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{{#Wiki_filter:REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RXDS)ACCESSZONNBR:9906080307DOC.DATE:99/06/02NOTARIZED:NODOCKETIPACZL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterGterG05000244AUTH.NAMEAUTHORAFFILIATIONSTMARTIN,J.T.RochesterGas&.ElectricCorp.MECREDY,R.C.~RochesterGas&.ElectricCorp.RECIP.NAME,RECIPIENTAFFILIATIONVISSXNG,G.S.
{{#Wiki_filter:REGULATORY INFORMATION DISTRIBUTION SYSTEM(RXDS)ACCESSZONNBR:9906080307 DOC.DATE:
99/06/02NOTARIZED:
NODOCKETIPACZL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GterG05000244AUTH.NAMEAUTHORAFFILIATION STMARTIN,J.T.
Rochester Gas&.ElectricCorp.MECREDY,R.C.
~Rochester Gas&.ElectricCorp.RECIP.NAME
,RECIPIENT AFFILIATION VISSXNG,G.S.


==SUBJECT:==
==SUBJECT:==
LER99-009-00:on990503,instrumentationdeclaredinoperableinmultiplechannelsresultedinconditionprohibitedbyTS.CausedbyunanticipatedhighfrequencyACvoltagerippe.EnteredTSLCO3.0.3.With990602ltr.DISTRIBUTIONCODEXE22TCOPIESRECEIVEDeLTRgENCL(SIZEaTITLE:50.73/50.9LicenseeEventReport(LER),XncidentRpt,etc.NOTES:LicenseExpdateinaccordancewith10CPR2,2.109(9/19/72).G050002440RECIPIENTZDCODE/NAMELPD1-1PDINTERNAL:AEOD/SPD/RRABNRR/DZPM/IOLBNRR/DRIP/REXBRES/DET/EIBEXTERNAL:LSTLOBBYWARDNOACPOORE,W.NRCPDRCOPIESLTTRENCL11111'1111111.111RECIPIENTXDCODE/NAMEVZSSXNG,G.FILECENTERR/DXPM/XQMBNRR/DSSA/SPLBRGN1PILE01LMXTCOMARSHALLNOACQUEENER,DSNUDOCSFULLTXTCOPIESLTTRENCL1111111111111111NOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATIONREMOVEDFROMDISTRIBUTIONLISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION<CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION41S-2083FULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR16ENCL16 4HDROCHESTfRGASANDE'ELECTRICCORFORATION~89EASTAVENUE,ROCHfSTER,N,YI46d9.000IAREACODE216586-27MRosERTc.MEcREDYVicePresislenlt4uc!eorOperosionsJune2,1999U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:GuyS.VissingProjectDirectorateI-1Washington,D.C.20555
LER99-009-00:on 990503,instrumentation declaredinoperable inmultiplechannelsresultedincondition prohibited byTS.Causedbyunanticipated highfrequency ACvoltagerippe.EnteredTSLCO3.0.3.With 990602ltr.DISTRIBUTION CODEXE22TCOPIESRECEIVEDeLTRgENCL(SIZEaTITLE:50.73/50.9 LicenseeEventReport(LER),XncidentRpt,etc.NOTES:License Expdateinaccordance with10CPR2,2.109(9/19/72)
.G050002440RECIPIENT ZDCODE/NAME LPD1-1PDINTERNAL:
AEOD/SPD/RRAB NRR/DZPM/IOLB NRR/DRIP/REXB RES/DET/EIB EXTERNAL:
LSTLOBBYWARDNOACPOORE,W.NRCPDRCOPIESLTTRENCL11111'1111111.111RECIPIENT XDCODE/NAME VZSSXNG,G.
FILECENTERR/DXPM/XQMB NRR/DSSA/SPLB RGN1PILE01LMXTCOMARSHALLNOACQUEENER,DS NUDOCSFULLTXTCOPIESLTTRENCL1111111111111111NOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION<
CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 41S-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
LTTR16ENCL16 4HDROCHESTfR GASANDE'ELECTRIC CORFORATION
~89EASTAVENUE, ROCHfSTER, N,YI46d9.000I AREACODE216586-27MRosERTc.MEcREDYVicePresislenl t4uc!eorOperosions June2,1999U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555


==Subject:==
==Subject:==
.LER1999-009,InstrumentationDeclaredInoperableinMultipleChannelsResultsinConditionProhibitedbyTechnicalSpecificationsR.E.GinnaNuclearPowerPlantDocketNo.50-244
.LER1999-009, Instrumentation DeclaredInoperable inMultipleChannelsResultsinCondition Prohibited byTechnical Specifications R.E.GinnaNuclearPowerPlantDocketNo.50-244


==DearMr.Vissing:==
==DearMr.Vissing:==
TheattachedLicenseeEventReportLER1999-009issubmittedinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperationorconditionprohibitedbytheplant'sTechnicalSpecifications".Veryrulyyours,XC:Mr.GuyS.Vissing(MailStop8C2)ProjectDirectorateI-1DivisionofReactorProjects-I/IIOfficeofNuclearReactorRegulationU.S.NuclearRegulatoryCommissionWashington,D.C.20555RegionalAdministrator,RegionIU.S.NuclearRegulatoryCommission475AllendaleRoadKingofPrussia,PA19406U.S.NRCGinnaSeniorResidentInspector+t990b080307'll's!0602PDRADQCK05000244SPDR NRCFORM866IBI%BIU.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEYENTREPORT(LER)fSoereverseforrequirednumberof'digitslcharactersforeachb(ocklM5Q''IkrNpNIIsp@ei''gA'P%88Sy'nformationcoBoctP)arortuost:50hrs.ReportedlessonslearnedarencorporatedkrtotheBcenskrgprocessandfodbacktohdustry.ForwardcommentsregardingburdenestimatetotheRecordsMsnagernontBranchp4F33),U.S.NudearRegulatoryCommfssbn,Wasfsngton,DC205554001~andtothePaperworkReductionProject(31500104),OfreeofManagementandBudget,WasNngton,DC20503.Ifaninformationcoeect'ondoesnotdisplayacurrendyvsMOMB,controlnumber,theNRCmaynotconductorsponsor.andaFACILITYNAMEI11R.E.GinnaNuc(earPowerPlantIDOCKETNUMBERI2)05000244PAGEI3)1OF7TITLEte)InstrumentationDeclaredInoperableinMultipleChannelsResultsinConditionProhibitedbyTechnicalSpecifications05031999,EVENTDATE(5)OAYLERNUMBER(6)SEOUFNTIALRENSIONNUMBERNUMBER1999",009-00MONTHON06021999REPORTDATE(7)DOCKETNUMSER05000OOCKETNUMSER05000FACfLITYNAMEFACILrTYNAMEOTHERFACILITIESINVOLVED(6)OPERATINGMODE(9)POWERLEVEL(10)090URSUANTTOTHEREQUIREMENTHISREPORTISSUBMITTFDP20.2203(a)(2)(v)20.2203(a)(3)(i)20.2201(b)20.2203(a)(1)20.2203(a)(3)(ii)20.2203(a)(2)(i)20.2203(a}(4)50.36(cl(1)20.2203(a)(2)(ii)20.2203(a)(2)(iii}50.36(c)(2)20.2203(a)(2)(iv)LICENSEECONTACTFORTHISLER(12)TSOF10CFRB:(Checkoneormore)(11)50.73(a)(2)(viii)50.73(a}(2}(x)X50.73(a)(2)(i)(B)50.73(a)(2)(ii)73.7150.73(a}(2l(iii)OTHER50.73(a)(2wiv)50.73(a)(2)(v)SpecifymAbstractbeloworinNRCForm355A50.73(a)(2)(vii)TELEPMONENUMSER(InrrudeAresCode)JohnT.St.Martin-TechnicalAssistant(716)771-3641CAUSESYSTEMCOMPONOITMANUFACTURERREPORTABLETOEPOSCAUSESYS'fEMMANUFACTURERREPORTABLETOEPIXSUPPLEMENTALREPORTEXPECTED(l4)YES(Ifyes,completeEXPECTEDSUBMISSIONDATE).NOXEXPECTEDSUBMISSIONDATER5)IlONTHOAYABSTRACT(Limitto1400spaces,i.e.,approximately15single.spacedtypewrittenlines}(16)OnMay3,1999,theplantwasinMode1atapproximately90%steadystatereactorpower.IthadpreviouslybeendeterminedthatOvertemperatureDeltaTandOverpowerDeltaTbistabletripsetpointswerepotentiallynon-conservativeonthreeoutoffourreactorprotectionsystemchannels,andanevaluationwasinprogress.Atapproximately2330EDST,instrumentationforthesethreechannelswasdeclaredinoperable.ImmediatecorrectiveactionwastoenteiTechnicalSpecificationLimitingConditionforOperation3.0.3,andtakeactionstorestorethechannelstooperablestatus.Followingreplacementoftheaffectedbistableswithbistab(esofadifferentdesign,thebistabletripsetpointswererecalibratedandthreeoffourchannelsweredeclaredoperable.TheplantexitedLimitingConditionforOperation3.0.3.TheunderlyingcauseoftheeventwasanunanticipatedhighfrequencyACvoltagerippleontheDeltaTsignalsthatadverselyaffectedthetripsetpointsforthebistables.CorrectiveactiontopreventrecurrenceisoutlinedinSectionV.B.  
TheattachedLicenseeEventReportLER1999-009issubmitted inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications".
Veryrulyyours,XC:Mr.GuyS.Vissing(MailStop8C2)ProjectDirectorate I-1DivisionofReactorProjects-I/IIOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555RegionalAdministrator, RegionIU.S.NuclearRegulatory Commission 475Allendale RoadKingofPrussia,PA19406U.S.NRCGinnaSeniorResidentInspector
+t990b080307
'll's!0602PDRADQCK05000244SPDR NRCFORM866IBI%BIU.S.NUCLEARREGULATORY COMMISSION LICENSEEEYENTREPORT(LER)fSoereverseforrequirednumberof'digitslcharacters foreachb(ocklM5Q''IkrNpNIIsp@ei''gA'P%88Sy'nformation coBoctP)a rortuost:
50hrs.Reportedlessonslearnedarencorporated krtotheBcenskrgprocessandfodbacktohdustry.Forwardcommentsregarding burdenestimatetotheRecordsMsnagernont Branchp4F33),U.S.NudearRegulatory Commfssbn, Wasfsngton, DC205554001
~andtothePaperwork Reduction Project(31500104),
OfreeofManagement andBudget,WasNngton, DC20503.Ifaninformation coeect'on doesnotdisplayacurrendyvsMOMB,controlnumber,theNRCmaynotconductorsponsor.andaFACILITYNAMEI11R.E.GinnaNuc(earPowerPlantIDOCKETNUMBERI2)05000244PAGEI3)1OF7TITLEte)Instrumentation DeclaredInoperable inMultipleChannelsResultsinCondition Prohibited byTechnical Specifications 05031999,EVENTDATE(5)OAYLERNUMBER(6)SEOUFNTIAL RENSIONNUMBERNUMBER1999",009-00MONTHON06021999REPORTDATE(7)DOCKETNUMSER05000OOCKETNUMSER 05000FACfLITYNAMEFACILrTYNAMEOTHERFACILITIES INVOLVED(6)OPERATING MODE(9)POWERLEVEL(10)090URSUANTTOTHEREQUIREMEN THISREPORTISSUBMITTFD P20.2203(a)(2)(v) 20.2203(a)
(3)(i)20.2201(b) 20.2203(a)(1) 20.2203(a)(3)
(ii)20.2203(a)
(2)(i)20.2203(a}(4) 50.36(cl(1) 20.2203(a)(2)(ii) 20.2203(a)
(2)(iii}50.36(c)(2) 20.2203(a)(2)(iv)
LICENSEECONTACTFORTHISLER(12)TSOF10CFRB:(Checkoneormore)(11)50.73(a)(2)
(viii)50.73(a}(2}(x)
X50.73(a)(2)(i)(B) 50.73(a)(2)(ii)73.7150.73(a}(2l(iii)
OTHER50.73(a)(2wiv) 50.73(a)(2)(v)
SpecifymAbstractbeloworinNRCForm355A50.73(a)(2)(vii)
TELEPMONE NUMSER(InrrudeAresCode)JohnT.St.Martin-Technical Assistant (716)771-3641CAUSESYSTEMCOMPONOIT MANUFACTURER REPORTABLE TOEPOSCAUSESYS'fEMMANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(l4)YES(Ifyes,completeEXPECTEDSUBMISSION DATE).NOXEXPECTEDSUBMISSION DATER5)IlONTHOAYABSTRACT(Limitto1400spaces,i.e.,approximately 15single.spacedtypewritten lines}(16)OnMay3,1999,theplantwasinMode1atapproximately 90%steadystatereactorpower.Ithadpreviously beendetermined thatOvertemperature DeltaTandOverpower DeltaTbistabletripsetpoints werepotentially non-conservative onthreeoutoffourreactorprotection systemchannels, andanevaluation wasinprogress.
Atapproximately 2330EDST,instrumentation forthesethreechannelswasdeclaredinoperable.
Immediate corrective actionwastoenteiTechnical Specification LimitingCondition forOperation 3.0.3,andtakeactionstorestorethechannelstooperablestatus.Following replacement oftheaffectedbistables withbistab(es ofadifferent design,thebistabletripsetpoints wererecalibrated andthreeoffourchannelsweredeclaredoperable.
TheplantexitedLimitingCondition forOperation 3.0.3.Theunderlying causeoftheeventwasanunanticipated highfrequency ACvoltagerippleontheDeltaTsignalsthatadversely affectedthetripsetpoints forthebistables.
Corrective actiontopreventrecurrence isoutlinedinSectionV.B.  


~'~~~III~~~~C~'SiI~~i~I'~~~~~I~'~~~'~~I'~~~~~~~~~~~~~~~~~~~~'~~~~'~;~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~~~~~~~~:~~'~~~~~~~~~~~~;~.~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~I~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~''~~~~~~~~~~~'~~~~~~.~;~~~:-IIIIo~~~.~~~~~~~~~'~~~~~~..I.~~~~.~~~~~~~~I~~~~~~~'~~*~~~~~~~~~~.I~~:~~~~~~I~~~~~~~~~~~~~~~~~:~~~'~~~~~:~~~~~~~~~~~~~~~I~~~~~~~'~~.e~~~~~'~~~~~~~~~~~~~~~~I~'~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~'.~~~~~~~~o~~~I~~~~~~~~'~~~~
~'~~~III~~~~C~'SiI~~i~I'~~~~~I~'~~~'~~I'~~~~~~~~~~~~~~~~~~~~'~~~~'~;~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~~~~~~~~:~~'~~~~~~~~~~~~;~.~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~I~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~''~~~~~~~~~~~'~~~~~~.~;~~~:-IIIIo~~~.~~~~~~~~~'~~~~~~..I.~~~~.~~~~~~~~I~~~~~~~'~~*~~~~~~~~~~.I~~:~~~~~~I~~~~~~~~~~~~~~~~~:~~~'~~~~~:~~~~~~~~~~~~~~~I~~~~~~~'~~.e~~~~~'~~~~~~~~~~~~~~~~I~'~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~'.~~~~~~~~o~~~I~~~~~~~~'~~~~
NRCFORM366A$1999)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSIONFACILITYNAME(1)DOCKET(2)LERNUMBER(6)PAGE(3)..R.E.GinnaNuclearPowerPlant05000244SEOUEMTIA(8EVSIOIIIIUMBNImMBN1999-009-003OF7TEXTIifmorespaceisrequired,useadditionalcopiesofNRCForm366'17)ThePlantOperationsReviewCommittee(PORC)wasconvenedatapproximately1900EDSTtoreviewthissituation.PORCconcurredthatreducingpowerto90%wasaprudentmeasure.Channel2bistables,inserviceformorethan18months,werenotaffectedbythiscondition.Channel2wasprovenfullyoperableandchannel1wascurrentlyinthetrippedmode.Thus,continuedplantoperationwaspermissible,whilebistableoperabilitywasassessedbyNESpersonnel.PreliminarycalculationsweresubsequentlyperformedbyNESstaff.ThesecalculationsindicatedthatRPSchannel1bistabletripsetpointswerewithindesignlimits.ThemarginforOTDTandOPDTwerelow,butthebistableswereconsideredoperable.II.DESCRIPTIONOFEVENT:A.DATESANDAPPROXIMATETIMESOFMAJOROCCURRENCES'ay3,1999,0820EDST:RPSchannel1isremovedfromserviceanddeclaredinoperabletoperformtroubleshooting((perCPI-TRIP-TEST-5.10)).May3,1999,dayshift:ACrippleisdiscoveredinRPSchannel1.Later,ACrippleisdiscoveredinRPSchannels3and4.May3,1999,2330EDST:EventDateandTimeandDiscoveryDateandTime.May3,1999,2347EDST:Plantshutdowninitiated.May4,1999,0136EDST:RPSchannel1isdeclaredoperable.May4,1999,0428EDST:RPSchannel3isdeclaredoperable.May4,1999,0428EDST:ITSLCO3.0.3isexited.Plantshutdownisstoppedat21%power.May4,1999,2121EDST:RPSchannel4isdeclaredoperable.EVENT:OnMay3,1999,theplantwasinMode1atapproximately90%steadystatereactorpowerafterthepowerdecreasefromfullpower,whichwasstartedatapproximately1840EDSTandcompletedatapproximately2000EDST.NESpersonnelcompletedthecalculations,whichnowindicatedthatRPSchannel1bistableswerenotoperable.TheShiftSupervisorandplantmanagementwereimmediatelynotified.Atapproximately2330EDST,basedontherevisedcalculationaldata,itwasdeterminedthatthreeaffectedchannelsofRPS(channels1,3and4)bedeclaredinoperable.  
NRCFORM366A$1999)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)DOCKET(2)LERNUMBER(6)PAGE(3)..R.E.GinnaNuclearPowerPlant05000244SEOUEMTIA(
8EVSIOIIIIUMBNImMBN1999-009-003OF7TEXTIifmorespaceisrequired, useadditional copiesofNRCForm366'17)ThePlantOperations ReviewCommittee (PORC)wasconvenedatapproximately 1900EDSTtoreviewthissituation.
PORCconcurred thatreducingpowerto90%wasaprudentmeasure.Channel2bistables, inserviceformorethan18months,werenotaffectedbythiscondition.
Channel2wasprovenfullyoperableandchannel1wascurrently inthetrippedmode.Thus,continued plantoperation waspermissible, whilebistableoperability wasassessedbyNESpersonnel.
Preliminary calculations weresubsequently performed byNESstaff.Thesecalculations indicated thatRPSchannel1bistabletripsetpoints werewithindesignlimits.ThemarginforOTDTandOPDTwerelow,butthebistables wereconsidered operable.
II.DESCRIPTION OFEVENT:A.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES'ay 3,1999,0820EDST:RPSchannel1isremovedfromserviceanddeclaredinoperable toperformtroubleshooting
((perCPI-TRIP-TEST-5.10)).
May3,1999,dayshift:
ACrippleisdiscovered inRPSchannel1.Later,ACrippleisdiscovered inRPSchannels3and4.May3,1999,2330EDST:EventDateandTimeandDiscovery DateandTime.May3,1999,2347EDST:Plantshutdowninitiated.
May4,1999,0136EDST:RPSchannel1isdeclaredoperable.
May4,1999,0428EDST:RPSchannel3isdeclaredoperable.
May4,1999,0428EDST:ITSLCO3.0.3isexited.Plantshutdownisstoppedat21%power.May4,1999,2121EDST:RPSchannel4isdeclaredoperable.
EVENT:OnMay3,1999,theplantwasinMode1atapproximately 90%steadystatereactorpowerafterthepowerdecreasefromfullpower,whichwasstartedatapproximately 1840EDSTandcompleted atapproximately 2000EDST.NESpersonnel completed thecalculations, whichnowindicated thatRPSchannel1bistables werenotoperable.
TheShiftSupervisor andplantmanagement wereimmediately notified.
Atapproximately 2330EDST,basedontherevisedcalculational data,itwasdetermined thatthreeaffectedchannelsofRPS(channels 1,3and4)bedeclaredinoperable.  


I'e~~sI~~~II~'~'I'~~~'~'~~~'~~~~~~~~~~~~~'~~~~~~~~~~~~~~~'~~~~~'~~~~I~~~~~~~~~'~~~~~'~~~~~'~~~~~~~~~~~~0~~~~~~~~~''~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~'~~~'~~~~~.~~~~~~~~~~~~~~~~~'~'~~~I~I~~~~~~~~~~~'~~~~~~a~I~~~~~~~~~~~~~~'~~~~~~~~~~~~.~~~~~~~~~~~~~~~~'~~~~~s~~~~~~~~~~~~o~'~~~~~~.~~~~~~~'~~~~~~~~~~~~~~'~~'~~~~~~~~~~~~~~~~~~  
I'e~~sI~~~II~'~'I'~~~'~'~~~'~~~~~~~~~~~~~'~~~~~~~~~~~~~~~'~~~~~'~~~~I~~~~~~~~~'~~~~~'~~~~~'~~~~~~~~~~~~0~~~~~~~~~''~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~'~~~'~~~~~.~~~~~~~~~~~~~~~~~'~'~~~I~I~~~~~~~~~~~'~~~~~~a~I~~~~~~~~~~~~~~'~~~~~~~~~~~~.~~~~~~~~~~~~~~~~'~~~~~s~~~~~~~~~~~~o~'~~~~~~.~~~~~~~'~~~~~~~~~~~~~~'~~'~~~~~~~~~~~~~~~~~~  
~'0~~~~~II~IggI~~'~t'I4~~~~~~~~~'~~~~~~~~~~~~~''~~~~~~~~0~~.~~~I'~~~~~~~~~I~~~~~~~~~~.~~:~.~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~t~~~~'~'~'~~~~~~~~~  
~'0~~~~~II~IggI~~'~t'I4~~~~~~~~~'~~~~~~~~~~~~~''~~~~~~~~0~~.~~~I'~~~~~~~~~I~~~~~~~~~~.~~:~.~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~t~~~~'~'~'~~~~~~~~~  
'I NRCFORM366A(CISSS)LlCENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSION~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERIe)YEARSEQUENTIALREYISIONNUMSERNUMSER1999-009-00PAGEI3)6OF7TEXT(Ifmorespaceisrequired,useadditionalcopiesofitiRCForm366AJI17)IV.ANALYSISOFEVENT:Thiseventisreportableinaccordancewith10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperationorconditionprohibitedbytheplant'sTechnicalSpecifications"~TheentryintoITSLCO3.0.3asaresultofdeclaringmorethanoneFunctioninITSTable3.3.1-1inoperableisconsideredtobeaconditionprohibitedbyTechnicalSpecifications.Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththefollowingresultsandconclusions:TherewerenooperationalorsafetyconsequencesattributedtothreeRPSchannelsforOTDTandOPDTbeinginoperable.Amoredetailedpost-eventreviewwasperformed.Ithassubsequentlybeendeterminedthatonlyonetripfunction(RPSchannel3OPDT)wasactuallyinoperable.Thisdeterminationisbasedontheas-founddataandamorerigorousanalysisoftheassociatedinstrumentuncertainties.AllfourOTDTchannelswerefoundtobewithinaccidentanalysisassumptions,afteraccountingfortheas-foundmargintotripsetpointandincorporatingtheappropriateinstrumentuncertainties.Hence,theonlyfunctionthatwouldnothaveactuatedwithintheboundsoftheGinnaStationaccidentanalysiswasonechannelofOPDT.Withthreeoperablechannelsavailableanda2outof4logictoprovidetherequiredtripfunction,thereisadequateassurancethatthereactorprotectionsystemwouldhaveperformedwithinitsrequiredenvelopeasassumedintheaccidentanalysis.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVEACTION:A.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUS:FollowingreplacementofbistablesandcalibrationofthebistablesinRPSchannels1and3,threechannels(channels1and3andpreviouslyunaffectedchannel2)weredeclaredoperable.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:NUSindicatedthattheywillbeupdatingthepartslisttoremovetheincorrectlysizedcomponent.NESpersonneldesignedamodificationtothemathmodulestoeliminatetheeffectsofACrippleontheOPDTandOTDTbistabletripsetpoints.Thismodificationhasbeenimplemented.  
'I NRCFORM366A(CISSS)LlCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION
~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERIe)YEARSEQUENTIAL REYISIONNUMSERNUMSER1999-009-00PAGEI3)6OF7TEXT(Ifmorespaceisrequired, useadditional copiesofitiRCForm366AJI17)IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications"
~TheentryintoITSLCO3.0.3asaresultofdeclaring morethanoneFunctioninITSTable3.3.1-1inoperable isconsidered tobeacondition prohibited byTechnical Specifications.
Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
Therewerenooperational orsafetyconsequences attributed tothreeRPSchannelsforOTDTandOPDTbeinginoperable.
Amoredetailedpost-event reviewwasperformed.
Ithassubsequently beendetermined thatonlyonetripfunction(RPSchannel3OPDT)wasactuallyinoperable.
Thisdetermination isbasedontheas-founddataandamorerigorousanalysisoftheassociated instrument uncertainties.
AllfourOTDTchannelswerefoundtobewithinaccidentanalysisassumptions, afteraccounting fortheas-foundmargintotripsetpointandincorporating theappropriate instrument uncertainties.
Hence,theonlyfunctionthatwouldnothaveactuatedwithintheboundsoftheGinnaStationaccidentanalysiswasonechannelofOPDT.Withthreeoperablechannelsavailable anda2outof4logictoprovidetherequiredtripfunction, thereisadequateassurance thatthereactorprotection systemwouldhaveperformed withinitsrequiredenvelopeasassumedintheaccidentanalysis.
Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTION:A.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:Following replacement ofbistables andcalibration ofthebistables inRPSchannels1and3,threechannels(channels 1and3andpreviously unaffected channel2)weredeclaredoperable.
ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:
NUSindicated thattheywillbeupdatingthepartslisttoremovetheincorrectly sizedcomponent.
NESpersonnel designedamodification tothemathmodulestoeliminate theeffectsofACrippleontheOPDTandOTDTbistabletripsetpoints.
Thismodification hasbeenimplemented.  


NRCFORM366AgIBBBILICENSEEEVENTREPORT(LER)TEXTCONTINUATIONU.S.NUCLEARREGULATORYCOMMISSION~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERI6)SB)UalTIAlRSNSIOHIIUMBIAIIUMBBI1999-003-00PAGEI3)7OF7TEXTllfmorespaceisrequired,useadditionalcopiesofNRCForm866AJI17)oThiseventisbeingreviewedforanypotentiallessonstobelearnedandappliedtotheappropriatepartsoftheGinnamodificationprocess:design,procurement,installation,testing.TheindustrywillbenotifiedofthiseventviaanentryintheNuclearNETWORKsystem.VI~ADDITIONALINFORMATION:A.FAILEDCOMPONENTS:NoneB.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:NodocumentationofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.C.SPECIALCOMMENTS:None}}
NRCFORM366AgIBBBILICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION
~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERI6)SB)UalTIAl RSNSIOHIIUMBIAIIUMBBI1999-003-00PAGEI3)7OF7TEXTllfmorespaceisrequired, useadditional copiesofNRCForm866AJI17)oThiseventisbeingreviewedforanypotential lessonstobelearnedandappliedtotheappropriate partsoftheGinnamodification process:design,procurement, installation, testing.TheindustrywillbenotifiedofthiseventviaanentryintheNuclearNETWORKsystem.VI~ADDITIONAL INFORMATION:
A.FAILEDCOMPONENTS:
NoneB.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.
C.SPECIALCOMMENTS:
None}}

Revision as of 12:33, 29 June 2018

LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr
ML17265A666
Person / Time
Site: Ginna Constellation icon.png
Issue date: 06/02/1999
From: MECREDY R C, ST MARTIN J T
ROCHESTER GAS & ELECTRIC CORP.
To: VISSING G S
NRC (Affiliation Not Assigned), NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-99-009, LER-99-9, NUDOCS 9906080307
Download: ML17265A666 (13)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEM(RXDS)ACCESSZONNBR:9906080307 DOC.DATE:

99/06/02NOTARIZED:

NODOCKETIPACZL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester GterG05000244AUTH.NAMEAUTHORAFFILIATION STMARTIN,J.T.

Rochester Gas&.ElectricCorp.MECREDY,R.C.

~Rochester Gas&.ElectricCorp.RECIP.NAME

,RECIPIENT AFFILIATION VISSXNG,G.S.

SUBJECT:

LER99-009-00:on 990503,instrumentation declaredinoperable inmultiplechannelsresultedincondition prohibited byTS.Causedbyunanticipated highfrequency ACvoltagerippe.EnteredTSLCO3.0.3.With 990602ltr.DISTRIBUTION CODEXE22TCOPIESRECEIVEDeLTRgENCL(SIZEaTITLE:50.73/50.9 LicenseeEventReport(LER),XncidentRpt,etc.NOTES:License Expdateinaccordance with10CPR2,2.109(9/19/72)

.G050002440RECIPIENT ZDCODE/NAME LPD1-1PDINTERNAL:

AEOD/SPD/RRAB NRR/DZPM/IOLB NRR/DRIP/REXB RES/DET/EIB EXTERNAL:

LSTLOBBYWARDNOACPOORE,W.NRCPDRCOPIESLTTRENCL11111'1111111.111RECIPIENT XDCODE/NAME VZSSXNG,G.

FILECENTERR/DXPM/XQMB NRR/DSSA/SPLB RGN1PILE01LMXTCOMARSHALLNOACQUEENER,DS NUDOCSFULLTXTCOPIESLTTRENCL1111111111111111NOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION<

CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 41S-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:

LTTR16ENCL16 4HDROCHESTfR GASANDE'ELECTRIC CORFORATION

~89EASTAVENUE, ROCHfSTER, N,YI46d9.000I AREACODE216586-27MRosERTc.MEcREDYVicePresislenl t4uc!eorOperosions June2,1999U.S.NuclearRegulatory Commission DocumentControlDeskAttn:GuyS.VissingProjectDirectorate I-1Washington, D.C.20555

Subject:

.LER1999-009, Instrumentation DeclaredInoperable inMultipleChannelsResultsinCondition Prohibited byTechnical Specifications R.E.GinnaNuclearPowerPlantDocketNo.50-244

DearMr.Vissing:

TheattachedLicenseeEventReportLER1999-009issubmitted inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications".

Veryrulyyours,XC:Mr.GuyS.Vissing(MailStop8C2)ProjectDirectorate I-1DivisionofReactorProjects-I/IIOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555RegionalAdministrator, RegionIU.S.NuclearRegulatory Commission 475Allendale RoadKingofPrussia,PA19406U.S.NRCGinnaSeniorResidentInspector

+t990b080307

'll's!0602PDRADQCK05000244SPDR NRCFORM866IBI%BIU.S.NUCLEARREGULATORY COMMISSION LICENSEEEYENTREPORT(LER)fSoereverseforrequirednumberof'digitslcharacters foreachb(ocklM5QIkrNpNIIsp@eigA'P%88Sy'nformation coBoctP)a rortuost:

50hrs.Reportedlessonslearnedarencorporated krtotheBcenskrgprocessandfodbacktohdustry.Forwardcommentsregarding burdenestimatetotheRecordsMsnagernont Branchp4F33),U.S.NudearRegulatory Commfssbn, Wasfsngton, DC205554001

~andtothePaperwork Reduction Project(31500104),

OfreeofManagement andBudget,WasNngton, DC20503.Ifaninformation coeect'on doesnotdisplayacurrendyvsMOMB,controlnumber,theNRCmaynotconductorsponsor.andaFACILITYNAMEI11R.E.GinnaNuc(earPowerPlantIDOCKETNUMBERI2)05000244PAGEI3)1OF7TITLEte)Instrumentation DeclaredInoperable inMultipleChannelsResultsinCondition Prohibited byTechnical Specifications 05031999,EVENTDATE(5)OAYLERNUMBER(6)SEOUFNTIAL RENSIONNUMBERNUMBER1999",009-00MONTHON06021999REPORTDATE(7)DOCKETNUMSER05000OOCKETNUMSER 05000FACfLITYNAMEFACILrTYNAMEOTHERFACILITIES INVOLVED(6)OPERATING MODE(9)POWERLEVEL(10)090URSUANTTOTHEREQUIREMEN THISREPORTISSUBMITTFD P20.2203(a)(2)(v) 20.2203(a)

(3)(i)20.2201(b) 20.2203(a)(1) 20.2203(a)(3)

(ii)20.2203(a)

(2)(i)20.2203(a}(4) 50.36(cl(1) 20.2203(a)(2)(ii) 20.2203(a)

(2)(iii}50.36(c)(2) 20.2203(a)(2)(iv)

LICENSEECONTACTFORTHISLER(12)TSOF10CFRB:(Checkoneormore)(11)50.73(a)(2)

(viii)50.73(a}(2}(x)

X50.73(a)(2)(i)(B) 50.73(a)(2)(ii)73.7150.73(a}(2l(iii)

OTHER50.73(a)(2wiv) 50.73(a)(2)(v)

SpecifymAbstractbeloworinNRCForm355A50.73(a)(2)(vii)

TELEPMONE NUMSER(InrrudeAresCode)JohnT.St.Martin-Technical Assistant (716)771-3641CAUSESYSTEMCOMPONOIT MANUFACTURER REPORTABLE TOEPOSCAUSESYS'fEMMANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(l4)YES(Ifyes,completeEXPECTEDSUBMISSION DATE).NOXEXPECTEDSUBMISSION DATER5)IlONTHOAYABSTRACT(Limitto1400spaces,i.e.,approximately 15single.spacedtypewritten lines}(16)OnMay3,1999,theplantwasinMode1atapproximately 90%steadystatereactorpower.Ithadpreviously beendetermined thatOvertemperature DeltaTandOverpower DeltaTbistabletripsetpoints werepotentially non-conservative onthreeoutoffourreactorprotection systemchannels, andanevaluation wasinprogress.

Atapproximately 2330EDST,instrumentation forthesethreechannelswasdeclaredinoperable.

Immediate corrective actionwastoenteiTechnical Specification LimitingCondition forOperation 3.0.3,andtakeactionstorestorethechannelstooperablestatus.Following replacement oftheaffectedbistables withbistab(es ofadifferent design,thebistabletripsetpoints wererecalibrated andthreeoffourchannelsweredeclaredoperable.

TheplantexitedLimitingCondition forOperation 3.0.3.Theunderlying causeoftheeventwasanunanticipated highfrequency ACvoltagerippleontheDeltaTsignalsthatadversely affectedthetripsetpoints forthebistables.

Corrective actiontopreventrecurrence isoutlinedinSectionV.B.

~'~~~III~~~~C~'SiI~~i~I'~~~~~I~'~~~'~~I'~~~~~~~~~~~~~~~~~~~~'~~~~'~;~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~~~~~~~~:~~'~~~~~~~~~~~~;~.~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~I~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~.~;~~~:-IIIIo~~~.~~~~~~~~~'~~~~~~..I.~~~~.~~~~~~~~I~~~~~~~'~~*~~~~~~~~~~.I~~:~~~~~~I~~~~~~~~~~~~~~~~~:~~~'~~~~~:~~~~~~~~~~~~~~~I~~~~~~~'~~.e~~~~~'~~~~~~~~~~~~~~~~I~'~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~'.~~~~~~~~o~~~I~~~~~~~~'~~~~

NRCFORM366A$1999)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)DOCKET(2)LERNUMBER(6)PAGE(3)..R.E.GinnaNuclearPowerPlant05000244SEOUEMTIA(

8EVSIOIIIIUMBNImMBN1999-009-003OF7TEXTIifmorespaceisrequired, useadditional copiesofNRCForm366'17)ThePlantOperations ReviewCommittee (PORC)wasconvenedatapproximately 1900EDSTtoreviewthissituation.

PORCconcurred thatreducingpowerto90%wasaprudentmeasure.Channel2bistables, inserviceformorethan18months,werenotaffectedbythiscondition.

Channel2wasprovenfullyoperableandchannel1wascurrently inthetrippedmode.Thus,continued plantoperation waspermissible, whilebistableoperability wasassessedbyNESpersonnel.

Preliminary calculations weresubsequently performed byNESstaff.Thesecalculations indicated thatRPSchannel1bistabletripsetpoints werewithindesignlimits.ThemarginforOTDTandOPDTwerelow,butthebistables wereconsidered operable.

II.DESCRIPTION OFEVENT:A.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES'ay 3,1999,0820EDST:RPSchannel1isremovedfromserviceanddeclaredinoperable toperformtroubleshooting

((perCPI-TRIP-TEST-5.10)).

May3,1999,dayshift:

ACrippleisdiscovered inRPSchannel1.Later,ACrippleisdiscovered inRPSchannels3and4.May3,1999,2330EDST:EventDateandTimeandDiscovery DateandTime.May3,1999,2347EDST:Plantshutdowninitiated.

May4,1999,0136EDST:RPSchannel1isdeclaredoperable.

May4,1999,0428EDST:RPSchannel3isdeclaredoperable.

May4,1999,0428EDST:ITSLCO3.0.3isexited.Plantshutdownisstoppedat21%power.May4,1999,2121EDST:RPSchannel4isdeclaredoperable.

EVENT:OnMay3,1999,theplantwasinMode1atapproximately 90%steadystatereactorpowerafterthepowerdecreasefromfullpower,whichwasstartedatapproximately 1840EDSTandcompleted atapproximately 2000EDST.NESpersonnel completed thecalculations, whichnowindicated thatRPSchannel1bistables werenotoperable.

TheShiftSupervisor andplantmanagement wereimmediately notified.

Atapproximately 2330EDST,basedontherevisedcalculational data,itwasdetermined thatthreeaffectedchannelsofRPS(channels 1,3and4)bedeclaredinoperable.

I'e~~sI~~~II~'~'I'~~~'~'~~~'~~~~~~~~~~~~~'~~~~~~~~~~~~~~~'~~~~~'~~~~I~~~~~~~~~'~~~~~'~~~~~'~~~~~~~~~~~~0~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~'~~~'~~~~~.~~~~~~~~~~~~~~~~~'~'~~~I~I~~~~~~~~~~~'~~~~~~a~I~~~~~~~~~~~~~~'~~~~~~~~~~~~.~~~~~~~~~~~~~~~~'~~~~~s~~~~~~~~~~~~o~'~~~~~~.~~~~~~~'~~~~~~~~~~~~~~'~~'~~~~~~~~~~~~~~~~~~

~'0~~~~~II~IggI~~'~t'I4~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~0~~.~~~I'~~~~~~~~~I~~~~~~~~~~.~~:~.~~~~~~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~~~~~~~~~~~~~~~~~'~~~~~'~~~~~~~~~~~~~~t~~~~'~'~'~~~~~~~~~

'I NRCFORM366A(CISSS)LlCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION

~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERIe)YEARSEQUENTIAL REYISIONNUMSERNUMSER1999-009-00PAGEI3)6OF7TEXT(Ifmorespaceisrequired, useadditional copiesofitiRCForm366AJI17)IV.ANALYSISOFEVENT:Thiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(i)(B),"Anyoperation orcondition prohibited bytheplant'sTechnical Specifications"

~TheentryintoITSLCO3.0.3asaresultofdeclaring morethanoneFunctioninITSTable3.3.1-1inoperable isconsidered tobeacondition prohibited byTechnical Specifications.

Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:

Therewerenooperational orsafetyconsequences attributed tothreeRPSchannelsforOTDTandOPDTbeinginoperable.

Amoredetailedpost-event reviewwasperformed.

Ithassubsequently beendetermined thatonlyonetripfunction(RPSchannel3OPDT)wasactuallyinoperable.

Thisdetermination isbasedontheas-founddataandamorerigorousanalysisoftheassociated instrument uncertainties.

AllfourOTDTchannelswerefoundtobewithinaccidentanalysisassumptions, afteraccounting fortheas-foundmargintotripsetpointandincorporating theappropriate instrument uncertainties.

Hence,theonlyfunctionthatwouldnothaveactuatedwithintheboundsoftheGinnaStationaccidentanalysiswasonechannelofOPDT.Withthreeoperablechannelsavailable anda2outof4logictoprovidetherequiredtripfunction, thereisadequateassurance thatthereactorprotection systemwouldhaveperformed withinitsrequiredenvelopeasassumedintheaccidentanalysis.

Basedontheabove,itcanbeconcluded thatthepublic'shealthandsafetywasassuredatalltimes.V.CORRECTIVE ACTION:A.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:Following replacement ofbistables andcalibration ofthebistables inRPSchannels1and3,threechannels(channels 1and3andpreviously unaffected channel2)weredeclaredoperable.

ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:

NUSindicated thattheywillbeupdatingthepartslisttoremovetheincorrectly sizedcomponent.

NESpersonnel designedamodification tothemathmodulestoeliminate theeffectsofACrippleontheOPDTandOTDTbistabletripsetpoints.

Thismodification hasbeenimplemented.

NRCFORM366AgIBBBILICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION

~FACILITYNAMEI1)R.E.GinnaNuclearPowerPlantDOCKETI2)05000244LERNUMBERI6)SB)UalTIAl RSNSIOHIIUMBIAIIUMBBI1999-003-00PAGEI3)7OF7TEXTllfmorespaceisrequired, useadditional copiesofNRCForm866AJI17)oThiseventisbeingreviewedforanypotential lessonstobelearnedandappliedtotheappropriate partsoftheGinnamodification process:design,procurement, installation, testing.TheindustrywillbenotifiedofthiseventviaanentryintheNuclearNETWORKsystem.VI~ADDITIONAL INFORMATION:

A.FAILEDCOMPONENTS:

NoneB.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.

C.SPECIALCOMMENTS:

None