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| {{#Wiki_filter:EOP: FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 1 of 5 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW PORC REVIE DATE PLANT SUPERINTENDENT E FECTIVE DATE CATEGORY 1.0 REVIEWED BY: 9305i40057 930505 PDR ADOCK 05000244~F PDR | | {{#Wiki_filter:EOP: |
| | REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 5 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW PORC REVIE DATE PLANT SUPERINTENDENT E FECTIVE DATE CATEGORY 1.0 REVIEWED BY: |
| | 9305i40057 930505 PDR ADOCK 05000244 |
| | ~F PDR |
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| FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 2 of 5 A.PURPOSE-This procedure provides actions to restore the core to an adequate shutdown condition. | | REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 2 of 5 A. PURPOSE This procedure provides actions to restore the core to an adequate shutdown condition. |
| B.ENTRY CONDITIONS/SYMPTOMS 1.ENTRY CONDITIONS | | B. ENTRY CONDITIONS/SYMPTOMS |
| -This procedure is entered from: a.F-0.1, SUBCRITICALITY Critical Safety Function Status Tree, on either YELLOW condition.
| | : 1. ENTRY CONDITIONS This procedure is entered from: |
| | : a. F-0.1, SUBCRITICALITY Critical Safety Function Status Tree, on either YELLOW condition. |
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| EOP: FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 3 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: o Adverse CNMT values should be used whenever CNMT pressure is greater than 4 psig or CNMT radiation is greater than 10+5 R/hr.o Adverse CNMT conditions or loss of forced air cooling may result in failure of NIS detectors. | | EOP: |
| 1 Check Intermediate Range Flux: a.Flux-EITHER CHANNEL LESS THAN 10-10 AMPS a.Continue with Ste~2.WHEN flux is LESS THAN 10 amps on any operable channel, THEN do Steps lb, c and d.b.Check the following: | | REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 3 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: o Adverse CNMT values should be used whenever CNMT pressure is greater than 4 psig or CNMT radiation is greater than 10+ 5 R/hr. |
| o Both intermediate range channels-LESS THAN 10 AMPS b.Continue with step 2.WHEN either condition met, THEN do Steps lc and d.-OR-o Greater than 20 minutes since reactor trip c.Verify source range detectors ENERGIZED cd Manually energize source range detectors by depressing P-6 permissive defeat pushbuttons (2 of 2).IF source ranges can NOT be restored, THEN refer to ER-NIS.1, SR MALFUNCTION, and go to Step 2.d, Transfer Rk-45 recorder to one sour'ce'ange and one intermediate range channel
| | o Adverse CNMT conditions or loss of forced air cooling may result in failure of NIS detectors. |
| | 1 Check Intermediate Range Flux: |
| | : a. Flux - EITHER CHANNEL LESS THAN a. Continue with Ste~ 2. WHEN flux 10-10 AMPS is LESS THAN 10 amps on any operable channel, THEN do Steps lb, c and d. |
| | : b. Check the following: b. Continue with step 2. WHEN either condition met, THEN do o Both intermediate range Steps lc and d. |
| | channels - LESS THAN 10 AMPS |
| | -OR-o Greater than 20 minutes since reactor trip |
| | : c. Verify source range detectors cd Manually energize source range ENERGIZED detectors by depressing P-6 permissive defeat pushbuttons (2 of 2). |
| | IF source ranges can NOT be restored, THEN refer to ER-NIS.1, SR MALFUNCTION, and go to Step 2. |
| | d, Transfer Rk-45 recorder to one sour'ce'ange and one intermediate range channel |
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| EOP: FR-Ss2 T!TLE: RESPONSE TO LOSS OF CORE SHUTDOWN REV'PAGE 4 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: If offsite power is lost coincident with SI, then MCC C and MCC D lockout relays must be reset to restore BA and RMW pumps.2 Initiate Immediate Boration Of RCS: a.Check SI status: o All SI annunciators-EXTINGUISHED o All SI pumps-OFF IN AUTO b.Verify at least one charging pump-RUNNING!c.Align boration path: 1)Start tue BA transfer pumps 2)Open MOV-350 I 3)Verify BA flow!d.Verify charging flow path:!o Ch'arging valve to loop B cold 18g"-'(AOV-294) | | EOP: T!TLE: |
| -OPEN~, g'Ch'arging flow control valve (HCV-142)-DEMAND AT 0%1)Complete the immediate actions of E-O, REACTOR TRIP OR SAFETY INJECTION, while continuing with this procedure 2)IF SI flow indicated, THEN go to Step 3.IF NOT, THEN go to Step 2b.b.Perform the following:
| | REV' FR-Ss2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 4 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: If offsite power is lost coincident with SI, then MCC C and MCC D lockout relays must be reset to restore BA and RMW pumps. |
| 1)Reset SI if necessary. | | 2 Initiate Immediate Boration Of RCS: |
| 2)Start one charging pump.c.Initiate normal boration at maximum rate using the boric acid flow control valve, FCV-110A.IF flow can NOT be established, THEN refer to ER-CVCS.l, REACTOR MAKEUP CONTROL MALFUNCTION. | | : a. Check SI status: |
| d.Manually align valves and verify flow. | | o All SI annunciators- 1) Complete the immediate EXTINGUISHED actions of E-O, REACTOR TRIP OR SAFETY INJECTION, while o All SI pumps - OFF IN AUTO continuing with this procedure |
| | : 2) IF SI flow indicated, THEN go to Step 3. IF NOT, THEN go to Step 2b. |
| | : b. Verify at least one charging b. Perform the following: |
| | pump - RUNNING |
| | : 1) Reset SI if necessary. |
| | : 2) Start one charging pump. |
| | : c. Align boration path: c. Initiate normal boration at maximum rate using the boric |
| | : 1) Start tue BA transfer pumps acid flow control valve, FCV-110A. IF flow can NOT be |
| | : 2) Open MOV-350 I established, THEN refer to ER-CVCS.l, REACTOR MAKEUP |
| | : 3) Verify BA flow CONTROL MALFUNCTION. |
| | : d. Verify charging flow path: ! |
| | : d. Manually align valves and verify flow. |
| | o Ch'arging valve to loop B cold 18g"-'(AOV-294) - OPEN |
| | ~, g' Ch'arging flow control valve (HCV-142) - DEMAND AT 0% |
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| EOP: FR-ST 2 TITLE: RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 5 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 3 Check Source Range Channels: o Source range channels-ENERGIZED o Source range channels startup rate-ZERO OR NEGATIVE Continue boration until adequate shutdown margin is verified by RCS sample (Refer to Figure SDM).4 Verify Adequate Shutdown Margin a.Direct HP to sample RCS for boron concentration I b.Verify boron concentration-GREATER THAN REQUIREMENTS OF FIGURE SDM b.Continue boration until adequate shutdown margin verified.c.Stop boration 5 Return To Procedure And Step In Effect.-END- | | EOP: TITLE: |
| | REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 5 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 3 Check Source Range Channels: Continue boration until adequate shutdown margin is verified by RCS o Source range channels - ENERGIZED sample (Refer to Figure SDM). |
| | o Source range channels startup rate - ZERO OR NEGATIVE 4 Verify Adequate Shutdown Margin |
| | : a. Direct HP to sample RCS for boron concentration I |
| | : b. Verify boron concentration- b. Continue boration until adequate GREATER THAN REQUIREMENTS OF shutdown margin verified. |
| | FIGURE SDM |
| | : c. Stop boration 5 Return To Procedure And Step In Effect. |
| | -END- |
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| FR-S.2 TITLE%RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 1 of 1 FR-S.2 APPENDIX LIST TITLE PAGES 1)FIGURE SDM | | TITLE% |
| | REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 1 FR-S. 2 APPENDIX LIST TITLE PAGES |
| | : 1) FIGURE SDM |
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| EOP: FR-ST 2 TITLE: RESPONSE TO LOSS OF CORE SHUTDOWN REV: 3 PAGE 1 of 1 FIGURE SDM NOTE: o Curve includes allowance for one stuck rod.Add 100 ppm for each additional stuck rod.o To obtain core burnup, use PPCS turn on code BURNUP.BORON CONCENTRATION (PPM)1800 1600 BORON INCREMENTS 20 PPM 1400 1200 1000 ADEQUATE SDM 100 PPH CONSERVATISH INCLUDED 800 600 400 TE BORA 200 BURNUP INCREMENTS 100 MWD/HTU 0 1000 2000 3000 4000 5000 6000 7000 8000 9000 10000 11000 CYCLE 23 BURNUP (HWD/HTU)}} | | EOP: TITLE: |
| | REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 1 FIGURE SDM NOTE: o Curve includes allowance for one stuck rod. Add 100 ppm for each additional stuck rod. |
| | o To obtain core burnup, use PPCS turn on code BURNUP. |
| | BORON CONCENTRATION (PPM) 1800 BORON INCREMENTS 20 PPM 1600 1400 ADEQUATE SDM 1200 100 PPH CONSERVATISH INCLUDED 1000 800 600 400 BORATE 200 BURNUP INCREMENTS 100 MWD/HTU 0 1000 2000 3000 4000 5000 6000 7000 8000 9000 10000 11000 CYCLE 23 BURNUP (HWD/HTU)}} |
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Text
EOP:
REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 5 ROCHESTER GAS AND ELECTRIC CORPORATION GINNA STATION CONTROLLED COPY NUMBER TECHNICAL REVIEW PORC REVIE DATE PLANT SUPERINTENDENT E FECTIVE DATE CATEGORY 1.0 REVIEWED BY:
9305i40057 930505 PDR ADOCK 05000244
~F PDR
REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 2 of 5 A. PURPOSE This procedure provides actions to restore the core to an adequate shutdown condition.
B. ENTRY CONDITIONS/SYMPTOMS
- 1. ENTRY CONDITIONS This procedure is entered from:
- a. F-0.1, SUBCRITICALITY Critical Safety Function Status Tree, on either YELLOW condition.
EOP:
REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 3 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: o Adverse CNMT values should be used whenever CNMT pressure is greater than 4 psig or CNMT radiation is greater than 10+ 5 R/hr.
o Adverse CNMT conditions or loss of forced air cooling may result in failure of NIS detectors.
1 Check Intermediate Range Flux:
- a. Flux - EITHER CHANNEL LESS THAN a. Continue with Ste~ 2. WHEN flux 10-10 AMPS is LESS THAN 10 amps on any operable channel, THEN do Steps lb, c and d.
- b. Check the following: b. Continue with step 2. WHEN either condition met, THEN do o Both intermediate range Steps lc and d.
channels - LESS THAN 10 AMPS
-OR-o Greater than 20 minutes since reactor trip
- c. Verify source range detectors cd Manually energize source range ENERGIZED detectors by depressing P-6 permissive defeat pushbuttons (2 of 2).
IF source ranges can NOT be restored, THEN refer to ER-NIS.1, SR MALFUNCTION, and go to Step 2.
d, Transfer Rk-45 recorder to one sour'ce'ange and one intermediate range channel
EOP: T!TLE:
REV' FR-Ss2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 4 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED NOTE: If offsite power is lost coincident with SI, then MCC C and MCC D lockout relays must be reset to restore BA and RMW pumps.
2 Initiate Immediate Boration Of RCS:
- a. Check SI status:
o All SI annunciators- 1) Complete the immediate EXTINGUISHED actions of E-O, REACTOR TRIP OR SAFETY INJECTION, while o All SI pumps - OFF IN AUTO continuing with this procedure
- 2) IF SI flow indicated, THEN go to Step 3. IF NOT, THEN go to Step 2b.
- b. Verify at least one charging b. Perform the following:
pump - RUNNING
- 1) Reset SI if necessary.
- 2) Start one charging pump.
- c. Align boration path: c. Initiate normal boration at maximum rate using the boric
- 1) Start tue BA transfer pumps acid flow control valve, FCV-110A. IF flow can NOT be
- 2) Open MOV-350 I established, THEN refer to ER-CVCS.l, REACTOR MAKEUP
- 3) Verify BA flow CONTROL MALFUNCTION.
- d. Verify charging flow path: !
- d. Manually align valves and verify flow.
o Ch'arging valve to loop B cold 18g"-'(AOV-294) - OPEN
~, g' Ch'arging flow control valve (HCV-142) - DEMAND AT 0%
EOP: TITLE:
REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 5 of 5 STEP ACTION/EXPECTED RESPONSE RESPONSE NOT OBTAINED 3 Check Source Range Channels: Continue boration until adequate shutdown margin is verified by RCS o Source range channels - ENERGIZED sample (Refer to Figure SDM).
o Source range channels startup rate - ZERO OR NEGATIVE 4 Verify Adequate Shutdown Margin
- a. Direct HP to sample RCS for boron concentration I
- b. Verify boron concentration- b. Continue boration until adequate GREATER THAN REQUIREMENTS OF shutdown margin verified.
FIGURE SDM
- c. Stop boration 5 Return To Procedure And Step In Effect.
-END-
TITLE%
REV: 3 FR-S.2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 1 FR-S. 2 APPENDIX LIST TITLE PAGES
- 1) FIGURE SDM
EOP: TITLE:
REV: 3 FR-ST 2 RESPONSE TO LOSS OF CORE SHUTDOWN PAGE 1 of 1 FIGURE SDM NOTE: o Curve includes allowance for one stuck rod. Add 100 ppm for each additional stuck rod.
o To obtain core burnup, use PPCS turn on code BURNUP.
BORON CONCENTRATION (PPM) 1800 BORON INCREMENTS 20 PPM 1600 1400 ADEQUATE SDM 1200 100 PPH CONSERVATISH INCLUDED 1000 800 600 400 BORATE 200 BURNUP INCREMENTS 100 MWD/HTU 0 1000 2000 3000 4000 5000 6000 7000 8000 9000 10000 11000 CYCLE 23 BURNUP (HWD/HTU)