ML18031A347: Difference between revisions

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| issue date = 01/22/1980
| issue date = 01/22/1980
| title = Interim Deficiency Rept Re Coped Structural Floor Beams Burned & Cut Beyond Prescribed Lines.Deficiency Is Under Continuous Evaluation.Final Rept Will Be Forwarded,If Necessary,Following Completion of Investigation
| title = Interim Deficiency Rept Re Coped Structural Floor Beams Burned & Cut Beyond Prescribed Lines.Deficiency Is Under Continuous Evaluation.Final Rept Will Be Forwarded,If Necessary,Following Completion of Investigation
| author name = CURTIS N W
| author name = Curtis N
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULAfURY'ORMATION OISTRIBUTIOiV SY~"'M(RIOS)ACCESSION NBRe8001290378 OOC~DATE$80/01/22NOTARIZED!
{{#Wiki_filter:REGULA fURY      'ORMATION OISTRIBUTIOiV SY~         "'M (RIOS)
NOlAGILE87Susquehanna SteamElectricStationrOn)tliPennsylva50388usquehanna SteamBlectricStationrOnit2r8'ennsylva AU~AUTHOHAFFILIATION CUHT'4..iv.Pennsylvanii Power5l.ightCo.AEGIP~iVAMEHE'CIPIKiV tAFlILIATIONDOCKET¹05000~8705000388
ACCESSION NBR e 8001290378                  OOC   DATE $ 80/01/22      NOTARIZED! NO          DOCKET  ¹ l AGILE        87 Susquehanna          Steam
                                                  ~
Electr ic  Stationr On) t    li  Pennsyl va 05000~87 50 388          usquehanna    Steam    Blectric Stationr Onit      2r 8'ennsylva   05000388 AU   ~                       AUTHOH  AFFILIATION CUH T  '4..iv.               Pennsylvanii Power 5 l.ight Co.
AEGIP ~ iVAME                HE'CIPIKiVt AFl ILIAT ION


==SUBJECT:==
==SUBJECT:==
InterimdeficiencyreptrecopedstructuralfloorbeamsburnedLcutbeyondprescribedlines,Deficiency isundercontinuous evaluation, Finalreptwillbeforwardedrif necessaryrfollowing completion ofinvest'igation, DIGfRIBUTION COOK:8019BCOPIESRECEIVED:L fR+ENCLSIZE:0TITLE:Construction Deficiency Repoit(10CF50,55K)q0pea:'5~+0cp8C'Y4'F'sppAG1'UN:HECIPIKNfCOPIESIOCOOK/iVAME LrTHENCL14PM~M~~20LA~~A~QHECIPIENl COPIESIOCUOK/NAMC LlfREN15dC4-w~~i21AO~)~~~iINTEHNAI; EXTKHr>AL:
Inter      im  def iciency rept re coped str uctural floor beams burned        L  cut beyond prescr ibed lines, Deficiency is under continuous evaluation, Final rept will be forwardedrif necessaryrfollowing completion of invest'igation, DIG fRIBUTION COOK: 8019B                COPIES RECEIVED:L fR +ENCL TITLE: Construction Deficiency Repoit (10CF 50,55K) 0      SIZE:
0RKGFII.K0'P5'8MPA10GAB12JOHOANrK/lK 16AOFORKNGAi7AOHKAGSFTY23OELD0IHECTOHOSK14CSYSBHMECHERGBHSHAiVAUKR03LPOR24A('.HS121i11i11i1111602NRCVOR07KDO4STAFF09OEPYDIROPMllSTANDHDSOEVi3FIKLDCQOR/IK17AOPLANTSYS22DIRDPMAD/SIfETECHGEOSCIENCE'H MAlLENGBHPO'HKRSYSBHSTRUCTKAlGBR04NSICJP,gS1>980g2TOTALNuMBKHOFGOPIKSHKaylHKO:
q0 pea:    '5~+0 c H EC IP IKN f p8  COPIES C'Y4 'F's pp HECIPIENl            COPIES IO COOK/iVAME              L r TH ENCL          IO CUOK/NAMC          LlfR  EN 1'UN:             PM~M~~
LTrH~ENCLng+>
                                    ~Q                        15 dC  4-w~~ i
TWONORTHNINTHSTREET,ALLENTOWN.
                                                                      ~) ~~~ i AG            14 20    LA~~A                                    21 AO INTEHNAI;     0      RKG F II.K                1              02 NRC VOR 0    'P5'8                      2              07 KDO 4 STAFF MPA                                      09 OEPY DIR OPM 10 GAB 12 JOHOANrK/lK 1
PA.18101PHONE:(215)821-5151NORMANW.CURTISVicePresident Engineering 8Construction 821-538IJanuary22,1980Mr.BoyceH.GrierDirector, RegionIU.S.NuclearRegulatory Commission 631ParkAvenueKingofPrussia,Pennsylvania 18406SUSQUEHANNA STEAMELECTRICSTATIONNOTIFICATION OFAPOTENTIAL DEFICIENCY ONCOPEDSTRUCTURAL FLOORBEAi~lSERs100450/100508 FILE840-4PLA-443
i 1
ll STANDHDS i 3F IKLD OEV CQOR/IK 16 AO FOR KNGA                  1              17 AO PLANT SYS i7 AO HKAG SFTY                  i              22 DIR  DPM 23 OELD                          1              AD/SIfE TECH 0 IHEC TOH OSK                  1              GEOSCIENCE'H 14C SYS BH                      i              MAlL  ENG BH MECH ERG          BH            1              PO'HKR SYS BH S  HAiVAUKR                      1              STRUCT KAlG BR EXTKHr>AL: 03 LPOR                              1              04 NSIC 24 A('.HS                      16 JP,g S1>980 g2 TOTAL NuMBKH OF GOP IKS HKaylHKO: L T r H                    ~     ENCL ng+>


==DearMr.Grier:==
TWO NORTH NINTH STREET,      ALLENTOWN. PA. 18101  PHONE: (215) 821-5151 NORMAN W. CURTIS Vice President Engineering 8 Construction 821-538 I January 22, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 18406 SUSQUEHANNA STEAM ELECTRIC STATION NOTIFICATION OF A POTENTIAL DEFICIENCY                ON COPED STRUCTURAL FLOOR BEAi~lS ERs 100450/100508                            FILE 840-4 PLA-443
Thisletterservestoconfirminformation providedbytelephone toNRCInspector Mr.R.GalloonDecember14,1979.Znthatconversationr Mr.Gallowasadvisedthattheabovesubjectcondition wasunderevaluation fozreportability undertheprovisions of10CFR50.55(e).
 
Thecondition wasreportedinNRCInspection Report50-387/79-28 and388/79-15 whichidentified severalcopedfloorbeamswhichwereburnedandcutbeyondpzescribed lines.BechtelNCR4288waspreparedonAugust1,1979todocumentthenoncompliances citedbytheinspection aswellassimilarnonconformances whichweresubsequently notedbyBechtelQualityControl.OnDecember'l, 1979,thenonconfozming conditions werenotedinBechtelMCAR1-43.TheMCARidentified 123beamssuppliedbyIndustrial Engineering Works(ZEW).Inspection resultstodateindicatetherehavebeenatotalof47beamsreportedashavingimproperradii(underradius,squarecut);seven(7)ashavingothercopingproblems(overcutlessthan12")2andeight(8)beamsthatarenotaccessible.
==Dear Mr.       Grier:==
Inspection ofbeamsprocuredfromothersuppliers underthesamespecification (C16)isunderway.
 
Theresultsoftheseinspections willbeusedtoevaluatetheextentandthesafetyimplications oftheconditions.
This    letter serves to confirm information provided by telephone to NRC Inspector Mr. R. Gallo on December 14, 1979. Zn that conversationr Mr.
Thispotentially reportable deficiency isundercontinued evaluation byBechtelandPP&LEngineering gzoups.WehavebeenadvisedbyBechtelEngineering thattheywillcompletetheirevaluation inMarch,1980.Baseduponthesatisfactory
Gallo was advised that the above subject condition was under evaluation foz reportability under the provisions of 10 CFR 50.55(e).
'Eo/9SoPENNSYLVANIA POWER8LIGHTCOMPANY8ottaseo Mr.BoyceH.GrierJanuary22,1980completion oftheinvestigation, wewilladvisetheCommission ofthedatebywhichafinalreportwillbesubmitted shouldtheconditions bedetermined tobereportable.
The    condition          was  reported in NRC Inspection Report 50-387/79-28 and 388/79-15 which            identified several coped floor beams which were burned and cut beyond pzescribed lines. Bechtel NCR 4288 was prepared on August 1, 1979 to document the noncompliances cited by the inspection as well as similar nonconformances which were subsequently noted by Bechtel Quality Control. On December'l, 1979, the nonconfozming conditions were noted in Bechtel MCAR 1-43.
Sincethedetailsofthisreportprovideinformation relevanttothereporting recgxirement of10CPR21,thiscorrespondence isconsidered toalsodischarge anyformalresponsibility PPaLmayhaveforreporting incompliance thereto.Verytrulyyours,N.W.CurtisVicePresident-Engineering 6Construction PLW/ARS:mcb cc:Mr.RobertM.GalloU.S.NuclearRegulatory Commission P.O.Box52Shickshinny; Pennsylvania 18655Mr.G.McDonaldOfficeofManagement Xnformation 6ProgramControlU.S.NuclearRegulatory Commission Washington, D.C.20555(15)Mr.VictorStelloDirectorOfficeofInspection
The MCAR        identified 123 beams supplied by Industrial Engineering Works (ZEW).
&Enforcement U.S.NuclearRegulatory Commission Washington, D.C20555}}
Inspection results to date indicate there have been a total of 47 beams reported as having improper radii (under radius, square cut); seven (7) as having other coping problems (overcut less than 12")2 and eight (8) beams that are not accessible.
Inspection of            beams  procured from other suppliers under the same specification (C16)     is  underway.       The results of these inspections will be used to evaluate the extent and the safety implications of the conditions.
This      potentially reportable deficiency is            under continued evaluation by Bechtel and PP&L Engineering gzoups.               We  have been advised by Bechtel Engineering that they    will complete their          evaluation in March, 1980. Based upon the satisfactory
                                                                                                      'Eo/9 So PENNSYLVANIA POWER    8  LIGHT COMPANY 8ottaseo
 
Mr. Boyce H. Grier                                            January 22, 1980 completion of the investigation, we will advise the Commission of the date by which a final report will be submitted should the conditions be determined to  be  reportable.
Since the details  of this report provide information relevant to the reporting recgxirement of 10  CPR  21, this correspondence is considered to also discharge any  formal responsibility PPaL may have for reporting in compliance thereto.
Very  truly yours, N. W. Curtis Vice President-Engineering   6  Construction PLW/ARS:mcb cc:   Mr. Robert M. Gallo U. S. Nuclear Regulatory Commission P. O. Box 52 Shickshinny; Pennsylvania     18655 Mr. G. McDonald Office of Management Xnformation 6 Program  Control U. S. Nuclear Regulatory Commission Washington, D.C.     20555 Mr. Victor Stello      (15)
Director Office of Inspection  & Enforcement U. S. Nuclear Regulatory Commission Washington, D.C      20555}}

Latest revision as of 00:22, 22 October 2019

Interim Deficiency Rept Re Coped Structural Floor Beams Burned & Cut Beyond Prescribed Lines.Deficiency Is Under Continuous Evaluation.Final Rept Will Be Forwarded,If Necessary,Following Completion of Investigation
ML18031A347
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 01/22/1980
From: Curtis N
PENNSYLVANIA POWER & LIGHT CO.
To:
References
NUDOCS 8001290378
Download: ML18031A347 (3)


Text

REGULA fURY 'ORMATION OISTRIBUTIOiV SY~ "'M (RIOS)

ACCESSION NBR e 8001290378 OOC DATE $ 80/01/22 NOTARIZED! NO DOCKET ¹ l AGILE 87 Susquehanna Steam

~

Electr ic Stationr On) t li Pennsyl va 05000~87 50 388 usquehanna Steam Blectric Stationr Onit 2r 8'ennsylva 05000388 AU ~ AUTHOH AFFILIATION CUH T '4..iv. Pennsylvanii Power 5 l.ight Co.

AEGIP ~ iVAME HE'CIPIKiVt AFl ILIAT ION

SUBJECT:

Inter im def iciency rept re coped str uctural floor beams burned L cut beyond prescr ibed lines, Deficiency is under continuous evaluation, Final rept will be forwardedrif necessaryrfollowing completion of invest'igation, DIG fRIBUTION COOK: 8019B COPIES RECEIVED:L fR +ENCL TITLE: Construction Deficiency Repoit (10CF 50,55K) 0 SIZE:

q0 pea: '5~+0 c H EC IP IKN f p8 COPIES C'Y4 'F's pp HECIPIENl COPIES IO COOK/iVAME L r TH ENCL IO CUOK/NAMC LlfR EN 1'UN: PM~M~~

~Q 15 dC 4-w~~ i

~) ~~~ i AG 14 20 LA~~A 21 AO INTEHNAI; 0 RKG F II.K 1 02 NRC VOR 0 'P5'8 2 07 KDO 4 STAFF MPA 09 OEPY DIR OPM 10 GAB 12 JOHOANrK/lK 1

i 1

ll STANDHDS i 3F IKLD OEV CQOR/IK 16 AO FOR KNGA 1 17 AO PLANT SYS i7 AO HKAG SFTY i 22 DIR DPM 23 OELD 1 AD/SIfE TECH 0 IHEC TOH OSK 1 GEOSCIENCE'H 14C SYS BH i MAlL ENG BH MECH ERG BH 1 PO'HKR SYS BH S HAiVAUKR 1 STRUCT KAlG BR EXTKHr>AL: 03 LPOR 1 04 NSIC 24 A('.HS 16 JP,g S1>980 g2 TOTAL NuMBKH OF GOP IKS HKaylHKO: L T r H ~ ENCL ng+>

TWO NORTH NINTH STREET, ALLENTOWN. PA. 18101 PHONE: (215) 821-5151 NORMAN W. CURTIS Vice President Engineering 8 Construction 821-538 I January 22, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 18406 SUSQUEHANNA STEAM ELECTRIC STATION NOTIFICATION OF A POTENTIAL DEFICIENCY ON COPED STRUCTURAL FLOOR BEAi~lS ERs 100450/100508 FILE 840-4 PLA-443

Dear Mr. Grier:

This letter serves to confirm information provided by telephone to NRC Inspector Mr. R. Gallo on December 14, 1979. Zn that conversationr Mr.

Gallo was advised that the above subject condition was under evaluation foz reportability under the provisions of 10 CFR 50.55(e).

The condition was reported in NRC Inspection Report 50-387/79-28 and 388/79-15 which identified several coped floor beams which were burned and cut beyond pzescribed lines. Bechtel NCR 4288 was prepared on August 1, 1979 to document the noncompliances cited by the inspection as well as similar nonconformances which were subsequently noted by Bechtel Quality Control. On December'l, 1979, the nonconfozming conditions were noted in Bechtel MCAR 1-43.

The MCAR identified 123 beams supplied by Industrial Engineering Works (ZEW).

Inspection results to date indicate there have been a total of 47 beams reported as having improper radii (under radius, square cut); seven (7) as having other coping problems (overcut less than 12")2 and eight (8) beams that are not accessible.

Inspection of beams procured from other suppliers under the same specification (C16) is underway. The results of these inspections will be used to evaluate the extent and the safety implications of the conditions.

This potentially reportable deficiency is under continued evaluation by Bechtel and PP&L Engineering gzoups. We have been advised by Bechtel Engineering that they will complete their evaluation in March, 1980. Based upon the satisfactory

'Eo/9 So PENNSYLVANIA POWER 8 LIGHT COMPANY 8ottaseo

Mr. Boyce H. Grier January 22, 1980 completion of the investigation, we will advise the Commission of the date by which a final report will be submitted should the conditions be determined to be reportable.

Since the details of this report provide information relevant to the reporting recgxirement of 10 CPR 21, this correspondence is considered to also discharge any formal responsibility PPaL may have for reporting in compliance thereto.

Very truly yours, N. W. Curtis Vice President-Engineering 6 Construction PLW/ARS:mcb cc: Mr. Robert M. Gallo U. S. Nuclear Regulatory Commission P. O. Box 52 Shickshinny; Pennsylvania 18655 Mr. G. McDonald Office of Management Xnformation 6 Program Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Victor Stello (15)

Director Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, D.C 20555