The inspectors observed radiation worker performance with respect to stated radiation protection work requirements.  The inspectors assessed whether workers were aware of
  effectiveness to the licensees E-plan, without prior NRC approval. However, in order to
the radiological conditions in their workplace and the radiation work permit controls/limits in place, and whether their performance reflected the level of radiological hazards present.
  determine if this is a performance deficiency of more than minor significance, additional
37  b. Findings
  information is required to understand if the RAC and EAC positions had equivalent
No findings were identified. .7 Radiation Protection Technician Proficiency (02.08) a. Inspection Scope
  capabilities as the qualified RPTs. The licensee has entered this issue in their
The inspectors observed the performance of the radiation protection technicians with respect to all radiation protection work r
  Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory
equirements.  The inspectors evaluated whether technicians were aware of the radiological conditions in their workplace and the radiation
  actions were taken while their staff gathers additional information, which included
work permit controls/limits, and whether their performance was consistent with their training and qualifications with respect to the radiological hazards and work activities. b. Findings
  requiring two additional qualified RPTs to respond to the Operations Support Center
No findings were identified. .8 Problem Identification and Resolution (02.09) a. Inspection Scope
  within 60 minutes prior to activating the facility in the event of a declared emergency.
The inspectors evaluated whether problems associated with radiation monitoring and exposure control were being identified by the licensee at an appropriate threshold and were properly addressed for resolution in the licensee's Corrective Action Program.  The
  The licensee stated that it will provide the inspectors with additional information within
inspectors assessed the appropriateness of the corrective actions for a selected sample
  30 days of the exit meeting.
of problems documented by the licensee that
  Therefore, a URI was identified pending additional information. Specifically,
involve radiation monitoring and exposure controls.  The inspectors assessed the licensee's process for applying operating
  documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC
experience to their plant. b. Findings
  are equivalent to the RPTs is necessary for the inspectors to determine whether the
No findings were identified. 2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02) The inspection activities supplement t
  performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)
hose documented in NRC Inspection Report 05000315-05000316/2014002 and constitute a partial sample as defined in Inspection
  occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency
Procedure 71124.02-05. .1 Radiation Worker Performance (02.05) a. Inspection Scope
  Responder Staffing Without Prior Approval)
The inspectors observed radiation worker and radiation protection technician performance during work activities being performed in radiation areas, airborne
                                            30
radioactivity areas, or high radiation areas. The inspectors evaluated whether workers
demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work activity scope and tools to be used, workers used ALARA low-dose waiting areas) and whether there were any procedure compliance issues (e.g., workers are not complying
with work activity controls).  The inspectors observed radiation worker performance to assess whether the training and skill level was sufficient with respect to the radiological hazards and the work involved. 
38  b. Findings
No findings were identified. 2RS7 Radiological Environmental Monitoring Program (71124.07) This inspection constituted one complete sample as defined in Inspection Procedure
71124.07-05. .1 Inspection Planning (02.01) a. Inspection Scope
The inspectors reviewed the annual radiological environmental operating reports and the results of any licensee assessments since the last inspection to assess whether the
Radiological Environmental Monitoring Program was implemented in accordance with the Technical Specifications and Offsite Dose Calculation Manual. This review included reported changes to the Offsite Dose Calculation Manual with respect to environmental
monitoring, commitments in terms of sampling locations, monitoring and measurement
frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of
data. The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of environmental monitoring stations. The inspectors reviewed the Final Safety Analysis Report for information regarding the environmental monitoring program and meteorological monitoring instrumentation. The inspectors reviewed quality assurance audit results of the program to assist in choosing inspection "smart samples."  The inspectors also reviewed audits and technical
evaluations performed on the vendor laboratory if used. The inspectors reviewed the annual effluent release report and the 10 CFR Part 61, "Licensing Requirements for Land Disposal of Radioactive Waste," report, to determine if the licensee was sampling, as appropriate, for the predominant and dose-causing radionuclides likely to be released in effluents. b. Findings
No findings were identified. .2 Site Inspection (02.02) a. Inspection Scope
The inspectors walked down select air sampling stations and dosimeter monitoring stations to determine whether they were located as described in the Offsite Dose Calculation Manual and to determine the equipment material condition.  Consistent with smart sampling, the air sampling stations were selected based on the locations with the
highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk significant locations (e.g., those that have the highest potential for public dose impact). 
39  For the air samplers and dosimeters selected, the inspectors reviewed the calibration and maintenance records to evaluate whether they demonstrated adequate operability of
these components. Additionally, the review included the calibration and maintenance
records of select composite water samplers. The inspectors assessed whether the licensee had initiated sampling of other appropriate media upon loss of a required sampling station. The inspectors observed the collection and preparation of environmental samples from different environmental media (e.g., ground and surface water, milk, vegetation, sediment, and soil) as available to determine whether environmental sampling was
representative of the release pathways as specified in the Offsite Dose Calculation Manual and if sampling techniques were in accordance with procedures. Based on direct observation and review of records, the inspectors assessed whether the meteorological instruments were operable, calibrated, and maintained in  
accordance with guidance contained in the Final Safety Analysis Report, NRC Regulatory Guide 1.23, "Meteorological Monitoring Programs for Nuclear Power Plants," and licensee procedures.  The inspectors assessed whether the meteorological data
readout and recording instruments in the control room and, if applicable, at the tower
were operable. The inspectors evaluated whether missed and/or anomalous environmental samples were identified and reported in the annual environmental monitoring report.  The
inspectors selected events that involved a missed sample, inoperable sampler, lost dosimeter, or anomalous measurement to determine if the licensee had identified the cause and had implemented corrective actions. The inspectors reviewed the licensee's
assessment of any positive sample results (i.e., licensed radioactive material detected above the lower limits of detection) and reviewed the associated radioactive effluent release data that was the source of the released material. The inspectors selected structures, systems, or components that involve or could reasonably involve licensed material for which there is a credible mechanism for licensed material to reach ground water, and assessed whether the licensee had implemented a sampling and monitoring program sufficient to detect leakage of these structures, systems, or components to ground water. The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks, spills, and remediation since the previous inspection were retained in a retrievable manner. The inspectors reviewed any significant changes made by the licensee to the Offsite Dose Calculation Manual as the result of changes to the land census, long-term
meteorological conditions (3-year average), or modifications to the sampler stations
since the last inspection.  They reviewed technical justifications for any changed sampling locations to evaluate whether the licensee performed the reviews required to ensure that the changes did not affect its ability to monitor the impacts of radioactive effluent releases on the environment. The inspectors assessed whether the appropriate detection sensitivities with respect to Technical Specifications/Offsite Dose Calculation Manual where used for counting 
40  samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation Manual required lower limits of detection). The inspectors reviewed quality control
charts for maintaining radiation measurement instrument status and actions taken for degrading detector performance. The licensee uses a vendor laboratory to analyze the radiological environmental monitoring program samples so the inspectors reviewed the
results of the vendor's quality control program, including the inter-laboratory comparison, to assess the adequacy of the vendor's program. The inspectors reviewed the results of the licensee's Inter-Laboratory Comparison Program to evaluate the adequacy of environmental sample analyses performed by the licensee.  The inspectors assessed whether the inter-laboratory comparison test included the media/nuclide mix appropriate for the facility.  If applicable, the inspectors reviewed the licensee's determination of any bias to the data and the overall effect on the radiological environmental monitoring program. b. Findings
No findings were identified. .3 Identification and Resolution of Problems (02.03) a. Inspection Scope
The inspectors assessed whether problems associated with the radiological environmental monitoring program were being identified by the licensee at an appropriate threshold and were properly addressed for resolution in the licensee's Corrective Action Program.  Additionally, they assessed the appropriateness of the
corrective actions for a selected sample of problems documented by the licensee that involved the radiological environmental monitoring program. b. Findings
No findings were identified. 4. OTHER ACTIVITIES Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, and Occupational and Public Radiation Safety 4OA1 Performance Indicator Verification (71151) .1 Mitigating Systems Performance
Index - Emergency AC Power System
a. Inspection Scope
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Emergency AC Power System performance
indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the second quarter 2014.  To determine the accuracy of the PI data reported
during those periods, PI definitions and guidance contained in the Nuclear Energy


Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator
2.    RADIATION SAFETY
Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
41  licensee's operator narrative logs, MSPI derivation reports, issue reports, event reports and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to
      The inspection activities supplement those documented in NRC Inspection Report
validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable
      05000315-05000316/2014002 and constitute one complete sample as defined in
NEI guidance. The inspectors also reviewed the licensee's issue report database to  
      Inspection Procedure 71124.01-05.
determine if any problems had been identified with the PI data collected or transmitted
.1  Radiological Hazard Assessment (02.02)
for this indicator and none were identified. Documents reviewed are listed in the  
  a. Inspection Scope
      The inspectors determined whether there have been changes to plant operations since
      the last inspection that may result in a significant new radiological hazard for onsite
      workers or members of the public. The inspectors evaluated whether the licensee
      assessed the potential impact of these changes and has implemented periodic
      monitoring, as appropriate, to detect and quantify the radiological hazard.
      The inspectors reviewed the last two radiological surveys from selected plant areas and
      evaluated whether the thoroughness and frequency of the surveys where appropriate for
      the given radiological hazard.
      The inspectors selected the following radiologically risk significant work activities that
      involved exposure to radiation:
      *      Refuel Cavity Decontamination Activities;
      *      Steam Generator Platform Activities;
      *      Valve Maintenance / Repair;
      *      Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted
              Areas; and
      *      Reactor Pit Very High Radiation Area (VHRA) Downpost Survey.
      For these work activities, the inspectors assessed whether the pre-work surveys
      performed were appropriate to identify and quantify the radiological hazard and to
      establish adequate protective measures. The inspectors evaluated the radiological
      survey program to determine if hazards were properly identified, including the following:
      *      identification of hot particles;
      *      the presence of alpha emitters;
      *      the potential for airborne radioactive materials, including the potential presence
              of transuranics and/or other hard-to-detect radioactive materials (This evaluation
              may include licensee planned entry into non-routinely entered areas subject to
              previous contamination from failed fuel.);
      *      the hazards associated with work activities that could suddenly and severely
              increase radiological conditions and that the licensee has established a means to
              inform workers of changes that could significantly impact their occupational dose;
              and
      *      severe radiation field dose gradients that can result in non-uniform exposures of
              the body.
                                                31


Attachment to this report. Portions of
    The inspectors observed work in potential airborne areas and evaluated whether the air
this inspection activity were credited in NRC Inspection Report 05000315-05000316/2014004. This inspection constituted one MSPI emergency AC power system sample as defined in  
    samples were representative of the breathing air zone. The inspectors evaluated
IP 71151-05. b. Findings
    whether continuous air monitors were located in areas with low background to minimize
No findings were identified. .2 Mitigating Systems Performance Index - High Pressure Injection Systems
    false alarms and were representative of actual work areas. The inspectors evaluated
a. Inspection Scope
    the licensees program for monitoring levels of loose surface contamination in areas of
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating Systems Performance Index - High Pressure Injection Systems performance indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru the third quarter of 2014.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02,
    the plant with the potential for the contamination to become airborne.
"Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 31,
  b. Findings
2013, were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports
    No findings were identified.
for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the
.2   Instructions to Workers (02.03)
previous inspection, and if so, that the change was in accordance with applicable
  a. Inspection Scope
NEI guidance.  The inspectors also reviewed the licensee's issue report database to  
    The inspectors reviewed the following radiation work permits used to access high
determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the
    radiation areas and evaluated the specified work control instructions or control barriers:
Attachment to this report.  Portions of  
    *      RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
this inspection activity were credited in NRC Inspection Report 05000315-05000316/2014004. This inspection constituted one MSPI high pressure injection system sample as defined
    *      RWP 141148; U1C26 - Steam Generator Platform Activities;
in IP 71151-05. b. Findings
    *      RWP 141145; U1C26 - Valve Maintenance / Repair;
No findings were identified.
    *      RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings &
42  .3 Mitigating Systems Performance Index - Heat Removal System
            Plant Restricted Areas; and
a. Inspection Scope
    *      RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey.
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Heat Removal System performance indicator
    For these radiation work permits, the inspectors assessed whether allowable stay times
for  Donald C. Cook Unit 1 and Unit 2 for the period from the
    or permissible dose (including from the intake of radioactive material) for radiologically
third quarter 2013 through the second quarter 2014.  To determine the accuracy of the PI data reported during those
    significant work under each radiation work permit were clearly identified. The inspectors
periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensee's operator narrative logs, issue reports,
    evaluated whether electronic personal dosimeter alarm set-points were in conformance
event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the
    with survey indications and plant policy.
period of July 2013 through June 2014 to validate the accuracy of the submittals.  The
    For work activities that could suddenly and severely increase radiological conditions, the
inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed
    inspectors assessed the licensees means to inform workers of changes that could
the licensee's issue report database to determine if any problems had been identified
    significantly impact their occupational dose.
with the PI data collected or transmitted for this indicator and none were identified. 
  b. Findings
Documents reviewed are listed in the Attachment to this report. Portions of this
    No findings were identified.
inspection activity were credited in NRC Inspection Report
.3   Contamination and Radioactive Material Control (02.04)
  a. Inspection Scope
    The inspectors observed locations where the licensee monitors potentially contaminated
    material leaving the radiological control area and inspected the methods used for
    control, survey, and release from these areas. The inspectors observed the
    performance of personnel surveying and releasing material for unrestricted use and
    evaluated whether the work was performed in accordance with plant procedures and
    whether the procedures were sufficient to control the spread of contamination and
    prevent unintended release of radioactive materials from the site. The inspectors
    assessed whether the radiation monitoring instrumentation had appropriate sensitivity for
    the type(s) of radiation present.
                                              32


05000315-05000316/2014004. This inspection constituted one MSPI heat removal system sample as defined in
    The inspectors reviewed the licensees criteria for the survey and release of potentially
IP 71151-05. b. Findings
    contaminated material. The inspectors evaluated whether there was guidance on how to
No findings were identified. .4 Mitigating Systems Performance Index - Residual Heat Removal System
    respond to an alarm that indicates the presence of licensed radioactive material.
a. Inspection Scope
    The inspectors reviewed the licensees procedures and records to verify that the
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Residual Heat Removal System performance indicator
    radiation detection instrumentation was used at its typical sensitivity level based on
for Donald C. Cook Unit 1 and Unit 2 for the period from the
    appropriate counting parameters. The inspectors assessed whether or not the licensee
third quarter 2013 through the second quarter 2014.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory
    has established a de facto release limit by altering the instruments typical sensitivity
Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were
    through such methods as raising the energy discriminator level or locating the instrument
used. The inspectors reviewed the licensee's operator narrative logs, issue reports,
    in a high-radiation background area.
MSPI derivation reports, event reports and
    The inspectors selected several sealed sources from the licensees inventory records
NRC Integrated Inspection Reports for the period of July 2013 through June 2014
    and assessed whether the sources were accounted for and verified to be intact.
to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the  
    The inspectors evaluated whether any transactions, since the last inspection, involving
change was in accordance with applicable NEI guidance. The inspectors also reviewed
    nationally tracked sources were reported in accordance with 10 CFR 20.2207.
the licensee's issue report database to determine if any problems had been identified
  b. Findings
with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report.  Portions of this inspection activity were credited in NRC Inspection Report
    No findings were identified.
05000315-05000316/2014004. 
.4  Radiological Hazards Control and Work Coverage (02.05)
43  This inspection constituted one MSPI residual heat removal system sample as defined in  
  a. Inspection Scope
IP 71151-05. b. Findings
    The inspectors evaluated ambient radiological conditions (e.g., radiation levels or
No findings were identified. .5 Mitigating Systems Performanc
    potential radiation levels) during tours of the facility. The inspectors assessed whether
e Index - Cooling Water Systems
    the conditions were consistent with applicable posted surveys, radiation work permits,
a. Inspection Scope
    and worker briefings.
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Cooling
    The inspectors evaluated the adequacy of radiological controls, such as required
Water Systems performance indicator
    surveys, radiation protection job coverage (including audio and visual surveillance for
for  Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the 
    remote job coverage), and contamination controls. The inspectors evaluated the
second quarter 2014.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory
    licensees use of electronic personal dosimeters in high noise areas as high radiation
Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used.  The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and  
    area monitoring devices.
NRC Integrated Inspection Reports for the period of July 2013 through June 2014
    The inspectors reviewed the application of dosimetry to effectively monitor exposure to
to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed
    personnel in high-radiation work areas with significant dose rate gradients.
by more than 25 percent in value since the previous inspection, and if so, that the
    The inspectors reviewed the following radiation work permits for work within airborne
change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. 
    radioactivity areas with the potential for individual worker internal exposures:
Documents reviewed are listed in the Attachment to this report. Portions of this
    *      RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
inspection activity were credited in NRC Inspection Report
    *      RWP 141148; U1C26 - Steam Generator Platform Activities; and
05000315-05000316/2014004. This inspection constituted one MSPI cooling water system sample as defined in
    *      RWP 141145; U1C26 - Valve Maintenance / Repair.
IP 71151-05. b. Findings
    For these radiation work permits, the inspectors evaluated airborne radioactive controls
No findings were identified. .6 Reactor Coolant System Leakage
    and monitoring, including potential for significant airborne levels (e.g., grinding, grit
a. Inspection Scope
    blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The
The inspectors sampled licensee submittals for the RCS Leakage performance indicator for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter
    inspectors assessed barrier (e.g., tent or glove box) integrity and temporary
2014.  To determine the accuracy of the PI data reported during those periods, PI
    high-efficiency particulate air ventilation system operation.
definitions and guidance contained in the NEI Document 99-02, "Regulatory
                                                33
Assessment Performance Indicator Guideline," Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensee's operator logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated Inspection Reports for the period of the  
fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the
submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report. 
44  This inspection constituted two RCS leakage samples as defined in IP 71151-05. b. Findings
No findings were identified. .7 Reactor Coolant System Specific Activity
a. Inspection Scope
The inspectors sampled licensee submittals for the RCS specific activity Performance Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third
quarter 2013 through the third quarter 2014.  The inspectors used Performance Indicator
definitions and guidance contained in the Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 2013, to determine the accuracy of the Performance Indicator data reported during those
periods. The inspectors reviewed the licensee's RCS chemistry samples, Technical


Specification requirements, issue reports, event reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the Performance Indicator data collected or transmitted for this indicator and none were
  The inspectors examined the licensees physical and programmatic controls for highly
identified. In addition to record reviews, the inspectors observed a chemistry technician
  activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other
obtain and analyze a RCS sample.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two RCS specific activity samples as defined in IP 71151-05. b. Findings
  storage pools. The inspectors assessed whether appropriate controls (i.e.,
No findings were identified. .8 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
  administrative and physical controls) were in place to preclude inadvertent removal of
Radiological Effluent Occurrences
  these materials from the pool.
a. Inspection Scope
  The inspectors examined the posting and physical controls for selected high radiation
The inspectors sampled licensee submittals for the radiological effluent Technical Specification/Offsite Dose Calculation Manual radiological effluent occurrences
  areas and very-high radiation areas to verify conformance with the occupational
Performance Indicator for the period from the third quarter 2013 through the third quarter
  performance indicator.
2014.  The inspectors used Performance Indicator definitions and guidance contained in  
b. Findings
the Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, dated August 2013, to determine the accuracy of the Performance Indicator data reported during those periods. The inspectors reviewed the  
  Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure
licensee's issue report database and selected individual reports generated since this
  Inadequacy
indicator was last reviewed to identify any potential occurrences such as unmonitored,
  Introduction: An NRC identified Green NCV of TS 5.4.1, Procedures, was identified for
uncontrolled, or improperly calculated effluent releases that may have impacted offsite
  inadequate procedures used to verify Locked High Radiation Controls in the Unit 2
dose.  The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates to determine if indicator results were accurately reported.  The inspectors also reviewed the licensee's methods for
  Containment.
quantifying gaseous and liquid effluents and determining effluent dose.  Documents reviewed are listed in the Attachment to this report. 
  Description: On July 24, 2014, the inspector walked down the Unit 2 containment cavity
45  This inspection constituted one Radiological Effluent Technical Specification/Offsite Dose Calculation Manual radiological effluent occurrences sample as defined in
  access ladder. At the time of the walkdown, the access to the cavity was posted LHRA
IP 71151 05. b. Findings
  and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot
No findings were identified. .9 Occupational Exposure Control Effectiveness
  high locked gate for access to the permanently installed cavity ladder. Discussions with
a. Inspection Scope
  Radiation Protection staff had identified that the ladder lock device was not in place in
The inspectors sampled licensee submittals for the Occupational Exposure Control Effectiveness Performance Indicator for the period from the third quarter 2013 through
  March 2014. Additionally, it was established that the locking cage was not placed back
the third quarter 2014. The inspectors used Performance Indicator definitions and
  on the ladder following the refueling outage in October 2013 when the area was
guidance contained in the Nuclear Energy Institute Document 99-02, "Regulatory
  conservatively posted as a LHRA as the dose rates in the containment cavity were not in
Assessment Performance Indicator Guideline," Revision 7, dated August 2013, to determine the accuracy of the Performance Indicator data reported during those periods. The inspectors reviewed the licensee's assessment of the Performance Indicator for
  excess of 1000 millirem per hour at 30 centimeters. The inspector reviewed Survey
occupational radiation safety to determine if the indicator related data was adequately
  Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final
assessed and reported.  To assess the adequacy of the licensee's Performance
  Containment Cavity Survey following the last refueling outage. This survey confirmed
Indicator data collection and analyses, the inspectors discussed with radiation protection
  that the highest dose in the accessible areas of the cavity were nominally 2400 millirem
staff the scope and breadth of its data review and the results of those reviews. The inspectors independently reviewed electronic personal dosimetry dose rate and accumulated dose alarms and dose reports and the dose assignments for any intakes
  per hour on contact, and 500 millirem per hour at 30 centimeters from the source with
that occurred during the time period reviewed to determine if there were potentially
  the highest readings in the cavity lift system pit area following the cavity
unrecognized occurrences. The inspectors also conducted walkdowns of numerous locked high and very-high radiation area entrances to determine the adequacy of the controls in place for these areas. Documents reviewed are listed in the Attachment to this report. This inspection constituted one occupational exposure control effectiveness sample as defined in IP 71151-05. b. Findings
  decontamination. These dose rates would not constitute a LHRA (greater than
No findings were identified. 4OA2 Identification and Resolution of Problems (71152) Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection .1 Routine Review of Items Entered into the Corrective Action Program
  1000 millirem per hour at 30 centimeters.) The survey showed that the gate to the cavity
a. Inspection Scope
  ladder was posted as a LHRA.
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensee's CAP at an
  Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access,
appropriate threshold, that adequate attention was being given to timely corrective 
  Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure
46  actions, and that adverse trends were identified and addressed. Attributes reviewed included:  identification of the problem was complete and accurate; timeliness was
  guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation
  Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional
  management expectations and a tracking tool for door/gate verifications while used as a
  field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified
  a substantial procedural weakness in this guidance in that the Data Sheet apparently did
  not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that
  the locked cage/ladder lock to the reactor cavity was in place and locked; a condition
  which is necessary to provide reasonable assurance that the area is secured against
  unauthorized access and cannot be easily circumvented. A review of the data verified
  that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity
  ladder during weekly LHRA verification from November 2013 through March 2014. The
  NRC inspectors also reviewed the LHRA and VHRA verification documentation in the
                                              34


commensurate with the safety significance; evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent-of-condition reviews, and previous occurrences reviews were proper and
RP station daily logs from November 2013 to March 2014 and the inspectors did not
adequate; and that the classification, prioritization, focus, and timeliness of corrective
identify any discrepancies noted in the logs associated with in LHRA controls during their
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action
Minor issues entered into the licensee's CAP as a result of the inspectors' observations are included in the Attachment to this report. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples.  Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report. b. Findings
Program documents did not identify a record of the missing ladder lock device or
No findings were identified. .2 Daily Corrective Action Program Reviews
identification of an unlocked LHRA. Therefore the licensee was not aware of the
a. Inspection Scope
deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the
In order to assist with the identification of repetitive equipment failures and specific human performance issues for followup, the inspectors performed a daily screening of items entered into the licensee's CAP.  This review was accomplished through inspection of the station's daily condition report packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples. b. Findings
inspectors. The failure to identify deficient LHRA controls could have the potential failure
No findings were identified. .3 Semiannual Trend Review
to identify and report a Performance Indicator (PI) occurrence.
a. Inspection Scope
Analysis: The inspectors determined that there was an inadequacy in the licensees
The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue.  The inspectors' review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results. The inspectors'
procedure for identifying a deficient Locked High Radiation Area for the barrier in their
review nominally considered the 6-month period of July 2014 through December 2014, although some examples expanded beyond those dates where the scope of the trend
weekly locked cage/ladder barrier to the cavity of Unit 2 containment. The inspectors
warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance 
determined that the procedure did not provide clear directions to assure the Radiation
47  reports, self-assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensee's CAP
Protection Technician would verify the required controls for LHRA is a performance
trending reports.  Corrective actions associated with a sample of the issues identified in
deficiency. The inspectors determined that the cause of the performance deficiency was
the licensee's trending reports were reviewed for adequacy. The inspectors observed some weaknesses in different aspects of the operability determination process.  There were some instances where AR's were written but were not flagged for an operability review.  Some had been already identified by the licensee
reasonably within the licensees ability to foresee and correct and should have been
upon questioning by the inspectors, others had not.  In these cases, the inspectors did
prevented.
not find any instances where equipment should have been called inoperable but was  
The finding was not subject to traditional enforcement since the incident did not have a
not.  The inspectors also found a functionality assessment associated with fire pumps where necessary compensatory measures were not formalized until the inspectors had
significant safety consequence, did not impact the NRCs ability to perform its regulatory
questioned the assessment. During the period of review, there were two NRC identified
function, and was not willful.
findings with identified weaknesses in the operability determination process.  One was
The inspectors determined that the performance deficiency was more than minor in
accordance with IMC 0612, Appendix B, Issue Screening, because if left uncorrected,
the performance deficiency could lead to a more significant safety concern. Specifically,
the failure to identify deficient LHRA controls could result in unintentional exposure to
high levels of radiation.
The finding was assessed using the Occupational Radiation Safety SDP and was
determined to be of very-low safety significance because the problem was not an
ALARA planning issue, there were no overexposures nor substantial potential for
overexposures given the highest dose rates present in the room, the scope of work, and
the licensees ability to assess dose was not compromised.
The inspectors did not identify a corresponding cross-cutting aspect for this performance
deficiency.
Enforcement: Technical Specification 5.4.1, Procedures, requires that written
procedures shall be established, implemented and maintained covering the activities
referenced in Appendix A of Regulatory Guide 1.33, Revision 2. Control of Radioactivity
procedures, including limiting personnel exposure, are specified in Appendix A.
Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and
Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate
verification in conjunction with Procedural Guidance THG-026, Locked High Radiation
Area, and Very-High Radiation Weekly Verification Process did not provide sufficient
details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was
in place and locked; a condition which is necessary to provide reasonable assurance
that the area is secured against unauthorized access and cannot be easily
circumvented. Consequently, weekly, from November 1, 2013, to March 2014 multiple
                                          35


documented in NRC Inspection Report 2014004 and dealt with a failure to provide
    RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure
adequate technical justification for operability of a TDAFW pump with respect to
    the area against unauthorized access.
governor oil levels.  Another issue is documented in Section 1R15 of this report and dealt with, in part, appropriate oil levels for TDAFW bearings.  The inspectors discussed the observations with licensee staff, who agreed with the assessment. The inspectors also observed weaknesses in work planning and execution.  Multiple instances were identified of scheduled work activities that had to be de-conflicted the  
    Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High,
day/week of execution.  In some cases, procedures had to be revised to support work, or
    Locked High, and Very-High Radiation Area Access, and the associated Procedural
post-maintenance test activities changed to appropriately cover the scope of work near
    Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly
time of execution. In some cases, where changes were made or expanded scope encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed to the site) was not updated appropriately.  A finding in Section 1R15 of this report
    Verification. Because this violation is of very-low safety significance and it was entered
documents a case where inadequate planning and execution unexpectedly rendered a
    into the licensees CAP as AR 2014-9001, this violation is being treated as an NCV
diesel fuel oil storage tank inoperable.  Inspectors have discussed the issue with licensee staff, who agreed with the assessment.   This review constituted one semiannual trend inspection sample as defined in 
    consistent with Section 2.3.2 of the NRC Enforcement Policy.
IP 71152-05. b. Findings
    (NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient
No findings were identified. .4 Selected Issue Followup Inspection:  Review of Operator Workarounds
    Locked High Radiation Area Controls Due to Procedure Inadequacy)
a. Inspection Scope
.5  Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06)
The inspectors evaluated the licensee's implementation of their process used to identify, document, track, and resolve operational challenges.  Inspection activities included, but
  a. Inspection Scope
were not limited to, a review of the cumulative effects of the operator workarounds
    The inspectors discussed with the radiation protection manager the controls and
(OWAs) on system availability and the potential for improper operation of the system, for potential impacts on multiple systems, and on the ability of operators to respond to plant
    procedures for high-risk, high radiation areas and very-high radiation areas. The
transients or accidents. The inspectors performed a review of the cumulative effects of OWAs.  The documents listed in the Attachment to this report were reviewed to accomplish the objectives of the inspection procedure. The inspectors reviewed both current and historical operational 
    inspectors discussed methods employed by the licensee to provide stricter control of
48  challenge records to determine whether the licensee was identifying operator challenges at an appropriate threshold, had entered them into their CAP and proposed or
    very-high radiation area access as specified in 10 CFR 20.1602, Control of Access to
implemented appropriate and timely corrective actions which addressed each issue.  Reviews were conducted to determine if any operator challenge could increase the possibility of an Initiating Event, if the challenge was contrary to training, required a
    Very-High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and
change from long-standing operational practices, or created the potential for
    Very-High Radiation Areas of Nuclear Plants. The inspectors assessed whether any
inappropriate compensatory actions. Additionally, all temporary modifications were
    changes to licensee procedures substantially reduce the effectiveness and level of
reviewed to identify any potential effect on the functionality of Mitigating Systems,
    worker protection.
impaired access to equipment, or required equipment uses for which the equipment was not designed.  Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also assessed to identify any potential sources of unidentified operator workarounds. This review constituted one in depth review of a selected issue sample (operator work arounds) as defined in IP 71152-05. b. Findings
    The inspectors discussed the controls in place for special areas that have the potential
No findings were identified. .5 Selected Issue Follow-up Inspection:  Follow-up to Previous NRC Findings
    to become very-high radiation areas during certain plant operations with first-line health
a. Inspection Scope
    physics supervisors (or equivalent positions having backshift health physics oversight
The inspectors selected a sample of previously issued NRC findings to assess the adequacy of licensee corrective actions.  Two instances were identified where the technical issues had been adequately addressed; however, it appeared there were no
    authority). The inspectors assessed whether these plant operations require
corrective actions for underlying performance issues.  In one case, a finding was issued regarding a change in the system pressures at which the fire pumps would automatically start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually
    communication beforehand with the health physics group, so as to allow corresponding
show the new setpoints were acceptable, nothing was done to explore potential breakdowns in the engineering change process or in human performance that allowed the change to occur without the additional reviews being done to begin with.  In another
    timely actions to properly post, control, and monitor the radiation hazards including
example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the
    re-access authorization.
guidance in the operability determination procedure.  Subsequently, the licensee used methods that were acceptable to validate the past operability of Emergency Core
    The inspectors evaluated licensee controls for very-high radiation areas and areas with
Cooling piping when a void was discovered.  However, any underlying issues in human performance or in the operability determination process were not explored at the time. The licensee acknowledged the inspectors' observations. Regarding the finding discussed above for the fire pump starting setpoints, the inspectors also identified that changes had been made to the plant design basis since
    the potential to become a very-high radiation areas to ensure that an individual was not
the licensee's previous corrective actions were completed.  Pursuant to the change to
    able to gain unauthorized access to the very-high radiation areas.
NFPA-805 standards of fire protection, additional sprinklers were added to the required
  b. Findings
Technical Requirements Manual fire suppression systems.  When this occurred, the licensee did not re-review the impacts on the fire pump starting setpoint issue which was the subject of the NRC finding.  Based on inspector questions, the licensee re-instituted
    No findings were identified.
compensatory measures to restore functionality of the fire suppression system pending
.6  Radiation Worker Performance (02.07)
approval of new calculations that will incorporate the new systems and starting setpoints of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire pump surveillance tests in light of the
NRC finding.  The inspectors discovered the 
49  licensee had already identified a discrepancy between the surveillance tests and design requirements and had written an AR in September of 2014.  Basically, a pump could
degrade to a point where it would still pass a surveillance, yet not meet all aspects of the design calculation requirements for the fire suppression system.  The licensee was able to demonstrate the pumps had not degraded to a point outside the design requirements, and was working to resolve the discrepancy between the tests and design requirements. This review constituted one in-depth review of a selected issue sample as defined in
IP 71152-05. 4OA3  Follow-up of Events and Notices of Enforcement Discretion (71153) .1 Dual Unit Trip Caused by Debris Intrusion in the Forebay
   a. Inspection Scope
   a. Inspection Scope
On November 1, 2014, the inspectors responded to the site following a dual unit trip caused by debris intrusion in the forebay
    The inspectors observed radiation worker performance with respect to stated radiation
of the screenhouse.  During the evening of October 31, and early morning of November 1, rough lake conditions and high wind
    protection work requirements. The inspectors assessed whether workers were aware of
mobilized and transported a large mass of sea grass and other debris.  This debris
    the radiological conditions in their workplace and the radiation work permit controls/limits
entered the D.C. Cook intake structure and collected on trash racks and travelling
    in place, and whether their performance reflected the level of radiological hazards
screens in the fore bay.  Prior to the unit shutdown, the licensee monitored forebay
    present.
conditions and took actions to maintain the travelling screens clean.  However, the rate of debris intrusion exceeded the equipment's ability to clean the screens.  As differential pressure increased across the screens, the licensee entered the Degraded Forebay
                                              36
abnormal procedure.  The licensee reduced power in Unit 2 to 50 percent and secured a
circulating water pump.  However, conditions in the fore bay continued to degrade to the
point that the licensee had to manually trip both units.  This action allowed the licensee to secure all circulating water pumps thus protecting the safety-related service water system.  Following the plant trip, the licensee notified the resident inspector who responded to the site.  The inspectors verified licensee actions in the control rooms were consistent with
plant procedures.  In addition, the inspectors focused on performance of safety-related
equipment supplied with service water.  The inspectors concluded that the service water system had not been impacted by the debris intrusion.  As part of the plant shutdown, several plant SSC's did not perform as expected.  For Unit 2, auto transfer between the unit aux
iliary transformer and reserve auxiliary transformer on turbine trip did not occur.  Auto transfer did occur after the licensee manually inserted a generator trip.  The licensee replaced a failed relay associated with  
a turbine stop valve to correct the condition.  In addition, a relay on the unit two reserve
auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee replaced this relay prior to unit startup. On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee throttled flow. Because both MDAFW pumps were operable, the licensee used the MDAFW pumps for steam generator level control.  The inspectors identified a finding as documented in Section 1R15 of this report.  Additionally, on Unit 2, an AFW flow control
valve appeared to not respond to a flow retention signal.  The flow retention circuit acts to prevent excessive flows to the steam
generators from the AFW pumps by throttling 
50  closed flow control valves.  Upon investigation, given instrument tolerances, tests of the circuitry, time delay settings, and actual
measured flow, it was determined the system acted appropriately. In addition, three steam safety valves lifted prior to their nominal set point tolerance band.  In reviewing the condition, the licensee documented that set point surveillances are conducted using a defined set of conditions that allow the safeties to achieve repeatable lift setpoints.  For an installed safety, several factors can influence actual lift
pressure.  These factors include vibration and temperature transients.  As a result, the  
licensee concluded that the valves responded in a fashion consistent with the design of
the valves.  The licensee plans on performing lift tests on the valves during the next
refueling outage to confirm valve operability.  This event follow-up review constituted one sample as defined in IP 71153-05. b. Findings
No findings were identified. 4OA6 Management Meetings
.1 Exit Meeting Summary
On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber and other members of the licensee staff.  The licensee acknowledged the issues
presented.  The inspectors confirmed that none of the potential report input discussed was considered proprietary. .2 Interim Exit Meetings
Interim exits were conducted for:
* The results of the inservice inspection were discussed with site vice president, Mr. J. Gebbie on October 10, 2014;
* The inspection results for the areas of radiological hazard assessment and exposure controls; occupational ALARA planning and controls; and occupational exposure control effectiveness performance indicator verification with 
Mr. J. Gebbie, Site Vice President, on October 17, 2014;
* The inspection results for the area of radiological hazard assessment and exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;
* The inspection results for the areas of radiological environmental monitoring; and RCS specific activity and RETS/ODCM radiological effluent occurrences performance indicator verification with Mr. J. Gebbe, Site Vice President, on
November 7, 2014;
* The results of the inspection of the permanent removal of shield/missile blocks with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff on December 01, 2014; and
* The Annual Review of Emergency Action Level and Emergency Plan Changes with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015. 
51  The inspectors confirmed that none of the potential report input discussed was considered proprietary.  Proprietary material received during the inspection was returned to the licensee.
ATTACHMENT:  SUPPLEMENTAL INFORMATION
  Attachment SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT
Licensee L. Weber, Chief Nuclear Officer J. Gebbie, Site Vice President
L. Baun, Director Performance Assurance
J. Beer, Principal Health Physicist
D. Bronicki, Interim Radiation Protection Manager


R. Hall, ISI Program Owner J. Harner, Environmental Manager G. Hill, Supervisor Nuclear Safety Analysis  
  b. Findings
S. Lies, Vice President Engineering
      No findings were identified.
S. Mitchell, Regulatory Affairs
.7  Radiation Protection Technician Proficiency (02.08)
D. Miller, Health Physicist J. Nimtz, Senior Licensing Activity Coordinator J. Ross, Engineering Director
  a. Inspection Scope
M. Scarpello, Regulatory Affairs Manager
      The inspectors observed the performance of the radiation protection technicians with
P. Schoepf, Nuclear Site Services Director R. Sieber, Emergency Preparedness Manager
      respect to all radiation protection work requirements. The inspectors evaluated whether
Nuclear Regulatory Commission
      technicians were aware of the radiological conditions in their workplace and the radiation
K. Riemer, Chief, Reactor Projects Branch 2 R. Daley, Chief, Engineering Branch 3  
      work permit controls/limits, and whether their performance was consistent with their
B. Dickson, Chief, Health Physics and Incident Response
      training and qualifications with respect to the radiological hazards and work activities.
N. Feliz-Adorno, Reactor Engineer J. Gilliam; Reactor Engineer 
  b. Findings
M. Mitchell, Health Physicist
      No findings were identified.
    
.8  Problem Identification and Resolution (02.09)
  2 LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
  a. Inspection Scope
Opened 05000315/2014005-01 NCV Failure to Identify Conditions Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System (Section 1R15.b(1))  
      The inspectors evaluated whether problems associated with radiation monitoring and
05000315/2014005-02;
      exposure control were being identified by the licensee at an appropriate threshold and
      were properly addressed for resolution in the licensees Corrective Action Program. The
      inspectors assessed the appropriateness of the corrective actions for a selected sample
      of problems documented by the licensee that involve radiation monitoring and exposure
      controls. The inspectors assessed the licensees process for applying operating
      experience to their plant.
  b. Findings
      No findings were identified.
2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)
      The inspection activities supplement those documented in NRC Inspection Report
      05000315-05000316/2014002 and constitute a partial sample as defined in Inspection
      Procedure 71124.02-05.
.1  Radiation Worker Performance (02.05)
  a. Inspection Scope
      The inspectors observed radiation worker and radiation protection technician
      performance during work activities being performed in radiation areas, airborne
      radioactivity areas, or high radiation areas. The inspectors evaluated whether workers
      demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work
      activity scope and tools to be used, workers used ALARA low-dose waiting areas) and
      whether there were any procedure compliance issues (e.g., workers are not complying
      with work activity controls). The inspectors observed radiation worker performance to
      assess whether the training and skill level was sufficient with respect to the radiological
      hazards and the work involved.
                                                37
 
  b. Findings
      No findings were identified.
2RS7 Radiological Environmental Monitoring Program (71124.07)
      This inspection constituted one complete sample as defined in Inspection Procedure
      71124.07-05.
.1  Inspection Planning (02.01)
  a. Inspection Scope
      The inspectors reviewed the annual radiological environmental operating reports and the
      results of any licensee assessments since the last inspection to assess whether the
      Radiological Environmental Monitoring Program was implemented in accordance with
      the Technical Specifications and Offsite Dose Calculation Manual. This review included
      reported changes to the Offsite Dose Calculation Manual with respect to environmental
      monitoring, commitments in terms of sampling locations, monitoring and measurement
      frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of
      data.
      The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of
      environmental monitoring stations.
      The inspectors reviewed the Final Safety Analysis Report for information regarding the
      environmental monitoring program and meteorological monitoring instrumentation.
      The inspectors reviewed quality assurance audit results of the program to assist in
      choosing inspection smart samples. The inspectors also reviewed audits and technical
      evaluations performed on the vendor laboratory if used.
      The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,
      Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if
      the licensee was sampling, as appropriate, for the predominant and dose-causing
      radionuclides likely to be released in effluents.
  b. Findings
      No findings were identified.
.2  Site Inspection (02.02)
  a. Inspection Scope
      The inspectors walked down select air sampling stations and dosimeter monitoring
      stations to determine whether they were located as described in the Offsite Dose
      Calculation Manual and to determine the equipment material condition. Consistent with
      smart sampling, the air sampling stations were selected based on the locations with the
      highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk
      significant locations (e.g., those that have the highest potential for public dose impact).
                                                38
 
For the air samplers and dosimeters selected, the inspectors reviewed the calibration
and maintenance records to evaluate whether they demonstrated adequate operability of
these components. Additionally, the review included the calibration and maintenance
records of select composite water samplers.
The inspectors assessed whether the licensee had initiated sampling of other
appropriate media upon loss of a required sampling station.
The inspectors observed the collection and preparation of environmental samples from
different environmental media (e.g., ground and surface water, milk, vegetation,
sediment, and soil) as available to determine whether environmental sampling was
representative of the release pathways as specified in the Offsite Dose Calculation
Manual and if sampling techniques were in accordance with procedures.
Based on direct observation and review of records, the inspectors assessed whether
the meteorological instruments were operable, calibrated, and maintained in
accordance with guidance contained in the Final Safety Analysis Report, NRC
Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants,
and licensee procedures. The inspectors assessed whether the meteorological data
readout and recording instruments in the control room and, if applicable, at the tower
were operable.
The inspectors evaluated whether missed and/or anomalous environmental samples
were identified and reported in the annual environmental monitoring report. The
inspectors selected events that involved a missed sample, inoperable sampler, lost
dosimeter, or anomalous measurement to determine if the licensee had identified the
cause and had implemented corrective actions. The inspectors reviewed the licensees
assessment of any positive sample results (i.e., licensed radioactive material detected
above the lower limits of detection) and reviewed the associated radioactive effluent
release data that was the source of the released material.
The inspectors selected structures, systems, or components that involve or could
reasonably involve licensed material for which there is a credible mechanism for
licensed material to reach ground water, and assessed whether the licensee had
implemented a sampling and monitoring program sufficient to detect leakage of these
structures, systems, or components to ground water.
The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks,
spills, and remediation since the previous inspection were retained in a retrievable
manner.
The inspectors reviewed any significant changes made by the licensee to the Offsite
Dose Calculation Manual as the result of changes to the land census, long-term
meteorological conditions (3-year average), or modifications to the sampler stations
since the last inspection. They reviewed technical justifications for any changed
sampling locations to evaluate whether the licensee performed the reviews required to
ensure that the changes did not affect its ability to monitor the impacts of radioactive
effluent releases on the environment.
The inspectors assessed whether the appropriate detection sensitivities with respect to
Technical Specifications/Offsite Dose Calculation Manual where used for counting
                                        39
 
      samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation
      Manual required lower limits of detection). The inspectors reviewed quality control
      charts for maintaining radiation measurement instrument status and actions taken for
      degrading detector performance. The licensee uses a vendor laboratory to analyze the
      radiological environmental monitoring program samples so the inspectors reviewed the
      results of the vendors quality control program, including the inter-laboratory comparison,
      to assess the adequacy of the vendors program.
      The inspectors reviewed the results of the licensees Inter-Laboratory Comparison
      Program to evaluate the adequacy of environmental sample analyses performed by the
      licensee. The inspectors assessed whether the inter-laboratory comparison test
      included the media/nuclide mix appropriate for the facility. If applicable, the inspectors
      reviewed the licensees determination of any bias to the data and the overall effect on
      the radiological environmental monitoring program.
  b. Findings
      No findings were identified.
.3  Identification and Resolution of Problems (02.03)
  a. Inspection Scope
      The inspectors assessed whether problems associated with the radiological
      environmental monitoring program were being identified by the licensee at an
      appropriate threshold and were properly addressed for resolution in the licensees
      Corrective Action Program. Additionally, they assessed the appropriateness of the
      corrective actions for a selected sample of problems documented by the licensee that
      involved the radiological environmental monitoring program.
  b. Findings
      No findings were identified.
4.   OTHER ACTIVITIES
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
      Preparedness, and Occupational and Public Radiation Safety
4OA1 Performance Indicator Verification (71151)
.1  Mitigating Systems Performance Index - Emergency AC Power System
  a. Inspection Scope
      In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
      Systems Performance Index (MSPI) - Emergency AC Power System performance
      indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013
      through the second quarter 2014. To determine the accuracy of the PI data reported
      during those periods, PI definitions and guidance contained in the Nuclear Energy
      Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
      Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the
                                                40
 
    licensees operator narrative logs, MSPI derivation reports, issue reports, event reports
    and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
    risk coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable
    NEI guidance. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator and none were identified. Documents reviewed are listed in the
    Attachment to this report. Portions of this inspection activity were credited in NRC
    Inspection Report 05000315-05000316/2014004.
    This inspection constituted one MSPI emergency AC power system sample as defined in
    IP 71151-05.
  b. Findings
    No findings were identified.
.2  Mitigating Systems Performance Index - High Pressure Injection Systems
  a. Inspection Scope
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
    Systems Performance Index - High Pressure Injection Systems performance indicator
    for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru
    the third quarter of 2014. To determine the accuracy of the PI data reported during
    those periods, PI definitions and guidance contained in the NEI Document 99-02,
    Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31,
    2013, were used. The inspectors reviewed the licensees operator narrative logs, issue
    reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports
    for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the
    accuracy of the submittals. The inspectors reviewed the MSPI component risk
    coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable
    NEI guidance. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator and none were identified. Documents reviewed are listed in the
    Attachment to this report. Portions of this inspection activity were credited in NRC
    Inspection Report 05000315-05000316/2014004.
    This inspection constituted one MSPI high pressure injection system sample as defined
    in IP 71151-05.
  b. Findings
    No findings were identified.
                                                41
 
.3   Mitigating Systems Performance Index - Heat Removal System
  a. Inspection Scope
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
    Systems Performance Index - Heat Removal System performance indicator for
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
    second quarter 2014. To determine the accuracy of the PI data reported during those
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
    event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
    by more than 25 percent in value since the previous inspection, and if so, that the
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
    the licensees issue report database to determine if any problems had been identified
    with the PI data collected or transmitted for this indicator and none were identified.
    Documents reviewed are listed in the Attachment to this report. Portions of this
    inspection activity were credited in NRC Inspection Report
    05000315-05000316/2014004.
    This inspection constituted one MSPI heat removal system sample as defined in
    IP 71151-05.
  b. Findings
    No findings were identified.
.4  Mitigating Systems Performance Index - Residual Heat Removal System
  a. Inspection Scope
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
    Systems Performance Index - Residual Heat Removal System performance indicator for
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
    second quarter 2014. To determine the accuracy of the PI data reported during those
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
    MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
    by more than 25 percent in value since the previous inspection, and if so, that the
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
    the licensees issue report database to determine if any problems had been identified
    with the PI data collected or transmitted for this indicator and none were identified.
    Documents reviewed are listed in the Attachment to this report. Portions of this
    inspection activity were credited in NRC Inspection Report
    05000315-05000316/2014004.
                                              42
 
    This inspection constituted one MSPI residual heat removal system sample as defined in
    IP 71151-05.
  b. Findings
    No findings were identified.
.5  Mitigating Systems Performance Index - Cooling Water Systems
  a. Inspection Scope
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
    Systems Performance Index - Cooling Water Systems performance indicator for
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
    second quarter 2014. To determine the accuracy of the PI data reported during those
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
    MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
    by more than 25 percent in value since the previous inspection, and if so, that the
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
    the licensees issue report database to determine if any problems had been identified
    with the PI data collected or transmitted for this indicator and none were identified.
    Documents reviewed are listed in the Attachment to this report. Portions of this
    inspection activity were credited in NRC Inspection Report
    05000315-05000316/2014004.
    This inspection constituted one MSPI cooling water system sample as defined in
    IP 71151-05.
  b. Findings
    No findings were identified.
.6  Reactor Coolant System Leakage
  a. Inspection Scope
    The inspectors sampled licensee submittals for the RCS Leakage performance indicator
    for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter
    2014. To determine the accuracy of the PI data reported during those periods, PI
    definitions and guidance contained in the NEI Document 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
    used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data,
    issue reports, event reports and NRC Integrated Inspection Reports for the period of the
    fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the
    submittals. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator and none were identified. Documents reviewed are listed in the
    Attachment to this report.
                                              43
 
    This inspection constituted two RCS leakage samples as defined in IP 71151-05.
  b. Findings
    No findings were identified.
.7  Reactor Coolant System Specific Activity
  a. Inspection Scope
    The inspectors sampled licensee submittals for the RCS specific activity Performance
    Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third
    quarter 2013 through the third quarter 2014. The inspectors used Performance Indicator
    definitions and guidance contained in the Nuclear Energy Institute Document 99-02,
    Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August
    2013, to determine the accuracy of the Performance Indicator data reported during those
    periods. The inspectors reviewed the licensees RCS chemistry samples, Technical
    Specification requirements, issue reports, event reports, and NRC Integrated Inspection
    Reports to validate the accuracy of the submittals. The inspectors also reviewed the
    licensees issue report database to determine if any problems had been identified with
    the Performance Indicator data collected or transmitted for this indicator and none were
    identified. In addition to record reviews, the inspectors observed a chemistry technician
    obtain and analyze a RCS sample. Documents reviewed are listed in the Attachment to
    this report.
    This inspection constituted two RCS specific activity samples as defined in IP 71151-05.
  b. Findings
    No findings were identified.
.8   Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
    Radiological Effluent Occurrences
  a. Inspection Scope
    The inspectors sampled licensee submittals for the radiological effluent Technical
    Specification/Offsite Dose Calculation Manual radiological effluent occurrences
    Performance Indicator for the period from the third quarter 2013 through the third quarter
    2014. The inspectors used Performance Indicator definitions and guidance contained in
    the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance
    Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the
    Performance Indicator data reported during those periods. The inspectors reviewed the
    licensees issue report database and selected individual reports generated since this
    indicator was last reviewed to identify any potential occurrences such as unmonitored,
    uncontrolled, or improperly calculated effluent releases that may have impacted offsite
    dose. The inspectors reviewed gaseous effluent summary data and the results of
    associated offsite dose calculations for selected dates to determine if indicator results
    were accurately reported. The inspectors also reviewed the licensees methods for
    quantifying gaseous and liquid effluents and determining effluent dose. Documents
    reviewed are listed in the Attachment to this report.
                                              44
 
      This inspection constituted one Radiological Effluent Technical Specification/Offsite
      Dose Calculation Manual radiological effluent occurrences sample as defined in
      IP 71151 05.
  b. Findings
      No findings were identified.
  .9  Occupational Exposure Control Effectiveness
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Occupational Exposure Control
      Effectiveness Performance Indicator for the period from the third quarter 2013 through
      the third quarter 2014. The inspectors used Performance Indicator definitions and
      guidance contained in the Nuclear Energy Institute Document 99-02, Regulatory
      Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to
      determine the accuracy of the Performance Indicator data reported during those periods.
      The inspectors reviewed the licensees assessment of the Performance Indicator for
      occupational radiation safety to determine if the indicator related data was adequately
      assessed and reported. To assess the adequacy of the licensees Performance
      Indicator data collection and analyses, the inspectors discussed with radiation protection
      staff the scope and breadth of its data review and the results of those reviews. The
      inspectors independently reviewed electronic personal dosimetry dose rate and
      accumulated dose alarms and dose reports and the dose assignments for any intakes
      that occurred during the time period reviewed to determine if there were potentially
      unrecognized occurrences. The inspectors also conducted walkdowns of numerous
      locked high and very-high radiation area entrances to determine the adequacy of the
      controls in place for these areas. Documents reviewed are listed in the Attachment to
      this report.
      This inspection constituted one occupational exposure control effectiveness sample as
      defined in IP 71151-05.
  b. Findings
      No findings were identified.
4OA2 Identification and Resolution of Problems (71152)
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
      Physical Protection
  .1  Routine Review of Items Entered into the Corrective Action Program
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify they were being entered into the licensees CAP at an
      appropriate threshold, that adequate attention was being given to timely corrective
                                                45
 
    actions, and that adverse trends were identified and addressed. Attributes reviewed
    included: identification of the problem was complete and accurate; timeliness was
    commensurate with the safety significance; evaluation and disposition of performance
    issues, generic implications, common causes, contributing factors, root causes,
    extent-of-condition reviews, and previous occurrences reviews were proper and
    adequate; and that the classification, prioritization, focus, and timeliness of corrective
    actions were commensurate with safety and sufficient to prevent recurrence of the issue.
    Minor issues entered into the licensees CAP as a result of the inspectors observations
    are included in the Attachment to this report.
    These routine reviews for the identification and resolution of problems did not constitute
    any additional inspection samples. Instead, by procedure they were considered an
    integral part of the inspections performed during the quarter and documented in
    Section 1 of this report.
  b. Findings
    No findings were identified.
.2  Daily Corrective Action Program Reviews
  a. Inspection Scope
    In order to assist with the identification of repetitive equipment failures and specific
    human performance issues for followup, the inspectors performed a daily screening of
    items entered into the licensees CAP. This review was accomplished through
    inspection of the stations daily condition report packages.
    These daily reviews were performed by procedure as part of the inspectors daily plant
    status monitoring activities and, as such, did not constitute any separate inspection
    samples.
  b. Findings
    No findings were identified.
.3  Semiannual Trend Review
  a. Inspection Scope
    The inspectors performed a review of the licensees CAP and associated documents to
    identify trends that could indicate the existence of a more significant safety issue. The
    inspectors review was focused on repetitive equipment issues, but also considered the
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
    licensee trending efforts, and licensee human performance results. The inspectors
    review nominally considered the 6-month period of July 2014 through December 2014,
    although some examples expanded beyond those dates where the scope of the trend
    warranted.
    The review also included issues documented outside the normal CAP in major
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
    problem/challenges lists, system health reports, quality assurance audit/surveillance
                                                46
 
    reports, self-assessment reports, and Maintenance Rule assessments. The inspectors
    compared and contrasted their results with the results contained in the licensees CAP
    trending reports. Corrective actions associated with a sample of the issues identified in
    the licensees trending reports were reviewed for adequacy.
    The inspectors observed some weaknesses in different aspects of the operability
    determination process. There were some instances where ARs were written but were
    not flagged for an operability review. Some had been already identified by the licensee
    upon questioning by the inspectors, others had not. In these cases, the inspectors did
    not find any instances where equipment should have been called inoperable but was
    not. The inspectors also found a functionality assessment associated with fire pumps
    where necessary compensatory measures were not formalized until the inspectors had
    questioned the assessment. During the period of review, there were two NRC identified
    findings with identified weaknesses in the operability determination process. One was
    documented in NRC Inspection Report 2014004 and dealt with a failure to provide
    adequate technical justification for operability of a TDAFW pump with respect to
    governor oil levels. Another issue is documented in Section 1R15 of this report and
    dealt with, in part, appropriate oil levels for TDAFW bearings. The inspectors discussed
    the observations with licensee staff, who agreed with the assessment.
    The inspectors also observed weaknesses in work planning and execution. Multiple
    instances were identified of scheduled work activities that had to be de-conflicted the
    day/week of execution. In some cases, procedures had to be revised to support work, or
    post-maintenance test activities changed to appropriately cover the scope of work near
    time of execution. In some cases, where changes were made or expanded scope
    encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed
    to the site) was not updated appropriately. A finding in Section 1R15 of this report
    documents a case where inadequate planning and execution unexpectedly rendered a
    diesel fuel oil storage tank inoperable. Inspectors have discussed the issue with
    licensee staff, who agreed with the assessment.
    This review constituted one semiannual trend inspection sample as defined in
    IP 71152-05.
  b. Findings
    No findings were identified.
.4  Selected Issue Followup Inspection: Review of Operator Workarounds
  a. Inspection Scope
    The inspectors evaluated the licensees implementation of their process used to identify,
    document, track, and resolve operational challenges. Inspection activities included, but
    were not limited to, a review of the cumulative effects of the operator workarounds
    (OWAs) on system availability and the potential for improper operation of the system, for
    potential impacts on multiple systems, and on the ability of operators to respond to plant
    transients or accidents.
    The inspectors performed a review of the cumulative effects of OWAs. The documents
    listed in the Attachment to this report were reviewed to accomplish the objectives of the
    inspection procedure. The inspectors reviewed both current and historical operational
                                                47


05000316/2014005-02 NCV Unplanned Inoperability of the AB Fuel Oil Storage Tank during Maintenance (Section 1R15.b(2))  
    challenge records to determine whether the licensee was identifying operator challenges
05000315/2014005-03;
    at an appropriate threshold, had entered them into their CAP and proposed or
    implemented appropriate and timely corrective actions which addressed each issue.
    Reviews were conducted to determine if any operator challenge could increase the
    possibility of an Initiating Event, if the challenge was contrary to training, required a
    change from long-standing operational practices, or created the potential for
    inappropriate compensatory actions. Additionally, all temporary modifications were
    reviewed to identify any potential effect on the functionality of Mitigating Systems,
    impaired access to equipment, or required equipment uses for which the equipment was
    not designed. Daily plant and equipment status logs, degraded instrument logs, and
    operator aids or tools being used to compensate for material deficiencies were also
    assessed to identify any potential sources of unidentified operator workarounds.
    This review constituted one in depth review of a selected issue sample (operator work
    arounds) as defined in IP 71152-05.
  b. Findings
    No findings were identified.
.5  Selected Issue Follow-up Inspection: Follow-up to Previous NRC Findings
  a. Inspection Scope
    The inspectors selected a sample of previously issued NRC findings to assess the
    adequacy of licensee corrective actions. Two instances were identified where the
    technical issues had been adequately addressed; however, it appeared there were no
    corrective actions for underlying performance issues. In one case, a finding was issued
    regarding a change in the system pressures at which the fire pumps would automatically
    start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually
    show the new setpoints were acceptable, nothing was done to explore potential
    breakdowns in the engineering change process or in human performance that allowed
    the change to occur without the additional reviews being done to begin with. In another
    example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the
    guidance in the operability determination procedure. Subsequently, the licensee used
    methods that were acceptable to validate the past operability of Emergency Core
    Cooling piping when a void was discovered. However, any underlying issues in human
    performance or in the operability determination process were not explored at the time.
    The licensee acknowledged the inspectors observations.
    Regarding the finding discussed above for the fire pump starting setpoints, the
    inspectors also identified that changes had been made to the plant design basis since
    the licensees previous corrective actions were completed. Pursuant to the change to
    NFPA-805 standards of fire protection, additional sprinklers were added to the required
    Technical Requirements Manual fire suppression systems. When this occurred, the
    licensee did not re-review the impacts on the fire pump starting setpoint issue which was
    the subject of the NRC finding. Based on inspector questions, the licensee re-instituted
    compensatory measures to restore functionality of the fire suppression system pending
    approval of new calculations that will incorporate the new systems and starting setpoints
    of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire
    pump surveillance tests in light of the NRC finding. The inspectors discovered the
                                                48


05000316/2014005-03 NCV Inadequate Review of Radiological Impact of the Removal of the Auxiliary Shield Blocks on the Containment
      licensee had already identified a discrepancy between the surveillance tests and design
Accident Shield Post LBLOCA (Section 1R18) 05000315/2014005-04 NCV Inadvertent Trip of the Unit 1 TDAFW Pump (Section 1R19) 05000315/2014005-05 URI Changes to Minimum 60-Minute Emergency Responder Staffing Without Prior Approval (Section 1EP4)
      requirements and had written an AR in September of 2014. Basically, a pump could
05000315/2014005-06;  
      degrade to a point where it would still pass a surveillance, yet not meet all aspects of the
      design calculation requirements for the fire suppression system. The licensee was able
      to demonstrate the pumps had not degraded to a point outside the design requirements,
      and was working to resolve the discrepancy between the tests and design requirements.
      This review constituted one in-depth review of a selected issue sample as defined in
      IP 71152-05.
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
.1  Dual Unit Trip Caused by Debris Intrusion in the Forebay
  a. Inspection Scope
      On November 1, 2014, the inspectors responded to the site following a dual unit trip
      caused by debris intrusion in the forebay of the screenhouse. During the evening of
      October 31, and early morning of November 1, rough lake conditions and high wind
      mobilized and transported a large mass of sea grass and other debris. This debris
      entered the D.C. Cook intake structure and collected on trash racks and travelling
      screens in the fore bay. Prior to the unit shutdown, the licensee monitored forebay
      conditions and took actions to maintain the travelling screens clean. However, the rate
      of debris intrusion exceeded the equipments ability to clean the screens. As differential
      pressure increased across the screens, the licensee entered the Degraded Forebay
      abnormal procedure. The licensee reduced power in Unit 2 to 50 percent and secured a
      circulating water pump. However, conditions in the fore bay continued to degrade to the
      point that the licensee had to manually trip both units. This action allowed the licensee
      to secure all circulating water pumps thus protecting the safety-related service water
      system.
      Following the plant trip, the licensee notified the resident inspector who responded to the
      site. The inspectors verified licensee actions in the control rooms were consistent with
      plant procedures. In addition, the inspectors focused on performance of safety-related
      equipment supplied with service water. The inspectors concluded that the service water
      system had not been impacted by the debris intrusion.
      As part of the plant shutdown, several plant SSCs did not perform as expected. For
      Unit 2, auto transfer between the unit auxiliary transformer and reserve auxiliary
      transformer on turbine trip did not occur. Auto transfer did occur after the licensee
      manually inserted a generator trip. The licensee replaced a failed relay associated with
      a turbine stop valve to correct the condition. In addition, a relay on the unit two reserve
      auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee
      replaced this relay prior to unit startup.
      On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee
      throttled flow. Because both MDAFW pumps were operable, the licensee used the
      MDAFW pumps for steam generator level control. The inspectors identified a finding as
      documented in Section 1R15 of this report. Additionally, on Unit 2, an AFW flow control
      valve appeared to not respond to a flow retention signal. The flow retention circuit acts
      to prevent excessive flows to the steam generators from the AFW pumps by throttling
                                                49


05000316/2014005-06 NCV Failure To Identify Deficient Locked High Radiation Area
      closed flow control valves. Upon investigation, given instrument tolerances, tests of the
Controls Due To Procedure Inadequacy (Section 2RS1.4)
      circuitry, time delay settings, and actual measured flow, it was determined the system
Closed 05000315/2014005-01 NCV Failure to Identify Conditions Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil
      acted appropriately.
System (Section 1R15.b(1))
      In addition, three steam safety valves lifted prior to their nominal set point tolerance
05000315/2014005-02;  
      band. In reviewing the condition, the licensee documented that set point surveillances
      are conducted using a defined set of conditions that allow the safeties to achieve
      repeatable lift setpoints. For an installed safety, several factors can influence actual lift
      pressure. These factors include vibration and temperature transients. As a result, the
      licensee concluded that the valves responded in a fashion consistent with the design of
      the valves. The licensee plans on performing lift tests on the valves during the next
      refueling outage to confirm valve operability.
      This event follow-up review constituted one sample as defined in IP 71153-05.
  b. Findings
      No findings were identified.
4OA6 Management Meetings
.1   Exit Meeting Summary
      On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber
      and other members of the licensee staff. The licensee acknowledged the issues
      presented. The inspectors confirmed that none of the potential report input discussed
      was considered proprietary.
.2  Interim Exit Meetings
      Interim exits were conducted for:
      *        The results of the inservice inspection were discussed with site vice president,
              Mr. J. Gebbie on October 10, 2014;
      *        The inspection results for the areas of radiological hazard assessment and
              exposure controls; occupational ALARA planning and controls; and occupational
              exposure control effectiveness performance indicator verification with
              Mr. J. Gebbie, Site Vice President, on October 17, 2014;
      *        The inspection results for the area of radiological hazard assessment and
              exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;
      *        The inspection results for the areas of radiological environmental monitoring; and
              RCS specific activity and RETS/ODCM radiological effluent occurrences
              performance indicator verification with Mr. J. Gebbe, Site Vice President, on
              November 7, 2014;
      *        The results of the inspection of the permanent removal of shield/missile blocks
              with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff
              on December 01, 2014; and
      *        The Annual Review of Emergency Action Level and Emergency Plan Changes
              with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015.
                                                50


05000316/2014005-02 NCV Unplanned Inoperability of the AB Fuel Oil Storage Tank during Maintenance (Section 1R15.b(2))
    The inspectors confirmed that none of the potential report input discussed was
05000315/2014005-03;
    considered proprietary. Proprietary material received during the inspection was returned
    to the licensee.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                            51


05000316/2014005-03 NCV Inadequate Review of Radiological Impact of the Removal of the Auxiliary Shield Blocks on the Containment
                                SUPPLEMENTAL INFORMATION
Accident Shield Post LBLOCA (Section 1R18) 05000315/2014005-04 NCV Inadvertent Trip of the Unit 1 TDAFW Pump (Section 1R19)
                                  KEY POINTS OF CONTACT
05000315/2014005-06;  
Licensee
L. Weber, Chief Nuclear Officer
J. Gebbie, Site Vice President
L. Baun, Director Performance Assurance
J. Beer, Principal Health Physicist
D. Bronicki, Interim Radiation Protection Manager
R. Hall, ISI Program Owner
J. Harner, Environmental Manager
G. Hill, Supervisor Nuclear Safety Analysis
S. Lies, Vice President Engineering
S. Mitchell, Regulatory Affairs
D. Miller, Health Physicist
J. Nimtz, Senior Licensing Activity Coordinator
J. Ross, Engineering Director
M. Scarpello, Regulatory Affairs Manager
P. Schoepf, Nuclear Site Services Director
R. Sieber, Emergency Preparedness Manager
Nuclear Regulatory Commission
K. Riemer, Chief, Reactor Projects Branch 2
R. Daley, Chief, Engineering Branch 3
B. Dickson, Chief, Health Physics and Incident Response
N. Feliz-Adorno, Reactor Engineer
J. Gilliam; Reactor Engineer
M. Mitchell, Health Physicist
                                                        Attachment


05000316/2014005-06 NCV Failure To Identify Deficient Locked High Radiation Area  
                LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Controls Due To Procedure Inadequacy (Section 2RS1.4)  
Opened
  Discussed None  
05000315/2014005-01  NCV  Failure to Identify Conditions Adverse to Quality
  3 LIST OF DOCUMENTS REVIEWED The following is a partial list of documents reviewed during the inspection. Inclusion on this list does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
                            associated with the Unit 1 TDAFW Pump Turbine Oil
selected sections or portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
                            System (Section 1R15.b(1))
any part of it, unless this is stated in the body of the inspection report.   1R01 Adverse Weather Protection
05000315/2014005-02;  NCV  Unplanned Inoperability of the AB Fuel Oil Storage Tank
- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21 - 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7 - 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22 - AR-2014-14403, 12-HV-DGH Appears to Have Failed  
05000316/2014005-02        during Maintenance (Section 1R15.b(2))
- Cook Seasonal Readiness Affirmation Letter, November 11, 2014 - PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22 1R04 Equipment Alignment
05000315/2014005-03;  NCV  Inadequate Review of Radiological Impact of the Removal
- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24 - 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4, Revision 14 - AR-2014-14089, CTS Nozzle Leaking - AR-2014-8502, Possible PORV Leakby - Drawing OP-1-5144-51, Containment Spray  
05000316/2014005-03        of the Auxiliary Shield Blocks on the Containment
- Drawing OP-2-5105D-22, Steam Generating System  
                            Accident Shield Post LBLOCA (Section 1R18)
- Drawing OP-2-5106A-55, Aux Feedwater - List of Open Work Orders, Unit 1 Containment Spray System 1R05 Fire Protection
05000315/2014005-04  NCV  Inadvertent Trip of the Unit 1 TDAFW Pump
- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room - AR-2014-12540, Unattended Test Equipment  
                            (Section 1R19)
- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011 - Fire Hazards Analysis, Revision 16 - PMP-2270-CCM-001, Control of Combustible Materials, Revision 24 - PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23  
05000315/2014005-05  URI  Changes to Minimum 60-Minute Emergency Responder
                            Staffing Without Prior Approval (Section 1EP4)
05000315/2014005-06NCV   Failure To Identify Deficient Locked High Radiation Area
05000316/2014005-06        Controls Due To Procedure Inadequacy (Section 2RS1.4)
Closed
  05000315/2014005-01  NCV  Failure to Identify Conditions Adverse to Quality
                            associated with the Unit 1 TDAFW Pump Turbine Oil
                            System (Section 1R15.b(1))
05000315/2014005-02;  NCV  Unplanned Inoperability of the AB Fuel Oil Storage Tank
  05000316/2014005-02        during Maintenance (Section 1R15.b(2))
  05000315/2014005-03; NCV  Inadequate Review of Radiological Impact of the Removal
05000316/2014005-03        of the Auxiliary Shield Blocks on the Containment
                            Accident Shield Post LBLOCA (Section 1R18)
05000315/2014005-04  NCV  Inadvertent Trip of the Unit 1 TDAFW Pump
                            (Section 1R19)
05000315/2014005-06;  NCV  Failure To Identify Deficient Locked High Radiation Area
05000316/2014005-06        Controls Due To Procedure Inadequacy (Section 2RS1.4)
Discussed
None
                                        2
 
                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
selected sections or portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
1R01 Adverse Weather Protection
- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22
- AR-2014-14403, 12-HV-DGH Appears to Have Failed
- Cook Seasonal Readiness Affirmation Letter, November 11, 2014
- PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22
1R04 Equipment Alignment
- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24
- 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4,
  Revision 14
- AR-2014-14089, CTS Nozzle Leaking
- AR-2014-8502, Possible PORV Leakby
- Drawing OP-1-5144-51, Containment Spray
- Drawing OP-2-5105D-22, Steam Generating System
- Drawing OP-2-5106A-55, Aux Feedwater
- List of Open Work Orders, Unit 1 Containment Spray System
1R05 Fire Protection
- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room
- AR-2014-12540, Unattended Test Equipment
- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011
- Fire Hazards Analysis, Revision 16
- PMP-2270-CCM-001, Control of Combustible Materials, Revision 24
- PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23
1R06 Flooding
1R06 Flooding
- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area, April 4, 1971  
- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area,
  April 4, 1971
1R07 Heat Sink Performance
1R07 Heat Sink Performance
- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9 - D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection Program, March 10, 2003 - Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger  
- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9
- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related  
- D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection
Equipment, July 18, 1989
  Program, March 10, 2003
1R08 Inservice Inspection Activities
- Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger
- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5 - 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII, Supplement 10 Dissimilar Metal Welds, Revision 0 - 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6 - 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6 - 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10  
- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related
- AR 2012-12105, Water Pooling Around U2 CST  
  Equipment, July 18, 1989
- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak  
                                                    3
- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak - AR 2013-4625, 1-CS-448-1 has a BA Leak - AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage  
 
- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting  
1R08 Inservice Inspection Activities
- AR 2013-6540, 1-SF-160 Leaking at Diaphragm  
- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5
- AR 2013-6839, U1C25 Refueling Cavity Leakage  
- 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII,
- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet - AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min - AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas  
  Supplement 10 Dissimilar Metal Welds, Revision 0
- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211  
- 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6
- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage  
- 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6
- AR 2013-8587, U1 Seal Table Thimble Leakage Identified - AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm - AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing  
- 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10
- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping  
- AR 2012-12105, Water Pooling Around U2 CST
- AR 2014-11339, Piping Wall Loss Near 1-WCR-942  
- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak
- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance  
- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak
- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum - AR 2014-11519, Two Data Points In Piping Found Below Design Minimum - AR 2014-11664, NESW Pipe Wall Below Manufacturer's Tolerance  
- AR 2013-4625, 1-CS-448-1 has a BA Leak
- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000  
- AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage
- AR 2014-12160, Technician Understanding of Range of Coverage Questioned  
- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting
- AR 2014-12162, NRC Inservice Inspection Observation - AR 2014-1218, AR for Boric Acid Leak Not Properly Screened - AR 2014-12384, NRC Observation During U1 Inservice Inspection  
- AR 2013-6540, 1-SF-160 Leaking at Diaphragm
- AR 2014-3762, Previously Identified BA Leak on 1-SI-128  
- AR 2013-6839, U1C25 Refueling Cavity Leakage
- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014  
- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet
- ETSS No. 1, Bobbin Coil, Revision 0  
- AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min
- ETSS No. 2, 3 Coil MRPC, Revision 0 - LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and Dissimilar Metal Welds, Revision 0 - LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7  
- AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas
- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic Piping Welds, Revision 0 - PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C - PMI-5070, Inservice Inspection, Revision 21  
- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211
- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17  
- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage
- PQR 136, ASME Procedure Qualification Record, Revision 1 - PQR 219, ASME Procedure Qualification Record, Revision 1 - PQR 256, ASME Procedure Qualification Record, Revision 1
- AR 2013-8587, U1 Seal Table Thimble Leakage Identified
- PQR 258, ASME Procedure Qualification Record, Revision 1 - QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3  
- AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm
- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0 - S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site Technique Validation, Revision 0 - U1-MT-14-001, Magnetic Particle Examination, October 4, 2014  
- AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing
- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014  
- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping
- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014  
- AR 2014-11339, Piping Wall Loss Near 1-WCR-942
- U1-VE-14-003, Ultrasonic Examination, October 2, 2014 - U1-VE-14-004, Ultrasonic Examination, October 2, 2014 - U1-VE-14-014, Ultrasonic Examination, October 8, 2014  
- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance
- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0" in Thickness, Revision 2 - WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014 - WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013 - WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012, March 8, 2013 - WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013  
- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum
- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z - WPS 8.12T, Welding Procedure Specification, Revision 1 - WPS 8.1TS, Welding Procedure Specification, Revision 4 1R11 Licensed Operator Requilification Program
- AR 2014-11519, Two Data Points In Piping Found Below Design Minimum
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25 - November 19, 2014, Training Exercise Guide and Drill Guide - PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4  
- AR 2014-11664, NESW Pipe Wall Below Manufacturers Tolerance
- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000
- AR 2014-12160, Technician Understanding of Range of Coverage Questioned
- AR 2014-12162, NRC Inservice Inspection Observation
- AR 2014-1218, AR for Boric Acid Leak Not Properly Screened
- AR 2014-12384, NRC Observation During U1 Inservice Inspection
- AR 2014-3762, Previously Identified BA Leak on 1-SI-128
- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014
- ETSS No. 1, Bobbin Coil, Revision 0
- ETSS No. 2, 3 Coil MRPC, Revision 0
- LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and
  Dissimilar Metal Welds, Revision 0
- LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7
- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic
  Piping Welds, Revision 0
- PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure
  Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C
- PMI-5070, Inservice Inspection, Revision 21
- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17
- PQR 136, ASME Procedure Qualification Record, Revision 1
- PQR 219, ASME Procedure Qualification Record, Revision 1
- PQR 256, ASME Procedure Qualification Record, Revision 1
                                              4
 
- PQR 258, ASME Procedure Qualification Record, Revision 1
- QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3
- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0
- S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site
  Technique Validation, Revision 0
- U1-MT-14-001, Magnetic Particle Examination, October 4, 2014
- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014
- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014
- U1-VE-14-003, Ultrasonic Examination, October 2, 2014
- U1-VE-14-004, Ultrasonic Examination, October 2, 2014
- U1-VE-14-014, Ultrasonic Examination, October 8, 2014
- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0 in Thickness,
  Revision 2
- WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014
- WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013
- WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012,
  March 8, 2013
- WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013
- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z
- WPS 8.12T, Welding Procedure Specification, Revision 1
- WPS 8.1TS, Welding Procedure Specification, Revision 4
1R11 Licensed Operator Requilification Program
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25
- November 19, 2014, Training Exercise Guide and Drill Guide
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4
1R12 Maintenance Effectiveness
- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11
- 2012-2013 AMSAC, Unavailability Hours Reports
- AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown
- AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open
- AR 2012-14364-1, 1-NRI-16 Found Out of Spec
- AR 2012-16048, 1-URV-125 Failed Drop Test
- AR 2012-4275, Steam Dump System Operation
- AR 2013-10252, 1-URV-136 Failed Drop Test
- AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance
- AR 2013-1164, 2-MRV-212 Failed Stroke Time
- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit
- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance
- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral
- AR 2013-4320, 1-URV-110 Failing to Open
- AR 2013-4349, 1-URV-112 Failed to Open When Required
- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D
- AR 2013-5060, 1-URV-111 Would not Stroke During Testing
- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times
- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded
- AR 2014-0045, 2-URV-120 Failed Drop Test
                                                5
 
- AR 2014-11324, Steam Dumps Did Not Operate Per Procedure
- AR 2014-11739, Critical Parameter Found Out of Tolerance
- AR 2014-12621, 1-URV-112 Drop Test Failed
- AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle
- AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25
- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process
- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process
- AR 2014-15004, As Found Data Out of Tolerance
- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement
- AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT
- AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve
- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013
- AR-2013-12121, RPI Failure Rod D8, August 19, 2013
- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013
- AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013
- AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013
- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,
  October 23, 2014
- ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document,
  Revision 1
- GT 2013-11467, U2 MS Maintenance Rule Action Tracking
- GT 2013-11615, 2013 Main Steam System Vulnerability Review
- Maintenance Rule Scoping Document, AMSAC System, Revision 1
- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3
- Maintenance Rule Scoping Document, Main Steam System, Revision 3
- Plant Health Committee Top Ten Equipment Issues, November 19, 2014
- System Health Report, Main Steam, Unit 1 and Unit 2, 3rd Quarter 2014
- Topical Report WCAP-7571, Rod Position Monitoring
- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014
- Various 2012-2013 AMSAC System Health Reports
- Various Operator Logs, October-November 2014
- Various System Health Reports, AMSAC
1R13 Maintenance Risk Assessments and Emergent Work Control
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22
- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18
- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak
- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut
- AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration
- Drawing 2-OP-5113-83, Essential Service Water
- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room
  Coolers, October 23, 2000
- Operating Logs, Week of November 30, 2014
- Part 1 Risk Assessments, Week of November 30, 2014
- PMP-2291-OLR-001, Online Risk Management, Revision 30
- Temporary Modification 2-TM-14-81, AFW Room Coolers
- WO 55457007-07, Install 2-TM-14-81
- WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection
                                              6
 
1R15 Operability Determinations
- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13
- 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves,
  November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System
  Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2
- AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014
- AR-2014-7259, Question from NRC Sr. Resident still not Resolved
- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5
- Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003
- Drawing E-8708, 765kV Schematic, Revision 5
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram
- EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25
- FSAR Section 8.0, Electrical Systems, Revision 25
- FSAR Section 8.3, Station Service Systems, Revision 25
- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003
- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979
1R18 Plant Modifications
- AR 2014-13016, Accident Shield Requirements
- Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources,
  Revision 06
- Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates,
  Revision 03
- Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01
- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including
  Revision 23
- Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal
  Project, Revision 00
- NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2
- PMI-601, Radiation Protection Plan, Revision 20
- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003
- PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment
  Access Hatch, Revision 00
1R19 Post-Maintenance Testing
- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7
- 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8
- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9
- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11
- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8
- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9
- 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32
                                                7
 
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34
- 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3
- 1-OHP-4030-156-017T, TDAFW System Test, Revision 16
- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip
- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted
- AR-2014-14188, Failure in Synch Circuit for 2A7
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5
- Drawing 1-OP-5106A-61, Auxiliary Feedwater
- Drawing E-8708, 765kV Schematic, Revision 5
- Drawing OP-2-5106A-55, Auxiliary Feedwater
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram
- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear
  Power Plants (NCIG-11)
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25
- FSAR Section 8.0, Electrical Systems, Revision 25
- FSAR Section 8.3, Station Service Systems, Revision 25
- Gasket Technical Data Sheets for 1CD EDG Aftercooler
- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems
- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps
- Plant Computer Printouts, AFW system, November 1, 2014
- PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25
- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage
- Terry Turbine Vendor Manual
- WO 55425039-15, Investigate Governor Valve
- WO 55432038-01, Replace 1-CRID-3-INV diodes
- WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay
1R20 Outage Activities
- 12-EHP-4030-002-356, Low Power Physics Tests with Dynamic Rod Worth Measurement,
  Revision 11
- 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System,
  Revision 27
- 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11
- 1-OHP-4021-001-002, Reactor Startup, Revision 52
- 1-OHP-4021-001-003, Power Reduction, Revision 55
- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25
- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4030-127-037, Refueling Surveillance, Revision 20
- 1-OHP-4030-127-041, Refueling Integrity, Revision 25
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20
                                              8
 
- 2-OHP-4021-001-002, Reactor Startup, Revision 51
- 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60
- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24
- AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,
  October 23, 2014
- DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of
  Shutdown Cooling
- Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System
- Forced Outage Schedule, November 4, 2014
- PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4
- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800
- Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed
- Tagout R-CRID-CRD4-0069, 120VAC Control Room
- UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25
- Unit 1 Post Trip Review Report, November 1, 2014 Trip
- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical
  Maintenance Departments
1R22 Surveillance Testing
- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8
- 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance,
  Revision 17-18
- 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16
- 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room
  Emergency Ventilation Surveillance
- AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force
- AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec
- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test
- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low
- AR-2014-12633, N SI Pump Calculated dP high
- AR-2014-12652, South SI Pump dP High Above Action Limit
- DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room
  Air Conditioning System
- Drawing OP-1-5149-48, Control Room Ventilation Unit 1
- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features,
  Revision 15
- Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year
  Interval, Revision 1
- WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014
- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014
- WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014
1EP4 Emergency Action Level and Emergency Plan Changes
- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing
- AR 2014-15685, Potential EP Finding
                                              9
 
- Emergency Plan, Revision 18, 19, 32, 33, 34, and 35
- PMI-2080, Emergency Plan and Implementing Procedures, Revision 18
- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes,
  March 5, 2003
2RS1 Radiological Hazard Assessment and Exposure Controls
- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15
- 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28
- 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34
- 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8
- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36
- 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19
- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6
- 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7
- 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger
  Room and Shot Plan of Elevation 609 E/W Hallway, October 10, 2014
- AR 2013-13969, Electronic Dosimeter Setpoints Often Set Considerably Higher Than Actual or
  Expected Radiological Conditions
- AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High
- AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP
- AR 2014-11975, Dose Alarm
- AR 2014-8964, Rad Worker Deficiency
- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained
  in Process
- AR 2014-9764, A Review of ED Setpoints
- CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013
- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013
- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014
- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23
- PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of
  the Rx Pit, October 16, 2014
- PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19
- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant
  Restricted Areas, Revision 0
- RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0
- RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change
  Modifications and Support Work, Revision 0
- RWP 141123, Install, Remove, Modify Temporary Shielding in Unit-1 Containment, Auxiliary
  Building and Plant Restricted Areas, and ALARA Plan, Revision 0
- RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2
- RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2
- RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0
- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0
- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit,
  October 16, 2014
- SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey
- THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process,
  Revision 14
- Work Order Package 55446099 01, RP Perform Semiannual Source Inventory,
  August 7, 2014
                                              10
 
2RS2 Occupational ALARA Planning and Controls
- ALARA Committee Meeting; A-14-33F; October 15, 2014
- D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014
- Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014
- PMP-6010-ALA-001; ALARA Program - Review of Plant Work Activities; Revision 27
2RS7 Radiological Environmental Monitoring Program
- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2
- 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007
- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010
- 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007
- 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007
- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel
  Calibration, Revision 0
- 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000
- 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009
- 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision
  Software, Revision 002
- 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013
- Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant
  Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013
- AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours
- AR 2013-15116, MET Tower Data Recovery
- AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD
  Collection and Change Out, TLD T-11 Could Not Be Located
- AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours
- AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours
- AR 2014-10063, 12-ELR-400, East Bucket Heater Broken
- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No
  Longer Produce Milk
- AR 2014-13656, Trace Cesium-137 in Broadleaf Sample
- AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24),
  Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental
  Monitoring Program (REMP) Surface Water Samples,
- AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1
  Lost Power for Approximately 39 minutes
- AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental
  Monitoring Program (REMP) Data
- AR 2014-8622, Primary Met Tower Carriage Control Switch
- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6
- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal
  and Radiation Protection System, Revision 25.0
- PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and
  Offsite Dose Calculation Manual, March 1, 2013
- PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24
- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014
                                              11
 
4OA1 Performance Indicator Verification
- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook
  Plant, July, 2013 to September 14, 2014
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly
  Operation Report Data, Reactor Coolant System Specific Activity, Revision 15
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly
  Operating Report Data, Revision 15
4OA2 Identification and Resolution of Problems
- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6
- AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room
- AR 2014-9531, 1-152-CICE4-2A Out of Position
- AR-2012-8187, Adequacy of Past Operability Questioned
- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation
- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411
- AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs
- AR-2014-14920, Racking Interlocks Potential to not Properly Reset
- AR-2014-14951, Primary Coolant Filters Wrong Parts
- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing
- AR-2014-15059, Cable 2-8167G Low Megger Readings
- AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand
- GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014
- Performance Assurance Audit PA-14-07, Operations, August 25, 2014
- Performance Assurance Quarterly Report, April - June 2014
- Performance Assurance Quarterly Report, July - September 2014
- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage,
  November 3, 2014
- Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014
- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014
- Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014
4OA3 Identification and Resolution of Problems
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
- AR 2014-13669 Task 2, Unit 1 Post-trip Report
- AR 2014-13669 Task 3, Unit 2 Post-trip Report
- E-0, Reactor Trip or Safety Injection, Revision 38
- ES-0.1, Reactor Trip Response, Revision 28
- Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report,
  December 22, 2014
                                                12


1R12 Maintenance Effectiveness
                          LIST OF ACRONYMS USED
- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11 - 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11
ADAMS Agencywide Document Access Management System
- 2012-2013 AMSAC, Unavailability Hours Reports - AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown - AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open
AFW   Auxiliary Feedwater
- AR 2012-14364-1, 1-NRI-16 Found Out of Spec
ALARA As-Low-As-Reasonably-Achievable
- AR 2012-16048, 1-URV-125 Failed Drop Test
AMB   Auxiliary Missile Blocks
- AR 2012-4275, Steam Dump System Operation
AR     Action Request
- AR 2013-10252, 1-URV-136 Failed Drop Test - AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance - AR 2013-1164, 2-MRV-212 Failed Stroke Time
ASME   American Society for Mechanical Engineers
- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit
BACC   Boric Acid Corrosion Control
- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance
CAP   Corrective Action Program
- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral - AR 2013-4320, 1-URV-110 Failing to Open - AR 2013-4349, 1-URV-112 Failed to Open When Required
CAQ   Condition Adverse to Quality
- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D
CDF   Core Damage Frequency
- AR 2013-5060, 1-URV-111 Would not Stroke During Testing
CFR   Code of Federal Regulations
- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times
dpm   drops per minute
- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded - AR 2014-0045, 2-URV-120 Failed Drop Test 
EAC   Environmental Assessment Coordinator
6  - AR 2014-11324, Steam Dumps Did Not Operate Per Procedure - AR 2014-11739, Critical Parameter Found Out of Tolerance
EDG   Emergency Diesel Generator
- AR 2014-12621, 1-URV-112 Drop Test Failed - AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle - AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25
EPRI   Electric Power Research Institute
- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process
ET     Eddy Current
- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process
FME   Foreign Material Exclusion
- AR 2014-15004, As Found Data Out of Tolerance
FOST   Fuel Oil Storage Tank
- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement - AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT - AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve
ISI   Inservice Inspection
- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013
LBLOCA Large Break Loss-of-Coolant Accident
- AR-2013-12121, RPI Failure Rod D8, August 19, 2013
LHRA   Locked High Radiation Area
- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013 - AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013 - AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013
LOCA   Loss-of-Coolant Accident
- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013
IMC   Inspection Manual Chapter
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power, October 23, 2014 - ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document, Revision 1 - GT 2013-11467, U2 MS Maintenance Rule Action Tracking
IP     Inspection Procedure
- GT 2013-11615, 2013 Main Steam System Vulnerability Review
IR     Inspection Report
- Maintenance Rule Scoping Document, AMSAC System, Revision 1
LCO   Limiting Condition for Operation
- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3 - Maintenance Rule Scoping Document, Main Steam System, Revision 3 - Plant Health Committee Top Ten Equipment Issues, November 19, 2014
MDAFW Motor-Driven Auxiliary Feedwater
- System Health Report, Main Steam, Unit 1 and Unit 2, 3
MSPI   Mitigating Systems Performance Index
rd Quarter 2014 - Topical Report WCAP-7571, Rod Position Monitoring
NCV   Non- Violation
- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014 - Various 2012-2013 AMSAC System Health Reports - Various Operator Logs, October-November 2014 - Various System Health Reports, AMSAC 1R13 Maintenance Risk Assessments and Emergent Work Control
NDE   Non-destructive Examination
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7 - 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22
NEI   Nuclear Energy Institute
- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18
NRC   U.S. Nuclear Regulatory Commission
- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak
PARS   Publicly Available Records System
- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut - AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration - Drawing 2-OP-5113-83, Essential Service Water
PI     Performance Indicator
- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room
RAC   Radiological Assessment Coordinator
Coolers, October 23, 2000 - Operating Logs, Week of November 30, 2014
RCS   Reactor Coolant System
- Part 1 Risk Assessments, Week of November 30, 2014 - PMP-2291-OLR-001, Online Risk Management, Revision 30 - Temporary Modification 2-TM-14-81, AFW Room Coolers
RG     Regulatory Guide
- WO 55457007-07, Install 2-TM-14-81 - WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection 
RPT   Radiation Protection Technician
7  1R15  Operability Determinations
SDP   Significance Determination Process
- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13 - 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves, November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System
SG     Steam Generator
Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2 - AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown - AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
SRA   Senior Reactor Analyst
- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014
SSC   Structure, System and Component
- AR-2014-7259, Question from NRC Sr. Resident still not Resolved
TDAFW Turbine-Driven Auxiliary Feedwater
- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms - DB-12-AFWS, Auxiliary Feedwater System, Revision 5 - Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003
TS     Technical Specification
- Drawing E-8708, 765kV Schematic, Revision 5
                                        13
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram - EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26 - FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25
- FSAR Section 8.0, Electrical Systems, Revision 25
- FSAR Section 8.3, Station Service Systems, Revision 25
- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003
- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979 1R18 Plant Modifications
- AR 2014-13016, Accident Shield Requirements - Calculation Number RS-C-0046, Doses and Dose
Rates from Post LOCA Airborne Sources, Revision 06 - Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates, Revision 03 - Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01
- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including
Revision 23 - Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal Project, Revision 00 - NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2 - PMI-601, Radiation Protection Plan, Revision 20
- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003 - PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment Access Hatch, Revision 00 1R19 Post-Maintenance Testing
- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7 - 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8
- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9
- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11
- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8
- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9 - 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32 
8  - 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24 - 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34 - 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3 - 1-OHP-4030-156-017T, TDAFW System Test, Revision 16
- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip
- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted - AR-2014-14188, Failure in Synch Circuit for 2A7 - DB-12-AFWS, Auxiliary Feedwater System, Revision 5
- Drawing 1-OP-5106A-61, Auxiliary Feedwater
- Drawing E-8708, 765kV Schematic, Revision 5
- Drawing OP-2-5106A-55, Auxiliary Feedwater - Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram - Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram
- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear
Power Plants (NCIG-11) - FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25 - FSAR Section 8.0, Electrical Systems, Revision 25
- FSAR Section 8.3, Station Service Systems, Revision 25
- Gasket Technical Data Sheets for 1CD EDG Aftercooler
- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems
- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps - Plant Computer Printouts, AFW system, November 1, 2014 - PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25
- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage
- Terry Turbine Vendor Manual
- WO 55425039-15, Investigate Governor Valve - WO 55432038-01, Replace 1-CRID-3-INV diodes - WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay 1R20 Outage Activities
- 12-EHP-4030-002-356, Low Power Physics Tests
with Dynamic Rod Worth Measurement, Revision 11 - 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System, Revision 27 - 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11 - 1-OHP-4021-001-002, Reactor Startup, Revision 52 - 1-OHP-4021-001-003, Power Reduction, Revision 55
- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25
- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24 - 1-OHP-4030-127-037, Refueling Surveillance, Revision 20 - 1-OHP-4030-127-041, Refueling Integrity, Revision 25
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20 
9  - 2-OHP-4021-001-002, Reactor Startup, Revision 51 - 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60
- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24 - AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014 - AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power, October 23, 2014 - DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of Shutdown Cooling - Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System - Forced Outage Schedule, November 4, 2014 - PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4
- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800 - Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed - Tagout R-CRID-CRD4-0069, 120VAC Control Room - UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25
- Unit 1 Post Trip Review Report, November 1, 2014 Trip
- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical Maintenance Departments 1R22 Surveillance Testing
- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8 - 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance, Revision 17-18 - 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16 - 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19 
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance - AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force - AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec
- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test
- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low
- AR-2014-12633, N SI Pump Calculated dP high
- AR-2014-12652, South SI Pump dP High Above Action Limit - DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room
Air Conditioning System - Drawing OP-1-5149-48, Control Room Ventilation Unit 1
- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features, Revision 15 - Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year
Interval, Revision 1 - WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014
- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014 - WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014 1EP4 Emergency Action Level and Emergency Plan Changes
- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing - AR 2014-15685, Potential EP Finding 
10  - Emergency Plan, Revision 18, 19, 32, 33, 34, and 35 - PMI-2080, Emergency Plan and Implementing Procedures, Revision 18
- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes, March 5, 2003 2RS1 Radiological Hazard Assessment and Exposure Controls
- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15 - 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28 - 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34 - 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8
- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36 - 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19
- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6 - 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7 - 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger Room and Shot Plan of Elevation 609' E/W Hallway, October 10, 2014 - AR 2013-13969, Electronic Dosimeter Setpoints
Often Set Considerably Higher Than Actual or Expected Radiological Conditions - AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High - AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP - AR 2014-11975, Dose Alarm
- AR 2014-8964, Rad Worker Deficiency
- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained
in Process - AR 2014-9764, A Review of ED Setpoints - CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013
- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013
- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014
- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23 - PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of the Rx Pit, October 16, 2014 - PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19
- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant Restricted Areas, Revision 0 - RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0 - RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change Modifications and Support Work, Revision 0 - RWP 141123, Install, Remove, Modify Temporary
Shielding in Unit-1 Containment, Auxiliary Building and Plant Restricted Areas, and ALARA Plan, Revision 0 - RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2 - RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2 - RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0
- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0
- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit, 
October 16, 2014 - SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey - THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process, Revision 14 - Work Order Package 55446099 01, RP Perform Semiannual Source Inventory, August 7, 2014 
11  2RS2 Occupational ALARA Planning and Controls
- ALARA Committee Meeting; A-14-33F; October 15, 2014 - D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014 - Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014 - PMP-6010-ALA-001; ALARA Program - Review
of Plant Work Activities; Revision 27 2RS7 Radiological Environmental Monitoring Program
- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2 - 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007
- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010 - 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007 - 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007
- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel Calibration, Revision 0 - 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000 - 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009 - 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision Software, Revision 002 - 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013 - Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013 - AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours
- AR 2013-15116 , MET Tower Data Recovery - AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD Collection and Change Out, TLD T-11 Could Not Be Located - AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours - AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours - AR 2014-10063, 12-ELR-400, East Bucket Heater Broken
- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No
Longer Produce Milk - AR 2014-13656, Trace Cesium-137 in Broadleaf Sample - AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24), Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental
Monitoring Program (REMP) Surface Water Samples, - AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1
Lost Power for Approximately 39 minutes - AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental Monitoring Program (REMP) Data - AR 2014-8622, Primary Met Tower Carriage Control Switch
- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6
- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal and Radiation Protection System, Revision 25.0 - PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and Offsite Dose Calculation Manual, March 1, 2013 - PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24
- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014
   
12  4OA1 Performance Indicator Verification
- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook
Plant, July, 2013 to September 14, 2014 - PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly Operation Report Data, Reactor Coolant System Specific Activity, Revision 15 - PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly
Operating Report Data, Revision 15 4OA2 Identification and Resolution of Problems
- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6 - AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room  - AR 2014-9531, 1-152-CICE4-2A Out of Position
- AR-2012-8187, Adequacy of Past Operability Questioned
- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation
- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411 - AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs - AR-2014-14920, Racking Interlocks Potential to not Properly Reset
- AR-2014-14951, Primary Coolant Filters Wrong Parts
- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing
- AR-2014-15059, Cable 2-8167G Low Megger Readings - AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand - GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014
- Performance Assurance Audit PA-14-07, Operations, August 25, 2014
- Performance Assurance Quarterly Report, April - June 2014
- Performance Assurance Quarterly Report, July - September 2014
- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage, November 3, 2014 - Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014
- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014 - Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014 4OA3 Identification and Resolution of Problems
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7 - AR 2014-13669 Task 2, Unit 1 Post-trip Report
- AR 2014-13669 Task 3, Unit 2 Post-trip Report
- E-0, Reactor Trip or Safety Injection, Revision 38 - ES-0.1, Reactor Trip Response, Revision 28 - Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report, December 22, 2014 
13  LIST OF ACRONYMS USED ADAMS Agencywide Document Access Management System AFW Auxiliary Feedwater  
ALARA As-Low-As-Reasonably-Achievable AMB Auxiliary Missile Blocks  
AR Action Request  
ASME American Society for Mechanical Engineers  
BACC Boric Acid Corrosion Control  
CAP Corrective Action Program CAQ Condition Adverse to Quality CDF Core Damage Frequency  
CFR Code of Federal Regulations  
dpm drops per minute  
EAC Environmental Assessment Coordinator EDG Emergency Diesel Generator EPRI Electric Power Research Institute  
ET Eddy Current
FME Foreign Material Exclusion  
FOST Fuel Oil Storage Tank ISI Inservice Inspection LBLOCA Large Break Loss-of-Coolant Accident  
LHRA Locked High Radiation Area  
LOCA Loss-of-Coolant Accident  
IMC Inspection Manual Chapter  
IP Inspection Procedure IR Inspection Report LCO Limiting Condition for Operation  
MDAFW Motor-Driven Auxiliary Feedwater  
MSPI Mitigating Systems Performance Index  
NCV Non- Violation NDE Non-destructive Examination NEI Nuclear Energy Institute  
NRC U.S. Nuclear Regulatory Commission  
PARS Publicly Available Records System  
PI Performance Indicator  
RAC Radiological Assessment Coordinator RCS Reactor Coolant System RG Regulatory Guide  
RPT Radiation Protection Technician  
SDP Significance Determination Process  
SG Steam Generator SRA Senior Reactor Analyst SSC Structure, System and Component  
TDAFW Turbine-Driven Auxiliary Feedwater TS Technical Specification
 
14  TTV Trip and Throttle Valve UFSAR Updated Final Safety Analysis Report
URI Unresolved Item UT Ultrasonic Test WO Work Order 
  L. Weber -2-
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public
inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
Sincerely,  /RA/  Kenneth Riemer, Chief
Branch 2 Division of Reactor Projects
 
Docket Nos. 50-315; 50-316 License Nos. DPR-58; DPR-74
Enclosure: 
IR 05000315/2014005; 05000316/2014005 w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV
  DISTRIBUTION w/encl
: Kimyata MorganButler
RidsNrrDorlLpl3-1 Resource 
RidsNrrPMDCCook Resource


RidsNrrDirsIrib Resource
TTV  Trip and Throttle Valve
Cynthia Pederson
UFSAR Updated Final Safety Analysis Report
Darrell Roberts
URI  Unresolved Item
Eric Duncan
UT    Ultrasonic Test
WO    Work Order
                                    14


Allan Barker Carole Ariano Linda Linn  
L. Weber                                                                  -2-
DRPIII  
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
DRSIII  
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy
Jim Clay Carmen Olteanu ROPreports.Resource@nrc.gov
of this letter, its enclosure, and your response (if any) will be available electronically for public
 
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)
  ADAMS Accession Number
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
:    Publicly Available  
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
Non-Publicly Available  
(the Public Electronic Reading Room).
Sensitive Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
                                                                          Sincerely,
  OFFICE RIII   RIII-EICS RIII
                                                                          /RA/
  RIII  NAME NS:rj PLougheed for  
                                                                          Kenneth Riemer, Chief
EDuncan KRiemer    DATE 02/09/15 02/09/15 02/10/15  
                                                                          Branch 2
  OFFICIAL RECORD COPY
                                                                          Division of Reactor Projects
Docket Nos. 50-315; 50-316
License Nos. DPR-58; DPR-74
Enclosure:
IR 05000315/2014005; 05000316/2014005
    w/Attachment: Supplemental Information
cc w/encl: Distribution via LISTSERV
DISTRIBUTION w/encl:
Kimyata MorganButler                                                                  Carole Ariano
RidsNrrDorlLpl3-1 Resource                                                            Linda Linn
RidsNrrPMDCCook Resource                                                              DRPIII
RidsNrrDirsIrib Resource                                                              DRSIII
Cynthia Pederson                                                                      Jim Clay
Darrell Roberts                                                                        Carmen Olteanu
Eric Duncan                                                                            ROPreports.Resource@nrc.gov
Allan Barker
ADAMS Accession Number:
    Publicly Available                           Non-Publicly Available                             Sensitive                       Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE             RIII                               RIII-EICS                       RIII                              RIII
  NAME               NS:rj                               PLougheed for                   KRiemer
                                                        EDuncan
DATE               02/09/15                           02/09/15                         02/10/15
                                                          OFFICIAL RECORD COPY
}}
}}

Revision as of 15:49, 31 October 2019

IR 05000315/2014005, 05000316/2014005; on 10/01/2014 - 12/31/2014; Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional Assessments; Plant Modifications; Post Maintenance Testing; Radiological Hazard
ML15042A380
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 02/10/2015
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Weber L
Indiana Michigan Power Co, Nuclear Generation Group
References
IR 2014005
Download: ML15042A380 (69)


See also: IR 05000315/2014005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE RD. SUITE 210

LISLE, IL 60532-4352

February 10, 2015

Mr. Larry Weber

Senior VP and Chief Nuclear Officer

Indiana Michigan Power Company

Nuclear Generation Group

One Cook Place

Bridgman, MI 49106

SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000315/2014005;

05000316/2014005

Dear Mr. Weber:

On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2. The enclosed report

documents the results of this inspection, which were discussed on January 20, 2015, with

yourself and members of your staff.

Based on the results of this inspection, three NRC-identified and two self-revealed findings of

very low safety significance were identified. The findings involved violations of NRC

requirements. However, because of their very low safety significance, and because the issues

were entered into your corrective action program, the NRC is treating the issues as

non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook

Nuclear Power Plant.

L. Weber -2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy

of this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket Nos. 50-315; 50-316

License Nos. DPR-58; DPR-74

Enclosure:

IR 05000315/2014005; 05000316/2014005

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 05000315; 05000316

License Nos: DPR-58; DPR-74

Report No: 05000315/2014005; 05000316/2014005

Licensee: Indiana Michigan Power Company

Facility: Donald C. Cook Nuclear Power Plant, Units 1 and 2

Location: Bridgman, MI

Dates: October 1 through December 31, 2014

Inspectors: J. Ellegood, Senior Resident Inspector

T. Taylor, Resident Inspector

J. Cassidy, Senior Health Physicist

M. Garza, Emergency Response Specialist

T. Go, Health Physicist

J. Lennartz, Project Engineer

M. Mitchell, Health Physicist

M. Phalen, Senior Health Physicist

E. Sanchez Santiago, Reactor Inspector

Approved by: Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 2

REPORT DETAILS ....................................................................................................................... 6

Summary of Plant Status ........................................................................................................... 6

1. REACTOR SAFETY ................................................................................................. 6

1R01 Adverse Weather Protection (71111.01) ............................................................ 6

1R04 Equipment Alignment (71111.04) ....................................................................... 7

1R05 Fire Protection (71111.05) .................................................................................. 8

1R06 Flooding (71111.06) ........................................................................................... 9

1R07 Annual Heat Sink Performance (71111.07) ...................................................... 10

1R08 Inservice Inspection Activities (71111.08P) ...................................................... 10

1R11 Licensed Operator Requalification Program (71111.11) .................................. 13

1R12 Maintenance Effectiveness (71111.12) ............................................................ 15

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15

1R15 Operability Determinations and Functional Assessments (71111.15) .............. 16

1R18 Plant Modifications (71111.18) ......................................................................... 21

1R19 Post-Maintenance Testing (71111.19) ............................................................. 24

1R20 Outage Activities (71111.20) ............................................................................ 27

1R22 Surveillance Testing (71111.22) ....................................................................... 28

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ............... 29

2. RADIATION SAFETY ............................................................................................. 31

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls

(71124.02) ........................................................................................................ 37

2RS7 Radiological Environmental Monitoring Program (71124.07) ........................... 38

4. OTHER ACTIVITIES .............................................................................................. 40

4OA1 Performance Indicator Verification (71151) ...................................................... 40

4OA2 Identification and Resolution of Problems (71152) ........................................... 45

4OA3 Followup of Events and Notices of Enforcement Discretion (71153) ............... 49

4OA6 Management Meetings ..................................................................................... 50

SUPPLEMENTAL INFORMATION ............................................................................................... 1

KEY POINTS OF CONTACT..................................................................................................... 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2

LIST OF DOCUMENTS REVIEWED......................................................................................... 3

LIST OF ACRONYMS USED .................................................................................................. 13

SUMMARY OF FINDINGS

Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;

Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional

Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment

and Exposure Controls.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Three Green findings were identified by the

inspectors. Additionally, there were two Green self-revealed findings. The findings were

considered non-cited violations (NCVs) of NRC regulations. The significance of inspection

findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and

determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects Within the

Cross-Cutting Areas effective date December 4, 2014. All violations of NRC requirements are

dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.

Cornerstone: Mitigating Systems

  • Green. A finding of very low safety significance, with an associated non-cited violation of

10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the

inspectors for the licensees failure to promptly identify and correct a condition adverse

to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW)

pump turbine bearing oil. Specifically, the licensee failed to identify that water was

entering the oil system after leakage had been identified directly above one of the

TDAFW pump turbine bearings. On April 7, 2014, a cooling water leak was identified

above the outboard turbine bearing. The leak was classified as about 1 drop-per-minute

(dpm). On April 11, 2014, the licensee discovered the turbine bearing oil level was

above the maximum mark on an attached sight glass. Several possible reasons were

postulated for the high level (which had been steady in-band for over a year), such as

rising turbine building temperatures and the fact that it was not uncommon for personnel

to do unnecessary oil adds to the machine. Oil was drained out until level returned to

the maximum mark. On May 22, 2014, the licensee again noted oil level to be above the

maximum mark. Oil was drained again, and similar reasons provided for the level

increase. Further, a statement was made that oil level had been steady for the past

month, neglecting the previous high level condition. In parallel, NRC inspectors had

questioned why level was being maintained at the maximum mark when the operator

logs and a sign stated level should be kept at the minimum mark. On May 23, the

licensee decided to drain the oil system; 620 ml of water was found. New oil was added,

and a temporary modification was installed which directed leakage away from the

bearing. The issue was entered into the Corrective Action Program (CAP), and an

apparent cause evaluation later determined the leakage to be the primary intrusion

pathway for the water.

The issue was more-than-minor because it adversely affected the Configuration Control

attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead

to a more significant safety concern. The inspectors assessed the finding for

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significance using IMC 0609, Significance Determination Process. Per Appendix A, the

finding screened as Green, or very low safety significance, in Exhibit 2. Specifically, all

questions were answered no under Section A for findings related to Mitigating

Structures, Systems and Components (SSCs) and Functionality. The inspectors

reviewed the licensees past operability evaluation and concluded that given the

projected amount of water that could be entrained in the oil during operation, along with

the duration of operation assumed in the safety analyses, that operability of the pump

would be maintained. The finding had an associated cross-cutting aspect in the Human

Performance area, specifically, H.11, Challenge the Unknown. Regarding the TDAFW

oil system, the licensee rationalized why the level was increasing without sufficient

investigation given the significance of the system, and did not seek further information

that was readily available regarding appropriate oil levels. (Section 1R15)

  • Green. A finding of very low safety significance, with an associated non-cited violation

of Technical Specification (TS) 5.4, Procedures, was self-revealed when a vacuum was

inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for

surveillance activities. The vacuum caused an indication of lowering level in the tank,

alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement

entry. The licensee was performing work activities in preparation for a leak test of the

FOST. The general sequence of activities should have been a loosening of the vent

filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator

(EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter

so test equipment could be connected to the tank. Due to ambiguous work instruction

steps and activities not being adequately controlled to ensure the proper sequence

occurred, workers first removed the vent filter completely and placed a Foreign Material

Exclusion (FME) bag over the vent. When operators later transferred fuel, a vacuum

was drawn in the tank and level appeared to be going down. Utilizing a manual method

of level measurement (which had also been affected by the vacuum), operators

determined fuel was actually being lost from the tank to the environment. Shortly

thereafter, the bag was found and removed, and level restored to normal (there was no

actual loss of fuel). Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances. Contrary to

these requirements, the FOST surveillance was performed with inadequate instructions

and was not coordinated appropriately. The licensee entered the issue into the CAP and

performed a root cause analysis.

The performance deficiency was more than minor because it adversely impacted the

Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The finding screened as Green, or very

low safety significance, utilizing IMC 0609, Appendix A, The Significance Determination

Process for Findings at Power. Specifically, all questions were answered no under

Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.

The FME bag was installed, which rendered the AB FOST inoperable, for approximately

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. This was less than the TS allowed outage time of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. The finding had

an associated cross-cutting aspect in the human performance area, specifically, H.5,

Work Management. Work activities should be planned, controlled, and executed with

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nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting

aspect, the work was planned and executed with inadequate work instructions. Further,

there was a lack of coordination between a number of work groups and activities

associated with the test. (Section 1R15)

  • Green. A finding of very low safety significance, with an associated non- violation

of TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1

TDAFW pump tripped during an emergent dual-unit shutdown. Both units were taken

offline by operators due to debris intrusion from Lake Michigan into the cooling water

screenhouse. The TDAFW pump started as expected but shutdown after a few minutes

of operation. Investigation by the licensee revealed that a cover for the trip solenoid had

been installed incorrectly. The cover was relatively loose and had been placed near

components involved with the proper latching of the Trip and Throttle valve (TTV) (the

valve which opens to let steam in to turn the pump on). After refuting several possible

causes and running the pump several times for testing, the licensee determined the

likely cause of the trip was the misplaced enclosure, which could have interfered with the

proper latching of the TTV. Technical Specification 5.4, Procedures, states, in part,

that written procedures shall be established, implemented, and maintained covering the

applicable procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33

states, in part, that maintenance that can affect the performance of safety-related

equipment should be properly preplanned and performed in accordance with written

procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to these requirements, the cause of the misplaced enclosure was due to a lack

of detailed instructions regarding the installation and removal of the enclosure. The

enclosure was most recently affected by maintenance performed during the fall 2014

refueling outage. The licensee worked with the vendor and reinstalled the enclosure

correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of

position and corrected. The licensee entered the issue into the CAP.

The performance deficiency was more than minor because it adversely impacted the

Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The inspectors utilized IMC 0609

Appendix A, The Significance Determination Process for Findings at Power, to assess

the significance of the finding. Per Exhibit 2, the finding represented a loss of function

for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time.

Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed

risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since

the last successful surveillance on October 23, 2014. Given the evidence available, this

was the likely opportunity for the conditions to be established to set-up the improper

engagement between the TTV and the trip hook. In the detailed analysis, the finding

screened as Green, or very low safety significance. The finding had an associated

cross-cutting aspect in the area of human performance, specifically, H.8, Procedure

Adherence. During maintenance, work proceeded on the trip enclosure despite a lack of

detailed instructions on the removal/installation of the enclosure. (Section 1R19)

Cornerstone: Barrier Integrity

Criterion 3 Design Control, for the licensees inadequate radiological review of

permanently removing the Auxiliary Missile Blocks (AMBs) from the Unit 1 and Unit 2

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containment accident shields. The finding was determined to be more than minor

because it was associated with the Barrier Integrity Cornerstone attribute of design

control; and adversely affected the cornerstone objective of maintaining radiological

barrier functionality of the safety-related accident shield. Specifically, the failure to

control plant design and adequately evaluate the radiological effects of permanently

removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not

ensure that the accident shield will provide its design function to ensure safe radiation

levels outside the containment building following a maximum design basis accident.

The inspectors evaluated the finding using the Significance Determination Process

(SDP) in accordance with IMC 0609, Significance Determination Process, Attachment

0609.04, Initial Characterization of Findings, dated June 19, 2012. Because the finding

impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

dated June 19, 2012, using Exhibit 3, Barrier Integrity Screening Questions. The

finding screened as very-low safety significance (Green) because the finding only

represented a degradation of the radiological barrier function provided for the Auxiliary

Building. The inspectors determined the cause of this finding did not represent current

licensee performance and, thus, no cross-cutting aspect was assigned. (Section 1R18)

Cornerstone: Occupational Radiation Safety

  • Green. The inspectors identified a finding of very-low safety significance for inadequate

procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with

an associated non- violation of TS 5.4, Procedures. As a result, weekly, from

November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the

Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area

against unauthorized access.

The inspectors determined that the performance deficiency was more than minor

because if left uncorrected the performance deficiency could lead to a more significant

safety concern. Specifically, the failure to identify deficient Locked High Radiation Area

(LHRA) controls could result in unintentional exposure to high levels of radiation. The

finding was determined to be of very-low safety significance because the problem was

not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no

overexposure, nor substantial potential for an overexposure, and the licensees ability to

assess dose was not compromised. The inspectors did not identify a corresponding

cross-cutting aspect for this performance deficiency. The licensee entered the

deficiency in their Corrective Action Program as Action Request (AR) 2014-9001

immediately upon discovery and presentation by the inspectors. (Section 2RS1.1)

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REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period in a refueling outage. On October 29, 2014, the plant was

restored to 100 percent power. On November 1, rough lake conditions generated substantial

amounts of debris that clogged trash racks and travelling screens. The licensee manually

tripped the reactor and maintained the plant in hot standby (Mode 3). On November 8, the

licensee restored the plant to 100 percent power.

Unit 2 began the inspection period at 100 percent power. On November 1, 2014, rough lake

conditions generated substantial amounts of debris that clogged trash racks and travelling

screens. The licensee reduced power to 50 percent to reduce circulating water flow.

Conditions continued to degrade; therefore the licensee manually tripped the reactor. The

licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.

On November 13, the plant was restored to 100 percent power.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed CAP items to verify that the licensee was identifying adverse

weather issues at an appropriate threshold and entering them into their CAP in

accordance with station corrective action procedures. Documents reviewed are listed in

the Attachment to this report. The inspectors reviews focused specifically on the

following plant systems due to their risk significance or susceptibility to cold weather

issues:

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

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.2 Readiness for Impending Adverse Weather ConditionHigh Wind Conditions

a. Inspection Scope

On November 6, 2014, the National Weather Service predicted high winds and rough

lake conditions in the vicinity of the plant. Since debris intrusion during similar conditions

the previous week had resulted in damage to equipment and a dual unit plant trip, the

inspectors validated the sites readiness for the adverse weather. The inspectors

reviewed the licensees overall preparations/protection for the expected weather

conditions. The inspectors walked down the service water screen house to assess the

licensee progress on repairing trash racks and traveling water screens. The inspectors

evaluated the licensee staffs preparations against the sites procedures and determined

that the staffs actions were adequate. During the inspection, the inspectors focused on

actions taken to minimize debris intrusion and operators preparations to address

degradation of raw water systems. The inspectors also reviewed a sample of CAP items

to verify that the licensee identified adverse weather issues at an appropriate threshold

and disposed them through the CAP in accordance with station corrective action

procedures. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

on other power-operated relief valves; and

  • Unit 2 AFW during maintenance on a single train.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

7

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted three partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings were identified.

.2 Semiannual Complete System Walkdown

a. Inspection Scope

On December 30, 2014, the inspectors completed a complete system alignment

inspection of the Unit 1 Containment Spray system to verify the functional capability of

the system. This system was selected because it was considered both safety significant

and risk significant in the licensees probabilistic risk assessment. The inspectors

walked down the system to review mechanical and electrical equipment lineups;

electrical power availability; system pressure and temperature indications, as

appropriate; component labeling; component lubrication; component and equipment

cooling; hangers and supports; operability of support systems; and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding WOs was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. Documents reviewed are listed in the

Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Unit 2 Quadrant cable tunnels; and

8

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources

within the plant, effectively maintained fire detection and suppression capability,

maintained passive fire protection features in good material condition, and implemented

adequate compensatory measures for out-of-service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flooding (71111.06)

.1 Underground Vaults

a. Inspection Scope

The inspectors selected underground bunkers/manholes subject to flooding that

contained cables whose failure could disable risk-significant equipment. The inspectors

determined that the cables were not submerged, that splices were intact, and that

appropriate cable support structures were in place. In those areas where dewatering

devices were used, such as a sump pump, the device was operable and level alarm

circuits were set appropriately to ensure that the cables would not be submerged. In

those areas without dewatering devices, the inspectors verified that drainage of the area

was available, or that the cables were qualified for submergence conditions. The

inspectors also reviewed the licensees corrective action documents with respect to past

submerged cable issues identified in the corrective action program to verify the

adequacy of the corrective actions. The inspectors performed a walkdown of the

following underground bunkers/manholes subject to flooding:

  • Bunkers/manholes containing security cabling; and
  • Bunkers/manholes with safety-related cabling supporting technical specification

offsite power sources

Specific documents reviewed during this inspection are listed in the Attachment to this

report. This inspection constituted one underground vaults sample as defined in

IP 71111.06-05.

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b. Findings

No findings were identified.

1R07 Annual Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed the licensees inspection of Unit 1 CD EDG north air aftercooler

to verify that potential deficiencies did not mask the licensees ability to detect degraded

performance, to identify any common cause issues that had the potential to increase

risk, and to ensure that the licensee was adequately addressing problems that could

result in initiating events that would cause an increase in risk. The inspectors observed

licensee visual observations of the internals of the heat exchanger to verify cleanliness

of the heat exchanger. Additionally, the inspectors reviewed eddy current testing results

and interviewed heat exchanger program engineers. Documents reviewed for this

inspection are listed in the Attachment to this document.

This annual heat sink performance inspection constituted one sample as defined in

IP 71111.07-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08P)

From September 29, 2014, through October 10, 2014, the inspector conducted a review

of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring

degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,

Emergency Feedwater Systems, Risk Significant Piping and Components, and

Containment Systems.

The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5

below constituted one inservice inspection sample as defined in IP 71111.08-05.

.1 Piping Systems Inservice Inspection

a. Inspection Scope

The inspectors observed and reviewed records of the following non-destructive

examinations (NDE) mandated by the American Society of Mechanical Engineers

(ASME)Section XI Code to evaluate compliance with the ASME Code Section XI

and Section V requirements, and if any indications and defects were detected, to

determine whether these were dispositioned in accordance with the ASME Code or an

NRC-approved alternative requirement:

  • Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to

elbow weld, 1-FW-12-02S;

  • UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius;

6-1-RC-7-IRS;

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  • UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;

4-1-RC-10-IRS; and

  • Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel

Support; 1-PRZ-26.

There were no recordable indications identified during the previous refueling outage.

The inspectors reviewed NDE records associated with the following pressure boundary

welds completed for risk significant components during the current refueling outage to

determine whether the licensee applied the pre-service NDE and acceptance criteria

required by the Construction Code and ASME Code,Section XI. Additionally, the

inspectors reviewed the welding procedure specification and supporting weld procedure

qualification records to determine whether the weld procedure was qualified in

accordance with the requirements of Construction Code and the ASME Code Section IX:

  • Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314

(Work Order 55440759-5); and

  • Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work

Order 55390312-01)

The inspectors also reviewed NDE records associated with the following pressure

boundary welds completed for risk significant systems since the beginning of the last

refueling:

  • Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve

1-NFP-222-V2 (Work Order 55421212-10/13); and

  • Welds OW-1 associated with the installation of pipe support 1-ARC-S4012

(WO Order 55404504-06).

b. Findings

No findings were identified.

.2 Reactor Pressure Vessel Upper Head Penetration Inspection Activities

a. Inspection Scope

For the Unit 1 reactor vessel head, no examination was required pursuant to

10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review

was completed for this inspection procedure attribute.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control (BACC)

a. Inspection Scope

The inspectors observed the licensees BACC visual examinations for portions of the

RCS, connected systems, and verified whether these visual examinations emphasized

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locations where boric acid leaks can cause degradation of safety significant

components.

The inspectors reviewed the following licensee evaluations of RCS components with

Boric Acid deposits to determine whether degraded components were documented in

the corrective action system. The inspectors also evaluated corrective actions for any

degraded RCS components to determine whether they met the component Construction

Code, ASME Section XI Code, and/or NRC approved alternative:

  • AR 2013-4317; 1-QRV-114, body to bonnet leak;
  • AR 2013-4625;1-CS-448-1 has a BA leak;
  • AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;
  • AR 2013-6839; U1C25 Refueling Cavity Leakage; and

The inspectors reviewed the following corrective actions related to evidence of

BA leakage to determine whether the corrective actions completed were consistent with

the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,

Criterion XVI:

  • AR 2013-0534; 12-CS-185 has a body to bonnet leak;
  • AR 2013-7220; Reactor Head and Pressure Vent Piping Area;
  • AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and
  • AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min.

b. Findings

No findings were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data

analysts, and reviewed documentation related to the SG ISI Program to determine

whether:

  • the numbers and sizes of SG tube flaws/degradation identified was consistent

with the licensees previous outage Operational Assessment predictions;

  • the SG tube ET examination scope and expansion criteria were sufficient to meet

the Technical Specifications, and the Electric Power Research Institute (EPRI)

Document 1013706, Pressurized Water Reactor Steam Generator Examination

Guidelines;

  • the SG tube ET examination scope included potential areas of tube degradation

identified in prior outage SG tube inspections and/or as identified in NRC generic

industry operating experience applicable to these SG tubes;

  • the licensee-identified new tube degradation mechanisms and implemented

adequate extent of condition inspection scope and repairs for the new tube

degradation mechanism;

  • the licensee implemented qualified depth sizing methods to degraded tubes

accepted for continued service;

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  • the ET probes and equipment configurations used to acquire data from the SG

tubes were qualified to detect the known/expected types of SG tube degradation

in accordance with Appendix H, Performance Demonstration for Eddy Current

Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam

Generator Examination Guidelines;

  • the licensee performed secondary side SG inspections for location and removal

of foreign materials;

  • The licensee implemented repairs for SG tubes damaged by foreign material;

and

  • Foreign objects were left within the secondary side of the SGs, and if so, that the

licensee implemented evaluations, which included the effects of foreign object

migration and/or tube fretting damage.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems entered into the licensees

CAP and conducted interviews with licensee staff to determine whether:

  • the licensee had established an appropriate threshold for identifying ISI-related

problems;

  • the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

  • the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On November 19, 2014, the inspectors observed a crew of licensed operators in the

plants simulator during licensed operator requalification training to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;

13

  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

simulator sample as defined in IP 71111.11

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)

a. Inspection Scope

On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the

RCS during the Unit 1 refueling outage. This was a high-risk (Orange) activity planned

during the outage. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms (if applicable);
  • correct use and implementation of procedures;
  • control board (or equipment) manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications (if applicable).

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11, and was done in conjunction with the requirements of

IP 71111.20.

14

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

  • Nuclear Instrumentation;
  • Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and
  • Rod Position Indication

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for SSCs/functions classified as (a)(2),

or appropriate and adequate goals and corrective actions for systems classified

as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Rough lake conditions during emergent trash rack work;

room ventilation unit

15

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed during this inspection are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

three samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • Water intrusion into the Unit 1 TDAFW turbine bearings;
  • Inability to make new ice during the Unit 1 refueling outage;
  • Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;
  • Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and

failure of automatic generator trip during dual-unit trip; and

  • Leakby on a Unit 2 AFW flow control valve.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted seven samples as defined in IP 71111.15-05.

16

b. Findings

(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW

Pump Turbine Oil System

Introduction: A finding of very low safety significance (Green) with an associated NCV of

10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the

inspectors for the licensees failure to promptly identify and correct a CAQ associated

with Unit 1 TDAFW pump turbine bearing oil. Specifically, the licensee failed to identify

that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage

had been identified directly above one of the TDAFW pump turbine bearings.

Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1

TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.

An AR was written (AR 2014-4473) which determined that due to the leak rate and the

apparent lack of any equipment impacts, there were no operability concerns. On

April 11, 2014, the licensee discovered that the turbine bearing oil level was

approximately 0.5 inches above the MAXIMUM mark on the sight glass. Level had been

recorded in the logs as being within band for over a year without any prior evidence of

high level. Additionally, there were no evolutions that had been performed which would

explain the high level. The licensee generated AR 2014-4684 to document this

condition. The AR documented several possible reasons for the unexplained level rise.

One was that turbine building temperature had gone up. Another was that it was not

uncommon for personnel to unnecessarily add oil to the machine from time to time. No

other information was provided to validate either potential cause. Additionally, there was

no mention of the leak identified above one of the turbine bearings four days prior. No

formal monitoring plan was established. An action was created to sample the oil for

water, but as of six weeks later, a work order had not been finalized and scheduled.

The only other action was a lessons-learned that was created for Mechanical

Maintenance department regarding unnecessary oil adds. The response to the action

from the group was that they dont typically do oil adds, but that they discussed the topic

anyway. The inspectors reviewed reference information with respect to oil levels and

their importance to machine operability. According to the vendor manual, EPRI

guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is

extremely critical in the turbine bearing pedestals. The references all concluded that oil

level above the MAXIMUM mark could lead to oil frothing, which could affect stable

operation of the turbine and loss of oil from the system. Further, the references, along

with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM

mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was

over-filled to the MAXIMUM mark. No further information was provided on why this

occurred or why it was acceptable to stay at the MAXIMUM mark. One quart of oil was

drained from the turbine bearing pedestals, bringing the level back to near the

MAXIMUM mark. Approximately five weeks later, an NRC inspector touring the plant

questioned why level was near the MAXIMUM mark given a placard near the sight glass

said to keep level at the MINIMUM mark (which aligned with the references above).

The licensee generated an AR (2014-6315) about one week later on May 22 when the

inspector asked about the condition again. In the AR, they documented the NRC

observation and also the fact that an operator had noted level to be above the

MAXIMUM mark by approximately 0.25 inches. Oil was again drained from the

machine, this time to right above the MINIMUM mark. The operability assessment

(which was not documented until the following day), stated that at time of discovery, the

17

machine was operable because of oil level not affecting operability of the turbine and a

history of overfilling that sometimes required draining of the oil. Further, a statement

was made that there had been a consistent oil level trend for the past month. Again,

the leakage above the bearing was not discussed. There was no discussion of the

previous high-level condition from April 11. On May 23, the licensee decided to

completely drain the oil and sample it for water; 620 ml of water was found in the 2.5

gallon system. New oil was added, and an apparent cause evaluation was performed.

The evaluation concluded that leakage above the bearing housing (documented

originally in AR 2014-4473), combined with a small casing steam leak that condensed

above the housing while the machine was in operation, caused the water intrusion in the

bearing oil. Later evaluation determined the leak rate from the pipe had increased to

8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources

were diverted away from the bearing housing with a temporary modification pending

repairs (which were completed in the September-October 2014 refueling outage).

Based on the above, the inspectors concluded the licensee had sufficient information to

promptly identify and correct water intrusion into the TDAFW turbine bearing oil system

on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential

operability impacts (as described in the multiple references above) on April 11 and

May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-

related oil systems is a CAQ.

Analysis: The failure to promptly identify and correct a CAQ, as required by

10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the

TDAFW turbine oil system was an issue warranting further review in the SDP. Per

IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the issue was

more-than-minor because it adversely affected the Configuration Control attribute of the

Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Additionally, if left uncorrected, the issue could lead to a more significant

safety concern. Specifically, not recognizing water intrusion into safety-related oil

systems can impact operability and affect how safety equipment operates.

The inspectors assessed the finding for significance using IMC 0609, Significance

Determination Process, issued June 2, 2012. Per Appendix A, The Significance

Determination Process (SDP) for Findings-at-Power, issued June 19, 2012, the finding

screened as Green, or very low safety significance, in Exhibit 2. Specifically, all

questions were answered no under Section A for findings related to Mitigating SSCs

and Functionality. The inspectors reviewed the licensees past operability evaluation

and concluded that given the projected amount of water that could be entrained in the oil

during operation, along with the duration of operation assumed in the safety analyses,

that operability of the pump would be maintained.

The inspectors determined the finding had an associated cross-cutting aspect in the

Human Performance area, specifically, H.11, Challenge the Unknown. Some of the

tenets of H.11, as described in NUREG-2165, Safety Culture Common Language

Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency

and continuously challenge existing conditions in order to identify discrepancies that

might result in error or inappropriate action. Further, it states that individuals challenge

unanticipated results rather than rationalize them, and that abnormal indications are not

attributed to indication problems. Regarding the TDAFW oil system, the licensee

rationalized why the level was increasing without sufficient investigation given the

18

significance of the system, and did not seek further information that was readily available

regarding appropriate oil levels.

Enforcement: 10 CFR Part 50, Appendix B, Criterion 16, Corrective Action, requires, in

part, that conditions adverse to quality, such as deficiencies, defective material and

equipment, and nonconformances are promptly identified and corrected.

Contrary to the above, between April 11 and May 23, 2014, the licensee failed to

promptly identify and correct a CAQ. Specifically, the licensee failed to promptly identify

and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system

despite multiple opportunities to do so. On April 7, the licensee became aware of a

water leak directly above the TDAFW pump turbine outboard bearing. On April 11, and

May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark. The

actions taken (draining the oil level) did not correct the condition adverse to quality in

that water continued to leak into the oil. On May 23, the licensee drained the oil system

and discovered approximately 620 ml of water.

For immediate corrective actions, the licensee added new oil to the system and installed

a temporary modification to prevent further water intrusion. Further corrective actions

included an apparent cause evaluation and past operability evaluation. Permanent

repairs to the cooling water leak above the bearing were completed during the Fall 2014

refueling outage. The licensee initiated AR-2014-6315 to document the condition and

track corrective actions.

This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy because it was of very low safety significance and was entered into

the licensees CAP. (NCV 05000315/2014005-01; Failure to Identify Conditions

Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System)

(2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance

Introduction: A finding of very low safety significance (Green) with an associated NCV of

TS 5.4, Procedures, was self-revealed when a vacuum was inadvertently drawn on the

AB FOST during preparations for surveillance activities. The vacuum caused an

indication of lowering level in the tank, alarms, and an unplanned TS LCO action

statement entry.

Description: On August 20, 2014, the licensee was performing work activities in

preparation for an upcoming, routine leak-test of the AB FOST. The AB FOST is one of

two underground tanks on site that supply fuel to the EDGs via the smaller day tanks

(which are provided for each EDG and offer a more limited, immediate fuel supply). The

test consists of establishing a vacuum in the tank and monitoring it for a period of time.

Several support activities are required to be performed prior to the test, some of which

include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the

FOST, and connection of vendor-supplied vacuum and test equipment to the vent. Per

the overarching surveillance procedure, the basic order of activities should have been to

loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST

from service, remove the vent cover, hook up the test equipment, and perform the test.

During the day shift on August 20, workers went out to work on the vent cover. The

associated work instruction did not provide adequate guidance on what exactly was to

be done. While the intent was just to loosen the cover at that point, the Subject of the

19

WO was Remove manway cover and vent cover. The instructions in the WO were

written as loosen/remove vent cover, and under the Precautions section the statement

Per tank procedure, as a minimum, we only have to loosen vent filter. The workers

ended up removing the cover instead of loosening it, and placed an FME bag over the

vent to prevent foreign material from entering the tank. Later on night shift, operations

staff commenced the transfer of fuel to the day tanks. With the FME bag installed, a

vacuum was drawn on the tank. Based on the configuration of the level instruments and

tank vent, the instruments indicated a lowering tank level and generated low level alarms

because of the vacuum. Operators performed a back-up measurement of tank level

using a dip stick, however, again, based on the tank construction, this method also

showed what appeared to be a lowering tank level. With this information, operators

believed an actual loss of fuel from the tank had occurred. Absent any indications in the

plant of fuel leaving the system, they concluded a release to the environment may have

occurred. Appropriate reports were made to state, federal, and local agencies.

Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed

level indications. During investigation soon after the abnormal level indications, the FME

bag was found on the vent. Once removed, level in the tank returned to normal. There

was no actual loss of fuel from the tank.

Analysis: The failure to have adequate instructions for performing work on safety-related

equipment, as required by TS 5.4, Procedures, was a performance deficiency

warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued

September 7, 2012. The performance deficiency was more than minor because it

adversely impacted the Configuration Control attribute of the Mitigating Systems

cornerstone, whose objective is ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

The finding screened as Green, or very low safety significance, utilizing IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process for Findings at Power, issued

June 19, 2012. Specifically, all questions were answered no under Section A of

Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag

was installed, which rendered the AB FOST inoperable, for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

This was less than the TS allowed outage time of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

The finding had an associated cross-cutting aspect in the human performance area,

specifically, H.5, Work Management. Work activities should be planned, controlled, and

executed with nuclear safety as the overriding priority. Contrary to the tenets of the

cross-cutting aspect, the work was planned and executed with inadequate work

instructions. Further, there was a lack of coordination between a number of work groups

and activities associated with the test.

Enforcement: Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances.

Contrary to those requirements, on August 20, 2014, the AB FOST leak test was

performed with inadequate procedures and with tasks done outside the proper

20

sequence. As a result, the AB FOST was rendered inoperable for approximately

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

Immediate corrective actions involved the removal of an FME bag which had been

placed over the AB FOST vent. The licensee also generated AR-2014-9877, which

included a root cause analysis. This violation is being treated as an NCV, consistent

with Section 2.3.2 of the Enforcement Policy because it was of very low safety

significance and was entered into the licensees CAP. (NCV 05000315/2014005-02;

05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank

During Maintenance)

1R18 Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the following modification(s):

  • Permanent removal of shield/missile blocks

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to

verify that the modification did not affect the operability or availability of the affected

system(s). The inspectors, as applicable, observed ongoing and completed work

activities to ensure that the modifications were installed as directed and consistent with

the design control documents; the modifications operated as expected; post-modification

testing adequately demonstrated continued system operability, availability, and reliability;

and that operation of the modifications did not impact the operability of any interfacing

systems. As applicable, the inspectors verified that relevant procedure, design, and

licensing documents were properly updated. Lastly, the inspectors discussed the plant

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how the operation with the plant modification in place could

impact overall plant performance. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one permanent plant modification sample as defined in

IP 71111.18-05.

b. Findings

Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks

from the Containment Accident Shield

Introduction: A finding of very-low safety significance (Green) and associated NCV of

Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, was identified by the

NRC inspectors for the licensees inadequate radiological review of permanently

removing the AMBs from the Unit 1 and Unit 2 containment accident shields.

Description: In March 2014, the NRC reviewed a licensee modification

(EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The

modification consisted of permanently removing the AMBs, located in front of the primary

containment equipment hatches on the 650 elevation of the Auxiliary Building. The

AMBs are portable and removable shield blocks and are a part of the safety-related

21

containment accident shield. The AMBs are in place during power operations for

shielding purposes. The AMBs are removed during plant outages to permit containment

access for equipment.

The main purpose of the accident shield, as a part of original plant design and currently

described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside

the containment building following a maximum design-basis accident; specifically, a

large break loss-of-coolant accident (LBLOCA). The plant containment and the accident

shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and

the general public are protected by adequate containment shielding, post LBLOCA. This

was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General

Design Criteria 1 Quality Standards and Records of Appendix A General Design

Criteria for Nuclear Power Plants, 10 CFR Part 20 Standards for Protection Against

Radiation, and 10 CFR Part 100 Reactor Site Criteria. The inspectors reviewed the

original and current plant design configuration and determined that, prior to plant

modification (EC-0000049191), the plant design met General Design Criteria 1 for

radiation safety. Specifically, RG 1.69 Concrete Radiation Shields for Nuclear Power

Plants was explicit in stating that General Design Criteria 1 for containment ensures

reasonable assurance for compliance to 10 CFR Part 20 Standards for Protection

Against Radiation under post-accident conditions. Additionally, initial plant design for

the containment accident shield was consistent with RG 1.69 Concrete Radiation

Shields for Nuclear Power Plants.

Using the licensees design basis source term, licensee calculation number RS-C-0046

Doses and Dose Rates from Post LOCA Airborne Sources determined that with the

AMBs in place, the Post LBLOCA dose rates were:

  • A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and
  • A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.

These dose rates provide for safe radiation levels outside the containment building

following a maximum design-basis accident consistent with the UFSAR design

statements and in accordance with the requirements of 10 CFR Part 20, Standards for

Protection Against Radiation.

The licensee provided no comparable post-modification dose rate calculations to the

inspectors specific to AB 650 elevation once the AMBs were removed. However, the

licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose

Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates

of 196.2 Rem/hr at 45 feet from the equipment hatch. Additionally, the licensee had

analogous Post-LBLOCA dose rate calculations for the containment personnel hatch.

These dose rates provide a frame of reference, in that, the calculations provide for no

AMB shielding. However, the calculations did include shielding benefit from the inside

containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from

Post LOCA Airborne Sources). Specific calculated dose rates were:

  • A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel

hatch; and

  • A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel

hatch.

22

The inspectors determined that post-modification dose rates on the AB 650 elevation

could result in lethal doses, as defined in NUREG/CR 6545 Probabilistic Accident

Consequence Uncertainty Analysis: Early Health Effects Uncertainty Assessment, to

individuals in a very short period of time (from fractions of a second to minutes,

depending on the location of personnel relative to the radiation source). By permanently

removing the AMBs, the licensee failed to provide for safe radiation levels outside the

containment building following a maximum design-basis accident, contrary to the design

bases and inconsistent with the requirements of 10 CFR Part 20.

Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use,

to the extent practical, engineering controls based upon sound radiation principles to

achieve occupational doses and doses to members of the public that are

as-low-as-reasonably-achievable (ALARA). Original plant design and the plants 40-year

operational history demonstrate that plant operation with the AMBs in place was both

practical and ALARA.

The licensee documented this issue in the CAP as AR 2014-13016. Corrective actions

included licensee determination to achieve radiation attenuation analogous to original

plant design of the AMBs in place.

Analysis: The inspectors determined that the licensees inadequate radiological review

of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident

shields was a performance deficiency. The performance deficiency was determined to

be more than minor (Green) because it was associated with the Barrier Integrity

Cornerstone attribute of design control; and adversely affected the cornerstone objective

of maintaining radiological barrier functionality of the safety-related containment accident

shield. Specifically, the failure to control plant design and adequately evaluate the

radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2

containment accident shields did not ensure that the accident shield will provide its

design function to ensure safe radiation levels outside the containment building following

a maximum design basis accident.

The inspectors evaluated the finding using the SDP in accordance with IMC 0609,

Significance Determination Process, Attachment 0609.04, Initial Characterization of

Findings, dated June 19, 2012. Because the finding impacted the Barrier Integrity

Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, The

Significance Determination Process for Findings At-Power, dated June 19, 2012, using

Exhibit 3, Barrier Integrity Screening Questions. The finding screened as of very-low

safety significance (Green) because the finding only represented a degradation of the

radiological barrier function provided for the Auxiliary Building.

The inspectors determined the cause of this finding did not represent current licensee

performance and, thus, no cross-cutting aspect was assigned.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, requires,

in part, that design changes be subject to design control measures commensurate with

those applied to the original design.

Contrary to the above, on February 6, 2009, the licensee performed a design change

and failed to subject it to design control measures commensurate with those applied to

the original design. Specifically, the licensee modified the original plant design by

23

removing the auxiliary missile blocks from the safety-related accident shield. However,

the design control measures applied to the modification failed to ensure safe radiation

levels outside the containment accident shield following a design basis loss-of-coolant

accident.

Because this violation was of very-low safety significance and was entered into the

licensees CAP (AR 2014-13016), this violation is being treated as an NCV, consistent

with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000315/2014005-03;

05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield

Blocks on the Containment Accident Shield Post LBLOCA)

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • Unit 1 AB EDG following governor replacement;
  • Unit 1 CRID III and IV maintenance;
  • Unit 2 UAT breakers following failure to close;
  • Unit 1 CD EDG governor replacement and aftercooler maintenance;
  • Unit 1 TDAFW governor overhaul;
  • Repair of Unit 2 AFW flow control valve flow retention issue;
  • Repair of circuitry associated with failure of fast transfer and generator trip during

dual-unit trip; and

  • Unit 1 TDAFW repairs following inadvertent trip.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted eight post-maintenance testing samples as defined in

IP 71111.19-05.

24

b. Findings

Introduction: A finding of very low safety significance (Green) with an associated NCV of

TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1 TDAFW

pump tripped during an emergent dual-unit shutdown. Both units were taken offline by

operators due to debris intrusion from Lake Michigan into the cooling water

screenhouse. The TDAFW pump started as expected but shutdown after a few minutes

of operation.

Description: On November 1, 2014, operators removed both units from service in

response to excessive debris intrusion into the cooling water screenhouse. Following

the trip of both reactors, AFW pumps started as expected. However, the Unit 1 TDAFW

unexpectedly turned off after a few minutes of operation while operators were adjusting

flow to the steam generators. Adequate flow continued to be provided by the two other

AFW pumps. During the ensuing forced outage to address the debris intrusion issue,

the licensee performed an investigation into why the pump tripped off. The licensee

explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry,

and governor control problems. The investigation included several test runs of the pump

while rapidly changing demand in an effort to stress the pump and replicate the trip

event. During continued troubleshooting, the licensee later discovered a protective

enclosure around an electronic component (the trip solenoid) had been installed

incorrectly. The enclosure was relatively loose, and the licensee found by moving it

slightly, it could be placed in a position where a threaded rod on the enclosure could

interfere with the proper latching of the TTV for the pump. When the pump turns on, the

TTV opens to admit steam to the turbine. As the valve stem moves up, an attachment

engages a trip hook. The trip hook basically acts to hold the valve open. On a trip

condition, such as a pump overspeed, the hook would move out of the way, allowing the

valve to shut and the pump to turn off. Precise engagement between the TTV and the

trip hook is required for the pump to operate correctly. In this case, the licensees

apparent cause evaluation determined the most likely cause was inadequate trip hook

engagement as a result of the interference from the trip solenoid enclosure. As part of

the extent-of-condition, the licensee discovered the same potential issue on the Unit 2

TDAFW pump. Further investigation revealed that the enclosure was not captured in

design diagrams, and that work instructions regarding its installation/removal were not

detailed. Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been

removed and reinstalled during the Fall 2014 refueling outage as part of planned

maintenance. Working with the pump vendor, the licensee identified the correct

configuration of the enclosure and reinstalled them correctly on both pumps. The

licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW

pump to operable status at the conclusion of the forced outage.

Analysis: The failure to have adequate instructions for performing work on safety-related

equipment, as required by TS 5.4, Procedures, was a performance deficiency

warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued

September 7, 2012. The performance deficiency was more than minor because it

adversely impacted the Configuration Control attribute of the Mitigating Systems

cornerstone, whose objective is ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

The inspectors utilized IMC 0609 Appendix A, The Significance Determination Process

for Findings at Power, issued June 19, 2012, to assess the significance of the finding.

25

Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater

than the TS allowed outage time. Therefore, the inspectors consulted the regional

Senior Reactor Analyst (SRA) for a detailed risk evaluation. The inspectors considered

the Unit 1 TDAFW pump inoperable since the last successful surveillance on

October 23. Given the evidence available, this was the likely opportunity for the

conditions to be established to set-up the improper engagement between the TTV and

the trip hook.

The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook

to perform a detailed risk evaluation. The model has internal and external event

initiators. The SRA assumed an exposure period for the condition of 9 days. The delta

core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low

safety significance (Green). The dominant risk sequence was a fire in the turbine

building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed.

Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the

potential impact of the finding on large early release frequency using IMC 0609

Appendix HProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix H" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Containment Integrity Significance Determination Process. The plant has

an ice condenser containment and sequences important to large early release frequency

are steam generator tube rupture, inter-system loss-of-coolant accident, and station

blackout. Some of the sequences that contributed to the change in CDF included station

blackout sequences but their contribution was less than 1E-7/yr. The SRA concluded

that the risk of this finding should be characterized by the overall change in CDF.

The finding had an associated cross-cutting aspect in the area of human performance,

specifically, H.8, Procedure Adherence. Safety Culture Common Language Initiative

NUREG-2165 provides an example of the aspect as individuals review procedures

before work to validate they are appropriate for scope of work, and ensure required

changes are completed before implementation. Contrary to this description, work

proceeded on the trip enclosure despite a lack of detailed instructions on the

removal/installation of the enclosure.

Enforcement: Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances.

Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip

solenoid enclosure with inadequate work instructions. As a result, an apparent cause

evaluation determined the misplaced enclosure was the likely cause of the pump

failure during an actual demand following a dual-unit trip. The violation existed from

October 23, 2014, until troubleshooting and post-maintenance testing activities were

completed on November 3, 2014, following the dual-unit trip.

For immediate corrective actions, the licensee initiated AR-2014-13668 and began

troubleshooting activities. The licensee investigation revealed the misplaced trip

solenoid enclosure to be the likely cause of the pump trip. Subsequently, the enclosures

were installed in the correct position. This violation is being treated as an NCV,

consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety

26

significance and was entered into the licensees CAP. (NCV 05000315/2014005-04;

Inadvertent Trip of the Unit 1 TDAFW Pump)

1R20 Outage Activities (71111.20)

.1 Refueling Outage Activities

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1

refueling outage, conducted September 24 - October 24, 2014, to confirm that the

licensee had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense-in-depth. During the refueling outage, the inspectors observed portions of

the shutdown and cooldown processes and monitored licensee controls over the outage

activities listed below:

  • licensee configuration management, including maintenance of defense-in-depth

commensurate with the Outage Safety Plan for key safety functions and

compliance with the applicable TS when taking equipment out of service;

  • implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing;

  • installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error;

  • controls over the status and configuration of electrical systems to ensure that

TS and Outage Safety Plan requirements were met, and controls over switchyard

activities;

  • controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system;

alternative means for inventory addition, and controls to prevent inventory loss;

  • controls over activities that could affect reactivity;
  • licensee fatigue management, as required by 10 CFR 26, Subpart I;
  • refueling activities, including fuel handling and sipping to detect fuel assembly

leakage;

  • startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left which could block emergency core cooling system suction strainers, and

reactor physics testing; and

  • licensee identification and resolution of problems related to refueling outage

activities.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05.

27

b. Findings

No findings were identified.

.2 Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014

a. Inspection Scope

On November 1, rough lake conditions generated substantial amounts of debris that

clogged trash racks and travelling screens. The licensee manually tripped the Unit 1

reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce

circulating water flow. Conditions continued to degrade; therefore the licensee

subsequently tripped the Unit 2 reactor. Unit 1 remained in Mode 3 and returned to

100 percent power on November 8. Unit 2 was cooled down to Mode 5 to repair an

intermediate range nuclear instrument. Unit 2 was returned to 100 percent power on

November 13. The inspectors toured portions of containment, observed shutdown and

startup activities, assessed plant risk, and observed maintenance activities.

This inspection constituted one Forced Outage sample as defined in IP 71111.20-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • 1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);
  • 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance,

(Ice Condenser Surveillance);

(Routine); and

  • Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • the effects of the testing were adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the USAR, procedures, and applicable commitments;

28

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two routine surveillance testing samples, one inservice

testing sample, one ice condenser surveillance, and one containment isolation valve

sample as defined in IP 71111.22, Sections-02 and-05.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The regional inspectors performed an in-office review of the latest revisions to the

Emergency Plan and Emergency Plan Implementing Procedures as listed in the

Attachment to this report.

The licensee transmitted the Emergency Plan and Emergency Action Level revisions to

the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,

Implementing Procedures. The NRC review was not documented in a safety

evaluation report and did not constitute approval of licensee-generated changes;

therefore, this revision is subject to future inspection. The specific documents reviewed

during this inspection are listed in the Attachment to this report.

29

This Emergency Action Level and Emergency Plan Change inspection constituted one

sample as defined in IP 71114.04-06.

b. Findings

Introduction: An Unresolved Item (URI) was identified because additional information is

required to determine whether a performance deficiency that is more than minor exists

and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of

concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the

number of Radiation Protection Technicians (RPTs) required to augment the on-shift

emergency response organization in 60 minutes of a declared emergency and replaced

them with a Radiological Assessment Coordinator (RAC) and an Environmental

Assessment Coordinator (EAC).

Description. During the review, the inspectors identified a change made in Table 1 of

Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced

the number of 60-minute response RPTs tasked with conducting offsite surveys from

three RPTs to two RPTs and one EAC. The second change reduced the number of

60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one

RPT and one RAC. According the licensees 10 CFR 2014 50.54(q) screening

evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and

B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and

B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute

responders in Revision 19 of the plan in March of 2004. Inspectors review of the

10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had

been done for this change. The inspectors reviewed Revision 18 of the E-Plan and the

associated March 21, 2003 licensee request for prior approval for changes to the E-plan

that was conducted, approved by the NRC, and implemented in this revision. The NRC

approved change request included specific numbers of RPTs for 60-minute response

tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.

The licensee indicated that the EAC and RAC were not currently qualified RPTs. This

suggests a performance deficiency, due to the appearance of a reduction in

effectiveness to the licensees E-plan, without prior NRC approval. However, in order to

determine if this is a performance deficiency of more than minor significance, additional

information is required to understand if the RAC and EAC positions had equivalent

capabilities as the qualified RPTs. The licensee has entered this issue in their

Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory

actions were taken while their staff gathers additional information, which included

requiring two additional qualified RPTs to respond to the Operations Support Center

within 60 minutes prior to activating the facility in the event of a declared emergency.

The licensee stated that it will provide the inspectors with additional information within

30 days of the exit meeting.

Therefore, a URI was identified pending additional information. Specifically,

documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC

are equivalent to the RPTs is necessary for the inspectors to determine whether the

performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)

occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency

Responder Staffing Without Prior Approval)

30

2. RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

The inspection activities supplement those documented in NRC Inspection Report

05000315-05000316/2014002 and constitute one complete sample as defined in

Inspection Procedure 71124.01-05.

.1 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors determined whether there have been changes to plant operations since

the last inspection that may result in a significant new radiological hazard for onsite

workers or members of the public. The inspectors evaluated whether the licensee

assessed the potential impact of these changes and has implemented periodic

monitoring, as appropriate, to detect and quantify the radiological hazard.

The inspectors reviewed the last two radiological surveys from selected plant areas and

evaluated whether the thoroughness and frequency of the surveys where appropriate for

the given radiological hazard.

The inspectors selected the following radiologically risk significant work activities that

involved exposure to radiation:

  • Refuel Cavity Decontamination Activities;
  • Valve Maintenance / Repair;
  • Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted

Areas; and

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if hazards were properly identified, including the following:

  • identification of hot particles;
  • the presence of alpha emitters;
  • the potential for airborne radioactive materials, including the potential presence

of transuranics and/or other hard-to-detect radioactive materials (This evaluation

may include licensee planned entry into non-routinely entered areas subject to

previous contamination from failed fuel.);

  • the hazards associated with work activities that could suddenly and severely

increase radiological conditions and that the licensee has established a means to

inform workers of changes that could significantly impact their occupational dose;

and

  • severe radiation field dose gradients that can result in non-uniform exposures of

the body.

31

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and were representative of actual work areas. The inspectors evaluated

the licensees program for monitoring levels of loose surface contamination in areas of

the plant with the potential for the contamination to become airborne.

b. Findings

No findings were identified.

.2 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors reviewed the following radiation work permits used to access high

radiation areas and evaluated the specified work control instructions or control barriers:

  • RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
  • RWP 141145; U1C26 - Valve Maintenance / Repair;
  • RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings &

Plant Restricted Areas; and

  • RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey.

For these radiation work permits, the inspectors assessed whether allowable stay times

or permissible dose (including from the intake of radioactive material) for radiologically

significant work under each radiation work permit were clearly identified. The inspectors

evaluated whether electronic personal dosimeter alarm set-points were in conformance

with survey indications and plant policy.

For work activities that could suddenly and severely increase radiological conditions, the

inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b. Findings

No findings were identified.

.3 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors observed locations where the licensee monitors potentially contaminated

material leaving the radiological control area and inspected the methods used for

control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the work was performed in accordance with plant procedures and

whether the procedures were sufficient to control the spread of contamination and

prevent unintended release of radioactive materials from the site. The inspectors

assessed whether the radiation monitoring instrumentation had appropriate sensitivity for

the type(s) of radiation present.

32

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to an alarm that indicates the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters. The inspectors assessed whether or not the licensee

has established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected several sealed sources from the licensees inventory records

and assessed whether the sources were accounted for and verified to be intact.

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

b. Findings

No findings were identified.

.4 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, radiation work permits,

and worker briefings.

The inspectors evaluated the adequacy of radiological controls, such as required

surveys, radiation protection job coverage (including audio and visual surveillance for

remote job coverage), and contamination controls. The inspectors evaluated the

licensees use of electronic personal dosimeters in high noise areas as high radiation

area monitoring devices.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high-radiation work areas with significant dose rate gradients.

The inspectors reviewed the following radiation work permits for work within airborne

radioactivity areas with the potential for individual worker internal exposures:

  • RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
  • RWP 141145; U1C26 - Valve Maintenance / Repair.

For these radiation work permits, the inspectors evaluated airborne radioactive controls

and monitoring, including potential for significant airborne levels (e.g., grinding, grit

blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The

inspectors assessed barrier (e.g., tent or glove box) integrity and temporary

high-efficiency particulate air ventilation system operation.

33

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other

storage pools. The inspectors assessed whether appropriate controls (i.e.,

administrative and physical controls) were in place to preclude inadvertent removal of

these materials from the pool.

The inspectors examined the posting and physical controls for selected high radiation

areas and very-high radiation areas to verify conformance with the occupational

performance indicator.

b. Findings

Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure

Inadequacy

Introduction: An NRC identified Green NCV of TS 5.4.1, Procedures, was identified for

inadequate procedures used to verify Locked High Radiation Controls in the Unit 2

Containment.

Description: On July 24, 2014, the inspector walked down the Unit 2 containment cavity

access ladder. At the time of the walkdown, the access to the cavity was posted LHRA

and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot

high locked gate for access to the permanently installed cavity ladder. Discussions with

Radiation Protection staff had identified that the ladder lock device was not in place in

March 2014. Additionally, it was established that the locking cage was not placed back

on the ladder following the refueling outage in October 2013 when the area was

conservatively posted as a LHRA as the dose rates in the containment cavity were not in

excess of 1000 millirem per hour at 30 centimeters. The inspector reviewed Survey

Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final

Containment Cavity Survey following the last refueling outage. This survey confirmed

that the highest dose in the accessible areas of the cavity were nominally 2400 millirem

per hour on contact, and 500 millirem per hour at 30 centimeters from the source with

the highest readings in the cavity lift system pit area following the cavity

decontamination. These dose rates would not constitute a LHRA (greater than

1000 millirem per hour at 30 centimeters.) The survey showed that the gate to the cavity

ladder was posted as a LHRA.

Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access,

Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure

guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation

Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional

management expectations and a tracking tool for door/gate verifications while used as a

field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified

a substantial procedural weakness in this guidance in that the Data Sheet apparently did

not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that

the locked cage/ladder lock to the reactor cavity was in place and locked; a condition

which is necessary to provide reasonable assurance that the area is secured against

unauthorized access and cannot be easily circumvented. A review of the data verified

that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity

ladder during weekly LHRA verification from November 2013 through March 2014. The

NRC inspectors also reviewed the LHRA and VHRA verification documentation in the

34

RP station daily logs from November 2013 to March 2014 and the inspectors did not

identify any discrepancies noted in the logs associated with in LHRA controls during their

weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action

Program documents did not identify a record of the missing ladder lock device or

identification of an unlocked LHRA. Therefore the licensee was not aware of the

deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the

inspectors. The failure to identify deficient LHRA controls could have the potential failure

to identify and report a Performance Indicator (PI) occurrence.

Analysis: The inspectors determined that there was an inadequacy in the licensees

procedure for identifying a deficient Locked High Radiation Area for the barrier in their

weekly locked cage/ladder barrier to the cavity of Unit 2 containment. The inspectors

determined that the procedure did not provide clear directions to assure the Radiation

Protection Technician would verify the required controls for LHRA is a performance

deficiency. The inspectors determined that the cause of the performance deficiency was

reasonably within the licensees ability to foresee and correct and should have been

prevented.

The finding was not subject to traditional enforcement since the incident did not have a

significant safety consequence, did not impact the NRCs ability to perform its regulatory

function, and was not willful.

The inspectors determined that the performance deficiency was more than minor in

accordance with IMC 0612, Appendix B, Issue Screening, because if left uncorrected,

the performance deficiency could lead to a more significant safety concern. Specifically,

the failure to identify deficient LHRA controls could result in unintentional exposure to

high levels of radiation.

The finding was assessed using the Occupational Radiation Safety SDP and was

determined to be of very-low safety significance because the problem was not an

ALARA planning issue, there were no overexposures nor substantial potential for

overexposures given the highest dose rates present in the room, the scope of work, and

the licensees ability to assess dose was not compromised.

The inspectors did not identify a corresponding cross-cutting aspect for this performance

deficiency.

Enforcement: Technical Specification 5.4.1, Procedures, requires that written

procedures shall be established, implemented and maintained covering the activities

referenced in Appendix A of Regulatory Guide 1.33, Revision 2. Control of Radioactivity

procedures, including limiting personnel exposure, are specified in Appendix A.

Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and

Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate

verification in conjunction with Procedural Guidance THG-026, Locked High Radiation

Area, and Very-High Radiation Weekly Verification Process did not provide sufficient

details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was

in place and locked; a condition which is necessary to provide reasonable assurance

that the area is secured against unauthorized access and cannot be easily

circumvented. Consequently, weekly, from November 1, 2013, to March 2014 multiple

35

RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure

the area against unauthorized access.

Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High,

Locked High, and Very-High Radiation Area Access, and the associated Procedural

Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly

Verification. Because this violation is of very-low safety significance and it was entered

into the licensees CAP as AR 2014-9001, this violation is being treated as an NCV

consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient

Locked High Radiation Area Controls Due to Procedure Inadequacy)

.5 Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06)

a. Inspection Scope

The inspectors discussed with the radiation protection manager the controls and

procedures for high-risk, high radiation areas and very-high radiation areas. The

inspectors discussed methods employed by the licensee to provide stricter control of

very-high radiation area access as specified in 10 CFR 20.1602, Control of Access to

Very-High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and

Very-High Radiation Areas of Nuclear Plants. The inspectors assessed whether any

changes to licensee procedures substantially reduce the effectiveness and level of

worker protection.

The inspectors discussed the controls in place for special areas that have the potential

to become very-high radiation areas during certain plant operations with first-line health

physics supervisors (or equivalent positions having backshift health physics oversight

authority). The inspectors assessed whether these plant operations require

communication beforehand with the health physics group, so as to allow corresponding

timely actions to properly post, control, and monitor the radiation hazards including

re-access authorization.

The inspectors evaluated licensee controls for very-high radiation areas and areas with

the potential to become a very-high radiation areas to ensure that an individual was not

able to gain unauthorized access to the very-high radiation areas.

b. Findings

No findings were identified.

.6 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors observed radiation worker performance with respect to stated radiation

protection work requirements. The inspectors assessed whether workers were aware of

the radiological conditions in their workplace and the radiation work permit controls/limits

in place, and whether their performance reflected the level of radiological hazards

present.

36

b. Findings

No findings were identified.

.7 Radiation Protection Technician Proficiency (02.08)

a. Inspection Scope

The inspectors observed the performance of the radiation protection technicians with

respect to all radiation protection work requirements. The inspectors evaluated whether

technicians were aware of the radiological conditions in their workplace and the radiation

work permit controls/limits, and whether their performance was consistent with their

training and qualifications with respect to the radiological hazards and work activities.

b. Findings

No findings were identified.

.8 Problem Identification and Resolution (02.09)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees Corrective Action Program. The

inspectors assessed the appropriateness of the corrective actions for a selected sample

of problems documented by the licensee that involve radiation monitoring and exposure

controls. The inspectors assessed the licensees process for applying operating

experience to their plant.

b. Findings

No findings were identified.

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)

The inspection activities supplement those documented in NRC Inspection Report

05000315-05000316/2014002 and constitute a partial sample as defined in Inspection

Procedure 71124.02-05.

.1 Radiation Worker Performance (02.05)

a. Inspection Scope

The inspectors observed radiation worker and radiation protection technician

performance during work activities being performed in radiation areas, airborne

radioactivity areas, or high radiation areas. The inspectors evaluated whether workers

demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work

activity scope and tools to be used, workers used ALARA low-dose waiting areas) and

whether there were any procedure compliance issues (e.g., workers are not complying

with work activity controls). The inspectors observed radiation worker performance to

assess whether the training and skill level was sufficient with respect to the radiological

hazards and the work involved.

37

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (71124.07)

This inspection constituted one complete sample as defined in Inspection Procedure

71124.07-05.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the annual radiological environmental operating reports and the

results of any licensee assessments since the last inspection to assess whether the

Radiological Environmental Monitoring Program was implemented in accordance with

the Technical Specifications and Offsite Dose Calculation Manual. This review included

reported changes to the Offsite Dose Calculation Manual with respect to environmental

monitoring, commitments in terms of sampling locations, monitoring and measurement

frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of

data.

The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of

environmental monitoring stations.

The inspectors reviewed the Final Safety Analysis Report for information regarding the

environmental monitoring program and meteorological monitoring instrumentation.

The inspectors reviewed quality assurance audit results of the program to assist in

choosing inspection smart samples. The inspectors also reviewed audits and technical

evaluations performed on the vendor laboratory if used.

The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,

Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if

the licensee was sampling, as appropriate, for the predominant and dose-causing

radionuclides likely to be released in effluents.

b. Findings

No findings were identified.

.2 Site Inspection (02.02)

a. Inspection Scope

The inspectors walked down select air sampling stations and dosimeter monitoring

stations to determine whether they were located as described in the Offsite Dose

Calculation Manual and to determine the equipment material condition. Consistent with

smart sampling, the air sampling stations were selected based on the locations with the

highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk

significant locations (e.g., those that have the highest potential for public dose impact).

38

For the air samplers and dosimeters selected, the inspectors reviewed the calibration

and maintenance records to evaluate whether they demonstrated adequate operability of

these components. Additionally, the review included the calibration and maintenance

records of select composite water samplers.

The inspectors assessed whether the licensee had initiated sampling of other

appropriate media upon loss of a required sampling station.

The inspectors observed the collection and preparation of environmental samples from

different environmental media (e.g., ground and surface water, milk, vegetation,

sediment, and soil) as available to determine whether environmental sampling was

representative of the release pathways as specified in the Offsite Dose Calculation

Manual and if sampling techniques were in accordance with procedures.

Based on direct observation and review of records, the inspectors assessed whether

the meteorological instruments were operable, calibrated, and maintained in

accordance with guidance contained in the Final Safety Analysis Report, NRC

Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants,

and licensee procedures. The inspectors assessed whether the meteorological data

readout and recording instruments in the control room and, if applicable, at the tower

were operable.

The inspectors evaluated whether missed and/or anomalous environmental samples

were identified and reported in the annual environmental monitoring report. The

inspectors selected events that involved a missed sample, inoperable sampler, lost

dosimeter, or anomalous measurement to determine if the licensee had identified the

cause and had implemented corrective actions. The inspectors reviewed the licensees

assessment of any positive sample results (i.e., licensed radioactive material detected

above the lower limits of detection) and reviewed the associated radioactive effluent

release data that was the source of the released material.

The inspectors selected structures, systems, or components that involve or could

reasonably involve licensed material for which there is a credible mechanism for

licensed material to reach ground water, and assessed whether the licensee had

implemented a sampling and monitoring program sufficient to detect leakage of these

structures, systems, or components to ground water.

The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks,

spills, and remediation since the previous inspection were retained in a retrievable

manner.

The inspectors reviewed any significant changes made by the licensee to the Offsite

Dose Calculation Manual as the result of changes to the land census, long-term

meteorological conditions (3-year average), or modifications to the sampler stations

since the last inspection. They reviewed technical justifications for any changed

sampling locations to evaluate whether the licensee performed the reviews required to

ensure that the changes did not affect its ability to monitor the impacts of radioactive

effluent releases on the environment.

The inspectors assessed whether the appropriate detection sensitivities with respect to

Technical Specifications/Offsite Dose Calculation Manual where used for counting

39

samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation

Manual required lower limits of detection). The inspectors reviewed quality control

charts for maintaining radiation measurement instrument status and actions taken for

degrading detector performance. The licensee uses a vendor laboratory to analyze the

radiological environmental monitoring program samples so the inspectors reviewed the

results of the vendors quality control program, including the inter-laboratory comparison,

to assess the adequacy of the vendors program.

The inspectors reviewed the results of the licensees Inter-Laboratory Comparison

Program to evaluate the adequacy of environmental sample analyses performed by the

licensee. The inspectors assessed whether the inter-laboratory comparison test

included the media/nuclide mix appropriate for the facility. If applicable, the inspectors

reviewed the licensees determination of any bias to the data and the overall effect on

the radiological environmental monitoring program.

b. Findings

No findings were identified.

.3 Identification and Resolution of Problems (02.03)

a. Inspection Scope

The inspectors assessed whether problems associated with the radiological

environmental monitoring program were being identified by the licensee at an

appropriate threshold and were properly addressed for resolution in the licensees

Corrective Action Program. Additionally, they assessed the appropriateness of the

corrective actions for a selected sample of problems documented by the licensee that

involved the radiological environmental monitoring program.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, and Occupational and Public Radiation Safety

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index - Emergency AC Power System

a. Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index (MSPI) - Emergency AC Power System performance

indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013

through the second quarter 2014. To determine the accuracy of the PI data reported

during those periods, PI definitions and guidance contained in the Nuclear Energy

Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the

40

licensees operator narrative logs, MSPI derivation reports, issue reports, event reports

and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report. Portions of this inspection activity were credited in NRC

Inspection Report 05000315-05000316/2014004.

This inspection constituted one MSPI emergency AC power system sample as defined in

IP 71151-05.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index - High Pressure Injection Systems

a. Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - High Pressure Injection Systems performance indicator

for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru

the third quarter of 2014. To determine the accuracy of the PI data reported during

those periods, PI definitions and guidance contained in the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31,

2013, were used. The inspectors reviewed the licensees operator narrative logs, issue

reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports

for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the

accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report. Portions of this inspection activity were credited in NRC

Inspection Report 05000315-05000316/2014004.

This inspection constituted one MSPI high pressure injection system sample as defined

in IP 71151-05.

b. Findings

No findings were identified.

41

.3 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Heat Removal System performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

This inspection constituted one MSPI heat removal system sample as defined in

IP 71151-05.

b. Findings

No findings were identified.

.4 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Residual Heat Removal System performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

42

This inspection constituted one MSPI residual heat removal system sample as defined in

IP 71151-05.

b. Findings

No findings were identified.

.5 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Cooling Water Systems performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

This inspection constituted one MSPI cooling water system sample as defined in

IP 71151-05.

b. Findings

No findings were identified.

.6 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage performance indicator

for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter

2014. To determine the accuracy of the PI data reported during those periods, PI

definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data,

issue reports, event reports and NRC Integrated Inspection Reports for the period of the

fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

43

This inspection constituted two RCS leakage samples as defined in IP 71151-05.

b. Findings

No findings were identified.

.7 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS specific activity Performance

Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third

quarter 2013 through the third quarter 2014. The inspectors used Performance Indicator

definitions and guidance contained in the Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August

2013, to determine the accuracy of the Performance Indicator data reported during those

periods. The inspectors reviewed the licensees RCS chemistry samples, Technical

Specification requirements, issue reports, event reports, and NRC Integrated Inspection

Reports to validate the accuracy of the submittals. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the Performance Indicator data collected or transmitted for this indicator and none were

identified. In addition to record reviews, the inspectors observed a chemistry technician

obtain and analyze a RCS sample. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted two RCS specific activity samples as defined in IP 71151-05.

b. Findings

No findings were identified.

.8 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the radiological effluent Technical

Specification/Offsite Dose Calculation Manual radiological effluent occurrences

Performance Indicator for the period from the third quarter 2013 through the third quarter

2014. The inspectors used Performance Indicator definitions and guidance contained in

the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the

Performance Indicator data reported during those periods. The inspectors reviewed the

licensees issue report database and selected individual reports generated since this

indicator was last reviewed to identify any potential occurrences such as unmonitored,

uncontrolled, or improperly calculated effluent releases that may have impacted offsite

dose. The inspectors reviewed gaseous effluent summary data and the results of

associated offsite dose calculations for selected dates to determine if indicator results

were accurately reported. The inspectors also reviewed the licensees methods for

quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

44

This inspection constituted one Radiological Effluent Technical Specification/Offsite

Dose Calculation Manual radiological effluent occurrences sample as defined in

IP 71151 05.

b. Findings

No findings were identified.

.9 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Exposure Control

Effectiveness Performance Indicator for the period from the third quarter 2013 through

the third quarter 2014. The inspectors used Performance Indicator definitions and

guidance contained in the Nuclear Energy Institute Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to

determine the accuracy of the Performance Indicator data reported during those periods.

The inspectors reviewed the licensees assessment of the Performance Indicator for

occupational radiation safety to determine if the indicator related data was adequately

assessed and reported. To assess the adequacy of the licensees Performance

Indicator data collection and analyses, the inspectors discussed with radiation protection

staff the scope and breadth of its data review and the results of those reviews. The

inspectors independently reviewed electronic personal dosimetry dose rate and

accumulated dose alarms and dose reports and the dose assignments for any intakes

that occurred during the time period reviewed to determine if there were potentially

unrecognized occurrences. The inspectors also conducted walkdowns of numerous

locked high and very-high radiation area entrances to determine the adequacy of the

controls in place for these areas. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one occupational exposure control effectiveness sample as

defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

45

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for followup, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings were identified.

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6-month period of July 2014 through December 2014,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

46

reports, self-assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees CAP

trending reports. Corrective actions associated with a sample of the issues identified in

the licensees trending reports were reviewed for adequacy.

The inspectors observed some weaknesses in different aspects of the operability

determination process. There were some instances where ARs were written but were

not flagged for an operability review. Some had been already identified by the licensee

upon questioning by the inspectors, others had not. In these cases, the inspectors did

not find any instances where equipment should have been called inoperable but was

not. The inspectors also found a functionality assessment associated with fire pumps

where necessary compensatory measures were not formalized until the inspectors had

questioned the assessment. During the period of review, there were two NRC identified

findings with identified weaknesses in the operability determination process. One was

documented in NRC Inspection Report 2014004 and dealt with a failure to provide

adequate technical justification for operability of a TDAFW pump with respect to

governor oil levels. Another issue is documented in Section 1R15 of this report and

dealt with, in part, appropriate oil levels for TDAFW bearings. The inspectors discussed

the observations with licensee staff, who agreed with the assessment.

The inspectors also observed weaknesses in work planning and execution. Multiple

instances were identified of scheduled work activities that had to be de-conflicted the

day/week of execution. In some cases, procedures had to be revised to support work, or

post-maintenance test activities changed to appropriately cover the scope of work near

time of execution. In some cases, where changes were made or expanded scope

encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed

to the site) was not updated appropriately. A finding in Section 1R15 of this report

documents a case where inadequate planning and execution unexpectedly rendered a

diesel fuel oil storage tank inoperable. Inspectors have discussed the issue with

licensee staff, who agreed with the assessment.

This review constituted one semiannual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings were identified.

.4 Selected Issue Followup Inspection: Review of Operator Workarounds

a. Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the operator workarounds

(OWAs) on system availability and the potential for improper operation of the system, for

potential impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

The inspectors performed a review of the cumulative effects of OWAs. The documents

listed in the Attachment to this report were reviewed to accomplish the objectives of the

inspection procedure. The inspectors reviewed both current and historical operational

47

challenge records to determine whether the licensee was identifying operator challenges

at an appropriate threshold, had entered them into their CAP and proposed or

implemented appropriate and timely corrective actions which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the

possibility of an Initiating Event, if the challenge was contrary to training, required a

change from long-standing operational practices, or created the potential for

inappropriate compensatory actions. Additionally, all temporary modifications were

reviewed to identify any potential effect on the functionality of Mitigating Systems,

impaired access to equipment, or required equipment uses for which the equipment was

not designed. Daily plant and equipment status logs, degraded instrument logs, and

operator aids or tools being used to compensate for material deficiencies were also

assessed to identify any potential sources of unidentified operator workarounds.

This review constituted one in depth review of a selected issue sample (operator work

arounds) as defined in IP 71152-05.

b. Findings

No findings were identified.

.5 Selected Issue Follow-up Inspection: Follow-up to Previous NRC Findings

a. Inspection Scope

The inspectors selected a sample of previously issued NRC findings to assess the

adequacy of licensee corrective actions. Two instances were identified where the

technical issues had been adequately addressed; however, it appeared there were no

corrective actions for underlying performance issues. In one case, a finding was issued

regarding a change in the system pressures at which the fire pumps would automatically

start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually

show the new setpoints were acceptable, nothing was done to explore potential

breakdowns in the engineering change process or in human performance that allowed

the change to occur without the additional reviews being done to begin with. In another

example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the

guidance in the operability determination procedure. Subsequently, the licensee used

methods that were acceptable to validate the past operability of Emergency Core

Cooling piping when a void was discovered. However, any underlying issues in human

performance or in the operability determination process were not explored at the time.

The licensee acknowledged the inspectors observations.

Regarding the finding discussed above for the fire pump starting setpoints, the

inspectors also identified that changes had been made to the plant design basis since

the licensees previous corrective actions were completed. Pursuant to the change to

NFPA-805 standards of fire protection, additional sprinklers were added to the required

Technical Requirements Manual fire suppression systems. When this occurred, the

licensee did not re-review the impacts on the fire pump starting setpoint issue which was

the subject of the NRC finding. Based on inspector questions, the licensee re-instituted

compensatory measures to restore functionality of the fire suppression system pending

approval of new calculations that will incorporate the new systems and starting setpoints

of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire

pump surveillance tests in light of the NRC finding. The inspectors discovered the

48

licensee had already identified a discrepancy between the surveillance tests and design

requirements and had written an AR in September of 2014. Basically, a pump could

degrade to a point where it would still pass a surveillance, yet not meet all aspects of the

design calculation requirements for the fire suppression system. The licensee was able

to demonstrate the pumps had not degraded to a point outside the design requirements,

and was working to resolve the discrepancy between the tests and design requirements.

This review constituted one in-depth review of a selected issue sample as defined in

IP 71152-05.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 Dual Unit Trip Caused by Debris Intrusion in the Forebay

a. Inspection Scope

On November 1, 2014, the inspectors responded to the site following a dual unit trip

caused by debris intrusion in the forebay of the screenhouse. During the evening of

October 31, and early morning of November 1, rough lake conditions and high wind

mobilized and transported a large mass of sea grass and other debris. This debris

entered the D.C. Cook intake structure and collected on trash racks and travelling

screens in the fore bay. Prior to the unit shutdown, the licensee monitored forebay

conditions and took actions to maintain the travelling screens clean. However, the rate

of debris intrusion exceeded the equipments ability to clean the screens. As differential

pressure increased across the screens, the licensee entered the Degraded Forebay

abnormal procedure. The licensee reduced power in Unit 2 to 50 percent and secured a

circulating water pump. However, conditions in the fore bay continued to degrade to the

point that the licensee had to manually trip both units. This action allowed the licensee

to secure all circulating water pumps thus protecting the safety-related service water

system.

Following the plant trip, the licensee notified the resident inspector who responded to the

site. The inspectors verified licensee actions in the control rooms were consistent with

plant procedures. In addition, the inspectors focused on performance of safety-related

equipment supplied with service water. The inspectors concluded that the service water

system had not been impacted by the debris intrusion.

As part of the plant shutdown, several plant SSCs did not perform as expected. For

Unit 2, auto transfer between the unit auxiliary transformer and reserve auxiliary

transformer on turbine trip did not occur. Auto transfer did occur after the licensee

manually inserted a generator trip. The licensee replaced a failed relay associated with

a turbine stop valve to correct the condition. In addition, a relay on the unit two reserve

auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee

replaced this relay prior to unit startup.

On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee

throttled flow. Because both MDAFW pumps were operable, the licensee used the

MDAFW pumps for steam generator level control. The inspectors identified a finding as

documented in Section 1R15 of this report. Additionally, on Unit 2, an AFW flow control

valve appeared to not respond to a flow retention signal. The flow retention circuit acts

to prevent excessive flows to the steam generators from the AFW pumps by throttling

49

closed flow control valves. Upon investigation, given instrument tolerances, tests of the

circuitry, time delay settings, and actual measured flow, it was determined the system

acted appropriately.

In addition, three steam safety valves lifted prior to their nominal set point tolerance

band. In reviewing the condition, the licensee documented that set point surveillances

are conducted using a defined set of conditions that allow the safeties to achieve

repeatable lift setpoints. For an installed safety, several factors can influence actual lift

pressure. These factors include vibration and temperature transients. As a result, the

licensee concluded that the valves responded in a fashion consistent with the design of

the valves. The licensee plans on performing lift tests on the valves during the next

refueling outage to confirm valve operability.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

No findings were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The results of the inservice inspection were discussed with site vice president,

Mr. J. Gebbie on October 10, 2014;

  • The inspection results for the areas of radiological hazard assessment and

exposure controls; occupational ALARA planning and controls; and occupational

exposure control effectiveness performance indicator verification with

Mr. J. Gebbie, Site Vice President, on October 17, 2014;

  • The inspection results for the area of radiological hazard assessment and

exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;

  • The inspection results for the areas of radiological environmental monitoring; and

RCS specific activity and RETS/ODCM radiological effluent occurrences

performance indicator verification with Mr. J. Gebbe, Site Vice President, on

November 7, 2014;

  • The results of the inspection of the permanent removal of shield/missile blocks

with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff

on December 01, 2014; and

  • The Annual Review of Emergency Action Level and Emergency Plan Changes

with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015.

50

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

ATTACHMENT: SUPPLEMENTAL INFORMATION

51

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

L. Weber, Chief Nuclear Officer

J. Gebbie, Site Vice President

L. Baun, Director Performance Assurance

J. Beer, Principal Health Physicist

D. Bronicki, Interim Radiation Protection Manager

R. Hall, ISI Program Owner

J. Harner, Environmental Manager

G. Hill, Supervisor Nuclear Safety Analysis

S. Lies, Vice President Engineering

S. Mitchell, Regulatory Affairs

D. Miller, Health Physicist

J. Nimtz, Senior Licensing Activity Coordinator

J. Ross, Engineering Director

M. Scarpello, Regulatory Affairs Manager

P. Schoepf, Nuclear Site Services Director

R. Sieber, Emergency Preparedness Manager

Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

R. Daley, Chief, Engineering Branch 3

B. Dickson, Chief, Health Physics and Incident Response

N. Feliz-Adorno, Reactor Engineer

J. Gilliam; Reactor Engineer

M. Mitchell, Health Physicist

Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000315/2014005-01 NCV Failure to Identify Conditions Adverse to Quality

associated with the Unit 1 TDAFW Pump Turbine Oil

System (Section 1R15.b(1))05000315/2014005-02; NCV Unplanned Inoperability of the AB Fuel Oil Storage Tank

05000316/2014005-02 during Maintenance (Section 1R15.b(2))05000315/2014005-03; NCV Inadequate Review of Radiological Impact of the Removal

05000316/2014005-03 of the Auxiliary Shield Blocks on the Containment

Accident Shield Post LBLOCA (Section 1R18)05000315/2014005-04 NCV Inadvertent Trip of the Unit 1 TDAFW Pump

(Section 1R19)05000315/2014005-05 URI Changes to Minimum 60-Minute Emergency Responder

Staffing Without Prior Approval (Section 1EP4)05000315/2014005-06; NCV Failure To Identify Deficient Locked High Radiation Area

05000316/2014005-06 Controls Due To Procedure Inadequacy (Section 2RS1.4)

Closed

05000315/2014005-01 NCV Failure to Identify Conditions Adverse to Quality

associated with the Unit 1 TDAFW Pump Turbine Oil

System (Section 1R15.b(1))05000315/2014005-02; NCV Unplanned Inoperability of the AB Fuel Oil Storage Tank

05000316/2014005-02 during Maintenance (Section 1R15.b(2))05000315/2014005-03; NCV Inadequate Review of Radiological Impact of the Removal

05000316/2014005-03 of the Auxiliary Shield Blocks on the Containment

Accident Shield Post LBLOCA (Section 1R18)05000315/2014005-04 NCV Inadvertent Trip of the Unit 1 TDAFW Pump

(Section 1R19)05000315/2014005-06; NCV Failure To Identify Deficient Locked High Radiation Area

05000316/2014005-06 Controls Due To Procedure Inadequacy (Section 2RS1.4)

Discussed

None

2

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22

- AR-2014-14403, 12-HV-DGH Appears to Have Failed

- Cook Seasonal Readiness Affirmation Letter, November 11, 2014

- PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22

1R04 Equipment Alignment

- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24

- 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4,

Revision 14

- AR-2014-14089, CTS Nozzle Leaking

- AR-2014-8502, Possible PORV Leakby

- Drawing OP-1-5144-51, Containment Spray

- Drawing OP-2-5105D-22, Steam Generating System

- Drawing OP-2-5106A-55, Aux Feedwater

- List of Open Work Orders, Unit 1 Containment Spray System

1R05 Fire Protection

- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room

- AR-2014-12540, Unattended Test Equipment

- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011

- Fire Hazards Analysis, Revision 16

- PMP-2270-CCM-001, Control of Combustible Materials, Revision 24

- PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23

1R06 Flooding

- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area,

April 4, 1971

1R07 Heat Sink Performance

- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9

- D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection

Program, March 10, 2003

- Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger

- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related

Equipment, July 18, 1989

3

1R08 Inservice Inspection Activities

- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5

- 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII,

Supplement 10 Dissimilar Metal Welds, Revision 0

- 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6

- 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6

- 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10

- AR 2012-12105, Water Pooling Around U2 CST

- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak

- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak

- AR 2013-4625, 1-CS-448-1 has a BA Leak

- AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage

- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting

- AR 2013-6540, 1-SF-160 Leaking at Diaphragm

- AR 2013-6839, U1C25 Refueling Cavity Leakage

- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet

- AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min

- AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas

- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211

- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage

- AR 2013-8587, U1 Seal Table Thimble Leakage Identified

- AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm

- AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing

- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping

- AR 2014-11339, Piping Wall Loss Near 1-WCR-942

- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance

- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum

- AR 2014-11519, Two Data Points In Piping Found Below Design Minimum

- AR 2014-11664, NESW Pipe Wall Below Manufacturers Tolerance

- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000

- AR 2014-12160, Technician Understanding of Range of Coverage Questioned

- AR 2014-12162, NRC Inservice Inspection Observation

- AR 2014-1218, AR for Boric Acid Leak Not Properly Screened

- AR 2014-12384, NRC Observation During U1 Inservice Inspection

- AR 2014-3762, Previously Identified BA Leak on 1-SI-128

- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014

- ETSS No. 1, Bobbin Coil, Revision 0

- ETSS No. 2, 3 Coil MRPC, Revision 0

- LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and

Dissimilar Metal Welds, Revision 0

- LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7

- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic

Piping Welds, Revision 0

- PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure

Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C

- PMI-5070, Inservice Inspection, Revision 21

- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17

- PQR 136, ASME Procedure Qualification Record, Revision 1

- PQR 219, ASME Procedure Qualification Record, Revision 1

- PQR 256, ASME Procedure Qualification Record, Revision 1

4

- PQR 258, ASME Procedure Qualification Record, Revision 1

- QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3

- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0

- S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site

Technique Validation, Revision 0

- U1-MT-14-001, Magnetic Particle Examination, October 4, 2014

- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014

- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014

- U1-VE-14-003, Ultrasonic Examination, October 2, 2014

- U1-VE-14-004, Ultrasonic Examination, October 2, 2014

- U1-VE-14-014, Ultrasonic Examination, October 8, 2014

- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0 in Thickness,

Revision 2

- WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014

- WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013

- WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012,

March 8, 2013

- WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013

- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z

- WPS 8.12T, Welding Procedure Specification, Revision 1

- WPS 8.1TS, Welding Procedure Specification, Revision 4

1R11 Licensed Operator Requilification Program

- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25

- November 19, 2014, Training Exercise Guide and Drill Guide

- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4

1R12 Maintenance Effectiveness

- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11

- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11

- 2012-2013 AMSAC, Unavailability Hours Reports

- AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown

- AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open

- AR 2012-14364-1, 1-NRI-16 Found Out of Spec

- AR 2012-16048, 1-URV-125 Failed Drop Test

- AR 2012-4275, Steam Dump System Operation

- AR 2013-10252, 1-URV-136 Failed Drop Test

- AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance

- AR 2013-1164, 2-MRV-212 Failed Stroke Time

- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit

- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance

- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral

- AR 2013-4320, 1-URV-110 Failing to Open

- AR 2013-4349, 1-URV-112 Failed to Open When Required

- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D

- AR 2013-5060, 1-URV-111 Would not Stroke During Testing

- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times

- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded

- AR 2014-0045, 2-URV-120 Failed Drop Test

5

- AR 2014-11324, Steam Dumps Did Not Operate Per Procedure

- AR 2014-11739, Critical Parameter Found Out of Tolerance

- AR 2014-12621, 1-URV-112 Drop Test Failed

- AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle

- AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25

- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process

- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process

- AR 2014-15004, As Found Data Out of Tolerance

- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement

- AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT

- AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve

- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013

- AR-2013-12121, RPI Failure Rod D8, August 19, 2013

- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013

- AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013

- AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013

- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013

- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,

October 23, 2014

- ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document,

Revision 1

- GT 2013-11467, U2 MS Maintenance Rule Action Tracking

- GT 2013-11615, 2013 Main Steam System Vulnerability Review

- Maintenance Rule Scoping Document, AMSAC System, Revision 1

- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3

- Maintenance Rule Scoping Document, Main Steam System, Revision 3

- Plant Health Committee Top Ten Equipment Issues, November 19, 2014

- System Health Report, Main Steam, Unit 1 and Unit 2, 3rd Quarter 2014

- Topical Report WCAP-7571, Rod Position Monitoring

- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014

- Various 2012-2013 AMSAC System Health Reports

- Various Operator Logs, October-November 2014

- Various System Health Reports, AMSAC

1R13 Maintenance Risk Assessments and Emergent Work Control

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22

- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18

- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak

- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut

- AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration

- Drawing 2-OP-5113-83, Essential Service Water

- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room

Coolers, October 23, 2000

- Operating Logs, Week of November 30, 2014

- Part 1 Risk Assessments, Week of November 30, 2014

- PMP-2291-OLR-001, Online Risk Management, Revision 30

- Temporary Modification 2-TM-14-81, AFW Room Coolers

- WO 55457007-07, Install 2-TM-14-81

- WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection

6

1R15 Operability Determinations

- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13

- 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves,

November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System

Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2

- AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown

- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed

- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014

- AR-2014-7259, Question from NRC Sr. Resident still not Resolved

- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms

- DB-12-AFWS, Auxiliary Feedwater System, Revision 5

- Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003

- Drawing E-8708, 765kV Schematic, Revision 5

- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram

- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram

- Drawing OP-2-98101-34, Turbine Control Elementary Diagram

- EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26

- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25

- FSAR Section 8.0, Electrical Systems, Revision 25

- FSAR Section 8.3, Station Service Systems, Revision 25

- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003

- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979

1R18 Plant Modifications

- AR 2014-13016, Accident Shield Requirements

- Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources,

Revision 06

- Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates,

Revision 03

- Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01

- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including

Revision 23

- Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal

Project, Revision 00

- NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2

- PMI-601, Radiation Protection Plan, Revision 20

- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003

- PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment

Access Hatch, Revision 00

1R19 Post-Maintenance Testing

- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7

- 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8

- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9

- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11

- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8

- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9

- 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32

7

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34

- 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3

- 1-OHP-4030-156-017T, TDAFW System Test, Revision 16

- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1

- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed

- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip

- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted

- AR-2014-14188, Failure in Synch Circuit for 2A7

- DB-12-AFWS, Auxiliary Feedwater System, Revision 5

- Drawing 1-OP-5106A-61, Auxiliary Feedwater

- Drawing E-8708, 765kV Schematic, Revision 5

- Drawing OP-2-5106A-55, Auxiliary Feedwater

- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram

- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram

- Drawing OP-2-98101-34, Turbine Control Elementary Diagram

- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear

Power Plants (NCIG-11)

- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25

- FSAR Section 8.0, Electrical Systems, Revision 25

- FSAR Section 8.3, Station Service Systems, Revision 25

- Gasket Technical Data Sheets for 1CD EDG Aftercooler

- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems

- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps

- Plant Computer Printouts, AFW system, November 1, 2014

- PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25

- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage

- Terry Turbine Vendor Manual

- WO 55425039-15, Investigate Governor Valve

- WO 55432038-01, Replace 1-CRID-3-INV diodes

- WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay

1R20 Outage Activities

- 12-EHP-4030-002-356, Low Power Physics Tests with Dynamic Rod Worth Measurement,

Revision 11

- 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System,

Revision 27

- 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11

- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11

- 1-OHP-4021-001-002, Reactor Startup, Revision 52

- 1-OHP-4021-001-003, Power Reduction, Revision 55

- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72

- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25

- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4030-127-037, Refueling Surveillance, Revision 20

- 1-OHP-4030-127-041, Refueling Integrity, Revision 25

- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35

- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20

8

- 2-OHP-4021-001-002, Reactor Startup, Revision 51

- 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60

- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24

- AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014

- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,

October 23, 2014

- DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of

Shutdown Cooling

- Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System

- Forced Outage Schedule, November 4, 2014

- PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4

- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4

- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800

- Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed

- Tagout R-CRID-CRD4-0069, 120VAC Control Room

- UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25

- Unit 1 Post Trip Review Report, November 1, 2014 Trip

- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical

Maintenance Departments

1R22 Surveillance Testing

- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8

- 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance,

Revision 17-18

- 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16

- 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19

- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35

- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room

Emergency Ventilation Surveillance

- AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force

- AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec

- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test

- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low

- AR-2014-12633, N SI Pump Calculated dP high

- AR-2014-12652, South SI Pump dP High Above Action Limit

- DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room

Air Conditioning System

- Drawing OP-1-5149-48, Control Room Ventilation Unit 1

- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features,

Revision 15

- Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year

Interval, Revision 1

- WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014

- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014

- WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014

1EP4 Emergency Action Level and Emergency Plan Changes

- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing

- AR 2014-15685, Potential EP Finding

9

- Emergency Plan, Revision 18, 19, 32, 33, 34, and 35

- PMI-2080, Emergency Plan and Implementing Procedures, Revision 18

- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes,

March 5, 2003

2RS1 Radiological Hazard Assessment and Exposure Controls

- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15

- 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28

- 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34

- 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8

- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36

- 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19

- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6

- 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7

- 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger

Room and Shot Plan of Elevation 609 E/W Hallway, October 10, 2014

- AR 2013-13969, Electronic Dosimeter Setpoints Often Set Considerably Higher Than Actual or

Expected Radiological Conditions

- AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High

- AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP

- AR 2014-11975, Dose Alarm

- AR 2014-8964, Rad Worker Deficiency

- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained

in Process

- AR 2014-9764, A Review of ED Setpoints

- CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013

- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013

- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014

- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23

- PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of

the Rx Pit, October 16, 2014

- PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19

- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant

Restricted Areas, Revision 0

- RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0

- RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change

Modifications and Support Work, Revision 0

- RWP 141123, Install, Remove, Modify Temporary Shielding in Unit-1 Containment, Auxiliary

Building and Plant Restricted Areas, and ALARA Plan, Revision 0

- RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2

- RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2

- RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0

- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0

- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit,

October 16, 2014

- SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey

- THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process,

Revision 14

- Work Order Package 55446099 01, RP Perform Semiannual Source Inventory,

August 7, 2014

10

2RS2 Occupational ALARA Planning and Controls

- ALARA Committee Meeting; A-14-33F; October 15, 2014

- D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014

- Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014

- PMP-6010-ALA-001; ALARA Program - Review of Plant Work Activities; Revision 27

2RS7 Radiological Environmental Monitoring Program

- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2

- 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007

- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010

- 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007

- 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007

- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel

Calibration, Revision 0

- 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000

- 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009

- 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision

Software, Revision 002

- 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013

- Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant

Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013

- AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours

- AR 2013-15116, MET Tower Data Recovery

- AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD

Collection and Change Out, TLD T-11 Could Not Be Located

- AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours

- AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours

- AR 2014-10063, 12-ELR-400, East Bucket Heater Broken

- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No

Longer Produce Milk

- AR 2014-13656, Trace Cesium-137 in Broadleaf Sample

- AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24),

Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental

Monitoring Program (REMP) Surface Water Samples,

- AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1

Lost Power for Approximately 39 minutes

- AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental

Monitoring Program (REMP) Data

- AR 2014-8622, Primary Met Tower Carriage Control Switch

- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6

- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal

and Radiation Protection System, Revision 25.0

- PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and

Offsite Dose Calculation Manual, March 1, 2013

- PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24

- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014

11

4OA1 Performance Indicator Verification

- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook

Plant, July, 2013 to September 14, 2014

- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly

Operation Report Data, Reactor Coolant System Specific Activity, Revision 15

- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly

Operating Report Data, Revision 15

4OA2 Identification and Resolution of Problems

- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6

- AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room

- AR 2014-9531, 1-152-CICE4-2A Out of Position

- AR-2012-8187, Adequacy of Past Operability Questioned

- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation

- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411

- AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs

- AR-2014-14920, Racking Interlocks Potential to not Properly Reset

- AR-2014-14951, Primary Coolant Filters Wrong Parts

- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing

- AR-2014-15059, Cable 2-8167G Low Megger Readings

- AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand

- GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014

- Performance Assurance Audit PA-14-07, Operations, August 25, 2014

- Performance Assurance Quarterly Report, April - June 2014

- Performance Assurance Quarterly Report, July - September 2014

- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage,

November 3, 2014

- Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014

- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014

- Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014

4OA3 Identification and Resolution of Problems

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- AR 2014-13669 Task 2, Unit 1 Post-trip Report

- AR 2014-13669 Task 3, Unit 2 Post-trip Report

- E-0, Reactor Trip or Safety Injection, Revision 38

- ES-0.1, Reactor Trip Response, Revision 28

- Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report,

December 22, 2014

12

LIST OF ACRONYMS USED

ADAMS Agencywide Document Access Management System

AFW Auxiliary Feedwater

ALARA As-Low-As-Reasonably-Achievable

AMB Auxiliary Missile Blocks

AR Action Request

ASME American Society for Mechanical Engineers

BACC Boric Acid Corrosion Control

CAP Corrective Action Program

CAQ Condition Adverse to Quality

CDF Core Damage Frequency

CFR Code of Federal Regulations

dpm drops per minute

EAC Environmental Assessment Coordinator

EDG Emergency Diesel Generator

EPRI Electric Power Research Institute

ET Eddy Current

FME Foreign Material Exclusion

FOST Fuel Oil Storage Tank

ISI Inservice Inspection

LBLOCA Large Break Loss-of-Coolant Accident

LHRA Locked High Radiation Area

LOCA Loss-of-Coolant Accident

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report

LCO Limiting Condition for Operation

MDAFW Motor-Driven Auxiliary Feedwater

MSPI Mitigating Systems Performance Index

NCV Non- Violation

NDE Non-destructive Examination

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

PARS Publicly Available Records System

PI Performance Indicator

RAC Radiological Assessment Coordinator

RCS Reactor Coolant System

RG Regulatory Guide

RPT Radiation Protection Technician

SDP Significance Determination Process

SG Steam Generator

SRA Senior Reactor Analyst

SSC Structure, System and Component

TDAFW Turbine-Driven Auxiliary Feedwater

TS Technical Specification

13

TTV Trip and Throttle Valve

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

UT Ultrasonic Test

WO Work Order 14

L. Weber -2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy

of this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket Nos. 50-315; 50-316

License Nos. DPR-58; DPR-74

Enclosure:

IR 05000315/2014005; 05000316/2014005

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

DISTRIBUTION w/encl:

Kimyata MorganButler Carole Ariano

RidsNrrDorlLpl3-1 Resource Linda Linn

RidsNrrPMDCCook Resource DRPIII

RidsNrrDirsIrib Resource DRSIII

Cynthia Pederson Jim Clay

Darrell Roberts Carmen Olteanu

Eric Duncan ROPreports.Resource@nrc.gov

Allan Barker

ADAMS Accession Number:

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII-EICS RIII RIII

NAME NS:rj PLougheed for KRiemer

EDuncan

DATE 02/09/15 02/09/15 02/10/15

OFFICIAL RECORD COPY