ML20065T242: Difference between revisions

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ll                                                                    l Iluke 1%rer Comtuny                                                    Mh nnun huelm Pn,ductwn tiert                                                  \he hrsiden!
Pil llos 10Hi                                                          haclear Di vatarns Charlotte N C &c'01-!iHl'                                              ! ?n tL!i:1:t s:il DUKE POWER December 21, 1990 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555
 
==Subject:==
Cate nba Nuclear Station, Units 1 and 2 Docket Nos. 50-413 and 50-414 NRC Inspection Report No. 50-413, 414/90-29 Violation 413/90-29-02 Reply to a Notice of Violation Gentlemen:
Enclosed is the response to the Notice of Violation issued November 21, 1990 by Alan R. Herdt concerning failure to follow an operating procedure which resulted in valve misalignment and the spray down of the 1A ND pump room.
Very truly yours, f'  -
c,hk /$. e                    -/
yp v M. S. Tuckman, Vice President Nuclear Operations WRC/220/lcs xc: Mr. Stewart D. Ebneter Regional Administrator, Region II U. S. Nuclear Regulatory Commission 101 Marietta St., NW., Suite 2900 Atlanta, Georgia 30323 Mr. W. T. Orders NRC Resident Inspector Catawba Nuclear Station 9012270400 901221 PDR O
ADOCK 05000413 PDR h'
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Duke Power Company Reply To A Notico Of Violation 413/90-29-02 Technical Specification 6.8.1 requires that written procedures be established, implemented, and maintained covering the activities referenced in Appendix A of Regulatory Guide 1.33, Revision 2,    February 1978 which includes surveillance testing.
Procedure PT/1/A/4230/53A, 1FW-28 Partial Stroke Test, Enclosure 13.2, step 8.0, requires that valve IND-7, the 1A Residual Heat Removal (ND) pump suction line drain valve, be closed and locked prior to opening 1FW-27A, the ND Pump suction valve from the Refueling Water Storage Tank in Step 11.0.
Contrary to the above, on October 18, 1990, a Non-Licensed Operator (NLO) failed to follow procedural requirements in that he signed-off Step 8.0 of PT/1/A/4200/53A indicatlag that valve IND-7 had been closed and locked when in fact the valve was locked open. Subsequently, the Control Room Operator performed Step 11.0 of the procedure which opened 1FW-27A, creating a direct flowpath from the Refueling Water Storage Tank, through an open vent valve downstream of 1ND-7, resulting in the spraydown of the ND pump room.
 
===RESPONSE===
: 1. Admission or Denial of Violation Duke Power admits the violation.
: 2. Reasons for Violation if Admitted The incident is attributed to Inappropriate action.
The operator in question signed off the valve as being in the closed position. The operator became confused in dealing with the reach rod resulting in the valve actually being left open.
: 3. Corrective Actions Taken to Avoid Further Violations And Results Achieved The operator involved in this event has been counseled on the importance of determining valve position and the need to notify supervision when questions arise.                        This was considered an isolated case.
A letter was written by Maintenance Engineering Services (MES) on 11/14/90 requesting Radiation Protection, Chemistry and Operations to provide l
contacts to help establish an appropriate Preventive Maintenance (PM) program for the reach rods.
 
l '. .
Response to-NRC Notice of Violation 413/90-29-02 Page 2
: 4. Corrective Actions to be Taken To Avoid Further Violations Maintenance Engineering Services will evaluate the reliability of valve reach rods and the need-for a Preventive Maintenance program for reach rods and improve general reliability, (no PM is currently performed). This evaluation will be complete by 3/1/91.                                                    ,
: 5. Date of Full Compliance Duke Power is now in full compliance.
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Latest revision as of 02:41, 6 January 2021

Forwards Response to Notice of Violation Re Insp Repts 50-413/90-29 & 50-414/90-29.Corrective Action:Operator Counseled on Importance of Determining Valve Position & Need to Notify Supervisor When Questions Arise
ML20065T242
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 12/21/1990
From: Tuckman S
DUKE POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9012270400
Download: ML20065T242 (3)


Text

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ll l Iluke 1%rer Comtuny Mh nnun huelm Pn,ductwn tiert \he hrsiden!

Pil llos 10Hi haclear Di vatarns Charlotte N C &c'01-!iHl'  ! ?n tL!i:1:t s:il DUKE POWER December 21, 1990 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555

Subject:

Cate nba Nuclear Station, Units 1 and 2 Docket Nos. 50-413 and 50-414 NRC Inspection Report No. 50-413, 414/90-29 Violation 413/90-29-02 Reply to a Notice of Violation Gentlemen:

Enclosed is the response to the Notice of Violation issued November 21, 1990 by Alan R. Herdt concerning failure to follow an operating procedure which resulted in valve misalignment and the spray down of the 1A ND pump room.

Very truly yours, f' -

c,hk /$. e -/

yp v M. S. Tuckman, Vice President Nuclear Operations WRC/220/lcs xc: Mr. Stewart D. Ebneter Regional Administrator, Region II U. S. Nuclear Regulatory Commission 101 Marietta St., NW., Suite 2900 Atlanta, Georgia 30323 Mr. W. T. Orders NRC Resident Inspector Catawba Nuclear Station 9012270400 901221 PDR O

ADOCK 05000413 PDR h'

(

1 l

l <

Duke Power Company Reply To A Notico Of Violation 413/90-29-02 Technical Specification 6.8.1 requires that written procedures be established, implemented, and maintained covering the activities referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978 which includes surveillance testing.

Procedure PT/1/A/4230/53A, 1FW-28 Partial Stroke Test, Enclosure 13.2, step 8.0, requires that valve IND-7, the 1A Residual Heat Removal (ND) pump suction line drain valve, be closed and locked prior to opening 1FW-27A, the ND Pump suction valve from the Refueling Water Storage Tank in Step 11.0.

Contrary to the above, on October 18, 1990, a Non-Licensed Operator (NLO) failed to follow procedural requirements in that he signed-off Step 8.0 of PT/1/A/4200/53A indicatlag that valve IND-7 had been closed and locked when in fact the valve was locked open. Subsequently, the Control Room Operator performed Step 11.0 of the procedure which opened 1FW-27A, creating a direct flowpath from the Refueling Water Storage Tank, through an open vent valve downstream of 1ND-7, resulting in the spraydown of the ND pump room.

RESPONSE

1. Admission or Denial of Violation Duke Power admits the violation.
2. Reasons for Violation if Admitted The incident is attributed to Inappropriate action.

The operator in question signed off the valve as being in the closed position. The operator became confused in dealing with the reach rod resulting in the valve actually being left open.

3. Corrective Actions Taken to Avoid Further Violations And Results Achieved The operator involved in this event has been counseled on the importance of determining valve position and the need to notify supervision when questions arise. This was considered an isolated case.

A letter was written by Maintenance Engineering Services (MES) on 11/14/90 requesting Radiation Protection, Chemistry and Operations to provide l

contacts to help establish an appropriate Preventive Maintenance (PM) program for the reach rods.

l '. .

Response to-NRC Notice of Violation 413/90-29-02 Page 2

4. Corrective Actions to be Taken To Avoid Further Violations Maintenance Engineering Services will evaluate the reliability of valve reach rods and the need-for a Preventive Maintenance program for reach rods and improve general reliability, (no PM is currently performed). This evaluation will be complete by 3/1/91. ,
5. Date of Full Compliance Duke Power is now in full compliance.

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