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COMPl.ETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC*        , REPORT ABLE                                                                  MANUFAC*          REPORTABLE
COMPl.ETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC*        , REPORT ABLE                                                                  MANUFAC*          REPORTABLE
                                                                                                                                                                                           ,............/
                                                                                                                                                                                           ,............/
CAUSE    SYSTEM        COMPONENT                        TUR ER            TO NPROS                CAUSE  SYSTEM          COMPONENT                    TUR ER          TO NPROS
CAUSE    SYSTEM        COMPONENT                        TUR ER            TO NPROS                CAUSE  SYSTEM          COMPONENT                    TUR ER          TO NPROS x      s  IJ          I I Ip                    w 13    I1 Ie            YES                                I          I I I                    I I I                                              ...
                                                                                                                                    -                                                                    ;
x      s  IJ          I I Ip                    w 13    I1 Ie            YES                                I          I I I                    I I I                                              ...
I          I I I                        I I I                                                    I          I I I                    I    I    I                            i ;
I          I I I                        I I I                                                    I          I I I                    I    I    I                            i ;
SUPPLEMENTAL REPORT EXPECTED 1141                                                                            MONTH        DAY        YEAR EXPECTED
SUPPLEMENTAL REPORT EXPECTED 1141                                                                            MONTH        DAY        YEAR EXPECTED

Latest revision as of 15:19, 23 February 2020

LER 95-003-00:on 950522,main FW Pump Transient Resulted in Rt.Evaluated MFP Governor Control Setpoint of 5250 RPM & Relationship to Overspeed Trip Setpoint
ML18064A818
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/21/1995
From: Hobe M
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
Shared Package
ML18064A817 List:
References
LER-95-003-01, LER-95-3-1, NUDOCS 9506290196
Download: ML18064A818 (4)


Text

NRC Form 388 U.S. NUCLEAR REGULATORY COMMISSION (9*831 APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI FACILITY NAME (1) DOCKET NUMBER (21 PAGE 131 Palisades Plant 016101010121616 1 I OF 0 14 nnE 141 LICENSEE EVENT REPORT 95-003- MAIN FEEDWATER PUMP TRANSIENT RESULTING IN A REACTOR TRIP EVENT DATE 161 LEA NUMBER 181 REPORT DATE (81

. OTHER FACILITIES INVOLVED (81 SEQUENTIAL REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER n NUMBER MONTH DAY YEAR N/A 0161010101 I ol5 212 9 5 915 olol3 olo ols 21 1 915 N/A THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: ICh<<k,,,,. °',,_.of die following/ (111 0161010101 I OPERATING N 20.402(bl 20.4061cl x 60.73(*)(2)(ivl 73.71(bl I

MODE(tll 20.4061*111 JUI 60.38(c)(11 60.731*H21M - 73.71(cl POWER I'*'

LEVEL -

20.406(oJ(1 )(iii 60.38(c)(21 60.73(*1121(Yiil OTHER (Specify in Abotroct

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1101 41 s 20.406(oJ(1 IOiil 60.731*112)(il 60. 731*112)(viiil IAI below end in Text, 20.4061*111 IUvl 20.4061*1111M - 60.731*112)(iil 60.731*1(2)6iil -

LICENSEE CONTACT FOR THIS LEA ( 121

60. 7 3 l*ll2)(viii)(BI 60.73(*11211xl NRC Form 388AI NAME TELEPHONE NUMBER MARJORIE HOBE sATA1CI°~ I1 I 6 I I -I 8 I .9 I J, I 3 4

COMPl.ETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC* , REPORT ABLE MANUFAC* REPORTABLE

,............/

CAUSE SYSTEM COMPONENT TUR ER TO NPROS CAUSE SYSTEM COMPONENT TUR ER TO NPROS x s IJ I I Ip w 13 I1 Ie YES I I I I I I I ...

I I I I I I I I I I I I I I i ;

SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED

~NO SUBMISSION

--rely -

- - , YES Uf ye-. e<<np#tti EXPECTED SUBMISSION DA TEI ABSTRACT Wtn1t ID 1400 ~ I.*., ling#-.,,.c* trP<1writtM llnnl 1181 DATE (161 I I I On May 22, 1995, at 1110, with the plant operating at 46% power, the reactor was manually tripped. At the time of the trip, K-7 A and K-78 main feedwater pump turbines had both tripped, resulting in a loss of all main feedwater. The vibration on K- 7 A had increased earlier and System Engineering was brought in to investigate the problem. A decision was made to reduce reactor power and take K-7 A off line. While preparing to reduce reactor power, K~7A tripped. Later, the trip was attributed to a failure in the layshaft assembly which uncoupled the governor controls from the main turbine shaft and resulted in the turbine tripping on overspeed. The control room operator took manual control of K-78 and ramped the turbine up to full speed, as required by Off Normal Procedure ONP-3, "Loss of Main Feedwater." Later when "8" Steam Generator (E-508) level was recovering too quickly, the control room operator took manual control of the feedwater regulating valve (CV~0703) to manually throttle the valve. The "8" Steam Generator level reached the high level override setpoint which immediately closed the feedwater regulating valve CV-0703. Rapidly closing the feed.water regulating valve CV-0703 caused an immediate drop in load and K-78 turbine speed increased above the overspeed trip, resulting in the turbine tripping on overs peed. After verifying that K-78 had tripped, the control room operator manually tripped the reactor.

The cause of this event was the failure of the locknut on the lays haft assembly of K- 7 A, allowing the layshaft drive gear to walk down the shaft.

9506290196 950621 PDR ADOCK 05000255 S PDR

NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION 19-831 APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant 0 I6 I0 I0 I0 I2 I6 I6 9 I5 - 0 I0 I3 - 0 I0 0 I2 OF 0 I 4 Event Description On the morning of May 22, 1995, the recorder for K-7A main feedwater pump turbine [SJ;P]

shaft displacement had a small movement and the pen for recording the vibration between the turbine and governor started marking a wider band than normal (Worthington Pump Driver; Turbine Frame ITV2X3). At 0700, the control room operator noticed the vibration increasing on the recorder and notified the Secondary Auxiliary Operator and the Shift Supervisor. The vibration went from 1.6 mils to 2.0 mils (the alert indication setpoint for vibration is 2.5 mils).

The pump and turbine were checked along with other local instruments. A rise in the noise level was the only abnormality noticed by the Shift Supervisor and Auxiliary Operator.

The Shift Supervisor contacted the System Engineer for further evaluation. After a review of K-7A, the System Engineer contacted the Plant Performance Engineer to take vibration readings and an oil sample. Chemistry checked the oil sample for water and small suspended solids, but both tests were negative. An oil sample was sent off site for testing and later found to be normal.

The Control Operators reviewed the Off Normal Procedure (ONP-3) for "Loss of Main Feedwater" in case of a Main Feedwater Pump (MFP) trip. A meeting was held with upper management to review the course of action. At around 1100 the decision was made to reduce reactor power and remove K-7 A from service so it could be checked out further. Just prior to starting the power reduction K-7 A tripped.

After K- 7 A tripped, the control room operator verified that "A" Main Feedwater Pump tripped, took manual control of K-78, and ramped the turbine up to full speed, as required by ONP-3. The "B" Main Feedwater Pump (MFP) was at maximum speed 24 seconds after A-MFP tripped.

Then, at 36 seconds, the same control room operator took manual control of the turbine and reduced load while the other control room operator continued to manually drive control rods in to reduce reactor power. In 58 seconds, the feedwater flow was equal to steam flow for both steam generators. (Per ONP-3, Section 4.1, subsequent actions, "Stop the power reduction when feed flow indication becomes slightly greater than steam flow indications for both S/Gs. ")

At 1 minute and 10 seconds the down power was momentarily halted at approximately 60%

power.

Because the "B" Steam Generator (S/Gl level was not recovering, the Control Room Supervisor directed an additional load decrease. At 1 minute 48 seconds, the control room operators started lowering reactor power and turbine load. At 2 minutes 48 seconds, the load decrease was stopped at approximately 46% power.

'a' NRC Form 3811A U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMB NO. 3160-0104 EXPIRES: B/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant 0 I5 I0 I0 I0 I2 I5 I5 9 I5 - 0 I0 I3 - 0 I0 0 I3 OF 0 I 4 The "B" S/G level began to rise rapidly and at 3 minutes 16 seconds the control room operator took manual control of "B" S/G feedwater regulating valve, CV-0703. The valve was manually closed to 20% at 3 minutes 52 seconds and not manually closed any further after that. At 4 minutes 28 seconds the "B" S/G level exceeded 84. 7% and the high steam generator level override circuit actuated to close CV-0703.

When CV-0703 rapidly closed from 20%, the result was a large drop in load for K-78. This immediate drop in load was enough to allow the speed of K-7B to increase above the overs peed trip. The "B" MFP tripped 4 minutes 40 seconds after "A" MFP tripped.

The control room operator then verified that "B" MFP had tripped and at 5 minutes 12 seconds the Reactor was manually tripped. The immediate actions of Emergency Operating Procedure (EOP-1 ), "Standard Post Trip Actions," and EOP-2, "Reactor Trip Recovery" were performed and verbal verification was completed. All EOP procedure steps were completed satisfactorily.

Plant and operator actions taken in response to MFP trips were in accordance with procedures, with no safety significant deviations or abnormalities. Although not required by the event, both trains of engineered safeguards equipment were operable and available for use at all times. This event did not have an adverse impact on the operational safety of the plant or upon the safety of plant personnel or the general public.

Cause of the Event The proximate cause of the event is the "A" main feed water pump lays haft locknut lockwasher tab failure which allowed the layshaft locknut and driven gear to walk off the shaft.

Contributing causes include:

1. The feedwater pump gain control setting is set as low as possible. As a result, the MFPs are slow to respond to a speed control signal. Because of this, operator action is required to take the MFP speed control to manual and increase pump speed if an attempt is made to provide the feedwater flow required to compensate for the loss of a main feedwater pump.

An Asea Brown Bovari (ABB) simulation ("Final Report Palisades Nuclear Plant; Feedwater Control System Evaluation, July 1992") recommended the feedwater control system be fine tuned to make the system responsive enough to handle this type of transient with the feedwater system left in automatic. This slow main feedwater pump response results in the MFP speed staying high on a Reactor trip. The high MFP speed, coupled with the automatic shift of the feed regulator valves to manual, assures that ample feedwater is maintained for core cooling; it also, however, requires that a control room operator manually trip both MFPs on a reactor trip to prevent overcooling the primary coolant system.

NRC Form 388A 19-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31/86 FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAi. REVISION YEAR NUMBER NUMBER Palisades Plant 0 I 6 I0 I0 I0 I2 I 5 I 6 9 I5 - 0 I0 I3 - 0 I0 0 I4 OF 0 I4

2. The "B" main feedwater pump governor control maximum speed is so close to the overspeed trip setpoint that it allows an overspeed trip on a ioss of load condition.

Correctjve Actions Corrective Actions are as follows:

1. Determine the root cause for the failure mode of the "A" MFP lays haft lockwasher locking tab. Make necessary changes to both MFPs.
2. Evaluate the feedwater control system for this event and the changes suggested by the 1992 ABB report. Review the effect of any changes on the response of the feedwater system for other events. Make any required changes to both feedwater control systems.
3. Evaluate the MFP governor control setpoint of 5250 RPM and its relationship to the overspeed trip setpoint.

Previous Events Licensee Event Reports since 1990 were reviewed. Four reactor trips resulted from a loss of one of the main feedwater pumps. The failure mechanisms and root causes, however, do not correspond with those identified for this event.

Additional Information The lockwasher failure is similar to an event described by D-PAL-91-122 when K-7A was ready to return to service on July 20, 1991, but was shut down because of noise. The layshaft locknut was found loose.