ML17317B114: Difference between revisions

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{{#Wiki_filter:NRC FORM 366 U.S.NUCLEAR REGULATORY COMMISSION
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{7-77)ENSEE EVENT REPORT~\CONTRIRIL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6[oatj II I 0 C C I Q 0 0 0 0 0 0 0 0 0 0 0 Q4 1 I 1 I O~Q 7 8 9 LICENSEE CODE 14 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T~o1"""~LQB 0 5 0 0 0 3 1 5 Q70 3 2 7 7 9 QB 0 4 I 7 7 Qe 7 8 60 61 DOCKET NUMBER 68 69'VENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO WHI E IN MODE 1 THE PRESSURE IN THE R ACT R C A BEL W 2220 PSIA~O3~O4 CONTRARY TO TECH.SPEC.3.2.5.b.ACTION STATES RESTORE WITHIN 2 HOURS.PRESSURE WAS BELOW LIMIT FOR 6 MINUTES AND LOWEST PRESSURE ATTAINED WAS 2190 PSIA.NO~OS PROBABLE CONSEQUENCES.
~OB~OB 80 7 8 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~CB Qll A Q12~A Q13: Z Z Z Z~Z Z Qll~Z Q15~Z Qlg 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.CODE TYPE NO.Qll REPoRT M29 U~M U~M0'C-U 21 22 23 24 26 27 28 29 30'31 1 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENTP NPRDP PRIME COMP, COMPONENT TAKEN ACTION ON PLANT METHOD HOURS+22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
~HQ15~Hog~ZQ25+2QET 0 0 0 ll+N Q23~NQ24~2 Q25 Z 9 9 9 QEg 33 34 35 36 37 40, 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o WHEN ATTEMPTING TO LEED P HE EA T R OP RATOR INADVE TENTL P N D RV-51.VALVE WAS CLOSED ON DISCOVERY THAT IMPR P ALVE WAS OPENED.OPERATORS 3 HAVE BEEN INSTRUCTED THAT CARE MUST BE OBSERVED WHEN OPERATING CONTROLS.4 METHOD OF OTHER STATUS~DISCOVERY NA~AQ31 44 45 45 44 NAME OF PREPARER JAMES D.DICKSON 7 8 9 FAG I LI ETY STATUS,--.'A POWER~l5 Ei Q25~IO 0 Q29 7 8 9 10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q36 ZZ uZQ33~Q34 NA 7 8 9 10 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39~l~~00 0 QET~EQ35 NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION 41 Pap~OO 08 NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION 9 Z Q42 NA 7 8 9 10 P U 8 L I CITY ISSUED DESCRIPTION
~S KZ Ladle 7 8 9 10 1 DISCOVERY DESCRIPTION Q32 OPERATOR OBSERVATION LOCATION OF RELEASE Q NA 80 80 80 80 80 80 NRC USE ONLY Eg O 80 45 0 68 69 (616)465-5901 ZO"K'(27 387
~~4~e}}

Revision as of 06:22, 24 October 2019

LER 79-021/03L-0 on 790327:pressure in RCS Was Found Below Tech Spec Limit While in Mode 1.Caused by Operator Inadvertantly Opening Auxiliary Spray Valve to Pressurizer QRV-51.Valve Closed Upon Discovery
ML17317B114
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/17/1979
From: Dickson J
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B111 List:
References
LER-79-021-03L, LER-79-21-3L, NUDOCS 7904240387
Download: ML17317B114 (2)


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