05000315/LER-1979-021-03, /03L-0 on 790327:pressure in RCS Was Found Below Tech Spec Limit While in Mode 1.Caused by Operator Inadvertantly Opening Auxiliary Spray Valve to Pressurizer QRV-51.Valve Closed Upon Discovery

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/03L-0 on 790327:pressure in RCS Was Found Below Tech Spec Limit While in Mode 1.Caused by Operator Inadvertantly Opening Auxiliary Spray Valve to Pressurizer QRV-51.Valve Closed Upon Discovery
ML17317B114
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/17/1979
From: Dickson J
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B111 List:
References
LER-79-021-03L, LER-79-21-3L, NUDOCS 7904240387
Download: ML17317B114 (2)


LER-1979-021, /03L-0 on 790327:pressure in RCS Was Found Below Tech Spec Limit While in Mode 1.Caused by Operator Inadvertantly Opening Auxiliary Spray Valve to Pressurizer QRV-51.Valve Closed Upon Discovery
Event date:
Report date:
3151979021R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION

{7-77)

ENSEE EVENT REPORT

~ \\

CONTRIRIL BLOCK:

Q1 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 1 6

[oatj II I

0 C

C I Q 0

0 0

0 0

0 0

0 0

0 0 Q4 1

I 1

I O~Q 7

8 9

LICENSEE CODE 14 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T

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""" ~LQB 0

5 0

0 0

3 1

5 Q70 3

2 7

7 9

QB 0

4 I

7 7

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8 60 61 DOCKET NUMBER 68 69

'VENTDATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO WHI E IN MODE 1

THE PRESSURE IN THE R ACT R

C A

BEL W 2220 PSIA

~O3

~O4 CONTRARY TO TECH.

SPEC. 3.2.5.b.

ACTION STATES RESTORE WITHIN 2 HOURS.

PRESSURE WAS BELOW LIMIT FOR 6 MINUTES AND LOWEST PRESSURE ATTAINED WAS 2190 PSIA.

NO

~OS PROBABLE CONSEQUENCES.

~OB

~OB 80 7

8 7

8 SYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

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Z Z

Z Z

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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.

CODE TYPE NO.

Qll REPoRT M29 U ~M U~

M0'C U

21 22 23 24 26 27 28 29 30

'31 1

32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENTP NPRDP PRIME COMP, COMPONENT TAKEN ACTION ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTURER

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9 QEg 33 34 35 36 37 40, 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o

WHEN ATTEMPTING TO LEED P HE EA T R

OP RATOR INADVE TENTL P

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RV-51.

VALVE WAS CLOSED ON DISCOVERY THAT IMPR P

ALVE WAS OPENED.

OPERATORS 3

HAVE BEEN INSTRUCTED THAT CARE MUST BE OBSERVED WHEN OPERATING CONTROLS.

4 METHOD OF OTHER STATUS ~

DISCOVERY NA

~AQ31 44 45 45 44 NAME OF PREPARER JAMES D.

DICKSON 7

8 9

FAGILIETY STATUS,--.'A POWER

~l5 Ei Q25 ~IO 0

Q29 7

8 9

10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ36 ZZ uZQ33

~Q34 NA 7

8 9

10 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39

~l~ ~00 0

QET ~EQ35 NA 7

8 9

11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION 41 Pap ~OO 08 NA 7

8 9

11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE

DESCRIPTION

9 Z

Q42 NA 7

8 9

10 P U8 LICITY ISSUED DESCRIPTION ~S KZ Ladle 7

8 9

10 1

DISCOVERY DESCRIPTION Q32 OPERATOR OBSERVATION LOCATIONOF RELEASE Q NA 80 80 80 80 80 80 NRC USE ONLY EgO 80 45 0

68 69 (616) 465-5901 ZO "K'(27 387

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