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| issue date = 06/21/1995
| issue date = 06/21/1995
| title = LER 95-003-00:on 950522,main FW Pump Transient Resulted in Rt.Evaluated MFP Governor Control Setpoint of 5250 RPM & Relationship to Overspeed Trip Setpoint
| title = LER 95-003-00:on 950522,main FW Pump Transient Resulted in Rt.Evaluated MFP Governor Control Setpoint of 5250 RPM & Relationship to Overspeed Trip Setpoint
| author name = HOBE M
| author name = Hobe M
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.),
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.),
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRC Form 388 U.S. NUCLEAR REGULATORY COMMISSION (9*831 APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI FACILITY NAME (1) DOCKET NUMBER (21 PAGE 131 Palisades Plant 016101010121616 1 I OF 0 14 nnE 141 LICENSEE EVENT REPORT 95-003-MAIN FEEDWATER PUMP TRANSIENT RESULTING IN A REACTOR TRIP EVENT DATE 161 LEA NUMBER 181 REPORT DATE (81 . OTHER FACILITIES INVOLVED (81 ***********
{{#Wiki_filter:NRC Form 388                                                                                                                                           U.S. NUCLEAR REGULATORY COMMISSION (9*831                                                                                                                                                           APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI FACILITY NAME (1)                                                                                                             DOCKET NUMBER (21                                     PAGE 131 Palisades Plant                                                                                                               016101010121616                                 1 I OF   0 14 nnE 141 LICENSEE EVENT REPORT 95-003- MAIN FEEDWATER PUMP TRANSIENT RESULTING IN A REACTOR TRIP EVENT DATE 161                             LEA NUMBER 181                         REPORT DATE (81
SEQUENTIAL n REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR N/A 0161010101 I --ol5 212 9 5 915 olol3 olo ols 21 1 915 N/A 0161010101 I THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: ICh<<k,,,,.  
                                                                                                          .                                 OTHER FACILITIES INVOLVED (81 SEQUENTIAL         REVISION                                               FACILITY NAMES MONTH     DAY     YEAR     YEAR                   NUMBER     n    NUMBER       MONTH       DAY   YEAR N/A                                         0161010101                       I ol5       212       9   5   915                 olol3               olo         ols       21 1   915           N/A THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: ICh<<k,,,,. &deg;',,_.of die following/ (111 0161010101                      I OPERATING N         20.402(bl                                       20.4061cl                       x   60.73(*)(2)(ivl                           73.71(bl I
&deg;',,_.of die following/  
MODE(tll 20.4061*111 JUI                                 60.38(c)(11                         60.731*H21M                         -    73.71(cl POWER I'*'
(111 OPERATING N MODE(tll 20.402(bl 20.4061cl x 60.73(*)(2)(ivl 73.71(bl ---POWER I 20.4061*111 JUI 60.38(c)(11 60.731*H21M 73.71(cl LEVEL ----1101 41 s I'*' 20.406(oJ(1  
LEVEL                    -
)(iii 60.38(c)(21 60.73(*1121(Yiil OTHER (Specify in Abotroct -= ---20.406(oJ(1 IOiil 60.731*112)(il  
20.406(oJ(1 )(iii                               60.38(c)(21                         60.73(*1121(Yiil                           OTHER (Specify in Abotroct
: 60. 731*112)(viiil IAI below end in Text, --20.4061*111 IUvl 60.731*112)(iil  
-=
: 60. 7 3 l*ll2)(viii)(BI NRC Form 388AI --20.4061*1111M 60.731*1(2)6iil 60.73(*11211xl LICENSEE CONTACT FOR THIS LEA ( 121 NAME TELEPHONE NUMBER MARJORIE HOBE I 1 I 6 I 4 I -I 8 I .9 I J, I 3 COMPl.ETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC* , REPORT ABLE MANUFAC* REPORTABLE  
1101    41    s 20.406(oJ(1 IOiil                               60.731*112)(il                     60. 731*112)(viiil IAI                     below end in Text, 20.4061*111 IUvl 20.4061*1111M                            -    60.731*112)(iil 60.731*1(2)6iil              -
/ CAUSE SYSTEM COMPONENT TUR ER TO NPROS CAUSE SYSTEM COMPONENT TUR ER TO NPROS , ............
LICENSEE CONTACT FOR THIS LEA ( 121
s I J I I Ip w 13 I 1 I e I I -I I I I I ; ... x YES I I I I I I I I I I I , I I I i ; SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED --, YES Uf ye-. e<<np#tti EXPECTED SUBMISSION DA TEI SUBMISSION I I I DATE (161 ABSTRACT Wtn1t ID 1400 I.*., --rely -ling#-.,,.c*
: 60. 7 3 l*ll2)(viii)(BI 60.73(*11211xl NRC Form 388AI NAME                                                                                                                                                    TELEPHONE NUMBER MARJORIE HOBE sATA1CI&deg;~ I1 I 6 I I -I 8 I .9 I J, I 3 4
trP<1writtM llnnl 1181 *, On May 22, 1995, at 1110, with the plant operating at 46% power, the reactor was manually tripped. At the time of the trip, K-7 A and K-78 main feedwater pump turbines had both tripped, resulting in a loss of all main feedwater.
COMPl.ETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC*         , REPORT ABLE                                                                 MANUFAC*           REPORTABLE
The vibration on K-7 A had increased earlier and System Engineering was brought in to investigate the problem. A decision was made to reduce reactor power and take K-7 A off line. While preparing to reduce reactor power, tripped. Later, the trip was attributed to a failure in the layshaft assembly which uncoupled the governor controls from the main turbine shaft and resulted in the turbine tripping on overspeed.
                                                                                                                                                                                          ,............/
The control room operator took manual control of K-78 and ramped the turbine up to full speed, as required by Off Normal Procedure ONP-3, "Loss of Main Feedwater." Later when "8" Steam Generator (E-508) level was recovering too quickly, the control room operator took manual control of the feedwater regulating valve to manually throttle the valve. The "8" Steam Generator level reached the high level override setpoint which immediately closed the feedwater regulating valve CV-0703. Rapidly closing the feed.water regulating valve CV-0703 caused an immediate drop in load and K-78 turbine speed increased above the overspeed trip, resulting in the turbine tripping on overs peed. After verifying that K-78 had tripped, the control room operator manually tripped the reactor. The cause of this event was the failure of the locknut on the lays haft assembly of K-7 A, allowing the layshaft drive gear to walk down the shaft. 9506290196 950621 PDR ADOCK 05000255 S PDR NRC Form 388A 19-831 FACILITY NAME 111 Palisades Plant Event Description LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER 121 LER NUMBER 131 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER 0 I 6 I 0 I 0 I 0 I 2 I 6 I 6 9 I 5 -0 I 0 I 3 -0 I 0 0 I 2 OF 0 I 4 On the morning of May 22, 1995, the recorder for K-7A main feedwater pump turbine [SJ;P] shaft displacement had a small movement and the pen for recording the vibration between the turbine and governor started marking a wider band than normal (Worthington Pump Driver; Turbine Frame ITV2X3). At 0700, the control room operator noticed the vibration increasing on the recorder and notified the Secondary Auxiliary Operator and the Shift Supervisor.
CAUSE     SYSTEM         COMPONENT                       TUR ER             TO NPROS               CAUSE   SYSTEM         COMPONENT                     TUR ER           TO NPROS x      s  IJ          I I Ip                    w 13     I1 Ie            YES                                I           I I I                     I I I                                               ...
The vibration went from 1.6 mils to 2.0 mils (the alert indication setpoint for vibration is 2.5 mils). The pump and turbine were checked along with other local instruments.
I           I I I                         I I I                                                     I           I I I                     I     I     I                           i ;
A rise in the noise level was the only abnormality noticed by the Shift Supervisor and Auxiliary Operator.
SUPPLEMENTAL REPORT EXPECTED 1141                                                                             MONTH       DAY       YEAR EXPECTED
The Shift Supervisor contacted the System Engineer for further evaluation.
                                                                          ~NO                                                                      SUBMISSION
After a review of K-7A, the System Engineer contacted the Plant Performance Engineer to take vibration readings and an oil sample. Chemistry checked the oil sample for water and small suspended solids, but both tests were negative.
                                      --rely -
An oil sample was sent off site for testing and later found to be normal. The Control Operators reviewed the Off Normal Procedure (ONP-3) for "Loss of Main Feedwater" in case of a Main Feedwater Pump (MFP) trip. A meeting was held with upper management to review the course of action. At around 1100 the decision was made to reduce reactor power and remove K-7 A from service so it could be checked out further. Just prior to starting the power reduction K-7 A tripped. After K-7 A tripped, the control room operator verified that "A" Main Feedwater Pump tripped, took manual control of K-78, and ramped the turbine up to full speed, as required by ONP-3. The "B" Main Feedwater Pump (MFP) was at maximum speed 24 seconds after A-MFP tripped. Then, at 36 seconds, the same control room operator took manual control of the turbine and reduced load while the other control room operator continued to manually drive control rods in to reduce reactor power. In 58 seconds, the feedwater flow was equal to steam flow for both steam generators. (Per ONP-3, Section 4.1, subsequent actions, "Stop the power reduction when feed flow indication becomes slightly greater than steam flow indications for both S/Gs. ") At 1 minute and 10 seconds the down power was momentarily halted at approximately 60% power. Because the "B" Steam Generator (S/Gl level was not recovering, the Control Room Supervisor directed an additional load decrease.
- - , YES Uf ye-. e<<np#tti EXPECTED SUBMISSION DA TEI ABSTRACT Wtn1t ID 1400 ~ I.*.,                                 ling#-.,,.c* trP<1writtM llnnl 1181 DATE (161          I          I            I On May 22, 1995, at 1110, with the plant operating at 46% power, the reactor was manually tripped. At the time of the trip, K-7 A and K-78 main feedwater pump turbines had both tripped, resulting in a loss of all main feedwater. The vibration on K- 7 A had increased earlier and System Engineering was brought in to investigate the problem. A decision was made to reduce reactor power and take K-7 A off line. While preparing to reduce reactor power, K~7A tripped. Later, the trip was attributed to a failure in the layshaft assembly which uncoupled the governor controls from the main turbine shaft and resulted in the turbine tripping on overspeed. The control room operator took manual control of K-78 and ramped the turbine up to full speed, as required by Off Normal Procedure ONP-3, "Loss of Main Feedwater." Later when "8" Steam Generator (E-508) level was recovering too quickly, the control room operator took manual control of the feedwater regulating valve (CV~0703) to manually throttle the valve. The "8" Steam Generator level reached the high level override setpoint which immediately closed the feedwater regulating valve CV-0703. Rapidly closing the feed.water regulating valve CV-0703 caused an immediate drop in load and K-78 turbine speed increased above the overspeed trip, resulting in the turbine tripping on overs peed. After verifying that K-78 had tripped, the control room operator manually tripped the reactor.
At 1 minute 48 seconds, the control room operators started lowering reactor power and turbine load. At 2 minutes 48 seconds, the load decrease was stopped at approximately 46% power.
The cause of this event was the failure of the locknut on the lays haft assembly of K- 7 A, allowing the layshaft drive gear to walk down the shaft.
'a' NRC Form 3811A (9-83) U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: B/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant 0 I 5 I 0 I 0 I 0 I 2 I 5 I 5 9 I 5 -0 I 0 I 3 -0 I 0 0 I 3 OF 0 I 4 The "B" S/G level began to rise rapidly and at 3 minutes 16 seconds the control room operator took manual control of "B" S/G feedwater regulating valve, CV-0703. The valve was manually closed to 20% at 3 minutes 52 seconds and not manually closed any further after that. At 4 minutes 28 seconds the "B" S/G level exceeded 84. 7% and the high steam generator level override circuit actuated to close CV-0703. When CV-0703 rapidly closed from 20%, the result was a large drop in load for K-78. This immediate drop in load was enough to allow the speed of K-7B to increase above the overs peed trip. The "B" MFP tripped 4 minutes 40 seconds after "A" MFP tripped. The control room operator then verified that "B" MFP had tripped and at 5 minutes 12 seconds the Reactor was manually tripped. The immediate actions of Emergency Operating Procedure (EOP-1 ), "Standard Post Trip Actions," and EOP-2, "Reactor Trip Recovery" were performed and verbal verification was completed.
9506290196 950621 PDR ADOCK 05000255 S                                         PDR
All EOP procedure steps were completed satisfactorily.
 
Plant and operator actions taken in response to MFP trips were in accordance with procedures, with no safety significant deviations or abnormalities.
NRC Form 388A                                                                         U.S. NUCLEAR REGULATORY COMMISSION 19-831                                                                                          APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111                DOCKET NUMBER 121                  LER NUMBER 131                        PAGE 141 SEQUENTIAL         REVISION YEAR       NUMBER           NUMBER Palisades Plant 0 I6 I0 I0 I0 I2 I6 I6  9  I5 -  0  I0 I3      -    0   I0    0 I2    OF  0   I 4 Event Description On the morning of May 22, 1995, the recorder for K-7A main feedwater pump turbine [SJ;P]
Although not required by the event, both trains of engineered safeguards equipment were operable and available for use at all times. This event did not have an adverse impact on the operational safety of the plant or upon the safety of plant personnel or the general public. Cause of the Event The proximate cause of the event is the "A" main feed water pump lays haft locknut lockwasher tab failure which allowed the layshaft locknut and driven gear to walk off the shaft. Contributing causes include: 1. The feedwater pump gain control setting is set as low as possible.
shaft displacement had a small movement and the pen for recording the vibration between the turbine and governor started marking a wider band than normal (Worthington Pump Driver; Turbine Frame ITV2X3). At 0700, the control room operator noticed the vibration increasing on the recorder and notified the Secondary Auxiliary Operator and the Shift Supervisor. The vibration went from 1.6 mils to 2.0 mils (the alert indication setpoint for vibration is 2.5 mils).
As a result, the MFPs are slow to respond to a speed control signal. Because of this, operator action is required to take the MFP speed control to manual and increase pump speed if an attempt is made to provide the feedwater flow required to compensate for the loss of a main feedwater pump. An Asea Brown Bovari (ABB) simulation  
The pump and turbine were checked along with other local instruments. A rise in the noise level was the only abnormality noticed by the Shift Supervisor and Auxiliary Operator.
("Final Report Palisades Nuclear Plant; Feedwater Control System Evaluation, July 1992") recommended the feedwater control system be fine tuned to make the system responsive enough to handle this type of transient with the feedwater system left in automatic.
The Shift Supervisor contacted the System Engineer for further evaluation. After a review of K-7A, the System Engineer contacted the Plant Performance Engineer to take vibration readings and an oil sample. Chemistry checked the oil sample for water and small suspended solids, but both tests were negative. An oil sample was sent off site for testing and later found to be normal.
This slow main feedwater pump response results in the MFP speed staying high on a Reactor trip. The high MFP speed, coupled with the automatic shift of the feed regulator valves to manual, assures that ample feedwater is maintained for core cooling; it also, however, requires that a control room operator manually trip both MFPs on a reactor trip to prevent overcooling the primary coolant system.
The Control Operators reviewed the Off Normal Procedure (ONP-3) for "Loss of Main Feedwater" in case of a Main Feedwater Pump (MFP) trip. A meeting was held with upper management to review the course of action. At around 1100 the decision was made to reduce reactor power and remove K-7 A from service so it could be checked out further. Just prior to starting the power reduction K-7 A tripped.
NRC Form 388A 19-831 FACILITY NAME 111
After K- 7 A tripped, the control room operator verified that "A" Main Feedwater Pump tripped, took manual control of K-78, and ramped the turbine up to full speed, as required by ONP-3. The "B" Main Feedwater Pump (MFP) was at maximum speed 24 seconds after A-MFP tripped.
* LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER 121 LER NUMBER 131 SEQUENTIAi.
Then, at 36 seconds, the same control room operator took manual control of the turbine and reduced load while the other control room operator continued to manually drive control rods in to reduce reactor power. In 58 seconds, the feedwater flow was equal to steam flow for both steam generators. (Per ONP-3, Section 4.1, subsequent actions, "Stop the power reduction when feed flow indication becomes slightly greater than steam flow indications for both S/Gs. ")
YEAR NUMBER U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31/86 REVISION NUMBER PAGE 141 Palisades Plant 0 I 6 I 0 I 0 I 0 I 2 I 5 I 6 9 I 5 -0 I 0 I 3 -0 I 0 0 I 4 OF 0 I 4 2. The "B" main feedwater pump governor control maximum speed is so close to the overspeed trip setpoint that it allows an overspeed trip on a ioss of load condition.
At 1 minute and 10 seconds the down power was momentarily halted at approximately 60%
Correctjve Actions Corrective Actions are as follows: 1 . Determine the root cause for the failure mode of the "A" MFP lays haft lockwasher locking tab. Make necessary changes to both MFPs. 2. Evaluate the feedwater control system for this event and the changes suggested by the 1992 ABB report. Review the effect of any changes on the response of the feedwater system for other events. Make any required changes to both feedwater control systems. 3. Evaluate the MFP governor control setpoint of 5250 RPM and its relationship to the overspeed trip setpoint.
power.
Previous Events Licensee Event Reports since 1990 were reviewed.
Because the "B" Steam Generator (S/Gl level was not recovering, the Control Room Supervisor directed an additional load decrease. At 1 minute 48 seconds, the control room operators started lowering reactor power and turbine load. At 2 minutes 48 seconds, the load decrease was stopped at approximately 46% power.
Four reactor trips resulted from a loss of one of the main feedwater pumps. The failure mechanisms and root causes, however, do not correspond with those identified for this event. Additional Information The lockwasher failure is similar to an event described by D-PAL-91-122 when K-7A was ready to return to service on July 20, 1991, but was shut down because of noise. The layshaft locknut was found loose.}}
 
'a' NRC Form 3811A                                                                           U.S. NUCLEAR REGULATORY COMMISSION (9-83)                                                                                            APPROVED OMB NO. 3160-0104 EXPIRES: B/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111                   DOCKET NUMBER 121                   LER NUMBER 131                       PAGE 141 SEQUENTIAL         REVISION YEAR       NUMBER           NUMBER Palisades Plant 0 I5 I0 I0 I0 I2 I5 I5  9  I5 -  0  I0 I3      -    0   I0    0 I3    OF  0   I 4 The "B" S/G level began to rise rapidly and at 3 minutes 16 seconds the control room operator took manual control of "B" S/G feedwater regulating valve, CV-0703. The valve was manually closed to 20% at 3 minutes 52 seconds and not manually closed any further after that. At 4 minutes 28 seconds the "B" S/G level exceeded 84. 7% and the high steam generator level override circuit actuated to close CV-0703.
When CV-0703 rapidly closed from 20%, the result was a large drop in load for K-78. This immediate drop in load was enough to allow the speed of K-7B to increase above the overs peed trip. The "B" MFP tripped 4 minutes 40 seconds after "A" MFP tripped.
The control room operator then verified that "B" MFP had tripped and at 5 minutes 12 seconds the Reactor was manually tripped. The immediate actions of Emergency Operating Procedure (EOP-1 ), "Standard Post Trip Actions," and EOP-2, "Reactor Trip Recovery" were performed and verbal verification was completed. All EOP procedure steps were completed satisfactorily.
Plant and operator actions taken in response to MFP trips were in accordance with procedures, with no safety significant deviations or abnormalities. Although not required by the event, both trains of engineered safeguards equipment were operable and available for use at all times. This event did not have an adverse impact on the operational safety of the plant or upon the safety of plant personnel or the general public.
Cause of the Event The proximate cause of the event is the "A" main feed water pump lays haft locknut lockwasher tab failure which allowed the layshaft locknut and driven gear to walk off the shaft.
Contributing causes include:
: 1.     The feedwater pump gain control setting is set as low as possible. As a result, the MFPs are slow to respond to a speed control signal. Because of this, operator action is required to take the MFP speed control to manual and increase pump speed if an attempt is made to provide the feedwater flow required to compensate for the loss of a main feedwater pump.
An Asea Brown Bovari (ABB) simulation ("Final Report Palisades Nuclear Plant; Feedwater Control System Evaluation, July 1992") recommended the feedwater control system be fine tuned to make the system responsive enough to handle this type of transient with the feedwater system left in automatic. This slow main feedwater pump response results in the MFP speed staying high on a Reactor trip. The high MFP speed, coupled with the automatic shift of the feed regulator valves to manual, assures that ample feedwater is maintained for core cooling; it also, however, requires that a control room operator manually trip both MFPs on a reactor trip to prevent overcooling the primary coolant system.
 
NRC Form 388A 19-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31/86 FACILITY NAME 111                  DOCKET NUMBER 121                    LER NUMBER 131                        PAGE 141 SEQUENTIAi.        REVISION YEAR      NUMBER            NUMBER Palisades Plant 0 I 6 I0 I0 I0 I2 I 5 I 6 9   I5 - 0   I0 I3      -   0   I0    0 I4    OF   0   I4
: 2.       The "B" main feedwater pump governor control maximum speed is so close to the overspeed trip setpoint that it allows an overspeed trip on a ioss of load condition.
Correctjve Actions Corrective Actions are as follows:
: 1.       Determine the root cause for the failure mode of the "A" MFP lays haft lockwasher locking tab. Make necessary changes to both MFPs.
: 2.       Evaluate the feedwater control system for this event and the changes suggested by the 1992 ABB report. Review the effect of any changes on the response of the feedwater system for other events. Make any required changes to both feedwater control systems.
: 3.       Evaluate the MFP governor control setpoint of 5250 RPM and its relationship to the overspeed trip setpoint.
Previous Events Licensee Event Reports since 1990 were reviewed. Four reactor trips resulted from a loss of one of the main feedwater pumps. The failure mechanisms and root causes, however, do not correspond with those identified for this event.
Additional Information The lockwasher failure is similar to an event described by D-PAL-91-122 when K-7A was ready to return to service on July 20, 1991, but was shut down because of noise. The layshaft locknut was found loose.}}

Latest revision as of 14:19, 23 February 2020

LER 95-003-00:on 950522,main FW Pump Transient Resulted in Rt.Evaluated MFP Governor Control Setpoint of 5250 RPM & Relationship to Overspeed Trip Setpoint
ML18064A818
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/21/1995
From: Hobe M
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
Shared Package
ML18064A817 List:
References
LER-95-003-01, LER-95-3-1, NUDOCS 9506290196
Download: ML18064A818 (4)


Text

NRC Form 388 U.S. NUCLEAR REGULATORY COMMISSION (9*831 APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI FACILITY NAME (1) DOCKET NUMBER (21 PAGE 131 Palisades Plant 016101010121616 1 I OF 0 14 nnE 141 LICENSEE EVENT REPORT 95-003- MAIN FEEDWATER PUMP TRANSIENT RESULTING IN A REACTOR TRIP EVENT DATE 161 LEA NUMBER 181 REPORT DATE (81

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- - , YES Uf ye-. e<<np#tti EXPECTED SUBMISSION DA TEI ABSTRACT Wtn1t ID 1400 ~ I.*., ling#-.,,.c* trP<1writtM llnnl 1181 DATE (161 I I I On May 22, 1995, at 1110, with the plant operating at 46% power, the reactor was manually tripped. At the time of the trip, K-7 A and K-78 main feedwater pump turbines had both tripped, resulting in a loss of all main feedwater. The vibration on K- 7 A had increased earlier and System Engineering was brought in to investigate the problem. A decision was made to reduce reactor power and take K-7 A off line. While preparing to reduce reactor power, K~7A tripped. Later, the trip was attributed to a failure in the layshaft assembly which uncoupled the governor controls from the main turbine shaft and resulted in the turbine tripping on overspeed. The control room operator took manual control of K-78 and ramped the turbine up to full speed, as required by Off Normal Procedure ONP-3, "Loss of Main Feedwater." Later when "8" Steam Generator (E-508) level was recovering too quickly, the control room operator took manual control of the feedwater regulating valve (CV~0703) to manually throttle the valve. The "8" Steam Generator level reached the high level override setpoint which immediately closed the feedwater regulating valve CV-0703. Rapidly closing the feed.water regulating valve CV-0703 caused an immediate drop in load and K-78 turbine speed increased above the overspeed trip, resulting in the turbine tripping on overs peed. After verifying that K-78 had tripped, the control room operator manually tripped the reactor.

The cause of this event was the failure of the locknut on the lays haft assembly of K- 7 A, allowing the layshaft drive gear to walk down the shaft.

9506290196 950621 PDR ADOCK 05000255 S PDR

NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION 19-831 APPROVED OMB NO. 3160-0104 EXPIRES: 8/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant 0 I6 I0 I0 I0 I2 I6 I6 9 I5 - 0 I0 I3 - 0 I0 0 I2 OF 0 I 4 Event Description On the morning of May 22, 1995, the recorder for K-7A main feedwater pump turbine [SJ;P]

shaft displacement had a small movement and the pen for recording the vibration between the turbine and governor started marking a wider band than normal (Worthington Pump Driver; Turbine Frame ITV2X3). At 0700, the control room operator noticed the vibration increasing on the recorder and notified the Secondary Auxiliary Operator and the Shift Supervisor. The vibration went from 1.6 mils to 2.0 mils (the alert indication setpoint for vibration is 2.5 mils).

The pump and turbine were checked along with other local instruments. A rise in the noise level was the only abnormality noticed by the Shift Supervisor and Auxiliary Operator.

The Shift Supervisor contacted the System Engineer for further evaluation. After a review of K-7A, the System Engineer contacted the Plant Performance Engineer to take vibration readings and an oil sample. Chemistry checked the oil sample for water and small suspended solids, but both tests were negative. An oil sample was sent off site for testing and later found to be normal.

The Control Operators reviewed the Off Normal Procedure (ONP-3) for "Loss of Main Feedwater" in case of a Main Feedwater Pump (MFP) trip. A meeting was held with upper management to review the course of action. At around 1100 the decision was made to reduce reactor power and remove K-7 A from service so it could be checked out further. Just prior to starting the power reduction K-7 A tripped.

After K- 7 A tripped, the control room operator verified that "A" Main Feedwater Pump tripped, took manual control of K-78, and ramped the turbine up to full speed, as required by ONP-3. The "B" Main Feedwater Pump (MFP) was at maximum speed 24 seconds after A-MFP tripped.

Then, at 36 seconds, the same control room operator took manual control of the turbine and reduced load while the other control room operator continued to manually drive control rods in to reduce reactor power. In 58 seconds, the feedwater flow was equal to steam flow for both steam generators. (Per ONP-3, Section 4.1, subsequent actions, "Stop the power reduction when feed flow indication becomes slightly greater than steam flow indications for both S/Gs. ")

At 1 minute and 10 seconds the down power was momentarily halted at approximately 60%

power.

Because the "B" Steam Generator (S/Gl level was not recovering, the Control Room Supervisor directed an additional load decrease. At 1 minute 48 seconds, the control room operators started lowering reactor power and turbine load. At 2 minutes 48 seconds, the load decrease was stopped at approximately 46% power.

'a' NRC Form 3811A U.S. NUCLEAR REGULATORY COMMISSION (9-83) APPROVED OMB NO. 3160-0104 EXPIRES: B/31 /86 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAL REVISION YEAR NUMBER NUMBER Palisades Plant 0 I5 I0 I0 I0 I2 I5 I5 9 I5 - 0 I0 I3 - 0 I0 0 I3 OF 0 I 4 The "B" S/G level began to rise rapidly and at 3 minutes 16 seconds the control room operator took manual control of "B" S/G feedwater regulating valve, CV-0703. The valve was manually closed to 20% at 3 minutes 52 seconds and not manually closed any further after that. At 4 minutes 28 seconds the "B" S/G level exceeded 84. 7% and the high steam generator level override circuit actuated to close CV-0703.

When CV-0703 rapidly closed from 20%, the result was a large drop in load for K-78. This immediate drop in load was enough to allow the speed of K-7B to increase above the overs peed trip. The "B" MFP tripped 4 minutes 40 seconds after "A" MFP tripped.

The control room operator then verified that "B" MFP had tripped and at 5 minutes 12 seconds the Reactor was manually tripped. The immediate actions of Emergency Operating Procedure (EOP-1 ), "Standard Post Trip Actions," and EOP-2, "Reactor Trip Recovery" were performed and verbal verification was completed. All EOP procedure steps were completed satisfactorily.

Plant and operator actions taken in response to MFP trips were in accordance with procedures, with no safety significant deviations or abnormalities. Although not required by the event, both trains of engineered safeguards equipment were operable and available for use at all times. This event did not have an adverse impact on the operational safety of the plant or upon the safety of plant personnel or the general public.

Cause of the Event The proximate cause of the event is the "A" main feed water pump lays haft locknut lockwasher tab failure which allowed the layshaft locknut and driven gear to walk off the shaft.

Contributing causes include:

1. The feedwater pump gain control setting is set as low as possible. As a result, the MFPs are slow to respond to a speed control signal. Because of this, operator action is required to take the MFP speed control to manual and increase pump speed if an attempt is made to provide the feedwater flow required to compensate for the loss of a main feedwater pump.

An Asea Brown Bovari (ABB) simulation ("Final Report Palisades Nuclear Plant; Feedwater Control System Evaluation, July 1992") recommended the feedwater control system be fine tuned to make the system responsive enough to handle this type of transient with the feedwater system left in automatic. This slow main feedwater pump response results in the MFP speed staying high on a Reactor trip. The high MFP speed, coupled with the automatic shift of the feed regulator valves to manual, assures that ample feedwater is maintained for core cooling; it also, however, requires that a control room operator manually trip both MFPs on a reactor trip to prevent overcooling the primary coolant system.

NRC Form 388A 19-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 EXPIRES: 8/31/86 FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAi. REVISION YEAR NUMBER NUMBER Palisades Plant 0 I 6 I0 I0 I0 I2 I 5 I 6 9 I5 - 0 I0 I3 - 0 I0 0 I4 OF 0 I4

2. The "B" main feedwater pump governor control maximum speed is so close to the overspeed trip setpoint that it allows an overspeed trip on a ioss of load condition.

Correctjve Actions Corrective Actions are as follows:

1. Determine the root cause for the failure mode of the "A" MFP lays haft lockwasher locking tab. Make necessary changes to both MFPs.
2. Evaluate the feedwater control system for this event and the changes suggested by the 1992 ABB report. Review the effect of any changes on the response of the feedwater system for other events. Make any required changes to both feedwater control systems.
3. Evaluate the MFP governor control setpoint of 5250 RPM and its relationship to the overspeed trip setpoint.

Previous Events Licensee Event Reports since 1990 were reviewed. Four reactor trips resulted from a loss of one of the main feedwater pumps. The failure mechanisms and root causes, however, do not correspond with those identified for this event.

Additional Information The lockwasher failure is similar to an event described by D-PAL-91-122 when K-7A was ready to return to service on July 20, 1991, but was shut down because of noise. The layshaft locknut was found loose.