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=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMON~0TIONSYSTEMREGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9108050066 DOC.DATE:
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMON~0 TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9108050066 DOC.DATE: 91/07/29 NOTARIZED:, NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1,, Rochester G AUTH.NAME AUTHOR AFFILIATION
91/07/29NOTARIZED:,
NOFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,,Rochester GAUTH.NAMEAUTHORAFFILIATION
.BACKUS,W.H.
.BACKUS,W.H.
Rochester Gas&ElectricCorp.MECREDY,R.C.
Rochester Gas&Electric Corp.MECREDY,R.C.
'ochester Gas&ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000244II
'ochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000244 II


==SUBJECT:==
==SUBJECT:==
LER91-006-00:on 910629,EDG Astartedautomatically duetoapparentundervoltage signalfromBus14undervoltage monitoring sys.Rootcausenotdetermined.Bus 14energized
LER 91-006-00:on 910629,EDG A started automatically due to apparent undervoltage signal from Bus 14 undervoltage monitoring sys.Root cause not determined.Bus 14 energized&EDG declared operable.W/910729 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR
&EDGdeclaredoperable.W/910729 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR
!ENCL I SIZE: 7 TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
!ENCLISIZE:7TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
D 05000244 A RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB SD NRRfDST~LBSD1 REG F~02 RGN1 FILE 01 EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POORE,W.~7&75 Htt<w'(COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1'1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICBSH3 NRR/DST/SRXB SE RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT'OPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1'1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS:
D05000244ARECIPIENT IDCODE/NAME PD1-3LAJOHNSON,A INTERNAL:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOiv!P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCU5!EiiTS YOU DON'T NEED!A D D S FULL TEXT CONVERSION REQUIRED-TOTAL NUMBER OF COPIES REQUIRED: LTTR 31 ENCL 31
ACNWAEOD/DSP/TPAB NRR/DET/ECMB 9HNRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB SDNRRfDST~LBSD1 REGF~02RGN1FILE01EXTERNAL:
EG&GBRYCE,J.H NRCPDRNSICPOORE,W.~7&75Htt<w'(COPIESLTTRENCL111122111111111111111'1331111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DOAAEOD/ROAB/DSP NRR/DET/EMEB 7ENRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICBSH3 NRR/DST/SRXB SERES/DSIR/EIB LSTLOBBYWARDNSICMURPHY,G.A NUDOCSFULLTXT'OPIES LTTRENCL111122111122111'11111111DDDNOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOiv!P1-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCU5!EiiTS YOUDON'TNEED!ADDSFULLTEXTCONVERSION REQUIRED-TOTALNUMBEROFCOPIESREQUIRED:
LTTR31ENCL31
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""/I'.;,rrrtii
""/I'.;,rrrtii
","ROCHESTER GASANDELECTRICCORPORATION ROSERTCh1ECREDYVicePresident CtnnaNucfearPrnducticrn oe'I'a','','
"," ROCHESTER GAS AND ELECTRIC CORPORATION ROSERTC h1ECREDY Vice President Ctnna Nucfear Prnducticrn oe'I'a','','~1th~~'r Stale., 89 EAST AVENUE, ROCHESTER N.K 14649-0001 i TELEPHONE AAEACODETIB 546 2700 July 29, 1991 I U.S.Nuclear Regulatory Commission Document Control Desk Washington,-
~1th~~'rStale.,89EASTAVENUE,ROCHESTER N.K14649-0001 iTELEPHONE AAEACODETIB 5462700July29,1991IU.S.NuclearRegulatory Commission DocumentControlDeskWashington,-
DC 20555
DC20555


==Subject:==
==Subject:==
LER91-006,ApparentVoltageDroponSafeguards 480VoltBus14CausesanAutomatic Startofthe"A"Emergency DieselGenerator R.E.GinnaNuclearPowerPlantDocketNo.50-244In-accordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),
LER 91-006, Apparent Voltage Drop on Safeguards 480 Volt Bus 14 Causes an Automatic Start of the"A" Emergency Diesel Generator R.E.Ginna Nuclear Power Plant Docket No.50-244 In-accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv),which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF),"including the Reactor Protection System (RPS)", the attached Licensee Event Report LER 91-006 is hereby submitted.
whichrequiresareportof,"anyeventorcondition thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF),"including theReactorProtection System(RPS)",theattachedLicenseeEventReportLER91-006isherebysubmitted.
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Mecr dy xc U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9 i 080s00g,(, PDR ADOCK Ort.iot)-4 i  
Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytrulyyours,RobertC.MecrdyxcU.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector 9i080s00g,(,
PDRADOCKOrt.iot)-4 i  


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NAC tas lli IOACI LICENSEE EVENT REPORT (LERI UA NUOLCAA AoovLATCAocc>>se&lcw Attleovto oleo NIL OIN olov CAOIACO.O)te/
~$)ACILITYNA<<)OIllR.E.GinnaNuclearPower.PlantOOCACTeeveeoCAOlo6ooo244ios ApparentVoltageDmpOnSafequards 480VoltBus14CausesanAutomatic StartoftheA"EmerencDieselGenerator CVCIITCATO14Lt1NveeocA14Al)O1TOATClllOTlet1)ACILITICC INVOLVCOIOI>>OI>>T>>eOAYYCAAYCAA~COveeee>>AL
~$)ACILITY NA<<)O Ill R.E.Ginna Nuclear Power.Plant OOCACT eeveeoCA Ol o 6 ooo244ios Apparent Voltage Dmp On Safequards 480 Volt Bus 14 Causes an Automatic Start of the A" Emer enc Diesel Generator CVCIIT CATO 14 Lt1 NveeocA 14 Al)O1T OATC lll OTlet1)ACILITICC INVOLVCO IOI>>OI>>T>>e OAY YCAA YCAA~COveeee>>AL
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~O.TONI Itl Ieell ICI N.TCNIltllel o TNC 1covl1 t<<ICNTo ot Io ct 1$: lc<<eeo<<ee a oeao o)o>>Ia>>ooe)I 0 I T%7141 TC.1 141 OTlet1 li)o)OV le AAeoeee~<<o>>e<<t S Te)L<<AC l<<s LICtNCCC CONTACT)OA Till Lt1 Iltl>>A<<et Wesley H.Backus Technical Assistant to the Operations Manager AIIOA COOl TILC)leONC NVQOCA 315 24-4 446 COeetLCTC ONC LINC)01 CAC>>l CO<<e)ONCNT)AILUAC OtlC1IOCO IN TNIC Att01T lltl cAvlc CYOTC<<e coco)oNCNT e)ANv t Ac TVACA ctoATACLC.+: "ke~~+p ju>>.~'TO Ie)AOC>>Aj~Yn~k,ee>>'~Qg, CAVlt CYOTCII s'>>>>>>'eh v+v;o>>>>~(e>>Q+PP+c~p, COee)ON C NT>>ANVtAC, TUACA CV)YLC4CNTAL AttOAT CA)CCTCO Ilel'YCC III tee, e<<ee<<e>>CA)CCTCO CV)<<IICCION CATO)X NO<<ACTAAcT IL<<evl s 1)00 eoas, I eeooeoeeev>>I)
~O.TONIItlIeellICIN.TCNIltllel oTNC1covl1t<<ICNTootIoct1$:lc<<eeo<<eeaoeaoo)o>>Ia>>ooe)I0IT%7141TC.1141OTlet1li)o)OVleAAeoeee~<<o>>e<<tSTe)L<<ACl<<sLICtNCCCCONTACT)OATillLt1Iltl>>A<<etWesleyH.BackusTechnical Assistant totheOperations ManagerAIIOACOOlTILC)leONC NVQOCA31524-4446COeetLCTC ONCLINC)01CAC>>lCO<<e)ONCNT
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<<esl 114 t1)CCTCO wo<<elttloN OATC Illl IIONT>>e CAY Y CAN On June 29, 1991 at 1754 EST with the reactor at approximately 98%full power, the"A" Emergency Diesel Generator started automatically due to an apparent undervoltage signal from the Bus 14 Undervoltage Monitoring System.The"A" Emergency Diesel Generator, after starting, attained proper voltage and frequency.
.+:"ke~~+pju>>.~'TOIe)AOC>>Aj~Yn~k,ee>>'~Qg, CAVltCYOTCIIs'>>>>>>'ehv+v;o>>>>~(e>>Q+PP+c~p, COee)ONCNT>>ANVtAC,TUACACV)YLC4CNTAL AttOATCA)CCTCOIlel'YCCIIItee,e<<ee<<e>>CA)CCTCOCV)<<IICCION CATO)XNO<<ACTAAcTIL<<evls1)00eoas,Ieeooeoeeev>>I)
By design, it did not close into Bus 14 because Bus 14 was at its proper voltage and being fed from its normal power supply.Immediate operator action was to verify that Bus 14 was energized and that the"A" Emergency Diesel Generator was operating normally.Subsequently) the"A" Emergency Diesel Generator was stopped and realigned for auto-standby.
III>>oee<<etvvoeee Itoeeee>>I>>o
The cause of the event has.not been positively determined, although off-site electrical disturbance is postulated.
<<esl114t1)CCTCOwo<<elttloN OATCIlllIIONT>>eCAYYCANOnJune29,1991at1754ESTwiththereactoratapproximately 98%fullpower,the"A"Emergency DieselGenerator startedautomatically duetoanapparentundervoltage signalfromtheBus14Undervoltage Monitoring System.The"A"Emergency DieselGenerator, afterstarting, attainedpropervoltageandfrequency.
Since the cause of this event has not been positively determined at this time, we will continue to investigate for the underlying cause.Any further corrective action will depend on the re'suits of this investigation.
Bydesign,itdidnotcloseintoBus14becauseBus14wasatitspropervoltageandbeingfedfromitsnormalpowersupply.Immediate operatoractionwastoverifythatBus14wasenergized andthatthe"A"Emergency DieselGenerator wasoperating normally.
eeAC toes ON IOACI
Subsequently) the"A"Emergency DieselGenerator wasstoppedandrealigned forauto-standby.
Thecauseoftheeventhas.notbeenpositively determined, althoughoff-siteelectrical disturbance ispostulated.
Sincethecauseofthiseventhasnotbeenpositively determined atthistime,wewillcontinuetoinvestigate fortheunderlying cause.Anyfurthercorrective actionwilldependonthere'suitsofthisinvestigation.
eeACtoesONIOACI
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~e~H(ICFMmdddA(045)L'ICENSEE EVENTREPORTILERITEXTCONTINUATION 3U.d.HUCLCA(IHKOULATOHY COMM(dd(OH AFFHOVEOOMdHO5150M(04dkF(Added(5((55 FACILITYHAMd(IIR.E.GinnaNuclearPowerPlantTEXTIN'cccMcccHmdvckd.vccNMcckncc(
~e~H(IC FMm dddA (045)L'ICENSEE EVENT REPORT ILERI TEXT CONTINUATION 3 U.d.HUCLCA(I HKOULATOHY COMM(dd(OH AFFHOVEO OMd HO 5150M(04 dkF(Added(5((55 FACILITY HAMd (II R.E.Ginna Nuclear Power Plant TEXT IN'ccc Mccc H mdvckd.vcc NMcckncc(4(NC Fckm J(d(4'cl ((T(OOC((ET HUMddll (1(0 s 0 0 0 24 491 Ld(I HUMddll (dl 5~OVCHZIAL 4 HVM k-006 kdVMIOH HUM 0 FAOd (51 02 DFO 6 PRE-EVE2iT PLANT CONDITIONS The plant was at approximately 984 steady state full power with no'ajor activities in progress.II.DESCRIPTION OF%TENT A.DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES:
4(NCFckmJ(d(4'cl((T(OOC((ETHUMddll(1(0s00024491Ld(IHUMddll(dl5~OVCHZIAL4HVMk-006kdVMIOHHUM0FAOd(5102DFO6PRE-EVE2iT PLANTCONDITIONS Theplantwasatapproximately 984steadystatefullpowerwithno'ajoractivities inprogress.
0 0 0 June 29, 1991, 1754 EDST: Event Date and Time h June 29, 1991, 1754 EDST: Discovery Date and Time June 29, 1991, 2013 EDST: "A" Emergency Diesel Generator stopped and realigned for Auto-standby B.EVENT: On June 29, 1991 at 1754 EDST, with the reactor at approximately 98%full power, the Control Room received the following alarms: L-14 (Bus 14.Undervoltage
II.DESCRIPTION OF%TENTA.DATESANDAPPROXIMATE TIMESOPMAJOROCCURRENCES:
-Safeguards) and J-24 (Emergency Diesel Gen 1A Panel).The Control Room operators immediately verified proper voltage on Bus 14 and that the normal power supply breaker was closed.The Control Room operators also verified that the"A" Emergency Diesel Generator had started and displayed proper voltage and frequency.
000June29,1991,1754EDST:EventDateandTimehJune29,1991,1754EDST:Discovery DateandTimeJune29,1991,2013EDST:"A"Emergency DieselGenerator stoppedandrealigned forAuto-standby B.EVENT:OnJune29,1991at1754EDST,withthereactoratapproximately 98%fullpower,theControlRoomreceivedthefollowing alarms:L-14(Bus14.Undervoltage
By design, the"A" Emergency Diesel Generator did not close into Bus, 14, as the bus voltage was normal and Bus 14 was still being supplied by its normal power supply.HAC FOAM 544*(I ddl
-Safeguards) andJ-24(Emergency DieselGen1APanel).TheControlRoomoperators immediately verifiedpropervoltageonBus14andthatthenormalpowersupplybreakerwasclosed.TheControlRoomoperators alsoverifiedthatthe"A"Emergency DieselGenerator hadstartedanddisplayed propervoltageandfrequency.
Bydesign,the"A"Emergency DieselGenerator didnotcloseintoBus,14,asthebusvoltagewasnormalandBus14wasstillbeingsuppliedbyitsnormalpowersupply.HACFOAM544*(Iddl
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~0~eNRCSotw295A(042IL'ICENSEE EVENTREPORTILERITEXTCONTINUATION U.S.NUCLEARREQVLATORY COMMI55ION ASSROVEOOM9NOSISOWI04JEXSIRES,9121/99SACILITYNAME111OOCKETNVMEER121LERNVMQEII19155QUENTIAL NUMREVISIONNUMSAOEl21R.E.GinnaNuclearPowerPlantTEXTIIJ~<<>>5~N~.v>>NAS55JNJHRCFOnn2OEA'5IIITIo5ooo244,0060003pF06Subsequently, Auxiliary operators weredispatched tochecktheBus14Undervoltage Monitoring Systemcabinetsandtheoperation ofthe"A"Emergency DieselGenerator.
~0~e NRC Sotw 295A (042 I L'ICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.NUCLEAR REQVLATORY COMMI55ION ASSROVEO OM9 NO SISOWI04 J EXSIRES, 9121/99 SACILITY NAME 111 OOCKET NVMEER 121 LER NVMQEII 191 55QUENTIAL NUM REVISION NUM SAOE l21 R.E.Ginna Nuclear Power Plant TEXT IIJ~<<>>5~N~.v>>NAS55JNJ HRC FOnn 2OEA'5I I ITI o 5 o o o2 44, 006 00 03pF 0 6 Subsequently, Auxiliary operators were dispatched to check the Bus 14 Undervoltage Monitoring System cabinets and the operation of the"A" Emergency Diesel Generator.
Theoperation ofthe"A"Emergency DieselGenerator wasfoundtobenormal.Noundervoltage triptargetswereobservedonBus14orBus18(boththesebusesarefedbythe"A"Emergency
The operation of the"A" Emergency Diesel Generator was found to be normal.No undervoltage trip targets were observed on Bus 14 or Bus 18 (both these buses are fed by the"A" Emergency.Diesel Generator).
.DieselGenerator).
During this event, routine activities were occurring at off-site Station 204.At approximately the same time as the apparent undervoltage condition occurred on Bus 14, a 34.5 kv capacitor bank was being removed from service.This is a routine action to correct off-site voltage situations.
Duringthisevent,routineactivities wereoccurring atoff-siteStation204.Atapproximately thesametimeastheapparentundervoltage condition occurredonBus14,a34.5kvcapacitor bankwasbeingremovedfromservice.Thisisaroutineactiontocorrectoff-sitevoltagesituations.
Station 204'eeds Circuit 751, which was the normal off-site power supply to Buses 14 and 18.Control=Room operators notified higher supervision and the Nuclear Regulatory Commission of the event.To prove operability of the Undervoltage Monitoring System, the Results and Test (R&T)Department performed Periodic Test procedure PT-9.1 (Undervoltage Protection 480 Volt Safeguards Busses)on Bus 14.After PT-9.1.was successfully completed, the"A" Emergency Diesel Generator was stopped and realigned for Auto-standby.
Station204'eedsCircuit751,whichwasthenormaloff-sitepowersupplytoBuses14and18.Control=Roomoperators notifiedhighersupervision andtheNuclearRegulatory Commission oftheevent.Toproveoperability oftheUndervoltage Monitoring System,theResultsandTest(R&T)Department performed PeriodicTestprocedure PT-9.1(Undervoltage Protection 480VoltSafeguards Busses)onBus14.AfterPT-9.1.wassuccessfully completed, the"A"Emergency DieselGenerator wasstoppedandrealigned forAuto-standby.
C.INOPERABLE STRUC'HIRES, COMPONENTS s OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None.D.OTEGsR SYSTEMS OR SECONDARY PUNCTIONS AFFECTED: E.None.METHOD OP DISCOVERY:
C.INOPERABLE STRUC'HIRES, COMPONENTS sORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:None.D.OTEGsRSYSTEMSORSECONDARY PUNCTIONS AFFECTED:
The events were immediately apparent due to alarms and indications in the Control Room.NRC SORM 255A I94ll
E.None.METHODOPDISCOVERY:
Theeventswereimmediately apparentduetoalarmsandindications intheControlRoom.NRCSORM255AI94ll
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<<ACSottoSSSA~eL'ICENSEE EVENTREPORT(LER)TEXTCONTINUATION V,S.<<UCLEAIIIlfOULATOIIY COMMISSIOII ASSAOYEOOMSHO3150MIOIIEXSIAES,SISIl95SACILITYNAMEIllR.E.GinnaNuclearPowerPlantTEXTillnave<<WCe<<nquseCvASOdakevWlYPCArm~'llIITIOOCKETIIUMSEII11Iosooo24LEII<<UMSEIIISI5~4UC<<VIAL'SV<<IONHUM<<'"<<UMf<<9-1-006-00~AOSISI04o~06F.OPERATORACTXON:Following theBus14Undervoltage Alarmandthe"A"Emergency DieselGenerator automatic start,theCo'ntrolRoomoperators immediately verifiedpropervoltageonBus14viathenormalpowersupplyand',thatthe"A"Emergency DieselGenerator displayed propervoltageandfrequency.
<<AC Sotto SSSA~e L'ICENSEE EVENT REPORT (LER)TEXT CONTINUATION V,S.<<UCLEAII Ilf OULATOIIY COMMISSIOII ASSAOYEO OMS HO 3150MIOI I EXSIAES, SISI l95 SACILITY NAME Ill R.E.Ginna Nuclear Power Plant TEXT ill nave<<WCe<<nquseC vAS OdakevW lYPC Arm~'ll I ITI OOCKET IIUMSEII 11I o s o o o 2 4 LEII<<UMSEII ISI 5~4UC<<VIAL'S V<<ION HUM<<'"<<UM f<<9-1-0 06-00~AOS ISI 0 4 o~0 6 F.OPERATOR ACTXON: Following the Bus 14 Undervoltage Alarm and the"A" Emergency Diesel Generator automatic start, the Co'ntrol Room operators immediately verified proper voltage on Bus 14 via the normal power supply and',that the"A" Emergency Diesel Generator displayed proper voltage and frequency.
Subsequently, Auxiliary operators weredis'patched tocheck-theBus14undervoltage monitoring systemand"A"Emergency DieselGenerator operation.
Subsequently, Auxiliary operators were dis'patched to check-the Bus 14 undervoltage monitoring system and"A" Emergency Diesel Generator operation.
The"A"Emergency DieselGenerator operation wasnormaland,noundervoltage triptargetswereobservedonBus14orBus18.'t"The"A"Emergency DieselGenerator wassubsequently stoppedandrealigned forAuto-standby.
The"A" Emergency Diesel Generator operation was normal and ,no undervoltage trip targets were observed on Bus 14 or Bus 18.'t" The"A" Emergency Diesel Generator was subsequently stopped and realigned for Auto-standby.
G.SAFETXSXSTEMRESPONSES:
G.SAFETX SXSTEM RESPONSES:
The"A"Emergency DieselGenerator automatically startedanddisplayed propervoltageandfrequency.
The"A" Emergency Diesel Generator automatically started and displayed proper voltage and frequency.
'IXI.CAUSEOFEV19Fl'.XMM1sDIATE CAUSE:Theautomatic actuation ofthe-"A"Emergency DieselGenerator wasduetoanapparentundervoltage signalfromtheBus14undervoltage monitoring system.B.ROOTCAUSE:Theunderlying, causeoftheapparentundervoltage signalfromtheBus14undervoltage monitoring systemisnotpositively determined atthistime..MACSO<<MSSSAI941l
'IXI.CAUSE OF EV19Fl'.XMM1sDIATE CAUSE: The automatic actuation of the-"A" Emergency Diesel Generator was due to an apparent undervoltage signal from the Bus 14 undervoltage monitoring system.B.ROOT CAUSE: The underlying, cause of the apparent undervoltage signal from the Bus 14 undervoltage monitoring system is not positively determined at this time..MAC SO<<M SSSA I941l
~0 IIACSovvvv444A14451~eoeL'ICENSEE EVENTREPORT(LERITEXTCONTINUATION U,E.NUCLEAAAEOULATOAY COMMIEEIOII
~0 IIAC Sovvvv 444A 14451~e oe L'ICENSEE EVENT REPORT (LERI TEXT CONTINUATION U,E.NUCLEAA AEOULATOAY COMMIEEIOII
/ASSAOVEOOMEIVO1150MIOeEXSIAES,4151/45SACILITYIIAMEIllR.E.GinnaNuclearPawerPlantTExTlllnaveMeceaeevveevLvvMvneeevalvYACSevvnSELAYlIITICOCKETIvUMEEA111osooo244vEAALEIIIIUMEEA14154004VVTIAL~VUM006ntvlelOMVVVM00SAOEIEI050F06IV.ANALYSISOFEVENTTheeventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),
/ASSAOVEO OME IVO 1150MIOe EXSIAES, 4151/45 SACILITY IIAME Ill R.E.Ginna Nuclear Pawer Plant TExT lll nave Mece a eevveevL vvM vneeeval vYAC Sevvn SELA Yl I ITI COCKET IvUMEEA 111 osooo244 vEAA LEII IIUMEEA 141 5 4 0 0 4 VV T I A L~VUM 0 0 6 ntvlelOM VVVM 0 0 SAOE IEI 0 50F 06 IV.ANALYSIS OF EVENT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires'eporting of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor.Protection System (RPS)".The starting of the"A" Emergency Diesel Generator was an automatic actuation of an ESF system.An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
whichrequires'eporting of,"anyeventorcondition thatresultedinmanualorautomatic actuation ofanyEngineered SafetyFeature(ESF)including theReactor.Protection System(RPS)".Thestartingofthe"A"Emergency DieselGenerator wasanautomatic actuation ofanESFsystem.Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
There were no operational or safety consequences or implications attributed to the starting of the"A" Emergency Diesel Generator because: 0 The"A" Emergency Diesel Generator operated as designed.o Both Bus 14 power supplies (i.e.normal and emergency) were either in use or available throughout the event.o The Bus 14 undervoltage monitoring system operation was in the conservative direction, (i.e.the operation actuated the automatic start of the"A" Emergency Diesel Generator).
Therewerenooperational orsafetyconsequences orimplications attributed tothestartingofthe"A"Emergency DieselGenerator because:0The"A"Emergency DieselGenerator operatedasdesigned.
Based on the above, it can be concluded that the public's health and safety was assured at all times.V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The R&T Department successfully completed PT-9.1 on Bus 14 and the"A" Emergency Diesel Generator was stopped and aligned for Auto-standby.
oBothBus14powersupplies(i.e.normalandemergency) wereeitherinuseoravailable throughout theevent.oTheBus14undervoltage monitoring systemoperation wasintheconservative direction, (i.e.theoperation actuatedtheautomatic startofthe"A"Emergency DieselGenerator).
~V A C S 0 VI M 544 A 14411
Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:oTheR&TDepartment successfully completed PT-9.1onBus14andthe"A"Emergency DieselGenerator wasstoppedandalignedforAuto-standby.
~1~0 NAC>arm SEEA I HEI~0 I.'ICENSEE EVENT REPORT (I.ER)TEXT CONTINUATION V.S.NVCLEAII IIEOVLATOIIY COMMISSION I Atf AOV EO OME HO$1$0MIOI E)CrllIES.
~VACS0VIM544A14411
EISI4$FACILITY NAME III OOCIIET NVMEEII IEI YEAA LEII NVMEEII IEI IEQVEHTIAL 4 M IA AEV ISIO<NVM IA~ACE ISI R.E.Ginna Nuclear Power Plant TEIL ill mort apece e mewaf.wt aAkenV HAC Fiwn DELI'Il I I Tl o s o o o.24 4 9 1 006 0 006'F 0 6 B.ACTXON TAKEN OR PLANNED TO PREVENT RECURRENCE:
~1~0 NAC>armSEEAIHEI~0I.'ICENSEE EVENTREPORT(I.ER)TEXTCONTINUATION V.S.NVCLEAIIIIEOVLATOIIY COMMISSION IAtfAOVEOOMEHO$1$0MIOIE)CrllIES.
0 0 0 As the underlying cause of the event has not been determined at this time, investigations will continue to positively determine the underlying cause of this event.Any further corrective actions will depend on the results of these investigations.
EISI4$FACILITYNAMEIIIOOCIIETNVMEEIIIEIYEAALEIINVMEEIIIEIIEQVEHTIAL 4MIAAEVISIO<NVMIA~ACEISIR.E.GinnaNuclearPowerPlantTEILillmortapeceemewaf.wtaAkenVHACFiwnDELI'IlIITlosooo.244910060006'F06B.ACTXONTAKENORPLANNEDTOPREVENTRECURRENCE:
Electrical system monitoring records have been reviewed, and indicate that removal of the capacitor bank resulted in a small and routine voltage transient.
000Astheunderlying causeoftheeventhasnotbeendetermined atthistime,investigations willcontinuetopositively determine theunderlying causeofthisevent.Anyfurthercorrective actionswilldependontheresultsoftheseinvestigations.
Electrical system monitoring has been increased on Circuit 751.0 The interface between the undervoltage monitoring system and diesel start circuitry will continue to be evaluated,'to determine if the undervoltage system is reacting as designed for small voltage fluctuations.
Electrical systemmonitoring recordshavebeenreviewed, andindicatethatremovalofthecapacitor bankresultedinasmallandroutinevoltagetransient.
ADDXTXONAL XNFORMATION A.B.PAXLED COMPONENTS:
Electrical systemmonitoring hasbeenincreased onCircuit751.0Theinterface betweentheundervoltage monitoring systemanddieselstartcircuitry willcontinuetobeevaluated,'to determine iftheundervoltage systemisreactingasdesignedforsmallvoltagefluctuations.
None.PREVXOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with an undetermined root cause at Ginna Station could be identified.
ADDXTXONAL XNFORMATION A.B.PAXLEDCOMPONENTS:
C.SPECIAL COMMENTS None.%AC SOIIM SEEA ISA l
None.PREVXOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswithanundetermined rootcauseatGinnaStationcouldbeidentified.
~0 1~f}}
C.SPECIALCOMMENTSNone.%ACSOIIMSEEAISAl
~01~f}}

Revision as of 13:18, 7 July 2018

LER 91-006-00:on 910629,EDG a Started Automatically Due to Apparent Undervoltage Signal from Bus 14 Undervoltage Monitoring Sys.Root Cause Not Determined.Bus 14 Energized & EDG Declared operable.W/910729 Ltr
ML17262A566
Person / Time
Site: Ginna Constellation icon.png
Issue date: 07/29/1991
From: BACKUS W H, MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-91-006, LER-91-6, NUDOCS 9108050066
Download: ML17262A566 (16)


Text

ACCELERATED DISTRIBUTION DEMON~0 TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9108050066 DOC.DATE: 91/07/29 NOTARIZED:, NO FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1,, Rochester G AUTH.NAME AUTHOR AFFILIATION

.BACKUS,W.H.

Rochester Gas&Electric Corp.MECREDY,R.C.

'ochester Gas&Electric Corp.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000244 II

SUBJECT:

LER 91-006-00:on 910629,EDG A started automatically due to apparent undervoltage signal from Bus 14 undervoltage monitoring sys.Root cause not determined.Bus 14 energized&EDG declared operable.W/910729 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR

!ENCL I SIZE: 7 TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).

D 05000244 A RECIPIENT ID CODE/NAME PD1-3 LA JOHNSON,A INTERNAL: ACNW AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB SD NRRfDST~LBSD1 REG F~02 RGN1 FILE 01 EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POORE,W.~7&75 Htt<w'(COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1'1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICBSH3 NRR/DST/SRXB SE RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT'OPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1'1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOiv!P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCU5!EiiTS YOU DON'T NEED!A D D S FULL TEXT CONVERSION REQUIRED-TOTAL NUMBER OF COPIES REQUIRED: LTTR 31 ENCL 31

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"," ROCHESTER GAS AND ELECTRIC CORPORATION ROSERTC h1ECREDY Vice President Ctnna Nucfear Prnducticrn oe'I'a',,'~1th~~'r Stale., 89 EAST AVENUE, ROCHESTER N.K 14649-0001 i TELEPHONE AAEACODETIB 546 2700 July 29, 1991 I U.S.Nuclear Regulatory Commission Document Control Desk Washington,-

DC 20555

Subject:

LER 91-006, Apparent Voltage Drop on Safeguards 480 Volt Bus 14 Causes an Automatic Start of the"A" Emergency Diesel Generator R.E.Ginna Nuclear Power Plant Docket No.50-244 In-accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv),which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF),"including the Reactor Protection System (RPS)", the attached Licensee Event Report LER 91-006 is hereby submitted.

This event has in no way affected the public's health and safety.Very truly yours, Robert C.Mecr dy xc U.S.Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 9 i 080s00g,(, PDR ADOCK Ort.iot)-4 i

NAC tas lli IOACI LICENSEE EVENT REPORT (LERI UA NUOLCAA AoovLATCAocc>>se&lcw Attleovto oleo NIL OIN olov CAOIACO.O)te/

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<<esl 114 t1)CCTCO wo<<elttloN OATC Illl IIONT>>e CAY Y CAN On June 29, 1991 at 1754 EST with the reactor at approximately 98%full power, the"A" Emergency Diesel Generator started automatically due to an apparent undervoltage signal from the Bus 14 Undervoltage Monitoring System.The"A" Emergency Diesel Generator, after starting, attained proper voltage and frequency.

By design, it did not close into Bus 14 because Bus 14 was at its proper voltage and being fed from its normal power supply.Immediate operator action was to verify that Bus 14 was energized and that the"A" Emergency Diesel Generator was operating normally.Subsequently) the"A" Emergency Diesel Generator was stopped and realigned for auto-standby.

The cause of the event has.not been positively determined, although off-site electrical disturbance is postulated.

Since the cause of this event has not been positively determined at this time, we will continue to investigate for the underlying cause.Any further corrective action will depend on the re'suits of this investigation.

eeAC toes ON IOACI

~0~0

~e~H(IC FMm dddA (045)L'ICENSEE EVENT REPORT ILERI TEXT CONTINUATION 3 U.d.HUCLCA(I HKOULATOHY COMM(dd(OH AFFHOVEO OMd HO 5150M(04 dkF(Added(5((55 FACILITY HAMd (II R.E.Ginna Nuclear Power Plant TEXT IN'ccc Mccc H mdvckd.vcc NMcckncc(4(NC Fckm J(d(4'cl ((T(OOC((ET HUMddll (1(0 s 0 0 0 24 491 Ld(I HUMddll (dl 5~OVCHZIAL 4 HVM k-006 kdVMIOH HUM 0 FAOd (51 02 DFO 6 PRE-EVE2iT PLANT CONDITIONS The plant was at approximately 984 steady state full power with no'ajor activities in progress.II.DESCRIPTION OF%TENT A.DATES AND APPROXIMATE TIMES OP MAJOR OCCURRENCES:

0 0 0 June 29, 1991, 1754 EDST: Event Date and Time h June 29, 1991, 1754 EDST: Discovery Date and Time June 29, 1991, 2013 EDST: "A" Emergency Diesel Generator stopped and realigned for Auto-standby B.EVENT: On June 29, 1991 at 1754 EDST, with the reactor at approximately 98%full power, the Control Room received the following alarms: L-14 (Bus 14.Undervoltage

-Safeguards) and J-24 (Emergency Diesel Gen 1A Panel).The Control Room operators immediately verified proper voltage on Bus 14 and that the normal power supply breaker was closed.The Control Room operators also verified that the"A" Emergency Diesel Generator had started and displayed proper voltage and frequency.

By design, the"A" Emergency Diesel Generator did not close into Bus, 14, as the bus voltage was normal and Bus 14 was still being supplied by its normal power supply.HAC FOAM 544*(I ddl

~0

~0~e NRC Sotw 295A (042 I L'ICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.NUCLEAR REQVLATORY COMMI55ION ASSROVEO OM9 NO SISOWI04 J EXSIRES, 9121/99 SACILITY NAME 111 OOCKET NVMEER 121 LER NVMQEII 191 55QUENTIAL NUM REVISION NUM SAOE l21 R.E.Ginna Nuclear Power Plant TEXT IIJ~<<>>5~N~.v>>NAS55JNJ HRC FOnn 2OEA'5I I ITI o 5 o o o2 44, 006 00 03pF 0 6 Subsequently, Auxiliary operators were dispatched to check the Bus 14 Undervoltage Monitoring System cabinets and the operation of the"A" Emergency Diesel Generator.

The operation of the"A" Emergency Diesel Generator was found to be normal.No undervoltage trip targets were observed on Bus 14 or Bus 18 (both these buses are fed by the"A" Emergency.Diesel Generator).

During this event, routine activities were occurring at off-site Station 204.At approximately the same time as the apparent undervoltage condition occurred on Bus 14, a 34.5 kv capacitor bank was being removed from service.This is a routine action to correct off-site voltage situations.

Station 204'eeds Circuit 751, which was the normal off-site power supply to Buses 14 and 18.Control=Room operators notified higher supervision and the Nuclear Regulatory Commission of the event.To prove operability of the Undervoltage Monitoring System, the Results and Test (R&T)Department performed Periodic Test procedure PT-9.1 (Undervoltage Protection 480 Volt Safeguards Busses)on Bus 14.After PT-9.1.was successfully completed, the"A" Emergency Diesel Generator was stopped and realigned for Auto-standby.

C.INOPERABLE STRUC'HIRES, COMPONENTS s OR SYSTEMS THAT CONTRIBUTED TO THE EVENT: None.D.OTEGsR SYSTEMS OR SECONDARY PUNCTIONS AFFECTED: E.None.METHOD OP DISCOVERY:

The events were immediately apparent due to alarms and indications in the Control Room.NRC SORM 255A I94ll

.OO

<<AC Sotto SSSA~e L'ICENSEE EVENT REPORT (LER)TEXT CONTINUATION V,S.<<UCLEAII Ilf OULATOIIY COMMISSIOII ASSAOYEO OMS HO 3150MIOI I EXSIAES, SISI l95 SACILITY NAME Ill R.E.Ginna Nuclear Power Plant TEXT ill nave<<WCe<<nquseC vAS OdakevW lYPC Arm~'ll I ITI OOCKET IIUMSEII 11I o s o o o 2 4 LEII<<UMSEII ISI 5~4UC<<VIAL'S V<<ION HUM<<'"<<UM f<<9-1-0 06-00~AOS ISI 0 4 o~0 6 F.OPERATOR ACTXON: Following the Bus 14 Undervoltage Alarm and the"A" Emergency Diesel Generator automatic start, the Co'ntrol Room operators immediately verified proper voltage on Bus 14 via the normal power supply and',that the"A" Emergency Diesel Generator displayed proper voltage and frequency.

Subsequently, Auxiliary operators were dis'patched to check-the Bus 14 undervoltage monitoring system and"A" Emergency Diesel Generator operation.

The"A" Emergency Diesel Generator operation was normal and ,no undervoltage trip targets were observed on Bus 14 or Bus 18.'t" The"A" Emergency Diesel Generator was subsequently stopped and realigned for Auto-standby.

G.SAFETX SXSTEM RESPONSES:

The"A" Emergency Diesel Generator automatically started and displayed proper voltage and frequency.

'IXI.CAUSE OF EV19Fl'.XMM1sDIATE CAUSE: The automatic actuation of the-"A" Emergency Diesel Generator was due to an apparent undervoltage signal from the Bus 14 undervoltage monitoring system.B.ROOT CAUSE: The underlying, cause of the apparent undervoltage signal from the Bus 14 undervoltage monitoring system is not positively determined at this time..MAC SO<<M SSSA I941l

~0 IIAC Sovvvv 444A 14451~e oe L'ICENSEE EVENT REPORT (LERI TEXT CONTINUATION U,E.NUCLEAA AEOULATOAY COMMIEEIOII

/ASSAOVEO OME IVO 1150MIOe EXSIAES, 4151/45 SACILITY IIAME Ill R.E.Ginna Nuclear Pawer Plant TExT lll nave Mece a eevveevL vvM vneeeval vYAC Sevvn SELA Yl I ITI COCKET IvUMEEA 111 osooo244 vEAA LEII IIUMEEA 141 5 4 0 0 4 VV T I A L~VUM 0 0 6 ntvlelOM VVVM 0 0 SAOE IEI 0 50F 06 IV.ANALYSIS OF EVENT The event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a)(2)(iv), which requires'eporting of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor.Protection System (RPS)".The starting of the"A" Emergency Diesel Generator was an automatic actuation of an ESF system.An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:

There were no operational or safety consequences or implications attributed to the starting of the"A" Emergency Diesel Generator because: 0 The"A" Emergency Diesel Generator operated as designed.o Both Bus 14 power supplies (i.e.normal and emergency) were either in use or available throughout the event.o The Bus 14 undervoltage monitoring system operation was in the conservative direction, (i.e.the operation actuated the automatic start of the"A" Emergency Diesel Generator).

Based on the above, it can be concluded that the public's health and safety was assured at all times.V.CORRECTIVE ACTION A.ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS: o The R&T Department successfully completed PT-9.1 on Bus 14 and the"A" Emergency Diesel Generator was stopped and aligned for Auto-standby.

~V A C S 0 VI M 544 A 14411

~1~0 NAC>arm SEEA I HEI~0 I.'ICENSEE EVENT REPORT (I.ER)TEXT CONTINUATION V.S.NVCLEAII IIEOVLATOIIY COMMISSION I Atf AOV EO OME HO$1$0MIOI E)CrllIES.

EISI4$FACILITY NAME III OOCIIET NVMEEII IEI YEAA LEII NVMEEII IEI IEQVEHTIAL 4 M IA AEV ISIO<NVM IA~ACE ISI R.E.Ginna Nuclear Power Plant TEIL ill mort apece e mewaf.wt aAkenV HAC Fiwn DELI'Il I I Tl o s o o o.24 4 9 1 006 0 006'F 0 6 B.ACTXON TAKEN OR PLANNED TO PREVENT RECURRENCE:

0 0 0 As the underlying cause of the event has not been determined at this time, investigations will continue to positively determine the underlying cause of this event.Any further corrective actions will depend on the results of these investigations.

Electrical system monitoring records have been reviewed, and indicate that removal of the capacitor bank resulted in a small and routine voltage transient.

Electrical system monitoring has been increased on Circuit 751.0 The interface between the undervoltage monitoring system and diesel start circuitry will continue to be evaluated,'to determine if the undervoltage system is reacting as designed for small voltage fluctuations.

ADDXTXONAL XNFORMATION A.B.PAXLED COMPONENTS:

None.PREVXOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with an undetermined root cause at Ginna Station could be identified.

C.SPECIAL COMMENTS None.%AC SOIIM SEEA ISA l

~0 1~f