ML17266A199: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(2 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 04/23/1980
| issue date = 04/23/1980
| title = LER 80-014/03L-0: on 800324,w/reactor Shutdown for refueling,6B2 Heater for Sbvs Discovered to Be Inoperable. Caused by Defective Thermocouple Amplifier (Fenwal Model 543) in 6B2 Heater Control Circuitry.Amplifier Replaced
| title = LER 80-014/03L-0: on 800324,w/reactor Shutdown for refueling,6B2 Heater for Sbvs Discovered to Be Inoperable. Caused by Defective Thermocouple Amplifier (Fenwal Model 543) in 6B2 Heater Control Circuitry.Amplifier Replaced
| author name = SHOPPMAN M
| author name = Shoppman M
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:0 8 OG508 NAC FORM SSO l7 TT I LICENSEE EVENT REPORT U.S NUCI EAR AECULATOAY COMMISSION
{{#Wiki_filter:0
[oOij 7 CON'T[oa~j 00Q341 1 1 1Q4~Q3 25 26 LICENSE TYPE 30 5~OA3 53 discovered to be ino erable.For the lant condi.tions existin at the CONTROL 9LOCKI I I I IQI (PLEASE PAINT OR TYPE ALL REOUIAED INFORMATIONI I 133 9 LlCEVSEE CODE 14.5 LICSI3$E 3'IUMSEil LOI'rl I I 33 60 M ODClCET NUMSER SS 69 EVKNT DATE 14 15 REPORT DATE SO EVENT DESCRIPTION
                                                                            'rl 8 OG508 NAC FORM SSO                                                                                                                       U. S NUCI EAR AECULATOAYCOMMISSION l7 TT I LICENSEE EVENT REPORT CONTROL 9LOCKI                         I     I         I     IQI                   (PLEASE PAINT OR TYPE ALL REOUIAED INFORMATIONI I
'NO PROGAELE CONSEOUENCES QIO With the reactor shutdown for refuelin the 6B2 heater for the SBVS was time of discovery the SBVS was not required.However, i.t is not possible 5 to determine the exact time that this failure occurred, and the reactor~08 ma have been o eratin with the 6B2 heater ino erable.It is im ortant~DT to note that the other SBVS train was full o erational at all times.~o 8 See LER 878-23 for revious SBVS roblems.30~09 3 5 9 SYSTEM CAUSE CAVSE COMP.VALVK COOK CODE$USCCDK CCMPONENT CODE SVSCODE SUSCDOK*R LJR L'JR~R LJR L'JR 6 9 10 11 ll ll 15'l9 20 SEDVENTIAI.
[oOij 7              9       LlCEVSEE CODE 133 14     .5                     LICSI3$ E 3'IUMSEil 00Q341  25      26 1
OCCVRRE'ICR RKPDRT AKVISION~Lr RIRO EVENT YKAA REPOAT NO, ,.3 CODE TYPE~NO.Qrr rrrorr~80~~01 4'M~03~L~0'2'l 24 26 21 lS 29 30 31 22~ACTION FUTVAE EFF EC SHUTDOWN ATTACNMENT 4PROK P.'IIM'E COMP.COMPONENT TAKEN ACTION'CN PLANT MKTNPD~NOVAS+22 SUSMITTEO FORMSUS.SUPPUER.MANUFACTURER rJRL'JR LJR LJR''IS LJS LJS~S 34 ,$5 56 40'41 42 4$44 41 CAUSE DESCRIPTION AND CORAECTIVE ACTIONS Q23 o A defective thermocou le am lif er FENWAL MODE NO.543 in the 6B2 heater control circuitr caused the heater to remain deener ized.The amplifier was re laced and the heater was retested satisfactoril
LICENSE TYPE 1  1Q4~Q3 30      5~  OA3 53 CON'T LOI 60           M             ODClCET NUMSER                 SS   69     EVKNT DATE               14       15 I
.All SBVS Shield Buildin Venti.lation S stem 3 9 FACILITY STATUS'I PD3YKA OTNEA STATUS Q N.A.METIIOD OF DISCOVERY OISCOVKAV OESCAlPTION QS2~BQDI ROUTINE SURVEILLANCE 4$LOCATION OF RELEASE Q28 N.A.~30 LUIS~R~3 S 10 IS 44 ACTIVITY CONTE."IT RELKASEO OF AKLKASE AMOUNTOF ACTIVITY QSS Q"~08 N.A.3 3 9 4 10 11 44 PERSONNEL EXPOSURES llUMSER TYPE DESCRIPTION QC9~i>~00 O IQ~ZQ33 5 11 12 PERSONNEL IIMUA36$aZ~Q'"'""-'Q N.A.30 N.A.SO 9 11 I'2 LC$5 OF CR OAMACE rO FACILITY Q42 TYPE OESCAlPTION
REPORT DATE I
~gQ42 IO PUSLICITV ISSUED DESCRIPT:ON LPJ~O'.A.7~6 30 NRC USE ONLY ASS 69 50;":(3'05), 552-.3802 N.A.0 1~0 NME OPREPREA"MIKE SCHOPPMAN~12 other'A'nd'B'rain SBVS heaters were verified o erational.
SO 33 EVENT DESCRIPTION 'NO PROGAELE CONSEOUENCES QIO
REPORTABLE OCCURRENCE 335-80-14 LICENSEE EVENT REPORT PAGE TWO.ADDITIONAL EVENT DESCRIPTION AND PROBABLE CONSE UENCES The SBVS 6B2 heater is the 1.5 Kw heater provided for humidity control of'he 300 cfm cooling air flow through the'A'BVS train when the train is idle.The 30 Kw (6A1)heater which provides humidity control for the 6000 cfm system operating flow was fully operational at all times.Thus, the engineered safety feature function of the'A'BVS train was not significantly degraded.Additionally, the'B'BVS train was'ully operational at all times.r}}
[oa~j            With the reactor shutdown                                     for refuelin                   the     6B2       heater for the                         SBVS was discovered to be ino erable. For the lant condi.tions existin at the time of discovery the SBVS was not required. However, i.t is not possible 5         to determine the exact time that this failure occurred,                                                                             and     the reactor
~08               ma have been o eratin with the 6B2 heater ino erable.                                                                                   It is       im       ortant
~DT                 to note that the other SBVS train was full                                                         o   erational at                     all     times.
~o 3
~09 8
5 9 6
See LER 878-23 for revious SBVS roblems.
LrRIRO 9
SYSTEM COOK EVENT YKAA
                                                *R 10
                                                        'l~
CAUSE CODE LJR L'JR 11 CAVSE
                                                                        $ USCCDK ll SEDVENTIAI.
REPOAT NO,
                                                                                            ~R ll
                                                                                                'M CCMPONENT CODE 15 OCCVRRE'ICR
                                                                                                                    ,.3 CODE COMP.
SVSCODE LJR L'JR
                                                                                                                                          'l9 RKPDRT TYPE     ~
VALVK SUSCDOK 20
                                                                                                                                                              ~
AKVISION NO.
                                                                                                                                                                                          ~
30
                                                                                                  'IS rrrorr         ~80                                                                         ~03
                                                                                                                                                                          ~S Qrr                                                        ~01 24 4                                                 ~L                                     0'2 26       21           lS         29             30               31               22
            ~ ACTION FUTVAE                     EFF EC         SHUTDOWN                                   ATTACNMENT           4PROK           P.'IIM'E COMP.               COMPONENT TAKEN ACTION                   'CN PLANT           MKTNPD           ~       NOVAS +22       SUSMITTEO         FORMSUS.               SUPPUER     .         MANUFACTURER rJRL'JR LJR LJR 34                 ,$ 5             56 40   '41 LJS LJS 42                   4$                 44                 41 CAUSE DESCRIPTION AND CORAECTIVE ACTIONS Q23 o         A   defective thermocou le am                                     lif       er FENWAL MODE NO. 543 in the                                                 6B2 heater control circuitr caused the heater to remain deener ized.                                                                                                 The amplifier was re laced and the heater was retested satisfactoril                                                                                           .        All
~12                other 'A'nd 'B'rain SBVS heaters were verified o erational.
~ 30 3
3 S
3 3
9 SBVS FACILITY STATUS LUIS ACTIVITY CONTE."IT RELKASEO OF AKLKASE 9  4 Q"
                              ~R~
10
                              ~08 10 Shield Buildin Venti.lation S stem
                                    'I PD3YKA PERSONNEL EXPOSURES 11 IS OTNEA STATUS N.A.
AMOUNTOF ACTIVITYQSS N.A.
Q 44 44 METIIOD OF DISCOVERY
                                                                                                  ~BQDI 4$
ROUTINE SURVEILLANCE OISCOVKAV OESCAlPTION QS2 LOCATION OF RELEASE Q28 N.A.
llUMSER               TYPE         DESCRIPTION QC9
~i> ~00                     O     IQ~ZQ33                                                           N.A.
aZ ~Q'"'""-'Q 5                      11      12                                                                                                                                                  30 PERSONNEL IIMUA36$
N.A.
9                 11       I'2 SO LC$ 5 OF CR OAMACE rO FACILITY Q42 7    ~  6 TYPE
              ~gQ42 OESCAlPTION IO
                                                                                                    '.A.
30 PUSLICITV DESCRIPT:ON         LPJ                                                                                                                   NRC USE ONLY 0      ~O ISSUED 1          ~
0 N.A.
ASS     69                               50 NME OPREPREA "MIKE                        SCHOPPMAN                                                        ;     ":(3'05), 552-.3802
 
REPORTABLE OCCURRENCE 335-80-14 LICENSEE EVENT REPORT PAGE TWO.
ADDITIONAL EVENT DESCRIPTION AND PROBABLE CONSE UENCES The SBVS 6B2 heater is the 1.5 Kw heater provided for humidity control of'he 300 cfm cooling air flow through the 'A'BVS train when the train is idle. The 30 Kw (6A1) heater which provides humidity control for the 6000 cfm system operating flow was fully operational at all times.
Thus, the engineered safety feature function of the 'A'BVS train was not significantly degraded. Additionally, the 'B'BVS train   was
'ully operational at all times.
r}}

Latest revision as of 10:04, 4 February 2020

LER 80-014/03L-0: on 800324,w/reactor Shutdown for refueling,6B2 Heater for Sbvs Discovered to Be Inoperable. Caused by Defective Thermocouple Amplifier (Fenwal Model 543) in 6B2 Heater Control Circuitry.Amplifier Replaced
ML17266A199
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/23/1980
From: Shoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A556 List:
References
LER-80-014-03L, LER-80-14-3L, NUDOCS 8005080467
Download: ML17266A199 (2)


Text

0

'rl 8 OG508 NAC FORM SSO U. S NUCI EAR AECULATOAYCOMMISSION l7 TT I LICENSEE EVENT REPORT CONTROL 9LOCKI I I I IQI (PLEASE PAINT OR TYPE ALL REOUIAED INFORMATIONI I

[oOij 7 9 LlCEVSEE CODE 133 14 .5 LICSI3$ E 3'IUMSEil 00Q341 25 26 1

LICENSE TYPE 1 1Q4~Q3 30 5~ OA3 53 CON'T LOI 60 M ODClCET NUMSER SS 69 EVKNT DATE 14 15 I

REPORT DATE I

SO 33 EVENT DESCRIPTION 'NO PROGAELE CONSEOUENCES QIO

[oa~j With the reactor shutdown for refuelin the 6B2 heater for the SBVS was discovered to be ino erable. For the lant condi.tions existin at the time of discovery the SBVS was not required. However, i.t is not possible 5 to determine the exact time that this failure occurred, and the reactor

~08 ma have been o eratin with the 6B2 heater ino erable. It is im ortant

~DT to note that the other SBVS train was full o erational at all times.

~o 3

~09 8

5 9 6

See LER 878-23 for revious SBVS roblems.

LrRIRO 9

SYSTEM COOK EVENT YKAA

  • R 10

'l~

CAUSE CODE LJR L'JR 11 CAVSE

$ USCCDK ll SEDVENTIAI.

REPOAT NO,

~R ll

'M CCMPONENT CODE 15 OCCVRRE'ICR

,.3 CODE COMP.

SVSCODE LJR L'JR

'l9 RKPDRT TYPE ~

VALVK SUSCDOK 20

~

AKVISION NO.

~

30

'IS rrrorr ~80 ~03

~S Qrr ~01 24 4 ~L 0'2 26 21 lS 29 30 31 22

~ ACTION FUTVAE EFF EC SHUTDOWN ATTACNMENT 4PROK P.'IIM'E COMP. COMPONENT TAKEN ACTION 'CN PLANT MKTNPD ~ NOVAS +22 SUSMITTEO FORMSUS. SUPPUER . MANUFACTURER rJRL'JR LJR LJR 34 ,$ 5 56 40 '41 LJS LJS 42 4$ 44 41 CAUSE DESCRIPTION AND CORAECTIVE ACTIONS Q23 o A defective thermocou le am lif er FENWAL MODE NO. 543 in the 6B2 heater control circuitr caused the heater to remain deener ized. The amplifier was re laced and the heater was retested satisfactoril . All

~12 other 'A'nd 'B'rain SBVS heaters were verified o erational.

~ 30 3

3 S

3 3

9 SBVS FACILITY STATUS LUIS ACTIVITY CONTE."IT RELKASEO OF AKLKASE 9 4 Q"

~R~

10

~08 10 Shield Buildin Venti.lation S stem

'I PD3YKA PERSONNEL EXPOSURES 11 IS OTNEA STATUS N.A.

AMOUNTOF ACTIVITYQSS N.A.

Q 44 44 METIIOD OF DISCOVERY

~BQDI 4$

ROUTINE SURVEILLANCE OISCOVKAV OESCAlPTION QS2 LOCATION OF RELEASE Q28 N.A.

llUMSER TYPE DESCRIPTION QC9

~i> ~00 O IQ~ZQ33 N.A.

aZ ~Q'"'""-'Q 5 11 12 30 PERSONNEL IIMUA36$

N.A.

9 11 I'2 SO LC$ 5 OF CR OAMACE rO FACILITY Q42 7 ~ 6 TYPE

~gQ42 OESCAlPTION IO

'.A.

30 PUSLICITV DESCRIPT:ON LPJ NRC USE ONLY 0 ~O ISSUED 1 ~

0 N.A.

ASS 69 50 NME OPREPREA "MIKE SCHOPPMAN  ; ":(3'05), 552-.3802

REPORTABLE OCCURRENCE 335-80-14 LICENSEE EVENT REPORT PAGE TWO.

ADDITIONAL EVENT DESCRIPTION AND PROBABLE CONSE UENCES The SBVS 6B2 heater is the 1.5 Kw heater provided for humidity control of'he 300 cfm cooling air flow through the 'A'BVS train when the train is idle. The 30 Kw (6A1) heater which provides humidity control for the 6000 cfm system operating flow was fully operational at all times.

Thus, the engineered safety feature function of the 'A'BVS train was not significantly degraded. Additionally, the 'B'BVS train was

'ully operational at all times.

r