ML17241A404: Difference between revisions

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: 3. Coil traces were obtained during rod movement and verified to be of proper waveform, timing, and that all phases were operating satisfactorily.
: 3. Coil traces were obtained during rod movement and verified to be of proper waveform, timing, and that all phases were operating satisfactorily.
: 4. The auxiliary contacts for MV-08-10 were cleaned under WO 99010433.
: 4. The auxiliary contacts for MV-08-10 were cleaned under WO 99010433.
: 5. The pressurizer heater control circuitry was repaired under WO 99010873 Post maintenance test requirements aze being developed for CEA sub group power
: 5. The pressurizer heater control circuitry was repaired under WO 99010873 Post maintenance test requirements aze being developed for CEA sub group power switches and minimum checks to be performed prior to removing a CEA subgroup from the hold bus.
                                                                                                                '.
switches and minimum checks to be performed prior to removing a CEA subgroup from the hold bus.
: 7. Guidelines are being developed for the repair of CEDMCS power switch modules including proper removal and installation.
: 7. Guidelines are being developed for the repair of CEDMCS power switch modules including proper removal and installation.
Additional Information Failed  Com    onents    Identified Component:                    Power Switch Assembly Manufacturer:                Combustion Engineering Model:                        Part No. 35200 Similar Events None NRO FOAM 3BBA (B.1998)}}
Additional Information Failed  Com    onents    Identified Component:                    Power Switch Assembly Manufacturer:                Combustion Engineering Model:                        Part No. 35200 Similar Events None NRO FOAM 3BBA (B.1998)}}

Latest revision as of 11:59, 4 February 2020

LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr
ML17241A404
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 07/06/1999
From: Frehafer K, Stall J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-99-149, LER-99-005, LER-99-5, NUDOCS 9907120142
Download: ML17241A404 (8)


Text

~ CATEGORY 10 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9907120142 DOC.DATE: 99/07/06 NOTARIZED: NO DOCKET FACIL:50-389 St. Lucie Plant, Unit 2, Florida Power &, Light Co. 05000389 AUTH. NAME AUTHOR AFFILIATION FREHAFER,K.W. Florida Power &. Light Co.

STALL,J.A. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 99-005-00:on 990604,CEA drop resulted in manual reactor trip. Caused by procedural inadequacies. Procedure changes are planned to correct lack of procedural guidance for CEA sub- A group power switch replacement.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR L ENCL TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

I SIZE:

NOTES:

RECIPIENT COPIES RECIPIENT COPIES 0 ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL LPD2-2 PD 1 1 GLEAVES,W 1 1 INTERNAL: ACRS 1 1 FILE CENTE~R 1 1 NRR/DZPM/IOLB 1 1 NRR'/DRIP/REXB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/ERAB 1 1 RES/DRAA/OERAB 1 1 RGN2 PILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LMZTCO MARSHALL 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 D N

NOTE TO ALL "RiDS" RFCIPiEN;S:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGAN:ZATiON REMOVED FROM DiSTRiBUTiON LISTS OR REDUCE THE NUMBER OF COPiES RECE:VE ". YOU OFL OUR CRGANiZAT ON, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2063 PULL TEXT CONVERSION REQUIRED TO.AL NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16

Florida Power & Light Company, 6351 S. Ocean Drive, Jensen Beach, FL 34967 July 6, 1999 L-99-149 10 CFR 5 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Unit 2 Docket No. 50-389 Reportable Event: 1999-005-00 Date of Event: June 4, 1999 CEA Drops Result in Manual Reactor Tri The attached Licensee Event Report 1999-005 is being submitted pursuant to the requirements of 10 CFR $ 50.73 to provide notification of the subject event.

Very truly yours, J. A. Stall Vice President St. Lucie Nuclear Plant JAS/EJW/KWF Attachment cc: Regional Administrator, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Nuclear Plant

'ir907i20i42 99070605000389 PDR ADOCtr 8 PDR an FPL Group company

,f NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150.0104 EXPIRES 06/30/2001 (6-1996)

Estimated burden per response to comply with this mandatory hfonnsgon collection request: 50 hrs. Reported lessons learned sre incorporated into lhe gcenstng process and fed back lo industry. Forward comments regsngng LICENSEE EVENT REPORT (LER) burden esbmste lo the Records Management Branch (TW F33), US. Rudear Reguhtory Commission, Washington, 1)C 205554001, and lo lhe Paperwork Rer)octan Project (315041M(, Office of Management snd Budget, (See reverse for required number of Washington, DC 20503. If an Informathn collecgon does not display a currently valid OMB control number, the NRC may not conduct or sponsor, digits/characters for each block) and a person hr not required lo respond lo, the Infonnsthn collection.

FACIUTY NAME (1) DOCKET NUMBER (2) PAGE (3)

St. Lucie Unit 2 05000389 Page 1 of 4 TITLE (4)

CEA Drops Result in Manual Reactor Trip EVENT DATE (5) LER NUMBER 6) REPORT DATE 7 OTHER FACILITIES INVOLVED (BI SEQUENTIAL REVISION FACIUTy NAME DOCKET NUMBER DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER FACiUTY NAME DOCKET NUMBER 06 04 1999 1999 005 00 07 06 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)

MODE (9) 20.2201(b) 20.2203(e) (2)(v) 50.73(a) (2)(i) 50.73(s) (2)(viii)

POWER 20.2203(e)(1) 20.2203(s) (3)(i) 50.73 (e) (2) (ii) 50.73(e) (2) (x)

LEVEL (10) 049 20.2203(e)(2)(i) 20.2203(a)(3) (ii) 50.73(e)(2)(ui) 73.71

20. 2203 (e) (2) (ii) 20.2203(s)(4) 50.73(e)(2)(iv) OTHER
20. 2203(a) (2) (iii) 50.36(c)(1) 50.73 (s) (2) (v) Specify in Abstract below or
20. 2203(s) (2) (iv) 50.36(c)(2) 50.73(e)(2) (vii) ln NAC Form 366A LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMSER tiricrvtro Aree Codat Kenneth W. Frehafer, Licensing Engineer (561) 467 - 7748 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 CAUSE SYSTEM COMPONENT MANUFACTURER AEPOATABLE REPORTABLE TO EPIX CAUSE SYSTEM COMPONENT MANUFACTURER To EPIX C490 YES D

SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY EXPECTED YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X NO DATE (15)

ABSTRACT /Limit to 1400 speces, l e., approximately 15 single-spaced typewritten lines/ (16)

On June 4, 1999, St. Lucie Unit 2 was in Mode 1 at approximately 49 percent reactor power. An event response team was in the process of trouble shooting recent control element assembly anomalies. Unit 2 was held in reduced power pending the event response team trouble shooting results.

At 0313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br />, four sub group 21 control element assemblies fully inserted into the core during replacement of the sub group 21 power supply. A Utility licensed operator, the nuclear plant supervisor, immediately directed a manual reactor trip. The plant was stabilized in Mode 3 for repairs. Repairs were implemented, and plant restart and power ascension commenced on June 11, 1999.

The control element assembly drop event was caused by procedural inadequacies that did not require verification of the proper seating of a power switch. This resulted in loss of power to the control element assemblies when their sub group was transferred off the hold bus.

Loss of power to the sub group 21 control element assemblies was corrected by reseating the sub group 21 power switch. Procedure changes are planned to correct the lack of procedural guidance for CEA sub group power switch replacement. The event response team conducted other corrective actions related to the original control element assembly anomalies.

NAC F0AM 366 (6-1999)

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-19991 LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER I2) LER NUMBER IS) PAGE (3)

SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 2 05000389 Page 2 of 4 1999 - 005 00 TEXT (Ifmore speceis required, use edditionel copies of NRC Form 366A/ (17)

Description of the Event On June 4, 1999, St. Lucie Unit 2 was in Mode 1 at approximately 49 percent reactor power. An event response team (ERT) was in the process of investigating recent control element assembly (CEA) [EIIS:AA] events (a CEA drop two days earlier and CEAs spontaneously transferring to their lower grippers). Unit 2 was being held in reduced power pending the ERT trouble shooting results.

The Unit 2 control element drive mechani.sm control system (CEDMCS) is designed to control the movement of the 91 control rod drive mechanisms. Each control rod mechanism has 5 coils, which engage various grippers within the CEDM motor to control CEA movement. Under normal conditions, the upper gripper maintains the CEA in its last position. Should power be removed from this gripper, and the other grippers not engage to provide movement, the CEA will drop into the core. Power for the gripper coils is provided by motor generator (MG) sets through the reactor trip switchgear The CEDM power source is three phase 240V AC and i.s desi.gned as a floating system to

~

tolerate single ground conditions.

Each CEA sub group utilizes a power switch that pxovides three-phase power for up to four CEAs. The power switch is controlled by logic timing boards and an automatic CEA timing module (ACTM) which decides which coils to fire during movement or holding of each CEA. The ACTM receives information as to the energy provided to the coil through a Hall effect transducer around each coil power cable. Should the ACTM see the possibility of a rod drop it will automatically apply additional power or transfer the CEA to the lower gripper to prevent the rod from dropping. This action is annunciated in the control room.

During trouble shooting a decision was made to install a spare power switch

[EIIS:AA:JX] in sub group 21, which required the affected CEAs to be transferred to the maintenance hold bus. After the power switch was replaced,, the sub group 21 CEAs were removed from the hold bus and transferred to sub group 21 while coil traces were obtained. It was observed that with the sub group 21 CEAs on the hold bus, the visicorder traces improved and with the CEAs powered by the sub group the traces were still degraded. The CEAs were placed back on the maintenance hold bus. After further testing and replacement of a logic board, sub group .21 was removed from the hold bus and transferred to the sub group. At 0313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br />, all four sub group 21 CEAs fully inserted into the core upon deenergization of the maintenance hold bus.

The nuclear plant supervisor (NPS) immediately directed a manual reactor trip and entry into Emergency Operating Procedure (EOP) -1, "Standard Post Trip Acti.ons". All safety functions were verified as being maintained and EOP-2, "Reactor Trip Recovery", was entered at 0323 hours0.00374 days <br />0.0897 hours <br />5.340608e-4 weeks <br />1.229015e-4 months <br />. The plant was stabilized in Mode 3. The trip was determined to be uncomplicated with the exception the following issues:

During the performance of EOP-1, the 2C main steam reheater (MSR) temperature control valve (TCV) block valve [EIIS:SB:V], MV-08-10, would not close. In accordance with contingency actions, the MSR TCVs were closed. MV-08-10 was subsequently de-energized and manually closed.

~ The "A" side pressurizer heaters [EIIS:AB:PZR1EHTR] were de-energized due to a lo-lo level signal from the pressurizer level "X" channel. However, the signal was not reset when pressurizer level was raised above the setpoint. A 72-hour action NRC FOIIM SBBA (9-1999)

NRC FORM 366A U.S. NUCLEAR REGUIATORY COMMISSION (6.1998)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION DOCKET LER NUMBER (6) PAGE (3)

FACILITYNAME (1) NUMBER (2)

SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 2 05000389 005 Page 3 of 4 1999 00 TEXT Iifmore spacois required, use addidonal copies of NRC Perm 366AI (17)

Description of the Event (cont'd) statement was entered in accordance with Technical Specification 3.4.3 at 0313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br /> on June 4, 1999, due to having less than the required number of pressurizer heaters being capable of being powered from a Class 1E electric bus.

Cause of the Event CEA Issues Sub group 21 CEAs spontaneously transferring to their lower grippers was caused by noise generated by the failure of the sub group 21 power switch. Disassembly of the power switch indicated a short, which most, likely developed over time between a "C" phase silicon controlled rectifier (SCR) (Q125) anode and ground. Measurements of the power switch "C" phase to ground indicate a shorted condition and detailed inspection of the SCR's mylar insulating washer show a visible breakdown of the insulation and an arc path to ground. Because this condition continued for some time, inducing high noise levels into the system, various ACTM cards interpreted this abnormal condition as unfavorable upper gripper voltage. As designed, the ACTM cards transferred the CEAs to their lower grippers to prevent rod drops. Upon replacement of the sub group 21 power switch and the failed fuse associated with phase "C" the noise was no longer seen on the sub group 21 CEAs.

The June 4, 1999 rod drop event was caused by a lack of procedural guidance that should have verified that the replacement CEA sub group 21 power switch was properly seated during trouble shooting activities. The improper seating of the power switch was not apparent because twice before the sub group 21 CEAs were successfully transferred from the hold bus to the sub group power switch and back. Theze were no indications that the power switch was not properly seated, and that intermittent power was being delivered to the CEAs. Eventually, the latent intermittent electrical power led to the full insertion of the sup group 21 CEAs when the hold bus was deenergized.

Post-Tri Issues The failure of the 2C MSR TCV block valve, MV-08-10, to close was caused by dirty auxiliary contacts in the MCC control circuit.

The failure of the "A" side pressurizer heaters to reset on rising pressurizer level was caused by a faulty crimped connection in Foxboro module LC-1110X.

Analysis of the Event This event is reportable under 10 CFR 50.73 (a)(2)(iv) as "any event or condition that resulted in a manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)."

Analysis of Safety Significance The CEDM control system does not provi.de any safety relat'ed functions and the identified problems would not have prevented the affected rods from dropping into the core to shut down the reactor. Additionally, the drop of a CEA subgroup is an analyzed event. Therefore, the condit'ions described above did not present an operability concern. Additionally, during CEA trouble shooting activiti.es, a pre-evolution tailboard was conducted with Operations to install a spare power'switch in NRC FORM 366A (6.1998)

~ NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)

LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITYNAME ('I) DOCKET NUMBER 2) LER NUMBER (6) PAGE (3)

SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 2 05000389 Page 4 of 4 1999 005 00 TEXT (Ifmore speceis required, use eddi(ionel copies of NRC Form 366AJ (17)

Analysis of Safety Significance (cont')

sub group 21. When all four sub group 21 CEAs fully inserted i,nto the core, Operations confirmed the rod drop indication and manually tripped the reactor in accordance with the pre-evoluti.on tailboard.

Based on the above, this event had no impact on the health and safety of the public.

Corrective Actions

l. All CEDMCS sub group power switches were verified to have proper electrical and mechanical contact under work order (WO) 99010204.
2. The system (CEA coils, CEDM power distribution and power switch components for each of the 24 sub groups) was verified to be free of grounds by a megger of 250V or greater to ground.
3. Coil traces were obtained during rod movement and verified to be of proper waveform, timing, and that all phases were operating satisfactorily.
4. The auxiliary contacts for MV-08-10 were cleaned under WO 99010433.
5. The pressurizer heater control circuitry was repaired under WO 99010873 Post maintenance test requirements aze being developed for CEA sub group power switches and minimum checks to be performed prior to removing a CEA subgroup from the hold bus.
7. Guidelines are being developed for the repair of CEDMCS power switch modules including proper removal and installation.

Additional Information Failed Com onents Identified Component: Power Switch Assembly Manufacturer: Combustion Engineering Model: Part No. 35200 Similar Events None NRO FOAM 3BBA (B.1998)