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{{#Wiki_filter:U.S.NUCLEAR REGULATORY COMMISSION NRC a~lRM 366 tu-'r7)-15 79-005/03L-0 LICENSEE EVENT REPORT I (CAR 1209)~O 7 8 CON'T~OT 7 8 Qi (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 0 0 0 0 0-0 OQ24 1 1 1 1QE~QE LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CONTROL BLOCK: 1 NYREG1Q200 9 LICENSEE CODE 14 15~LQB 0 5 0 0 0 2 4 4 Q7 0 2 0 6 7 9 Qs 0 3 0 6 7 9 QB 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES IO After RHR system hydro test containment recirc sump outlet MOV 851B failed'to re-open (T.S.5.9.2.b2)Its redundant counterpart had been successfully cycled and returned to the normal open position.As discussed in Cause Description, MOV 851B was~OS closed for the test only and operated properly on the second attempt.This was moni-tored by maintenance personnel after they had examined conditions and found no apparent reason for failure.~OS 7 8 9 80~OB 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~>>QTT E Q" L~JO>>V A I.V 0 F Q14~AQ75~ZQ75 9 10 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LEAIAO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPQRT~79+~00 5+~~03+L 0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPAD.4 PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
{{#Wiki_filter:NRC a~lRM 366                                                                                                                      U. S. NUCLEAR REGULATORY COMMISSION tu-'r7) -15                                                                           79-005/03L-0 LICENSEE EVENT REPORT I                       (CAR 1209)
~ZQPR~ZQPR~ZQEO~ZQ>>0 0 0 0~NQ22~NQ24~NQ25 L 2 0 0 Qss 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 Flexibility of long extension rod between Limitorque SMB-00 operator and valve possibly allowed valve to close tighter than required.First attempted opening stopped on overtorque but relieved overtorque condition permitting proper opening on second further problems.80 7 8 9 FACILITY STATUS'¹POWER OTHER STATUS Q E 0 8 8 NA METHOD OF DISCOVEAY DISCOVERY DESCRIPTION Q32~BQ31 Performing RHR Hydro 44 45 46 5 Q25~Q25 7 8 9 10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q~6~Z Q33 Z Q34 NA 7 8 9 10 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q30~OO O Q27~ZQRR NA 7 8 9 11 12 13 PERSONNEL INJURIES 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION 5~ZQ42 NA 7 8 9 10 PUBI.ICITY 7 8 9 10 80 LOCATION OF RELEASE Q36 NA 80 45 44 80 80 80 NRC USE ONLY>908 1800-'I'68 69 80 45 PHDNE 7 1 6 54 6-2 700, ext~2 9 1-2 1 5 S.Spector NAME OF PREPARER 3 attempt~.Va lve wi 1 1 continu e to be stroked monthly and timed quarterly to identify any}}
CONTROL BLOCK:                                                Qi                 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1                                  6
  ~O 7        8    9 NYREG1Q200 LICENSEE CODE              14      15 0     0     0   0 LICENSE NUMBER 0     0       OQ24 25      26 1     1 LICENSE TYPE 1     1QE~QE 30   57 CAT 58 CON'T
  ~OT                              ~LQB           0   5       0     0   0     2     4   4   Q7     0     2   0   6     7     9 Qs         0     3     0   6   7   9   QB 7        8                      60           61               DOCKET NUMBER               68     69       EVENT DATE             74       75       REPORT DATE         80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                               IO After RHR system hydro test containment recirc sump outlet MOV 851B failed'to re-open (T.S. 5.9.2.b2)                   Its redundant counterpart had been successfully cycled and returned to the normal open position. As discussed in Cause Description, MOV 851B was
  ~OS               closed for the test only and operated properly on the second attempt.                                                                     This was moni-tored by maintenance personnel after they had examined conditions and found no apparent reason for failure.
  ~OS 7         8 9                                                                                                                                                                         80 SYSTEM             CAUSE         CAUSE                                                         COMP.           VALVE CODE               CODE       SUBCODE                   COMPONENT CODE                     SUBCODE           SUBCODE
  ~OB                                ~>>QTT     10 E Q"       L~JO>>             V A         I. V     0   F     Q14       ~AQ75           ~ZQ75 7        8                        9                                     12             13                               18           19               20 SEQUENTIAL                         OCCURRENCE             REPORT                       REVISION Q17 LEAIAO REPQRT ACTION FUTURE EVENT YEAR
                                        ~79 21        22 EFFECT
                                                              +23 SHUTDOWN
                                                                            ~00 24 REPORT NO.
5 26
                                                                                                      +~
27
                                                                                                                    ~03 28 ATTACHMENT CODE 29 NPAD.4 TYPE
                                                                                                                                            +L 30 PRIME COMP.
31 NO.
32 0
COMPONENT TAKEN ACTION                   ON PLANT           METHOD                   HOURS Q22         SUBMITTED         FORM SUB.         SUPPLIER           MANUFACTURER
                  ~ZQPR ~ZQPR                   ~ZQEO             ~ZQ>>               0   0     0     0       ~NQ22             ~NQ24             ~NQ25             L   2   0     0   Qss 33         34                 35                 36             37                   40     41               42                 43             44                 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 Flexibility of long extension                             rod between Limitorque SMB-00 operator and valve attempt possibly allowed valve to close tighter than required. First attempted opening stopped on overtorque but relieved overtorque condition permitting proper opening on second 3
                                    . Va lve      wi1 1 continu e to be stroked monthly and timed quarterly to identify any further problems.
7         8     9                                                                                                                                                                       80 FACILITY
                                    '¹ POWER                                         Q        METHOD OF 7
5 8
STATUS 9
E   Q25    ~Q25 10 0 8 8 12      13 OTHER STATUS NA 44 DISCOVEAY
                                                                                                  ~BQ31 45        46 Performing RHR Hydro DISCOVERY DESCRIPTION Q32 80 ACTIVITY CONTENT
~6 RELEASED OF RELEASE
                ~Z      Q33      Z AMOUNT OF ACTIVITY NA Q                                       NA LOCATION OF RELEASE Q36 Q34 7         8   9               10                                                       44            45                                                                              80 PERSONNEL EXPOSURES NUMBER               TYPE       DESCRIPTION Q30
                ~OO             O Q27     ~ZQRR               NA 7         8   9               11       12         13                                                                                                                               80 PERSONNEL INJURIES 7         8   9               11       12                                                                                                                                           80 LOSS OF OR DAMAGE TO FACILITY TYPE         DESCRIPTION                   Q43 5       ~ZQ42                                           NA 7         8     9           10                                                                                                                                                         80 PUBI.ICITY
                                                                                                >   908 1800-'I'                                                 NRC USE ONLY 7        8    9          10                                                                                                                    68   69                             80   45 NAME OF PREPARER                            S. Spector                                                PHDNE 7 1 6         54 6-2 700, ext       ~ 2 9 1 -2 1 5}}

Latest revision as of 18:08, 29 October 2019

LER 79-005/03L-0 on 790206:containment Recirculation Sump Failed to Reopen After Hydro Testing.Caused by Flexibility of Long Extension Rod Between Limitorque SMB-00 Operator & Valve.Valve Stroked Monthly & Timed Quarterly
ML17261A107
Person / Time
Site: Ginna Constellation icon.png
Issue date: 03/06/1979
From: Spector S
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17244A394 List:
References
LER-79-005-03L, LER-79-5-3L, NUDOCS 7903120294
Download: ML17261A107 (2)


Text

NRC a~lRM 366 U. S. NUCLEAR REGULATORY COMMISSION tu-'r7) -15 79-005/03L-0 LICENSEE EVENT REPORT I (CAR 1209)

CONTROL BLOCK: Qi (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

~O 7 8 9 NYREG1Q200 LICENSEE CODE 14 15 0 0 0 0 LICENSE NUMBER 0 0 OQ24 25 26 1 1 LICENSE TYPE 1 1QE~QE 30 57 CAT 58 CON'T

~OT ~LQB 0 5 0 0 0 2 4 4 Q7 0 2 0 6 7 9 Qs 0 3 0 6 7 9 QB 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES IO After RHR system hydro test containment recirc sump outlet MOV 851B failed'to re-open (T.S. 5.9.2.b2) Its redundant counterpart had been successfully cycled and returned to the normal open position. As discussed in Cause Description, MOV 851B was

~OS closed for the test only and operated properly on the second attempt. This was moni-tored by maintenance personnel after they had examined conditions and found no apparent reason for failure.

~OS 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OB ~>>QTT 10 E Q" L~JO>> V A I. V 0 F Q14 ~AQ75 ~ZQ75 7 8 9 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LEAIAO REPQRT ACTION FUTURE EVENT YEAR

~79 21 22 EFFECT

+23 SHUTDOWN

~00 24 REPORT NO.

5 26

+~

27

~03 28 ATTACHMENT CODE 29 NPAD.4 TYPE

+L 30 PRIME COMP.

31 NO.

32 0

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~ZQPR ~ZQPR ~ZQEO ~ZQ>> 0 0 0 0 ~NQ22 ~NQ24 ~NQ25 L 2 0 0 Qss 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 Flexibility of long extension rod between Limitorque SMB-00 operator and valve attempt possibly allowed valve to close tighter than required. First attempted opening stopped on overtorque but relieved overtorque condition permitting proper opening on second 3

. Va lve wi1 1 continu e to be stroked monthly and timed quarterly to identify any further problems.

7 8 9 80 FACILITY

'¹ POWER Q METHOD OF 7

5 8

STATUS 9

E Q25 ~Q25 10 0 8 8 12 13 OTHER STATUS NA 44 DISCOVEAY

~BQ31 45 46 Performing RHR Hydro DISCOVERY DESCRIPTION Q32 80 ACTIVITY CONTENT

~6 RELEASED OF RELEASE

~Z Q33 Z AMOUNT OF ACTIVITY NA Q NA LOCATION OF RELEASE Q36 Q34 7 8 9 10 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q30

~OO O Q27 ~ZQRR NA 7 8 9 11 12 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 5 ~ZQ42 NA 7 8 9 10 80 PUBI.ICITY

> 908 1800-'I' NRC USE ONLY 7 8 9 10 68 69 80 45 NAME OF PREPARER S. Spector PHDNE 7 1 6 54 6-2 700, ext ~ 2 9 1 -2 1 5