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| issue date = 03/17/1980
| issue date = 03/17/1980
| title = RO 335-80-13:on 800314,while Plant Was in Cold Shutdown, Field Leads to Excitors on Both Diesel Generator Units Were Found Undersized.Caused by Design Error.Field Leads Will Be Replaced & Permanent Repair Studied
| title = RO 335-80-13:on 800314,while Plant Was in Cold Shutdown, Field Leads to Excitors on Both Diesel Generator Units Were Found Undersized.Caused by Design Error.Field Leads Will Be Replaced & Permanent Repair Studied
| author name = WETHY C M
| author name = Wethy C
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:.-ak.894P.O.OOX5ZG,FT.PIPfICP.,FL3345(Io+Ifr,J.P.O'Railly, DirectorKegiorfTlUfficeofXnspection andEnforcef",.i'nt U.STNuclearPcgulatory Co~issioT5.
{{#Wiki_filter:.-
Atlanta,Georgia30303~::epicsTo.'I;IH',
ak. 894                                                                                    P.O. OOX 5ZG, FT. PIP fICP.,                               FL 3345(
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'SLORIfffl PO'A'EffILUGHTgQN'cb17~1980~<ffVCaVPW4y-"rG.II.Vetlqr,PlantManagert.LuciePlant-DPK67gloxidaPower6Lip'tftCotlpanyIfifcmi,l'loridaLb)eat:k>UHOFOKFACSI'.IILE.'ERAIlSNISSiO."
:.F,fsitc:           AIIS, Jaa, CQl~, >~S,.RZuENu
ToCo".PIRIf PRO'=IPTREPO.".TABLP.
                                                                                                ~~w          l.                                                     ~    <ffV g ygfffltlfI  'SLORIfffl         PO'A'Eff                  IL  UGHT Ca VPW Io+      Ifr, J.      P. O'Railly, Director    Kegiorf Tl                          gQN Uffice of Xnspection and Enforcef",.i'nt                                                        'cb 17~                             1980 U. ST Nuclear Pcgulatory Co~issioT5.
.OCCUR)'1'llf'F.
Atlanta, Georgia 30303 rG. II. Vetlqr, Plant Manager YoTi+ y
335-80-l3 0IDieselGenerator
: t. Lucie Plant  DPK 67                                            4y-"                                                                        -f C:
'FieldhiringError~~Onetoa.design,error thefield.'l.aads, tothecffcitors onboth0unitsareundersized; The.pl.antvaaincoldshutdufwwhenthiswasdiscovered.
gloxida Power 6 Lip'tft Cotlpany Ififcmi,       l'lorida Lb)eat:         k>UHO    FOK FACSI'.IILE.'ERAIlSNISSiO."       To Co".PIRIf       PRO'=IPT REPO.".TABLP.
Ii'ai'~'On3/14/80tileD/G'svererunatdesignloadforsurveil?fiYice tasting.,
90 OCCUR)'1'llf'F. 335-80-l3                                                                                               0            ~P5 I                                                                                                                    lg C)
"A"D/Gwoulclnotacceptfulldesignload.Duringinvestioation ofthisproble;ii itwasnotedthatthefirldleadsverehotandthon,thatthein"ulation wasburnt.Theleads'86wire)verereplacedandtha"A"D/GthenacceptedfulLdesignload,Theleadscn"8"D/Gfrereinspected andnodaf.".agc crI5igkteu'.perature fo',ind.'lbs.engineering departrent vasaskedtoeva5uatethcproblaf.-i
Diesel Generator 'Field hiring Error                                                                                  ~ ~             -    3f")
~On.3/L5/80thaplantco~.".enced shut-dof'nandcoaldovnforrefueling."
u),;
On'/17/8Q (Ikoffday) atabout1,0500&#xc3;I,engineering reportedt'llffttheleadsareinffcctunflarfcizad.
  ."5 qir 5          One    to a. design,error the field .'l.aads, to the cffcitors on both 0 units are undersized; The. pl.ant vaa in cold shutdufw when this was    discovered.
Theyslfouldbeatleast3-oifphtsizetohandlethefullfieldcurrantpoiaibleunde~highload/transient conditions.
i'aI i'                           ~
Tld.svasconfirned ontheD/GunitsvendorprintsbuttiveA/Einstff33Iitiori draciinps incorrectly specified ticefI6wtreiThisaffectsthelonpterfffreliability oftheD/Gunits.Hovever,itsho>>ldbe,notedthattheAD/Gwiringshof.cddarageonlyafter0yearsofoperation and3sti)1showsnoffe.Alsoon3/l6/SQtheintegrated safeguards/Diesa) generator testwasper-.'or".~cd andbothunitsacceptedtheloadingsequenceand(partial),
                    'On 3/14/80 tile D/G's vere run at design load for surveil?fiYice tasting., "A" D/G woulcl not accept full design load. During investioation of this proble;ii             it    was noted that the firld leads vere hot and thon, that the in"ulation was burnt. The leads wire) vere replaced and tha "A" D/G then accepted fulL                                                  '86 design load, The leads cn "8" D/G frere inspected and no daf.".agc cr I5igk teu'.perature fo',ind. 'lbs. engineering departrent vas asked to eva5uate thc problaf.-i ~ On. 3/L5/80 tha plant co~.".enced shut-dof'n and coal dovn for refueling."
loadrefection andrestart,perthe.applicable Tcchniea1 Specificati YoTi+y-fC:90~P5lgC)-3f")u),;."5qir5ons,.oirectiveAction:15'>>Thef&#xc3;e3dl.eadff5:illbeim.".ediately replacedonatlefist"ID/GDueg'"tothesizeoftheinstalled conduititr:n>-benecessary initially todothisinat'ai,porary r:armer.Theperrfanent fixwillbepersuedL~ionanerpidf-ted basissotheD/Gcfcnbereturnedtofulloperability
On'/17/8Q       (Ikoffday) at about 1,0500 &#xc3;I, engineering reported t'llfft the leads are in ffcct unflarfcizad. They slfould be at least 3-oifpht size to handle the full field currant poiaible unde~ high load/
'ertheTechnical Specifications.
transient conditions. Tld.s vas confirned on the D/G units vendor prints but tive A/E instff33Iitiori draciinps incorrectly specified tice fI6 wtrei This affects the lonp terfff reliability of the D/G units.
Thescheduleforthipcannotbeacaiirately estimated atthistif..e.A}so,otherdesignbytheindi"iduals involvedwillbeinvestigated butthe.details,scope.andschcdulcarecurrently unl'.nown VgI~~~8004030I6'QHELPItVGf3I/If,.D~t0TIIO6"."<<~~'~g~'g~tgg~-RKUlgg.A.
Hovever,     it  sho>>ld be, noted that the A D/G wiring shof.cd darage only af ter 0 years of operation and 3 sti) 1 shows noffe. Also on 3/l6/SQ the integrated safeguards/Diesa) generator test was and both units accepted the loading sequence and (partial),
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              ~i on an erpidf-ted basis so the D/G cfcn be returned to full operability L
the Technical Specifications. The schedule for thip cannot be                                                                  'er acaiirately estimated at this tif..e. A}so, other design by the indi"iduals involved will be investigated but the. details, scope
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Latest revision as of 10:04, 4 February 2020

RO 335-80-13:on 800314,while Plant Was in Cold Shutdown, Field Leads to Excitors on Both Diesel Generator Units Were Found Undersized.Caused by Design Error.Field Leads Will Be Replaced & Permanent Repair Studied
ML17266A160
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 03/17/1980
From: Wethy C
FLORIDA POWER & LIGHT CO.
To:
References
NUDOCS 8004030167
Download: ML17266A160 (2)


Text

.-

ak. 894 P.O. OOX 5ZG, FT. PIP fICP., FL 3345(

~::epics To.'I;IH', JHB, CAQ, G'.1V, MZ

t. 0'+ii<"
.F,fsitc: AIIS, Jaa, CQl~, >~S,.RZuENu

~~w l. ~ <ffV g ygfffltlfI 'SLORIfffl PO'A'Eff IL UGHT Ca VPW Io+ Ifr, J. P. O'Railly, Director Kegiorf Tl gQN Uffice of Xnspection and Enforcef",.i'nt 'cb 17~ 1980 U. ST Nuclear Pcgulatory Co~issioT5.

Atlanta, Georgia 30303 rG. II. Vetlqr, Plant Manager YoTi+ y

t. Lucie Plant DPK 67 4y-" -f C:

gloxida Power 6 Lip'tft Cotlpany Ififcmi, l'lorida Lb)eat: k>UHO FOK FACSI'.IILE.'ERAIlSNISSiO." To Co".PIRIf PRO'=IPT REPO.".TABLP.

90 OCCUR)'1'llf'F. 335-80-l3 0 ~P5 I lg C)

Diesel Generator 'Field hiring Error ~ ~ - 3f")

u),;

."5 qir 5 One to a. design,error the field .'l.aads, to the cffcitors on both 0 units are undersized; The. pl.ant vaa in cold shutdufw when this was discovered.

i'aI i' ~

'On 3/14/80 tile D/G's vere run at design load for surveil?fiYice tasting., "A" D/G woulcl not accept full design load. During investioation of this proble;ii it was noted that the firld leads vere hot and thon, that the in"ulation was burnt. The leads wire) vere replaced and tha "A" D/G then accepted fulL '86 design load, The leads cn "8" D/G frere inspected and no daf.".agc cr I5igk teu'.perature fo',ind. 'lbs. engineering departrent vas asked to eva5uate thc problaf.-i ~ On. 3/L5/80 tha plant co~.".enced shut-dof'n and coal dovn for refueling."

On'/17/8Q (Ikoffday) at about 1,0500 ÃI, engineering reported t'llfft the leads are in ffcct unflarfcizad. They slfould be at least 3-oifpht size to handle the full field currant poiaible unde~ high load/

transient conditions. Tld.s vas confirned on the D/G units vendor prints but tive A/E instff33Iitiori draciinps incorrectly specified tice fI6 wtrei This affects the lonp terfff reliability of the D/G units.

Hovever, it sho>>ld be, noted that the A D/G wiring shof.cd darage only af ter 0 years of operation and 3 sti) 1 shows noffe. Also on 3/l6/SQ the integrated safeguards/Diesa) generator test was and both units accepted the loading sequence and (partial),

per-.'or".~cd load refection and restart, per the. applicable Tcchniea1 Specificati ons,

.oi rective Action:

1 5'>> The fÃe3d l.eadff 5:ill be im.".ediately replaced on at lefist" I D/G Due g'" to the size of the installed conduit it r:n>- be necessary to do this in a t'ai,porary r:armer. The perrfanent fix will be persued initially

~i on an erpidf-ted basis so the D/G cfcn be returned to full operability L

the Technical Specifications. The schedule for thip cannot be 'er acaiirately estimated at this tif..e. A}so, other design by the indi"iduals involved will be investigated but the. details, scope

.and schcdulc are currently unl'.nown V

I ~ ~ ~

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