ML18102A305: Difference between revisions

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| issue date = 08/13/1996
| issue date = 08/13/1996
| title = Forward Corrected Copy of LER Re Potential Hydrogen Embrittlement on 4kV Breaker Parts
| title = Forward Corrected Copy of LER Re Potential Hydrogen Embrittlement on 4kV Breaker Parts
| author name = GARCHOW D F
| author name = Garchow D
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 13 1996 LR-N96237
{{#Wiki_filter:PS~G*
* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 13 1996         CORRECTED COPY LR-N96237
: u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
: u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
LER 272/96-014-00 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 CORRECTED COPY This Licensee Event Report entitled Hydrogen.Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 1OCFR50.73 (a) ( 2) ( i) (B) . Attachment SORC Mtg. 96-106 DVH/tcp C Distribution LER File 3.7 9608200195 960813 PDR ADOCK 05000272 S PDR l11e paver is in )t1ur hanJs. Sincerely, (1y r.
LER 272/96-014-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled                   "Pot~ntial      Hydrogen.Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50.73 (a) ( 2) ( i) (B) .
David F.
Sincerely, (1y r. J()m-~
General Manager -Salem Operations
David F. ~archow General Manager -
*V1/ /', *\7* 95*2168 REV. 6 '94 Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-00  
Salem Operations Attachment SORC Mtg. 96-106 DVH/tcp C     Distribution LER File 3.7
). The commitments are as follows: 1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are to be transferred to another bus. 2. A QA stop work order was issued to NLI on July 26, 1996. 3. The circuit breakers will be removed for replacement and refurbishment.
                                                                                              *V1/
This will be completed for each breaker prior to that breaker being required to be operable.
                                                                                        *\7*
: 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted.
                                                                                          /',
Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to .this LER.}}
9608200195 960813 PDR ADOCK 05000272 S                         PDR l11e paver is in )t1ur hanJs.
95*2168 REV. 6 '94
 
Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-00 ). The commitments are as follows:
: 1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are ~vailable to be transferred to another bus.
: 2. A QA stop work order was issued to NLI on July 26, 1996.
: 3. The circuit breakers will be removed for replacement and refurbishment. This will be completed for each breaker prior to that breaker being required to be operable.
: 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to
  .this LER.}}

Latest revision as of 17:42, 7 November 2019

Forward Corrected Copy of LER Re Potential Hydrogen Embrittlement on 4kV Breaker Parts
ML18102A305
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/13/1996
From: Garchow D
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A306 List:
References
LR-N96237, NUDOCS 9608200195
Download: ML18102A305 (2)


Text

PS~G*

  • Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 13 1996 CORRECTED COPY LR-N96237
u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

LER 272/96-014-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled "Pot~ntial Hydrogen.Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50.73 (a) ( 2) ( i) (B) .

Sincerely, (1y r. J()m-~

David F. ~archow General Manager -

Salem Operations Attachment SORC Mtg.96-106 DVH/tcp C Distribution LER File 3.7

  • V1/
  • \7*

/',

9608200195 960813 PDR ADOCK 05000272 S PDR l11e paver is in )t1ur hanJs.

95*2168 REV. 6 '94

Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-00 ). The commitments are as follows:

1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are ~vailable to be transferred to another bus.
2. A QA stop work order was issued to NLI on July 26, 1996.
3. The circuit breakers will be removed for replacement and refurbishment. This will be completed for each breaker prior to that breaker being required to be operable.
4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to

.this LER.