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Ci NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQISNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORHATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORNATIONANDRECORDSHANAGEKEHTBRANCH(HHBB7714),U.S.NUCLEARREGULATORYCOHHISSION,WASHINGTON,DC20555-0001AND'O"THEPAPERWORKREDUCTIONPROJECT(3110-0104),OFFICEOFNANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETNWBER205000244YEAR94--006--00LERNNNIER6SEQUENTIALREVISIONPAGE37OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)~ThedegradedtubeswereidentifiedandrepairedpriortoanysignificantleakageorS/Gtuberuptureoccurring.~EvenassumingacompleteseveranceofaS/Gtubeatfullpower,asstatedintheR.E.GinnaNuclearPowerPlantUpdatedFinalSafetyAnalysisReport(GinnaUFSAR)section15.6.3(SteamGeneratorTubeRupture),thesequenceofrecoveryactionsensuresearlyterminationofprimarytosecondaryleakagewithorwithoutoffsitepoweravailablethuslimitingoffsiteradiationdosestowithintheguidelinesof10CFR100.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassured'atalltimes.V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUSOfthe164tubesrepairedinthe"A"S/G,143tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese143tubeswillremaininservice.Theremaining21tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Atotalof215tubesinthe"A"S/Garecurrentlypluggedand811tubesaresleeved.Ofthe134tubesrepairedinthe"B"S/G,103tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese103tubeswillremaininservice.30tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Theremainingtubewaspreviouslypluggedandexhibitedacrackindicationintheplug.Thesubjecttubeplugwasremovedandanewpluginstalled.Atotalof315tubesinthe"B"S/Garecurrentlypluggedand1390tubesaresleeved.Alltheaboverepairsonthe"A"and"B"S/GswerecompletedonMarch27,1994,atapproximately2235EST.HRCFORH366A(5-92)
Ci NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQISNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORHATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORNATIONANDRECORDSHANAGEKEHTBRANCH(HHBB7714),U.S.NUCLEARREGULATORYCOHHISSION,WASHINGTON,DC20555-0001AND'O"THEPAPERWORKREDUCTIONPROJECT(3110-0104),OFFICEOFNANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETNWBER205000244YEAR94--006--00LERNNNIER6SEQUENTIALREVISIONPAGE37OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)~ThedegradedtubeswereidentifiedandrepairedpriortoanysignificantleakageorS/Gtuberuptureoccurring.~EvenassumingacompleteseveranceofaS/Gtubeatfullpower,asstatedintheR.E.GinnaNuclearPowerPlantUpdatedFinalSafetyAnalysisReport(GinnaUFSAR)section15.6.3(SteamGeneratorTubeRupture),thesequenceofrecoveryactionsensuresearlyterminationofprimarytosecondaryleakagewithorwithoutoffsitepoweravailablethuslimitingoffsiteradiationdosestowithintheguidelinesof10CFR100.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassured'atalltimes.V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUSOfthe164tubesrepairedinthe"A"S/G,143tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese143tubeswillremaininservice.Theremaining21tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Atotalof215tubesinthe"A"S/Garecurrentlypluggedand811tubesaresleeved.Ofthe134tubesrepairedinthe"B"S/G,103tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese103tubeswillremaininservice.30tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Theremainingtubewaspreviouslypluggedandexhibitedacrackindicationintheplug.Thesubjecttubeplugwasremovedandanewpluginstalled.Atotalof315tubesinthe"B"S/Garecurrentlypluggedand1390tubesaresleeved.Alltheaboverepairsonthe"A"and"B"S/GswerecompletedonMarch27,1994,atapproximately2235EST.HRCFORH366A(5-92)
HRCFORM366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIOHZiICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQQINO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONAMDRECORDSMANAGEMENTBRANCH(HNBB771C),U.S.NUCLEARREGULATORYCONHISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGET'WASHINGTOMDC20503.FACILITYNAME1R.E.GinnaNuclearPowerPlantMxxETHIM(BER205000244YEAR94-006--00LERNWBER6SEQUENTIALREVISIONPAGE38OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE-Theoccurrence/presenceofIGA,SCC,andPWSCCisaPWRS/Gproblem.UtilitieswithsusceptibletubingandpartiallyrolledcrevicesmustdealwiththisrecurringattackonS/Gtubing.R.E.GinnaNuclearPowerPlantwillcontinuecarefulmonitoringofbothprimaryRCSandsecondarysidewaterchemistryparameters.Thesewaterchemistryparameterswillcontinuetobeevaluated'againstacceptedindustryguidelinesinordertominimizeharmfulprimaryand/orsecondarysideenvironments.DegradedS/Gtubesshallbesleevedorpluggedinaccordancewiththeinserviceinspectionprogramandacceptedindustryrepairmethods.\VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:ThedegradedcomponentsareInconel600MillAnnealedU-Bendtubeshavinganoutside.diameterof0.875inchesandanominalwallthicknessof0.050inches.ThetubesweremanufacturedbyHuntingtonAlloyCompany.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:ThecreviceindicationsaresimilartothosereportedinA0-74-02,AO-75-07,R0-75-013,andLERs76-008,77008'8003I79006'9022I80003g81009g82003I8202283-013,89-001,90-004,91-005,92-005,and93-002.C.SPECIALCOMMENTS:Amorein-depthfinalreportwillbesubmittedtotheNRC,asrequiredbytheGinnaQAManual.Asanoteofinterest,RG&EhasorderednewsteamgeneratorsforR.E.GinnaNuclearPowerPlanttobeinstalledin1996.HRCFORH366A(592)
HRCFORM366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIOHZiICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQQINO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONAMDRECORDSMANAGEMENTBRANCH(HNBB771C),U.S.NUCLEARREGULATORYCONHISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGET'WASHINGTOMDC20503.FACILITYNAME1R.E.GinnaNuclearPowerPlantMxxETHIM(BER205000244YEAR94-006--00LERNWBER6SEQUENTIALREVISIONPAGE38OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE-Theoccurrence/presenceofIGA,SCC,andPWSCCisaPWRS/Gproblem.UtilitieswithsusceptibletubingandpartiallyrolledcrevicesmustdealwiththisrecurringattackonS/Gtubing.R.E.GinnaNuclearPowerPlantwillcontinuecarefulmonitoringofbothprimaryRCSandsecondarysidewaterchemistryparameters.Thesewaterchemistryparameterswillcontinuetobeevaluated'againstacceptedindustryguidelinesinordertominimizeharmfulprimaryand/orsecondarysideenvironments.DegradedS/Gtubesshallbesleevedorpluggedinaccordancewiththeinserviceinspectionprogramandacceptedindustryrepairmethods.\VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:ThedegradedcomponentsareInconel600MillAnnealedU-Bendtubeshavinganoutside.diameterof0.875inchesandanominalwallthicknessof0.050inches.ThetubesweremanufacturedbyHuntingtonAlloyCompany.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:ThecreviceindicationsaresimilartothosereportedinA0-74-02,AO-75-07,R0-75-013,andLERs76-008,77008'8003I79006'9022I80003g81009g82003I8202283-013,89-001,90-004,91-005,92-005,and93-002.C.SPECIALCOMMENTS:Amorein-depthfinalreportwillbesubmittedtotheNRC,asrequiredbytheGinnaQAManual.Asanoteofinterest,RG&EhasorderednewsteamgeneratorsforR.E.GinnaNuclearPowerPlanttobeinstalledin1996.HRCFORH366A(592)
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Revision as of 12:31, 18 May 2018

LER 94-006-00:on 940323,SG Tube Degradation Due to Iga/Scc, Caused QA Manual Reportable Limits to Be Reached.Caused by Pwscc.Tubes repaired.W/940422 Ltr
ML17263A627
Person / Time
Site: Ginna Constellation icon.png
Issue date: 04/22/1994
From: MARTIN J T, MECREDY R C
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-94-006, LER-94-6, NUDOCS 9404280277
Download: ML17263A627 (12)


Text

ACCELERATlDOCUMENTDISTRIBUTIONSYSTEMREGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9404280277DOC.DATE:94/04/22NOTARIZED:NOFACIL:50-244RobertEmmetGinnaNuclearPlant,Unit1,RochesterGAUTH.NAMEAUTHORAFFILIATIONMARTIN,J.T.RochesterGas&ElectricCorp.MECREDY,R.C.RochesterGas&ElectricCorp.RECIP.NAMERECIPIENTAFFILIATIONDOCKETg05000244RtDP/DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRENCLSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),ncident,Rpt,etc.NOTES:LicenseExpdateinaccordancewith10CFR2,2.109(9/19/72).05000244D

SUBJECT:

LER94-006-00:on940323,both"A"&"B"steamWestinghouseSeries44steamgenerators,requiredcorrectiveactionduetotubedegradation.CausewasPWS.Correctiveaction:tubeswerereaired.W940422ltr.RECIPIENTIDCODE/NAMEPD1-3PDINTERNAL:AEOD/DOAAEOD/ROAB/DSPNRR/DE/EMEBNRR/DRCH/HHFBNRR/DRCH/HOLBNRR/DRSS/PRPBNRR/DSSA/SRXBRES/DSIR/EIBEXTERNAL:EG&GBRYCE,J.HNRCPDRNSICPOOREiWCOPIESLTTRENCL111122111111221111221111RECIPIENTIDCODE/NAMEJOHNSON,AAEOD/DSP/TPABNRR/DE/EELBNRR/DORS/OEABNRR/DRCH/HICBNRR/DRIL/RPEBN./DSSAQSPLBG~~~02RGN1FILE01LSTLOBBYWARDNSICMURPHY,G.ANUDOCSFULLTXTCOPIESLTTRENCL111111111111111111111111DDDNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTEICONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!FULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR27ENCL27D ITlrlrlr'PIISI1'lR,'I',"IIC~~~4~~IIr'oarsscarcROCHFSTERGASANDELECTRICCORPORATION489EASTAVENUE,ROCHESTERN.K14649-0001ROBERTCMECREDYVicePresideniCinnaNuclearProducrionTELEPHONEAREACOOEi165462700April22,1994U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonProjectDirectorateI-3Washington,D.C.20555

Subject:

LER94-006,SteamGeneratorTubeDegradationDuetoIGA/SCC,CausesQualityAssuranceManualReportableLimitstobeReachedR.E.GinnaNuclearPowerPlantDocketNo.50-244IInaccordancewith10CFR50.73,Licensee.EventReportSystem,item(Other),andtheGinnaStationQualityAssuranceManualAppendixB,whichrequiresthat,"Ifthenumberoftubesinageneratorfallingintocategories(a)or(b)belowexceedsthecriteria,thenresultsoftheinspectionshallbeconsideredaReportableEventpursuantto10CFR50,73,"theattachedLicenseeEventReportLER94-006isherebysubmitted.Thiseventhasinnowayaffectedthepublic'shealthandsafety.Verytlyyours,RobertC.MecredyXC:U.S.NuclearRegulatoryCommissionRegionI475AllendaleRoadKingofPrussia,PA19406GinnaSeniorResidentInspector9404280277500024+qe0422PDRADOCK0PDP8/7 NRCFORM3665-92)U.SNUCLEARREGULATORYCQIIISSIONAPPROVEDBY(IHINO.3150-0104EXPIRES5/31/95LICENSEEEVENTREPORT(LER)(Seereverseforrequirednunberofdigits/charactersforeachblock)ESTIMATEDBURDENPERRESPONSETOCOMPLY'WITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHEIHFORMATIONANDRECORDSMANAGEMENTBRANCH(MNBB7714),U.S.NUCLEARREGULATORYCOMMISSION/WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140.0104),OFFICEOFHANAGEMENTANDBUDGETWASHINGTONDC20503.FAGILITYNAIK(1)R.E~GinnaNuclearPowerPlantIDOCKETNQQIER(2)05000244PAGE(3)1OF8TITLE(6)SteamGeneratorTubeDegradationDuetoIGA/SCC,CausesQualityAssuranceManualReportableLimitstobeReachedEVENTDATE5LERNWBER6REPORTDATE7OTHERFACILITIESINVOLVED0HONTH03DAYYEAR2394YEAR94SEQUENTIALHUMBER--006--REVISIONNUMBER00MONTH04DAYYEAR2294FACILITYNAMEFACILITYNAMEDOCKETNUMBERDOCKETNUMBERGRATINGNX)E(9)RRKRLEVEL(10)N000THISREPORTISSUBMITTEDPURSUANT20.402(b)20'05(a)(1)(i)20.405(a)(1)(ii)20.405(a)(1)(iii)20.405(a)(1)(iv)20.405(a)(1)(v)20.405(c)50.36(c)(1)50'6(c)(2)50.73(a)(2)(i)50.73(a)(2)(ii)50.73(a)(2)(iii)50'3(a)(2)(iv)50.73(a)(2)(v)50'3(a)(2)(vii)50.73(a)(2)(viii)(A)50.73(a)(2)(viii)(B)50.73(a)(2)(x)73.71(b)73.71(c)OTHER(SpecifyinAbstractbelowandinText,HRCForm366ATOTHEREQUIREMENTSOF10CFR:Checkoneormore11LICENSEECONTACTFORTHISLER12NAMEJohnT.St.Martin.Director,OperatingExperienceTELEPHONENUMBER(IncludeAreaCode)(315)524-4446C(NPLETEONELINEFOREACHC(NPOHENTFAILUREDESCRIBEDINTHISREPORT13CAUSESYSTEMBABCOMPONENTTBGMANUFACTURERH314REPORTABLETOHPRDSCAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETOHPRDSSUPPLEMENTALREPORTEXPECTED14YES(Ifyes,completeEXPECTEDSUBMISSIOHDATE).XNOEXPECTEDSUBMISSIONDATE(15)MONTHDAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately15single-spacedtypewrittenlines),(16)Duringthe1994AnnualRefuelingandMaintenanceOutage,subsequenttotheeddycurrentexaminationperformedonboththe"A"and"B"WestinghouseSeries44steamgenerators,164tubesinthe"A"steamgeneratorand134tubesinthe"B"steamgeneratorrequiredcorrectiveactionduetotubedegradation.Theimmediatecauseoftheeventwasthatthe"A"and"B"steamgeneratortubedegradationwasinexcessoftheGinnaStationQualityAssuranceManualreportablelimits.TheunderlyingcauseofthetubedegradationisacommonsteamgeneratorproblemofapartiallyrolledtubesheetcrevicewithrecurringIntergranularAttack/StressCorrosionCracking(IGA/SCC)andPrimaryWaterStressCorrosionCracking(PWSCC)attackonsteamgeneratortubing.ThiseventisNRCPerformanceIndicatorSystemCauseCode5.8.4.3andNUREG-1022CauseCode(B).Correctiveactiontakenwastoeithersleeveorplugtheaffectedtubeswithacceptedindustryrepairmethods.HRCFORM366(5.92)

HRCFORH366A(5-92)US.NUCLEARREGULATORYC(NIIISSIOHL'ICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBY(NIBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPOHSETOCOHPLYWITHTHISIHFORHATIOHCOLLECTIONREQUEST:50.0HRS.FORWARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORMATIONANDRECORDSHANAGEHEHTBRANCH(HNBB7714),U.S.NUCLEARREGULATORYCOHHISSION,WASHINGTON,DC20555-0001,ANDTOTHEPAPERWORKREDUCTIONPROJECT(3150-0104),OFFICEOFHANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNAHE1R.E.GinnaNuclearPowerPlantDOCKETNNBER2YEAR0500024494LERNNBER6SEQUEHTIAL--006--REVISION00PAGE32OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)PRE-EVENTPLANTCONDITIONSiTheplantwasinthecold/refuelingshutdownconditionforthe1994AnnualRefuelingandMaintenanceOutage.TheReactorCoolantSystem(RCS)wasdepressurizedandRCStemperaturewasapproximately66degreesF.SteamGenerator(S/G)eddycurrentexaminationwasinprogress.II.DESCRIPTIONOFEVENTA.DATESANDAPPROXIMATETIMESOFMAJOROCCURRENCES:March23,1994,1500EST:ThenumberofdegradedS/GtubeswasknowntoexceedGinnaStationQualityAssurance(QA)Manualreportablelimits,basedoncompletionof"A>>and"B"S/Ghotlegand"A"S/Gcoldleginspectionprogram.Event.dateandtime.fMarch23,1994,1500EST:Discoverydateandtime.March24,1994,1300EST:OralnotificationmadetotheNRCOfficeofNuclearReactorRegulation(NRR)thatthenumberofdegradedS/GtubesexceededQAManualreportablelimits.March26,1994,1800EST:Alleddycurrentprogramscompleted,andtheevaluationofthe1994inserviceinspectionofS/Gtubescompleted.March27,1994,2235EST:S/Grepairscompleted.April8,1994:ASpecialReportwassenttotheUSNRC,reportingthenumberoftubespluggedorsleevedineachS/G.HRCFORH366A(5-92)

NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBY(NBNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISIHFORHATIOHCOLLECTIONREQUEST:50.0HRS.FORllARDCONHEHTSREGARDINGBURDENESTIHATETOTHEIHFORNATIOHANDRECORDSHANAGEHEHTBRANCH(HHBB7714),U.S.NUCLEARREGULATORYCOHNISSIOH,UASHIHGTOH,DC20555-0001ANDTOTHEPAPERIIORKREDUCTIONPROJECT(3140-0104),OFFICEOFHANAGEHENTANDBUDGETllASHIHGTONDC20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETIRNBER205000244LERNINBER6YEARSEQUENTIAL94--006--REVISION00PAGE33OF8TEXl'Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)B.EVENT:Duringthe1994AnnualRefuelingandMaintenanceOutage,aneddycurrentexaminationwasperformedinboththe>>A>>(EMSOlA)and>>B>>(EMSOlB)WestinghouseSeries44designrecirculatingsteamgenerators.Thepurposeoftheeddycurrentexaminationwastoassessanycorrosionormechanicaldamagethatmayhaveoccurredduringthecyclesincethe1993examination.TheexaminationwasperformedbypersonnelfromRochesterGasandElectric(RG&E)andABBCombustionEngineering.All-personnelweretrainedandqualifiedintheeddycurrentexaminationmethod.andhavebeencertifiedtoaminimumofLevelIfordataacquisitionandLevelIIfordataanalysis.Theinitialeddycurrentexaminationsofthe>>A>>and>>B>>S/GswereperformedutilizingastandardbobbincoiltechniquewithdataacquisitionbeingperformedwiththeEDDYNETAcquisitionSystem.Thefrequenciesselectedwere400,200,100,and25KHz.Additionaleddycurrentexaminationsofthe>>A>>and>>B>>S/GswereperformedutilizingtheZetec3-coilMotorizedRotatingPancakeCoil(MRPC)probetoexaminetherolltransitionregion,selectedcrevicesandsupportplates.Thefrequenciesusedfortheseexaminationswere400,300,100,and25KHz.I,Theinletorhotlegexaminationprogramplanwasgeneratedtoprovidetheexaminationof100%ofeachopenunsleevedS/Gtubefromthetubeendthroughthefirsttubesupportplate,alongwith20%ofthesetubesbeingselectedandexaminedfortheirfulllength(204randomsampleasrecommendedintheElectricPowerResearchInstitute.(EPRI)guidelines]withthebobbincoil.Inaddition,204ofeachtypeofsleevewasexaminedandtheremainingtubewasexaminedfulllength.AllRow1andRow2U-BendregionswereexaminedwiththeMRPCbetweentheg6tubesupportplatehotsideandtheg6tubesupportplatecoldsidefromthecoldlegside.HRCFORH366A(5.92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDSYQ(BNO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYWITHTHISINFORMATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONANDRECORDSMANAGEMENTBRAHCH(MHBB7714),U.STNUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGETWASHINGTONDC20503.FACILITYNAJK1R.E.GinnaNuclearPowerPlantDOCKETlRNBER205000244YEAR94LERNINBER6SEQUENTIALREVISIONM-006--00PAGE34OF8EXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)Resultsoftheaboveexaminationsindicatedthat164tubesinthe>>A>>S/Grequiredrepair(21newrepairsbypluggingand143newrepairsbysleeving).134tubesinthe>>B>>S/Grequiredrepair(31newrepairsbypluggingand103newrepairsbysleeving).Correctiveactionswerethereforetakenfor164tubesinthe>>A>>S/G,andfor134tubesinthe>>B>>S/G.OnMarch26,1994,atapproximately1800EST,withtheRCSdepressurizedandtemperatureatapproximately66degreesF,finalreviewofthe1994S/Geddycurrentexaminationresultswascompleted.Priortocompletionofthisreview(onMarch23,1994,atapproximately1500EST),itwasevidentthatmorethanonepercentofthetotaltubesinspectedweredegraded(i.e.,imperfectionsgreaterthantherepairlimit).Becauseoftheabove,theresultsoftheinspectionareconsideredareportableeventpursuantto10CFR50.73perAppendixBoftheQAManual.OnMarch24,1994,atapproximately1300EST,oralnotificationwasmadetotheNRCOfficeofNuclearReactorRegulationpursuanttoAppendixBoftheQAManual.OnApril8,1994,aSpecialReportlistingthenumberoftubesrequiredtobepluggedorsleevedineachS/G,wasreportedtotheNRC,pursuanttoAppendixBoftheQAManual.C~INOPERABLESTRUCTURESiCOMPONENTSIORSYSTEMSTHATCONTRIBUTEDTOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARYFUNCTIONSAFFECTED:NoneE.METHODOFDISCOVERY:Thiseventwasapparentduringthereviewofthe>>A>>and>>B>>S/Geddycurrentexaminationresults.NRCFORM366A(5-92)

NRCFORM366A(5-92)U.S.NUCLEARREGULATORYC(IIIISSI(NILICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYIGNINO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYWITHTHISINFORMATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOMMENTSREGARDINGBURDENESTIMATETOTHEINFORMATIONANDRECORDSMANAGEMENTBRAHCH(MHBB7714),U.S.NUCLEARREGULATORYCOMMISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140.0104),OFFICEOF.MANAGEMENTAHDBUDGETWASHIHGTOHDC20503.FACILITYNAME1DOCKETNEER2R.E.GinnaNuclearPowerPlantp5ppp244LERNIMBER6YEARSEQUENTIAL94--006--REVISION00PAGE35OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)F.OPERATORACTION:TheControlRoomoperatorswerenotifiedthatthenumberofdegradedtubesexceededthereportablelimitsoftheQAManual,andthattheNRC(NRR)hadalreadybeennotifiedbycorporatestaff.TheControlRoomoperatorscompletedthenotificationsandevaluationsrequiredbytheA-25.1(GinnaStationEventReport),submittedfortheeventbytheS/Gexaminationandrepairsupervision.G.SAFETYSYSTEMRESPONSES:NoneIII.CAUSEOFEVENTA.IMMEDIATECAUSE:Theimmediatecauseoftheeventwasthe"A"and"B"S/GtubedegradationwasinexcessoftheQAManualreportablelimits.B.ROOTCAUSE:TheresultsoftheexaminationindicatethatIntergranularAttack(IGA)andIntergranularStressCorrosionCracking(IGSCCorSCC)continuetobeactivewithinthetubesheetcreviceregionontheinletsideofeachS/G.Asinthepast,IGA/SCCismuchmoreprevalentinthe"B"S/Gwith74newcreviceindicationsreportedin1994.Inthe"A"S/G,42newcreviceindicationswerereportedin1994.In1993,41newcreviceindicationswerereportedinthe"A"S/G,and103newcreviceindicationswerereportedinthe>>B"S/G.In1994,42newcreviceindicationswerereportedinthe"A"S/G,and74newcreviceindicationswerereportedinthe"B"S/G.Comparisonof1993and1994resultsdoesnotsuggestanysignificantchangeintherateoftubedegradationduetoIGA/SCC.HRCFORM366A(5-92)

HRCFORM366A(5-92)U.S.NUCLEARREGULATORYCQHISSIOHLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYWNO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOMPLYllITHTHISINFORMATIONCOLLECTIOHREQUEST:50.0HRS.FORNARDCOMMENTSREGARDINGBURDENESTIMATETOTHEINFORMATIONAHDRECORDSMAHAGEMEHTBRANCH(MHBB7714),U.S.NUCLEARREGULATORYCOMMISSION,MASHIHGTOH,DC20555-0001AHDTOTHEPAPERNORKREDUCTIONPROJECT(31400104),OFFICEOFMANAGEHEHTANDBUDGETl!ASHIHGTONDC20503.FACILITYIUNE1R.E.GinnaNuclearPowerPlantDOCKETHINBER205000244YEARLERIWIER6SEQUENTIAL--006--REVISION00PAGE36OF8TEXT(IfmorespeceisreqUIred,useedditionelcopiesofHRCForm366A)(17)ThemajorityoftheinlettubesheetcrevicecorrosionindicationsareIGA/SCCoftheMillAnnealedInconel600tubematerial.Thisformofcorrosionisbelievedtobetheresultofanalkalineenvironmentforminginthetubesheetcrevices.Thisenvironmenthasdevelopedovertheyearsasdepositsandactivespecies,suchassodiumandphosphate,havereacted,changinganeutralorinhibitedcreviceenvironmentintotheaggressiveenvironmentthatpresentlyexists.AlongwithIGA/SCCinthecrevices,PrimaryWaterStressCorrosionCracking(PWSCC)attherolltransitioncontinuedtobeactiveduringthelastoperatingcycle.Thismechanismwasfirstaddressedin1989,andthisyeartherewere120rolltransition(PWSCC)indicationsinthe"A"S/Gand66rolltransition(PWSCC)indicationsinthe"B"S/G..ThesenumbersincludetubesthatmayhavePWSCCincombinationwithIGAorSCCinthecrevice.ThiseventisNRCPerformanceIndicatorSystemCauseCode5.8.4.3,"MaintenanceEquipmentFailure",andNUREG-1022CauseCode(B),"Design,Manufacturing,Construction/Installation."IV.ANALYSISOFEVENTThiseventisreportableinaccordancewith10CFR.50.73,LicenseeEventReportSystem,item(Other)andtheQAManualAppendixBwhichrequiresthat,"Ifthenumberoftubesinageneratorfallingintocategories(a)or(b)belowexceedsthecriteria,thenresultsoftheinspectionshallbeconsideredaReportableEventpursuantto10CFR50.73."Thetubedegradationinthe"A"and"B"S/Gsexceededthecriterionof(b)whichstates,"Morethan1percentofthetotaltubesinspectedaredegraded(imperfectionsgreaterthantherepairlimit)".Anassessmentwasperformedconsideringboththesafetyconsequencesandimplicationsofthiseventwiththe'followingresultsandconclusions:TherewerenooperationalorsafetyconsequencesresultingfromtheS/GtubedegradationinexcessoftheQAManualreportablelimitsbecause:HRCFORM366A(5-92)

Ci NRCFORH366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQISNO.3150-0104EXPIRES5/31/95ESTIHATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORHATIONCOLLECTIOHREQUEST:50.0HRS.FORWARDCOHHENTSREGARDINGBURDENESTIHATETOTHEINFORNATIONANDRECORDSHANAGEKEHTBRANCH(HHBB7714),U.S.NUCLEARREGULATORYCOHHISSION,WASHINGTON,DC20555-0001AND'O"THEPAPERWORKREDUCTIONPROJECT(3110-0104),OFFICEOFNANAGEHENTANDBUDGETWASHINGTONDC20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETNWBER205000244YEAR94--006--00LERNNNIER6SEQUENTIALREVISIONPAGE37OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofNRCForm366A)(17)~ThedegradedtubeswereidentifiedandrepairedpriortoanysignificantleakageorS/Gtuberuptureoccurring.~EvenassumingacompleteseveranceofaS/Gtubeatfullpower,asstatedintheR.E.GinnaNuclearPowerPlantUpdatedFinalSafetyAnalysisReport(GinnaUFSAR)section15.6.3(SteamGeneratorTubeRupture),thesequenceofrecoveryactionsensuresearlyterminationofprimarytosecondaryleakagewithorwithoutoffsitepoweravailablethuslimitingoffsiteradiationdosestowithintheguidelinesof10CFR100.Basedontheabove,itcanbeconcludedthatthepublic'shealthandsafetywasassured'atalltimes.V.CORRECTIVEACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENTNORMALSTATUSOfthe164tubesrepairedinthe"A"S/G,143tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese143tubeswillremaininservice.Theremaining21tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Atotalof215tubesinthe"A"S/Garecurrentlypluggedand811tubesaresleeved.Ofthe134tubesrepairedinthe"B"S/G,103tubeswererepairedusinga203/4inchBabcockandWilcoxkineticallyweldedtubesheetsleeveinthehotleg.Allofthese103tubeswillremaininservice.30tubeswereremovedfromservicebypluggingboththehotandcoldlegtubeends.Theremainingtubewaspreviouslypluggedandexhibitedacrackindicationintheplug.Thesubjecttubeplugwasremovedandanewpluginstalled.Atotalof315tubesinthe"B"S/Garecurrentlypluggedand1390tubesaresleeved.Alltheaboverepairsonthe"A"and"B"S/GswerecompletedonMarch27,1994,atapproximately2235EST.HRCFORH366A(5-92)

HRCFORM366A(5-92)U.S.NUCLEARREGULATORYCQIIISSIOHZiICENSEEEVENTREPORT(LER)TEXTCONTINUATIONAPPROVEDBYQQINO.3150-0104EXPIRES5/31/95ESTIMATEDBURDENPERRESPONSETOCOHPLYWITHTHISINFORMATIONCOLLECTIONREQUEST:50.0HRS.FORWARDCOMMENTSREGARDIHGBURDENESTIMATETOTHEINFORMATIONAMDRECORDSMANAGEMENTBRANCH(HNBB771C),U.S.NUCLEARREGULATORYCONHISSION,WASHINGTON,DC20555-0001ANDTOTHEPAPERWORKREDUCTIONPROJECT(3140-0104),OFFICEOFMANAGEMENTANDBUDGET'WASHINGTOMDC20503.FACILITYNAME1R.E.GinnaNuclearPowerPlantMxxETHIM(BER205000244YEAR94-006--00LERNWBER6SEQUENTIALREVISIONPAGE38OF8TEXT(Ifmorespaceisrequired,useadditionalcopiesofHRCForm366A)(17)B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE-Theoccurrence/presenceofIGA,SCC,andPWSCCisaPWRS/Gproblem.UtilitieswithsusceptibletubingandpartiallyrolledcrevicesmustdealwiththisrecurringattackonS/Gtubing.R.E.GinnaNuclearPowerPlantwillcontinuecarefulmonitoringofbothprimaryRCSandsecondarysidewaterchemistryparameters.Thesewaterchemistryparameterswillcontinuetobeevaluated'againstacceptedindustryguidelinesinordertominimizeharmfulprimaryand/orsecondarysideenvironments.DegradedS/Gtubesshallbesleevedorpluggedinaccordancewiththeinserviceinspectionprogramandacceptedindustryrepairmethods.\VI.ADDITIONALINFORMATIONA.FAILEDCOMPONENTS:ThedegradedcomponentsareInconel600MillAnnealedU-Bendtubeshavinganoutside.diameterof0.875inchesandanominalwallthicknessof0.050inches.ThetubesweremanufacturedbyHuntingtonAlloyCompany.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistoricalsearchwasconductedwiththefollowingresults:ThecreviceindicationsaresimilartothosereportedinA0-74-02,AO-75-07,R0-75-013,andLERs76-008,77008'8003I79006'9022I80003g81009g82003I8202283-013,89-001,90-004,91-005,92-005,and93-002.C.SPECIALCOMMENTS:Amorein-depthfinalreportwillbesubmittedtotheNRC,asrequiredbytheGinnaQAManual.Asanoteofinterest,RG&EhasorderednewsteamgeneratorsforR.E.GinnaNuclearPowerPlanttobeinstalledin1996.HRCFORH366A(592)

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