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| | issue date = 12/21/1979 | | | issue date = 12/21/1979 |
| | title = LER 79-023/01T-0:on 791207,during Inservice Insp of Pressurizer Relief nozzle-to-safe-end Weld,Liquid Penetrant Examination Showed Linear Indications.Possibly Caused by Original Fabrication Contamination or Chloride | | | title = LER 79-023/01T-0:on 791207,during Inservice Insp of Pressurizer Relief nozzle-to-safe-end Weld,Liquid Penetrant Examination Showed Linear Indications.Possibly Caused by Original Fabrication Contamination or Chloride |
| | author name = CURTIS A E | | | author name = Curtis A |
| | author affiliation = ROCHESTER GAS & ELECTRIC CORP. | | | author affiliation = ROCHESTER GAS & ELECTRIC CORP. |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:NRCFORM366I7.77+78CONTROLBLOCK:INYREG1Q2009LICENSEECODE141579-023/01T-0 U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORTQi{PLEASEPRINTORTYPEALLREQUIREDINFORMATION) 600000-00Q341111QE~QRLICENSENUMBER2526LICENSETYPE3057CAT58CON'T,~078~03~04~OS~06R"DRT~L~B0500024471207798122179QgSOURCE6061DOCKETNUMBEREVENTDATE7475REPORTDATE80EVENTDESCRIPTION ANDPROBABLECONSEQUENCES Q10Duringnormalinservice inspection ofpressurizer reliefnozzle-to-safe-end weld,liquidpenetrant exa'mshowedlinearindications l-l/8"and3/8"long.(T.S.6.9.2.a(3))UTdidnotshowany.FollowupX-rayexamshowednovolumetric indications. | | {{#Wiki_filter:NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION I7.77+ 79-023/01T-0 LICENSEE EVENT REPORT CONTROL BLOCK: Qi {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) |
| Furtherliquidpenetrant andreplication showedareaofattack6-7"by1/8"consisting ofafamilyoffinecrackssimilartointergranular typeattack.Allpressurizer headnozzle-to-safe-end weldareaswereexaminedwithUTandliquidpenetrant withno~0878otherrelevantindications noted.80~OgSYSTEMCAUSECAUSECOMP.VALVECODECODESUBCODECOMPONENT CODESUBCODESUBCODE~CBQ>>'~EQ12~DQTRP1PEXXQ14~BQEE~ZQs78910111213181920SEQUENTIAL OCCURRENCE REPORTREVISIONLERIROEVENTYEARREPORTNO.CODETYPENO.Q17REPQRT~79+~023QX~01QT-QO2122232426272829303132ACTIONFUTUREEFFECTSHUTDOWNATTACHMENT NPRDXPRIMECOMP.COMPONENT TAKENACTIONONPLANTMETHODHOURS~22SUBMITTED FORMSUB.SUPPLIERMANUFACTURER
| | I 6 N Y R E G 1 Q20 0 0 0 0 0 0 - 0 0Q34 1 1 1 1QE~QR 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T R"DRT ~L~B 0 5 0 0 0 2 4 4 7 1 2 0 7 7 9 8 1 2 2 1 7 9 |
| ~BQTR~XPTg~APER~AP270416~YP23~YQ24~NQ25Y17120QER3334353637404'I42434447CAUSEDESCRIPTION ANDCORRECTIVE ACTIONSQ270Possiblecauses:originalfabrication contamination orchlorideconcentration occurring duringoperation. | | ,~0 SOURCE Qg 7 8 60 61 DOCKET NUMBER EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During normal inservice inspection of pressurizer relief nozzle-to-safe-end weld, |
| Investigation includesexamining boatsamplewithscanningelectronmicroscope todetermine corrosive species,andinsulation leachinchemicalanalsis.34Clothcoverreplacedwithfiberglass. | | ~03 liquid penetrant exa'm showed linear indications l-l/8" and 3/8" long. (T.S. 6.9.2. |
| Reportofmetallurgical analysisresultstobesubmitted later.Pressurizer headnozzle-to-safe-end weldareastobereexamined in1980AI&O.789FACILITYSTATUS%POWERs~GQEs~000PER789101213ACTIVITYCONTENTRELEASEDOFRELEASEAMOUNTOFACTIVITYQ3s6~~Q33~+Q34NA7891011PERSONNEL EXPOSURES NUMBERTYPEDESCRIPTION Q3g~77~000Q37ZQssNA78911'1213PERSONNEL INJURIESLOCATIONOFRELEASEQB4445METHODOFOTHERSTATUSQDISCOVERY DISCOVERY DESCRIPTION Q32NA~BQ3IRoutineISI444546808080807891112LOSSOFORDAMAGETOFACILITYQ43TYPEDESCRIPTION g~ZQ42NA78910PUBLICITY ISSUEDDESCRIPTION
| | ~04 a(3)) UT did not show any. Followup X-ray exam showed no volumetric indications. |
| ~XQ44NewsreleasewasmadeDecemberll,1979.78910A.E.CurtisIIINAMEOFPREPARER8080NRCUSEONLYEgI686980o16/546-2700,ext. | | ~OS Further liquid penetrant and replication showed area of attack 6-7" by 1/8" consisting |
| : 2329,
| | ~06 of a family of fine cracks similar to intergranular type attack. All pressurizer head nozzle-to-safe-end weld areas were examined with UT and liquid penetrant with no |
| | ~08 other relevant indications noted. |
| | 7 8 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE |
| | ~Og ~CB Q>> '~EQ12 ~DQTR P 1 P E X X Q14 ~BQEE ~Z Qs 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LERIRO REPQRT ACTION FUTURE EVENT YEAR |
| | ~79 21 22 EFFECT |
| | +23 SHUTDOWN 24 REPORT NO. |
| | ~02 3 26 QX 27 |
| | ~01 28 ATTACHMENT CODE 29 NPRDX TYPE QT 30 PRIME COMP. |
| | 31 NO. |
| | QO 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER |
| | ~BQTR ~XPTg ~APER ~AP27 0 4 1 6 ~YP23 ~YQ24 ~NQ25 Y17 1 2 0 QER 33 34 35 36 37 40 4'I 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 0 Possible causes: original fabrication contamination or chloride concentration occurring during operation. Investigation includes examining boat sample with scanning electron microscope to determine corrosive species, and insulation leachin chemical anal sis. |
| | 3 Cloth cover replaced with fiberglass. Report of metallurgical analysis results to be submitted later. Pressurizer head nozzle-to-safe-end weld areas to be reexamined in 4 1980 AI&O. |
| | 7 8 9 80 FACILITY STATUS % POWER OTHER STATUS Q METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 s ~GQEs ~00 0 PER NA ~BQ3I Routine IS I 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITYQ3s LOCATION OF RELEASE QB 6 ~~ Q33 ~+Q34 NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3g |
| | ~77 ~00 0 Q37 |
| | '12 Z Qss NA 7 8 9 11 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 g ~ZQ42 NA 7 8 9 10 80 PUBLICITY NRC USE ONLY 7 8 ISSUED |
| | ~XQ44 9 |
| | DESCRIPTION 10 News release was made December ll, 1979. 68 69 80 o Eg NAME OF PREPARER A. E. Curtis III I 16/546-2700,ext. 2329, |
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| Attachnant tcLER79+3/01T-0 Rochester GasandElectricCorporation R.E.GinnaNuclearPowerPlant,UnitNo.1DocketNo.50-244EventDescritionOnFriday,December7,1979,duringanormalinservice inspection programexamination onthepressurizer reliefnozzle-to-safe-end weld,linearindications l-l/8"longand3/8"longwerenotedbytheliquidpene-trantexamination method.Theultrasonic examination performed didnotrevealanyindications. | | Attachnant tc LER 79+3/01T-0 Rochester Gas and Electric Corporation R. E. Ginna Nuclear Power Plant, Unit No. 1 Docket No. 50-244 Event Descri tion On Friday, December 7, 1979, during a normal inservice inspection program examination on the pressurizer relief nozzle-to-safe-end weld, linear indications l-l/8" long and 3/8" long were noted by the liquid pene-trant examination method. The ultrasonic examination performed did not reveal any indications. On Saturday, December 8, 1979, the area of the indications was prepared by mechanical means with a flapper wheel and light grinding. A reexamination with liquid penetrant revealed an area of attack approximately 6-7 inches long by 1/8" wide. Due to other work being performed in the pressurizer head area supplementary examinations were not performed until Sunday night, December 9, 1979. These examina-tions included more liquid penetrant examinations and radiographic g-ray) examination of the area where the original liquid penetrant indication was found. The radiographs of the affected area revealed no apparent volumetric indications. Supplemental ultrasonic examinations of the area also revealed no apparent volumetric indications. |
| OnSaturday, December8,1979,theareaoftheindications waspreparedbymechanical meanswithaflapperwheelandlightgrinding.
| | Inplace metallography was attempted without much success due to the restrictions imposed by the piping system that attaches to the relief nozzle. Replication using a plastic material revealed a family of very fine cracks. In a 2 inch long area the indications were ground*out ah about 1/8 inch depth. Confirmation of this finding occurred when in an additional 3 inch long area the indications were ground out after less than 1/8 of an inch of material was removed. On Wednesday, December 12, 1979, a boat sample was removed for further investigation and analysis of the cracks. The results of the investigations made in the field revealed that the cracks were in the 309 weld material that was used for the dissimilar weld between the carbon steel nozzle (SA-216-GR.WCC) and the stainless steel'safe-end material (SA-182 TP, 316) and not the safe-end material as originally thought. |
| Areexamination withliquidpenetrant revealedanareaofattackapproximately 6-7incheslongby1/8"wide.Duetootherworkbeingperformed inthepressurizer headareasupplementary examinations werenotperformed untilSundaynight,December9,1979.Theseexamina-tionsincludedmoreliquidpenetrant examinations andradiographic g-ray)examination oftheareawheretheoriginalliquidpenetrant indication wasfound.Theradiographs oftheaffectedarearevealednoapparentvolumetric indications.
| | The repair procedure included removal of the remaining cracked mate-rial, preparing the excavated area for weld repair and welding with the Gas Tungsten Arc Welding Process utilizing ER-309 base filler metal. Post prep-aration, first weld pass and final weld liquid penetrant examinations were performed. A final weld preservice ultrasonic examination of the repaired area was also performed. The results of all examinations did not reveal any indications . |
| Supplemental ultrasonic examinations oftheareaalsorevealednoapparentvolumetric indications. | | Also examined during this investigation were all the nozzle-to-safe-end weld areas on the pressurizer head utilizing the liquid penetrant and ultrasonic examination methods. The ultrasonic examinations included a normal inservice inspection technique and a special stress corrosion tech- |
| Inplacemetallography wasattempted withoutmuchsuccessduetotherestrictions imposedbythepipingsystemthatattachestothereliefnozzle.Replication usingaplasticmaterialrevealedafamilyofveryfinecracks.Ina2inchlongareatheindications wereground*out ahabout1/8inchdepth.Confirmation ofthisfindingoccurredwheninanadditional 3inchlongareatheindications weregroundoutafterlessthan1/8ofaninchofmaterialwasremoved.OnWednesday, December12,1979,aboatsamplewasremovedforfurtherinvestigation andanalysisofthecracks.Theresultsoftheinvestigations madeinthefieldrevealedthatthecrackswereinthe309weldmaterialthatwasusedforthedissimilar weldbetweenthecarbonsteelnozzle(SA-216-GR.WCC) andthestainless steel'safe-end material(SA-182TP,316)andnotthesafe-endmaterialasoriginally thought.Therepairprocedure includedremovaloftheremaining crackedmate-rial,preparing theexcavated areaforweldrepairandweldingwiththeGasTungstenArcWeldingProcessutilizing ER-309basefillermetal.Postprep-aration,firstweldpassandfinalweldliquidpenetrant examinations wereperformed.
| | |
| Afinalweldpreservice ultrasonic examination oftherepairedareawasalsoperformed.
| | ~ + |
| Theresultsofallexaminations didnotrevealanyindications
| | Attachment to LER 79- 3/01T-0 2. |
| .Alsoexaminedduringthisinvestigation wereallthenozzle-to-safe-endweldareasonthepressurizer headutilizing theliquidpenetrant andultrasonic examination methods.Theultrasonic examinations includedanormalinservice inspection technique andaspecialstresscorrosion tech-
| | nique. Welds in associated piping of the four nozzles were also examined utilizing the liquid penetrant method with no further relevant indications noted. There were no health or safety consequences to the public or to plant personnel due to this event. |
| ~+ | | Cause Descri tion Replication of the as polished weld surface revealed a very tight crack pattern, similar to an intergranular stress corrosion. The boat sample analysis revealed three cracks as follows: |
| Attachment toLER79-3/01T-02.nique.Weldsinassociated pipingofthefournozzleswerealsoexaminedutilizing theliquidpenetrant methodwithnofurtherrelevantindications noted.Therewerenohealthorsafetyconsequences tothepublicortoplantpersonnel duetothisevent.CauseDescritionReplication oftheaspolishedweldsurfacerevealedaverytightcrackpattern,similartoanintergranular stresscorrosion. | | Crack 41 1. 4 mm from carbon steel fusion line |
| Theboatsampleanalysisrevealedthreecracksasfollows:Crack41-1.4mmfromcarbonsteelfusionline0.4mmindepthCrack42-2.3mmfromcarbonsteelfusionline0.7mmindepthCrack43-3.5mmfromcarbonsteelfusionline1.1mmindepthtouchingcarbonsteelbevelFurtheranalysisutilizing thescanningelectronmicroscope isongoingtodetermine ifanycorrosive speciescanbeidentified.
| | : 0. 4 mm in depth Crack 42 2.3 mm from carbon steel fusion line |
| Presently onlyspeculation canbemadeonthecauseofthiscracking. | | : 0. 7 mm in depth Crack 43 3.5 mm from carbon steel fusion line 1.1 mm in depth touching carbon steel bevel Further analysis utilizing the scanning electron microscope is ongoing to determine if any corrosive species can be identified. |
| Itmayhavebeencausedbyoriginalfabrication contamination orbyachlorideconcentration thathasoccurredduringoperation.
| | Presently only speculation can be made on the cause of this cracking. |
| Aspartofthisinvestigation achemicalanalysisofleachable contaminants fromthethermalinsulation thatsurrounded thereliefnozzlewasperformed asprescribed inRegulatory Guidel.36,Nonmetallic ThermalInsulation forAustenitic Stainless Steel.Theresultsofthisanalysisareasfollowsforsample1-wovenclothcoverandsample2-glassfibrouslayeredmaterial:
| | It may have been caused by original fabrication contamination or by a chloride concentration that has occurred during operation. As part of this investigation a chemical analysis of leachable contaminants from the thermal insulation that surrounded the relief nozzle was performed as prescribed in Regulatory Guide |
| SamplePPMPPMCIFPPMPPMCI+FNaPPMSi03PPMNa+Si03989.4107.4100207307301.631.64099139Basedonthisanalysisaccording toFigureIofRegulatory Guide1.36,Sample2-theglassinsulation isacceptable, howeverSample1-theclothcoverisnotwithintheacceptable region.Althoughitwouldbelogicaltoassumethattheinsulating clothprovidedthechlorides thatmighthavecausedthiscrackingphenomena, theclothcouldhavebeencontaminated duringthehandlingofremoval.Therefore, theresultsofthescanningelectronmicro-scopewillhavetobefurtheranalyzedbeforeconfirming theinsulation involvement.
| | : l. 36, Nonmetallic Thermal Insulation for Austenitic Stainless Steel. The results of this analysis are as follows for sample 1 woven cloth cover and sample 2 glass fibrous layered material: |
| n Attachment toLER79-3/01T-0Aspartofthecorrective actiontheinsulation materialwaschangedonthepressurizer nozzlestoassurethatpotential leachable contaminants frominsulating materialwillrequirenofurtherconsideration. | | PPM PPM PPM PPM PPM PPM Sample CI F CI+F Na Si03 Na+ Si03 98 9.4 107.4 100 207 307 30 1.6 31.6 40 99 139 Based on this analysis according to Figure I of Regulatory Guide 1.36, Sample 2 the glass insulation is acceptable, however Sample 1 the cloth cover is not within the acceptable region. Although it would be logical to assume that the insulating cloth provided the chlorides that might have caused this cracking phenomena, the cloth could have been contaminated during the handling of removal. Therefore, the results of the scanning electron micro-scope will have to be further analyzed before confirming the insulation involvement. |
| Alsoeachnozzle-to-safe-end areawascleanedtoremoveanycontaminants priortoreinsulation.
| | |
| Afullreportonthefinalresultsofthemetallurgical analysiswillbesubmitted whentheinvestigations arecomplete.
| | n Attachment to LER 79- 3/01T-0 As part of the corrective action the insulation material was changed on the pressurizer nozzles to assure that potential leachable contaminants from insulating material will require no further consideration. Also each nozzle-to-safe-end area was cleaned to remove any contaminants prior to reinsulation. A full report on the final results of the metallurgical analysis will be submitted when the investigations are complete. These nozzle-to-safe-end weld areas will be reexamined during the 1980 refueling and main-tenance outage.}} |
| Thesenozzle-to-safe-endweldareaswillbereexamined duringthe1980refueling andmain-tenanceoutage.}}
| |
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Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION I7.77+ 79-023/01T-0 LICENSEE EVENT REPORT CONTROL BLOCK: Qi {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I 6 N Y R E G 1 Q20 0 0 0 0 0 0 - 0 0Q34 1 1 1 1QE~QR 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T R"DRT ~L~B 0 5 0 0 0 2 4 4 7 1 2 0 7 7 9 8 1 2 2 1 7 9
,~0 SOURCE Qg 7 8 60 61 DOCKET NUMBER EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During normal inservice inspection of pressurizer relief nozzle-to-safe-end weld,
~03 liquid penetrant exa'm showed linear indications l-l/8" and 3/8" long. (T.S. 6.9.2.
~04 a(3)) UT did not show any. Followup X-ray exam showed no volumetric indications.
~OS Further liquid penetrant and replication showed area of attack 6-7" by 1/8" consisting
~06 of a family of fine cracks similar to intergranular type attack. All pressurizer head nozzle-to-safe-end weld areas were examined with UT and liquid penetrant with no
~08 other relevant indications noted.
7 8 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
~Og ~CB Q>> '~EQ12 ~DQTR P 1 P E X X Q14 ~BQEE ~Z Qs 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LERIRO REPQRT ACTION FUTURE EVENT YEAR
~79 21 22 EFFECT
+23 SHUTDOWN 24 REPORT NO.
~02 3 26 QX 27
~01 28 ATTACHMENT CODE 29 NPRDX TYPE QT 30 PRIME COMP.
31 NO.
QO 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER
~BQTR ~XPTg ~APER ~AP27 0 4 1 6 ~YP23 ~YQ24 ~NQ25 Y17 1 2 0 QER 33 34 35 36 37 40 4'I 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 0 Possible causes: original fabrication contamination or chloride concentration occurring during operation. Investigation includes examining boat sample with scanning electron microscope to determine corrosive species, and insulation leachin chemical anal sis.
3 Cloth cover replaced with fiberglass. Report of metallurgical analysis results to be submitted later. Pressurizer head nozzle-to-safe-end weld areas to be reexamined in 4 1980 AI&O.
7 8 9 80 FACILITY STATUS % POWER OTHER STATUS Q METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 s ~GQEs ~00 0 PER NA ~BQ3I Routine IS I 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITYQ3s LOCATION OF RELEASE QB 6 ~~ Q33 ~+Q34 NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3g
~77 ~00 0 Q37
'12 Z Qss NA 7 8 9 11 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 g ~ZQ42 NA 7 8 9 10 80 PUBLICITY NRC USE ONLY 7 8 ISSUED
~XQ44 9
DESCRIPTION 10 News release was made December ll, 1979. 68 69 80 o Eg NAME OF PREPARER A. E. Curtis III I 16/546-2700,ext. 2329,
Attachnant tc LER 79+3/01T-0 Rochester Gas and Electric Corporation R. E. Ginna Nuclear Power Plant, Unit No. 1 Docket No. 50-244 Event Descri tion On Friday, December 7, 1979, during a normal inservice inspection program examination on the pressurizer relief nozzle-to-safe-end weld, linear indications l-l/8" long and 3/8" long were noted by the liquid pene-trant examination method. The ultrasonic examination performed did not reveal any indications. On Saturday, December 8, 1979, the area of the indications was prepared by mechanical means with a flapper wheel and light grinding. A reexamination with liquid penetrant revealed an area of attack approximately 6-7 inches long by 1/8" wide. Due to other work being performed in the pressurizer head area supplementary examinations were not performed until Sunday night, December 9, 1979. These examina-tions included more liquid penetrant examinations and radiographic g-ray) examination of the area where the original liquid penetrant indication was found. The radiographs of the affected area revealed no apparent volumetric indications. Supplemental ultrasonic examinations of the area also revealed no apparent volumetric indications.
Inplace metallography was attempted without much success due to the restrictions imposed by the piping system that attaches to the relief nozzle. Replication using a plastic material revealed a family of very fine cracks. In a 2 inch long area the indications were ground*out ah about 1/8 inch depth. Confirmation of this finding occurred when in an additional 3 inch long area the indications were ground out after less than 1/8 of an inch of material was removed. On Wednesday, December 12, 1979, a boat sample was removed for further investigation and analysis of the cracks. The results of the investigations made in the field revealed that the cracks were in the 309 weld material that was used for the dissimilar weld between the carbon steel nozzle (SA-216-GR.WCC) and the stainless steel'safe-end material (SA-182 TP, 316) and not the safe-end material as originally thought.
The repair procedure included removal of the remaining cracked mate-rial, preparing the excavated area for weld repair and welding with the Gas Tungsten Arc Welding Process utilizing ER-309 base filler metal. Post prep-aration, first weld pass and final weld liquid penetrant examinations were performed. A final weld preservice ultrasonic examination of the repaired area was also performed. The results of all examinations did not reveal any indications .
Also examined during this investigation were all the nozzle-to-safe-end weld areas on the pressurizer head utilizing the liquid penetrant and ultrasonic examination methods. The ultrasonic examinations included a normal inservice inspection technique and a special stress corrosion tech-
~ +
Attachment to LER 79- 3/01T-0 2.
nique. Welds in associated piping of the four nozzles were also examined utilizing the liquid penetrant method with no further relevant indications noted. There were no health or safety consequences to the public or to plant personnel due to this event.
Cause Descri tion Replication of the as polished weld surface revealed a very tight crack pattern, similar to an intergranular stress corrosion. The boat sample analysis revealed three cracks as follows:
Crack 41 1. 4 mm from carbon steel fusion line
- 0. 4 mm in depth Crack 42 2.3 mm from carbon steel fusion line
- 0. 7 mm in depth Crack 43 3.5 mm from carbon steel fusion line 1.1 mm in depth touching carbon steel bevel Further analysis utilizing the scanning electron microscope is ongoing to determine if any corrosive species can be identified.
Presently only speculation can be made on the cause of this cracking.
It may have been caused by original fabrication contamination or by a chloride concentration that has occurred during operation. As part of this investigation a chemical analysis of leachable contaminants from the thermal insulation that surrounded the relief nozzle was performed as prescribed in Regulatory Guide
- l. 36, Nonmetallic Thermal Insulation for Austenitic Stainless Steel. The results of this analysis are as follows for sample 1 woven cloth cover and sample 2 glass fibrous layered material:
PPM PPM PPM PPM PPM PPM Sample CI F CI+F Na Si03 Na+ Si03 98 9.4 107.4 100 207 307 30 1.6 31.6 40 99 139 Based on this analysis according to Figure I of Regulatory Guide 1.36, Sample 2 the glass insulation is acceptable, however Sample 1 the cloth cover is not within the acceptable region. Although it would be logical to assume that the insulating cloth provided the chlorides that might have caused this cracking phenomena, the cloth could have been contaminated during the handling of removal. Therefore, the results of the scanning electron micro-scope will have to be further analyzed before confirming the insulation involvement.
n Attachment to LER 79- 3/01T-0 As part of the corrective action the insulation material was changed on the pressurizer nozzles to assure that potential leachable contaminants from insulating material will require no further consideration. Also each nozzle-to-safe-end area was cleaned to remove any contaminants prior to reinsulation. A full report on the final results of the metallurgical analysis will be submitted when the investigations are complete. These nozzle-to-safe-end weld areas will be reexamined during the 1980 refueling and main-tenance outage.