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| issue date = 11/16/1979
| issue date = 11/16/1979
| title = LER 79-021/03L-0:on 791018,Tech Spec Requirement 4.8.5 Re Stroking Crossover Valves Omitted from Procedure for Testing Standby Auxiliary Feedwater Pumps.Caused by Personnel Error. Test Personnel Briefed & Performed Tests
| title = LER 79-021/03L-0:on 791018,Tech Spec Requirement 4.8.5 Re Stroking Crossover Valves Omitted from Procedure for Testing Standby Auxiliary Feedwater Pumps.Caused by Personnel Error. Test Personnel Briefed & Performed Tests
| author name = GENT D R
| author name = Gent D
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRCF~R,36617-779'8U.S.NUCLEARREGULATORY COMMISSION 79-021/03L-0 CENSEEEVENTREPORT(CAR1240)CONTROLBLOCK:Q(PLEASEPRINTORTYPEALLREQUIREDINFORMATION1 I6NYEEG1Q200-00000-0OQ34111lps~ps9LICENSEECODE1415LICENSENUMBER26LICENSETYPE3057CAT58CON'T~0178~LQB05000244Q7101879B111679Qg6061DOCKETNUMBER6869EVENTDATE7475RFPORTDATE80EVENTDESCRIPTION ANDPROBABLECONSEQUENCES
{{#Wiki_filter:NRC F~R,366                                                                                                                        U. S. NUCLEAR REGULATORY COMMISSION 17-779'                                                                                79-021/03L-0 CENSEE EVENT REPORT (CAR 1240)
+10DuringaperiodicreviewofPlantTec&nical Specifications forcoverageoftestrequire-mentsitwasdiscovered thatTech.Spec.requirement 4~8~5onstrokingcrossover valves,issued8/24/79,wasnotincludedintheprocedure fortestingthestandbyauxiliary feedwater pumps(SBAFWP)~Therefore thestrokingofthesevalves,required6duringSeptember testing,wasnotaccomplished atthattime.Nevertheless, theSBAFWPmaindischarge valveswereoperable.
CONTROL BLOCK:
Also,periodictestingdetermined that~008Bthetota1auxiliaryfeedwatersystemwasoperab1eatthattime80789SYSTEMCAUSECAUSECOMP.VALVECODECODESUBCODECOMPONENT CODESUBCODESUBCODE~CHQ71~XQ12~ZQ73ZZZZZZQ4~p>>gfQT'8910111213181920SEOUENTIALOCCURRENCE REPORTREVISIONLER/ROEVENTYEARREPORTNO.CODETYPENO.Q17REPQRT~y9~~021~W~09~L-~042122232426272829303132ACTIONFUTUREEFFECTSHUTDOWNATTACHMENT NPRDPPRIMECOMP.COMPONENT TAKENACTIONONPLANTMETHODHOURSQ22SUBMITI'ED FORMSUB.SUPPLIERMANUFACTURER
I                                6 Q                 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 8    9 N Y E LICENSEE CODE E      G      1Q20 14      15 0  -     0    0  0      0 LICENSE NUMBER 0    0        OQ34 26 1
~GQTR~NQ>>
LICENSE 1    1 TYPE30 lps~ps 57 CAT 58 CON'T
~ZQER~ZQ27OOOONQ23~NQ24~ZQ25Z999Q253334353637404142434447CAUSEDESCRIPTION ANDCORRECTIVE ACTIONSQ270TheSBAFWP'swereperiodically testedinrecirculation modesincethetimeofaccept-ance.DuetothetimedelayinissuanceofTech.Specs.fortesting,atestprocedure wasestablished.
~01                                ~LQB            0    5      0      0  0    2    4    4    Q7      1    0    1    8  7      9    B      1    1    1  6    7    9    Qg 7          8                      60            61            DOCKET NUMBER              68      69      EVENT DATE              74      75        RFPORT DATE          80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES +10 During a periodic review of Plant Tec&nical Specifications for coverage of test require-ments        it was        discovered that Tech. Spec. requirement                                   4 ~ 8 ~ 5 on          stroking crossover valves, issued 8/24/79, was not included in the procedure for testing the standby auxiliary feedwater pumps                             (SBAFWP)       ~   Therefore the stroking of these valves, required 6          during September testing, was not accomplished at that time. Nevertheless, the SBAFWP main discharge                              valves were operable.                   Also, periodic testing determined that
UponissuanceoftheTech.Spec.theprocedure usedpriortoissu-ancewasupdatedtotestwithflowtothesteamgenerators, butthenewcrossover valvetestingrequirement hadbeenoverlooked.
~7 0  8B 8 9 t h e t o ta 1 SYSTEM CODE f
Theprocedure wascorrected andtestpersonnel werebriefedonthenewrequirement.
a u x ilia ry e e d wa t e r s y s t e m wa s o p e ra b 1 e a t th a t CAUSE CODE CAUSE SUBCODE                COMPONENT CODE t im e COMP.
Testpersonnel havesinceperformed thereuiredtests.CZ3ACTIVITYCONTENTRELEASEDOFRELEASEAMOUNTOFACTIVITY5~zQ33~ZQ34NA789IO1144PERSONNEL EXPOSURES NUMBERTYPEDESCRIPTION
SUBCODE VALVE SUBCODE 80 8
~000Q~ZQRsNA789111213PERSONNEL INJURIESNUMBERDESCRIPTION 41~ls~000Q457891112LOSSOFORDAMAGETOFACILITY43TYPEDESCRIPTION
                                      ~CH 9          10 Q71      ~XQ12 11
~19ZQ42NA78910PUBLICITY ISSUEDDESCRIPTION Q~20L~JQ44NA7891045NAMEOFPREPARERDennisR.Gent789FACILITY~30METHODOFSTATUS99POWEROTHERSTATUS~DISCOVERY 75~EEQ2R~110000Q2RNA~ZZQ3789101213444546DISCOVERY DESCRIPTION Q32NALOCATIONOFRELEASEQ36NA8080808080NRCUSEONLY60686980EsPHDNE,716/546-2700,ext.291-216 0EV}}
                                                                              ~ZQ73 12            13 Z Z        Z    Z    Z    Z Q4 18
                                                                                                                                          ~p>> gf 19              20 QT' SEOUEN TIAL                        OCCURRENCE            REPORT                      REVISION 4
Q17 LER/RO REPQRT ACTION FUTURE EVENT YEAR
                                        ~y9 21        22 EFFECT
                                                              ~
23 SHUTDOWN
                                                                              ~02 24 REPORT NO.
1 26
                                                                                                      ~W 27
                                                                                                                    ~09 28 ATTACHMENT CODE 29 NPRDP TYPE
                                                                                                                                            ~L 30 PRIME COMP.
31
                                                                                                                                                                        ~0 NO.
32 COMPONENT TAKEN ACTION                    ON PLANT            METHOD                  HOURS Q22          SUBMITI'ED       FORM SUB.           SUPPLIER          MANUFACTURER
                  ~GQTR~NQ>>                       ~ZQER             ~ZQ27            O    O    O    O          N  Q23      ~NQ24               ~ZQ25            Z    9    9 9  Q25 33          34                  35                36            37                    40    41              42                  43            44              47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 0        The SBAFWP's were periodically tested in                                          recirculation mode since the time of accept-ance.           Due to the time delay in issuance                                of Tech. Specs. for testing,                             a test procedure was established. Upon issuance of the Tech. Spec. the procedure used prior to issu-ance was updated to test with flow to the steam generators, but the new crossover valve testing requirement had been overlooked. The procedure was corrected and test personnel were briefed on the new requirement. Test personnel have since performed the re uired tests.
7        8    9                                                                                                                                                                    80 FACILITY STATUS
                                ~1100 99  POWER 0Q2R OTHER STATUS NA
                                                                                    ~
                                                                                    ~30      METHOD OF DISCOVERY                              DISCOVERY DESCRIPTION Q32 CZ3 7  5 8
                ~EEQ2R 9                10                12      13                            44
                                                                                                  ~Z 45 ZQ3    7 46 NA 80 ACTIVITY        CONTENT RELEASED OF RELEASE                          AMOUNT OF ACTIVITY                                                        LOCATION OF RELEASE Q36 5      ~z      Q33    ~ZQ34                                NA                                                          NA 7        8    9                IO            11                                        44            45                                                                          80 PERSONNEL EXPOSURES NUMBER                TYPE        DESCRIPTION 8
                ~00            0    Q~ZQRs                          NA 7              9                11        12          13                                                                                                                          80 PERSONNEL INJURIES NUMBER                DESCRIPTION 41
~ls ~00                        0 Q45 7          8    9                11        12                                                                                                                                      80 LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION 43
~19              Z    Q42                                          NA 7          8    9            10                                                                                                                                                      60 PUBLICITY
~20 ISSUED L~JQ44 DESCRIPTION       Q                    NA NRC USE ONLY 7          8    9            10                                                                                                                    68    69                          80  Es NAME OF PREPARER Dennis R. Gent                                          PHDNE,7 1        6/5 46 -2700, ext . 2 9 1 -2 1 6
 
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Latest revision as of 10:04, 4 February 2020

LER 79-021/03L-0:on 791018,Tech Spec Requirement 4.8.5 Re Stroking Crossover Valves Omitted from Procedure for Testing Standby Auxiliary Feedwater Pumps.Caused by Personnel Error. Test Personnel Briefed & Performed Tests
ML17261A148
Person / Time
Site: Ginna Constellation icon.png
Issue date: 11/16/1979
From: Gent D
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17249A275 List:
References
LER-79-021-03L, LER-79-21-3L, NUDOCS 7911200407
Download: ML17261A148 (2)


Text

NRC F~R,366 U. S. NUCLEAR REGULATORY COMMISSION 17-779' 79-021/03L-0 CENSEE EVENT REPORT (CAR 1240)

CONTROL BLOCK:

I 6 Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 8 9 N Y E LICENSEE CODE E G 1Q20 14 15 0 - 0 0 0 0 LICENSE NUMBER 0 0 OQ34 26 1

LICENSE 1 1 TYPE30 lps~ps 57 CAT 58 CON'T

~01 ~LQB 0 5 0 0 0 2 4 4 Q7 1 0 1 8 7 9 B 1 1 1 6 7 9 Qg 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 RFPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES +10 During a periodic review of Plant Tec&nical Specifications for coverage of test require-ments it was discovered that Tech. Spec. requirement 4 ~ 8 ~ 5 on stroking crossover valves, issued 8/24/79, was not included in the procedure for testing the standby auxiliary feedwater pumps (SBAFWP) ~ Therefore the stroking of these valves, required 6 during September testing, was not accomplished at that time. Nevertheless, the SBAFWP main discharge valves were operable. Also, periodic testing determined that

~7 0 8B 8 9 t h e t o ta 1 SYSTEM CODE f

a u x ilia ry e e d wa t e r s y s t e m wa s o p e ra b 1 e a t th a t CAUSE CODE CAUSE SUBCODE COMPONENT CODE t im e COMP.

SUBCODE VALVE SUBCODE 80 8

~CH 9 10 Q71 ~XQ12 11

~ZQ73 12 13 Z Z Z Z Z Z Q4 18

~p>> gf 19 20 QT' SEOUEN TIAL OCCURRENCE REPORT REVISION 4

Q17 LER/RO REPQRT ACTION FUTURE EVENT YEAR

~y9 21 22 EFFECT

~

23 SHUTDOWN

~02 24 REPORT NO.

1 26

~W 27

~09 28 ATTACHMENT CODE 29 NPRDP TYPE

~L 30 PRIME COMP.

31

~0 NO.

32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITI'ED FORM SUB. SUPPLIER MANUFACTURER

~GQTR~NQ>> ~ZQER ~ZQ27 O O O O N Q23 ~NQ24 ~ZQ25 Z 9 9 9 Q25 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 0 The SBAFWP's were periodically tested in recirculation mode since the time of accept-ance. Due to the time delay in issuance of Tech. Specs. for testing, a test procedure was established. Upon issuance of the Tech. Spec. the procedure used prior to issu-ance was updated to test with flow to the steam generators, but the new crossover valve testing requirement had been overlooked. The procedure was corrected and test personnel were briefed on the new requirement. Test personnel have since performed the re uired tests.

7 8 9 80 FACILITY STATUS

~1100 99 POWER 0Q2R OTHER STATUS NA

~

~30 METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 CZ3 7 5 8

~EEQ2R 9 10 12 13 44

~Z 45 ZQ3 7 46 NA 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Q36 5 ~z Q33 ~ZQ34 NA NA 7 8 9 IO 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 8

~00 0 Q~ZQRs NA 7 9 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTION 41

~ls ~00 0 Q45 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION 43

~19 Z Q42 NA 7 8 9 10 60 PUBLICITY

~20 ISSUED L~JQ44 DESCRIPTION Q NA NRC USE ONLY 7 8 9 10 68 69 80 Es NAME OF PREPARER Dennis R. Gent PHDNE,7 1 6/5 46 -2700, ext . 2 9 1 -2 1 6

E 0 V