ML17331A469: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(3 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 10/03/1980
| issue date = 10/03/1980
| title = LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
| title = LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
| author name = MURPHY C E
| author name = Murphy C
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRCFORM366P.77)LlCENSEEEVENTREPORTU.S.NUCLEARREGULATORY COMMISSION (PLEASEPRINTORTYPEALLREQUIREDINFORMATION) 03Q4~Qs2526LICENSETYPE3057CAT58908Q9QEVENTDATE7475REPORTDATE80CONTROLBLOCK:Q1I6MIDCC2Q200789LICENSEECODE1415LICENSENUMBERCON'TsoURGE~LQB05000316Q70786061DOCKETNUMBER6869EVENTDESCRIPTION ANDPROBABLECONSEQUENCES Q10~02WHIEPERFORMING ASURVEIAEESTTO~03MAINTENANCE THEPUMPWASUNSTABLEANDDECLAREDINOPERABLE.
{{#Wiki_filter:NRC FORM 366                                                                                                                          U. S. NUCLEAR REGULATORY COMMISSION P.77)
THEREDUNDANT RH~04WASOPERABLE.
Ll    CENSE E    EV EN T R E PORT CONTROL BLOCK:                                                    Q1                (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
THISISTHEFIRSTEVENTOFTHISTYPE.~06~06~07~0878980~0978SYSTEMCAUSECAUSECOMP.VALVECODECODESUBCODECOMPONENT CODESUBCODESUBCODEFQTTL~LQLZJQ>>Z'ZZZZQE4~ZQTE~ZQTR910111213181920SEQUENTIAL OCCURRENCE REPORTREVISIONLER]RPEVENTYEARREPORTNO.CODETYPENO.Q17REPORT~3Q2122232426272829303132ACTIONFUTUREEFFECTSHUTDOWNATTACHMENT NPRDPPRIMECOMP.COMPONENT TAKENACTION'NPLANTMETHODHOURSQ22SUBMITTED FORMSUB.SUPPLIERMANUFACTURER
I                                    6 7      8    9 M    I    D LICENSEE CODE C      C      2Q2 14    15 0  0 LICENSE NUMBER                      25 03 26      LICENSE TYPE        30 Q4~ 57 CAT 58 Qs CON'T 7        8 soURGE      ~LQB 60            61 0    5    0    0    0 DOCKET NUMBER 3    1  6 68 Q7 69 0    9    0 EVENT DATE              74 Q 8 75      REPORT DATE            80 Q9 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                  Q10
~0QTR~ZQ15~ZQ25~ZQ210000~NQ22~NQ24~ZQ25Z999Q>>33343536,37404142434447CAUSEDESCRIPTION ANDCORRECTIVE ACTIONSQ27oTHETESTPROCEDURE DID"PVIFTHEPROEOUREWASHGRWSTWHICHSWEEPSTHEAIROUTOFTHEHEATEXCHAG3THERHRSYSTEMHASBEENDRAINEDANOREFILLEDTWICESIE~14CHANGEDPROCEDURE RETURNEDTHESYSTEMTOSERVICEWITH0DIFFI.ULTY.789FACILITYSTATUS99POWEROTHERSTATUSQI5E28100294478o7891112LOSSOFORDAMAGETOFACILITY43TYPEDESCRIPTION ZP42910PUBLICITY ISSIIEPDESCRIPTION
~02              WHI E PERFORMING A SURVEI                                A      E    EST TO
~+NQnn9'0NAMEPFPREPARER~E~MURPHYNACCIMQ~QACTIVITYCONTENTRELEASEDOFRELEASEAMOUNTOFACTIVITY~s~ZQss~ZQ54NA789101145PERSONNEL EXPOSURES NUMBERTYPEDESCRIPTION Q39Lo¹0JQETzQ>>NA789111213PERSONNEL, INJURIESNUMBERDESCRIPTION 415~000Q45NADISCOVERY DESCRIPTION Q32OPERATOROBSERVATION NALOCATIONOFRELEASEQgoioopo34 g'RCUSEONLY6869P)IONA,616-465-5901 X-1305808080808080c4ER80~TR0a49 af!
  ~0  3          MAINTENANCE THE PUMP WAS UNSTABLE AND DECLARED INOPERABLE.                                                                 THE REDUNDANT RH
ATTACHMENT P1CAUSEDESCRIPTION ANDCORRECTIVE ACTIONS:NOFURTHERACTIONISREQUIREDASARESULTOFTHISEVENT.
  ~04            WAS      OPERABLE.                THIS IS THE FIRST EVENT OF THIS TYPE.
iIrI}}
~06
  ~06
~07
  ~08 7      8 9                                                                                                                                                                                  80 SYSTEM              CAUSE            CAUSE                                                        COMP.          VALVE CODE                CODE        SUBCODE                    COMPONENT CODE                    SUBCODE          SUBCODE
~09                                            F    QTT L~LQ            LZJQ>>           Z           Z    Z    Z    Z      QE4      ~ZQTE           ~Z      QTR 7        8                          9            10          11              12              13                              18          19              20 SEQUENTIAL                          OCCURRENCE             REPORT                        REVISION LER]RP        EVENT YEAR                                  REPORT NO.                             CODE                TYPE                            NO.
Q17    REPORT
                                      ~3Q 21          22        23              24            26        27            28        29          30              31            32 ACTION FUTURE TAKEN ACTION                'N  EFFECT PLANT SHUTDOWN METHOD                  HOURS Q22 ATTACHMENT SUBMITTED NPRDP FORM SUB.
PRIME COMP.
SUPPLIER COMPONENT MANUFACTURER
                ~0QTR ~ZQ15                     ~ZQ25               ~ZQ21              0    0    0    0          ~N    Q22        ~NQ24             ~Z    Q25        Z      9      9  9      Q>>
33          34                    35                36    ,         37                    40    41                42                43              44                    47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o        THE TEST PROCEDURE DID                                 "P      VI      F THE PRO EOURE WAS                        H    G RWST WHICH SWEEPS                      THE AIR OUT OF THE HEAT EXCHA                            G 3          THE RHR SYSTEM HAS BEEN DRAINED ANO REFILLED TWICE S                                                    I      E
~14              CHANGED PROCEDURE RETURNED THE SYSTEM TO SERVICE WITH                                                          0 DIFF I        .ULTY .
                              ~Q 7      8    9                                                                                                                                                                              80 FACILITY STATUS              99 POWER                        OTHER STATUS      Q                                                DISCOVERY DESCRIPTION Q32 CCI I 5      MQ  E   28          1      0    0 29                                                                    OPERATOR OBSERVATION 80 ACTIVITY CONTENT
~s RELEASED OF RELEASE                            AMOUNT OF ACTIVITY NA LOCATION OF RELEASE          Q
              ~Z      Qss    ~ZQ54              NA 7      8    9              10            11                                            44            45                                                                                  80 PERSONNEL EXPOSURES NUMBER                TYPE          DESCRIPTION Q39 Lo¹0JQET                      z Q>>                                                   NA 7        8    9                11        12          13                                                                                                                                    80 PERSONNEL, INJURIES NUMBER                DESCRIPTION 41 5      ~00            0    Q45                                                              NA 9                11        12                                                                                                                                                  80 LOSS OF OR DAMAGE TO FACILITY                  43 TYPE        DESCRIPTION Z  P42 goioopo34 7      8    9            10                                                                                                                                                      g'RC 80 o
ISSIIEP
              +NQnn PUBLICITY DESCRIPTION        ~                                                      NA USE ONLY c4 ER 7      8    9        '0                                                                                                                          68    69                                80  ~ TR 0
NAME PF PREPARER
                                                                  ~  E ~ MURPHY                                                    P)IONA,616-465-5901 X-1305                                    a 49
 
a f
 
ATTACHMENT P1 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS:
NO FURTHER ACTION IS REQUIRED AS A RESULT OF THIS EVENT.
 
i I
r I}}

Latest revision as of 01:34, 4 February 2020

LER 80-032/03L-0:on 800904,while Returning East RHR Pump to Svc After Maint,Pump Became Unstable & Declared Inoperable. Caused by Air in Sys During Fill & Vent.Procedure Changed & Problem Eliminated
ML17331A469
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 10/03/1980
From: Murphy C
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A467 List:
References
LER-80-032-03L, LER-80-32-3L, NUDOCS 8010090368
Download: ML17331A469 (4)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION P.77)

Ll CENSE E EV EN T R E PORT CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 7 8 9 M I D LICENSEE CODE C C 2Q2 14 15 0 0 LICENSE NUMBER 25 03 26 LICENSE TYPE 30 Q4~ 57 CAT 58 Qs CON'T 7 8 soURGE ~LQB 60 61 0 5 0 0 0 DOCKET NUMBER 3 1 6 68 Q7 69 0 9 0 EVENT DATE 74 Q 8 75 REPORT DATE 80 Q9 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10

~02 WHI E PERFORMING A SURVEI A E EST TO

~0 3 MAINTENANCE THE PUMP WAS UNSTABLE AND DECLARED INOPERABLE. THE REDUNDANT RH

~04 WAS OPERABLE. THIS IS THE FIRST EVENT OF THIS TYPE.

~06

~06

~07

~08 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~09 F QTT L~LQ LZJQ>> Z Z Z Z Z QE4 ~ZQTE ~Z QTR 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER]RP EVENT YEAR REPORT NO. CODE TYPE NO.

Q17 REPORT

~3Q 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE TAKEN ACTION 'N EFFECT PLANT SHUTDOWN METHOD HOURS Q22 ATTACHMENT SUBMITTED NPRDP FORM SUB.

PRIME COMP.

SUPPLIER COMPONENT MANUFACTURER

~0QTR ~ZQ15 ~ZQ25 ~ZQ21 0 0 0 0 ~N Q22 ~NQ24 ~Z Q25 Z 9 9 9 Q>>

33 34 35 36 , 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE TEST PROCEDURE DID "P VI F THE PRO EOURE WAS H G RWST WHICH SWEEPS THE AIR OUT OF THE HEAT EXCHA G 3 THE RHR SYSTEM HAS BEEN DRAINED ANO REFILLED TWICE S I E

~14 CHANGED PROCEDURE RETURNED THE SYSTEM TO SERVICE WITH 0 DIFF I .ULTY .

~Q 7 8 9 80 FACILITY STATUS 99 POWER OTHER STATUS Q DISCOVERY DESCRIPTION Q32 CCI I 5 MQ E 28 1 0 0 29 OPERATOR OBSERVATION 80 ACTIVITY CONTENT

~s RELEASED OF RELEASE AMOUNT OF ACTIVITY NA LOCATION OF RELEASE Q

~Z Qss ~ZQ54 NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 Lo¹0JQET z Q>> NA 7 8 9 11 12 13 80 PERSONNEL, INJURIES NUMBER DESCRIPTION 41 5 ~00 0 Q45 NA 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z P42 goioopo34 7 8 9 10 g'RC 80 o

ISSIIEP

+NQnn PUBLICITY DESCRIPTION ~ NA USE ONLY c4 ER 7 8 9 '0 68 69 80 ~ TR 0

NAME PF PREPARER

~ E ~ MURPHY P)IONA,616-465-5901 X-1305 a 49

a f

ATTACHMENT P1 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS:

NO FURTHER ACTION IS REQUIRED AS A RESULT OF THIS EVENT.

i I

r I