ML17266A373: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
(6 intermediate revisions by the same user not shown) | |||
Line 3: | Line 3: | ||
| issue date = 09/15/1980 | | issue date = 09/15/1980 | ||
| title = LER 80-039/03L-0:on 800814,dose Equivalent Iodine Exceeded Tech Spec 3.4.8a Limit.Caused by Dropped Control Element assembly.I-131 Level Decreased to Nominal Levels After 96-h | | title = LER 80-039/03L-0:on 800814,dose Equivalent Iodine Exceeded Tech Spec 3.4.8a Limit.Caused by Dropped Control Element assembly.I-131 Level Decreased to Nominal Levels After 96-h | ||
| author name = | | author name = Pace P | ||
| author affiliation = FLORIDA POWER & LIGHT CO. | | author affiliation = FLORIDA POWER & LIGHT CO. | ||
| addressee name = | | addressee name = | ||
Line 15: | Line 15: | ||
| page count = 7 | | page count = 7 | ||
}} | }} | ||
=Text= | |||
{{#Wiki_filter:NRC PORM 344 U. S. NUCLEAR REOULATORY COMMISS'ION I7.77 I LICENSEE EVENT REPORT I I I Ql IPLEJLIE PRINT OR TYPE ALL RECUIREO INPORMATIONI 4 | |||
~OI F IL S L S IllQ. 2 0 0 0 I010fO IOI- 0 0 | |||
.0, 4(l I 1 1 04 | |||
'UJLI | |||
> f I Qs | |||
'oo~~" | |||
4 9 LICENSEE CQOE LICCArsa N4M4CA ~5 IS LaCINSC TVrc 40 $1 *a 34 CON'T | |||
~O I 5 40 oi' 41 QQClCET NUM4CR Gl 44 44 CVCNT O*TC IS ACIQAT QA 4 50 oe EVENTOESCRIPTION AND SRQSABLE CONSEQUENCES Qlo Durin a short (12 hour) maintenance shutdown, while in a startup mode, dose equivalent iodine (DE/) exceeded T.S. 3;4.8.a limit of 1.0IICi/gram DE I-131. The DE iodine was first measured above this limit at 0320 s on 8-14-80 and remained above the limit for a roximatel 8.5 hours. The 0 lj o ai inforlnation re uired b T.S. 3.4.8.d. This is | |||
~a I the fourth occurrence of this t e. | |||
~04 7 4 9 5v5Tsu cAUSS cAUsc Cour, vALvc | |||
~O9 I 4 | |||
~l~ | |||
9 CQQC 10 Q>> | |||
cQQE | |||
~EQ>> | |||
II 5uscooc | |||
~X 11 Q>> | |||
11 CQMSQNCNT CQOC U E L X X IQ14 I~ | |||
SUS QOS | |||
~ZQS 19 5USCQCE | |||
~Z 0 | |||
Q6 SCCUCNTIAI OCCVAAENCE AErQAT REVISION Or LEAIAO iso ACTION SUTURE r ~80'1 11 CrrCC ~ | |||
~ SAauTQOWN | |||
~03 14 AEroAT NQ. | |||
9 14 | |||
~~ | |||
11 | |||
~03 ac | |||
*T AQNMSNT CQQC 19 vrelw Tvr 4 | |||
~L IO pall adc | |||
~ | |||
cour 11 | |||
~0 NO. | |||
11 CourQNCNT TAKEN ACTION CN rLANT METHQQ AQUAS +22 errrrrS oJS owr 1$ 14 40 SusulTTCO MS 41 rQAMSUS. | |||
wmS 41 SurrUCA Mir 44 uAVurACTUACA 47 CAUSE OPSCRIPTION ANO CORRECI'IVE ACTIONS Q27 o After an extended eriod of ower o eration with a nominal level of fuel leakage, a dropped CEA (LER 335-80-38, CEA I/7), and the plant shutdown for f a sien s to cause iodine build-u | |||
~iodine splkin 1-131 level decreesed to below | |||
~S~ | |||
henomenon). The 030 a | |||
1.0IICi/ ram after 8.5 hours and to nominal levels after 96 hours. | |||
I 4 r ACILITY 5 ATUS '0 rOIISII QTbe CA STATUS Q 'aO AIETNQQ Qr OISCQVCAV olscovccv ocscAISTIQN ten I 4 raJS 9 10 11 11 44 | |||
~AQSI Operator Observation QS2 ACTIVITY CONTENT 40 AELEAsco Qr RELEASE AuoUNT Qr ACTIV>Tv QSS LOCATION or RELEASE Q16 2 ~QSS NA I 4 9 IO 11 44 45 r ASQNNEL EXrosuAES I 4 | |||
~I~Q>>~Q>9 | |||
~ 11 I 'I 11 | |||
~ SASQNNSL IIIIUAIES 50 i QLIILJg 10i !IA I 4 9 11 11 LCSS Qr CA QAM4CE To SACILITV 40 Tvrc ocscAlr TIQN QAS QJQ42 NA I 4 I 10 W SU CITY | |||
:ssuco ocscAIPT:QN Q49 NRC USE ONLV a '.0 44 49 40 NAME OP PREPARER P.L. Pace PIICNE (305) 552-3801 SOXS ZOO "~1 | |||
REPORTABLB OCCURRENCE 335-80-39 LICENSEE EVENT REPORT PAGE 2 SUPPLElKNTARY INFO[NATION TECHNICAL SPECIFICATION REPORT DOSE E UIVALENT IODINE Reactor ower histor startin 48 hours rior to the first sam le in which the limit was exceeded. | |||
DATE TIHE AVEP>GE REACTOR PO)KR 8-12-80 03:00'4:OOJ 100% | |||
8-13-80 8-13-80 15:00 73% | |||
8-13-80 16:00 71% | |||
8-13-80 17 00 83% | |||
8-13-80 18 00 95% | |||
8-13-80 19:00 100% | |||
8-13-80 21:00~ | |||
8-13-80 22:00 90% | |||
8-13-80 23:00 56% | |||
8-14-80 :00 25% | |||
8-14-80 01 00 1% | |||
8-14-80 02:007 0% | |||
8-14-80 04 00 Fuel burnu b core re ion. | |||
See Attachment "A" | |||
: 3. Clean-u flow histor startin 48 hours rior to the first sam le in which the limit was exceeded. | |||
Purification flow was a constant 80 GPH for the entire 48 hour period. prior to exceeding, the DEQ iodine limit. | |||
: 4. ~Hister of de assin o aration it an startin 48 hours rior to the first sam le in which the limit was exceeded. | |||
There were no degassing operations during the 48 hours prior to exceeding the DEQ iodine limit. | |||
: 5. The time duration when the s ecific activit of the rimar coolant exceeded 1.0 Ci/ ram dose e uivalent I-131. | |||
DEQ iodine exceeded 1.0pCi/gram for approximately 8.5 hours. | |||
REPORTABLE OCCURRENCE 335-80-39 LICENSEE EVENT REPORT | |||
~PAGE 3 RESULTS OF COOLANT SPECIFIC ACTIVITY ANALYSIS gCiIt ram} | |||
DATE 1-131 2-132 1-133 I-135 ~DE 8-13-80 0905 0.0768 8-13-80 1400 Dropped CEA 87 8-13-80 1515 0.105 1715 0.152 8-14-80 0320 0.7144 0.2256 2.169 0.2362 1.317 0400 0.8044 0.2234 0.6963 0.2550 . 1.021 0453 1.136 0.2621 1.910 0.3403 1.69 0745 1.065 0.1646 0.8874 0.2631 1.332 0952 0.8939 0.1119 1.828 0.1697 1.406 1155 0.8283 0.0951 0.6375 0.1320 1.015 1400 0.88 Q DEQ iodine continued decreasing and pCi/gram on 8-18-80. | |||
stabilized at approximately 0.025 | |||
4e A | |||
~ | |||
4 | |||
Florida Power 5 Light Company FUEL BURNUP PER ASSEMBLY St. Lucie Plant Unit No. 1 g~~~ ~>>~~ | |||
LlcF~K Ev&~ NEPh~ | |||
gas-zo PAre M A~ca/w&vr A Y X N V T S R P NML K J HG F E D C 8 A | |||
~ | |||
lL12. 1$ Ll 20 | |||
~ | |||
1 l.08 1.9X I.090 .15"l .t@ .135 | |||
.ez.:1'! .g@ .258 ( .)3$ | |||
.~?1 ZW1 .220 | |||
,lQ, 5'1 1.W .Sg 1.QS . >? I.lSS lg lAA5 ~ | |||
u3 ).)~6 Zi I&7 1.013 1.'1<4 KS 4101 ).SI5 ).H6 1 ).7oB,Sbh | |||
),O15 A't& .ZlS )RO> .208 ),$ 1 Zl5 ).Gal .21 7 ).08tl 1.9z .ng 2041 [.C )xR z@S ).187 1<) ) lb' >,Sob | |||
).%5 341 ~ 211 1.@2 | |||
.13'l | |||
.nZ .'l'l5 )ASl .a01 l 70l SQ bio .Sm | |||
.2% | |||
1 IO 135 .95 | |||
.)g. | |||
0}} |
Latest revision as of 09:56, 4 February 2020
ML17266A373 | |
Person / Time | |
---|---|
Site: | Saint Lucie |
Issue date: | 09/15/1980 |
From: | Pace P FLORIDA POWER & LIGHT CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML17209A419 | List: |
References | |
LER-80-039-03L, LER-80-39-3L, NUDOCS 8012100479 | |
Download: ML17266A373 (7) | |
Text
NRC PORM 344 U. S. NUCLEAR REOULATORY COMMISS'ION I7.77 I LICENSEE EVENT REPORT I I I Ql IPLEJLIE PRINT OR TYPE ALL RECUIREO INPORMATIONI 4
~OI F IL S L S IllQ. 2 0 0 0 I010fO IOI- 0 0
.0, 4(l I 1 1 04
'UJLI
> f I Qs
'oo~~"
4 9 LICENSEE CQOE LICCArsa N4M4CA ~5 IS LaCINSC TVrc 40 $1 *a 34 CON'T
~O I 5 40 oi' 41 QQClCET NUM4CR Gl 44 44 CVCNT O*TC IS ACIQAT QA 4 50 oe EVENTOESCRIPTION AND SRQSABLE CONSEQUENCES Qlo Durin a short (12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />) maintenance shutdown, while in a startup mode, dose equivalent iodine (DE/) exceeded T.S. 3;4.8.a limit of 1.0IICi/gram DE I-131. The DE iodine was first measured above this limit at 0320 s on 8-14-80 and remained above the limit for a roximatel 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The 0 lj o ai inforlnation re uired b T.S. 3.4.8.d. This is
~a I the fourth occurrence of this t e.
~04 7 4 9 5v5Tsu cAUSS cAUsc Cour, vALvc
~O9 I 4
~l~
9 CQQC 10 Q>>
cQQE
~EQ>>
II 5uscooc
~X 11 Q>>
11 CQMSQNCNT CQOC U E L X X IQ14 I~
SUS QOS
~ZQS 19 5USCQCE
~Z 0
Q6 SCCUCNTIAI OCCVAAENCE AErQAT REVISION Or LEAIAO iso ACTION SUTURE r ~80'1 11 CrrCC ~
~ SAauTQOWN
~03 14 AEroAT NQ.
9 14
~~
11
~03 ac
- T AQNMSNT CQQC 19 vrelw Tvr 4
~L IO pall adc
~
cour 11
~0 NO.
11 CourQNCNT TAKEN ACTION CN rLANT METHQQ AQUAS +22 errrrrS oJS owr 1$ 14 40 SusulTTCO MS 41 rQAMSUS.
wmS 41 SurrUCA Mir 44 uAVurACTUACA 47 CAUSE OPSCRIPTION ANO CORRECI'IVE ACTIONS Q27 o After an extended eriod of ower o eration with a nominal level of fuel leakage, a dropped CEA (LER 335-80-38, CEA I/7), and the plant shutdown for f a sien s to cause iodine build-u
~iodine splkin 1-131 level decreesed to below
~S~
henomenon). The 030 a
1.0IICi/ ram after 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> and to nominal levels after 96 hours.
I 4 r ACILITY 5 ATUS '0 rOIISII QTbe CA STATUS Q 'aO AIETNQQ Qr OISCQVCAV olscovccv ocscAISTIQN ten I 4 raJS 9 10 11 11 44
~AQSI Operator Observation QS2 ACTIVITY CONTENT 40 AELEAsco Qr RELEASE AuoUNT Qr ACTIV>Tv QSS LOCATION or RELEASE Q16 2 ~QSS NA I 4 9 IO 11 44 45 r ASQNNEL EXrosuAES I 4
~I~Q>>~Q>9
~ 11 I 'I 11
~ SASQNNSL IIIIUAIES 50 i QLIILJg 10i !IA I 4 9 11 11 LCSS Qr CA QAM4CE To SACILITV 40 Tvrc ocscAlr TIQN QAS QJQ42 NA I 4 I 10 W SU CITY
- ssuco ocscAIPT:QN Q49 NRC USE ONLV a '.0 44 49 40 NAME OP PREPARER P.L. Pace PIICNE (305) 552-3801 SOXS ZOO "~1
REPORTABLB OCCURRENCE 335-80-39 LICENSEE EVENT REPORT PAGE 2 SUPPLElKNTARY INFO[NATION TECHNICAL SPECIFICATION REPORT DOSE E UIVALENT IODINE Reactor ower histor startin 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> rior to the first sam le in which the limit was exceeded.
DATE TIHE AVEP>GE REACTOR PO)KR 8-12-80 03:00'4:OOJ 100%
8-13-80 8-13-80 15:00 73%
8-13-80 16:00 71%
8-13-80 17 00 83%
8-13-80 18 00 95%
8-13-80 19:00 100%
8-13-80 21:00~
8-13-80 22:00 90%
8-13-80 23:00 56%
8-14-80 :00 25%
8-14-80 01 00 1%
8-14-80 02:007 0%
8-14-80 04 00 Fuel burnu b core re ion.
See Attachment "A"
- 3. Clean-u flow histor startin 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> rior to the first sam le in which the limit was exceeded.
Purification flow was a constant 80 GPH for the entire 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> period. prior to exceeding, the DEQ iodine limit.
- 4. ~Hister of de assin o aration it an startin 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> rior to the first sam le in which the limit was exceeded.
There were no degassing operations during the 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to exceeding the DEQ iodine limit.
- 5. The time duration when the s ecific activit of the rimar coolant exceeded 1.0 Ci/ ram dose e uivalent I-131.
DEQ iodine exceeded 1.0pCi/gram for approximately 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
REPORTABLE OCCURRENCE 335-80-39 LICENSEE EVENT REPORT
~PAGE 3 RESULTS OF COOLANT SPECIFIC ACTIVITY ANALYSIS gCiIt ram}
DATE 1-131 2-132 1-133 I-135 ~DE 8-13-80 0905 0.0768 8-13-80 1400 Dropped CEA 87 8-13-80 1515 0.105 1715 0.152 8-14-80 0320 0.7144 0.2256 2.169 0.2362 1.317 0400 0.8044 0.2234 0.6963 0.2550 . 1.021 0453 1.136 0.2621 1.910 0.3403 1.69 0745 1.065 0.1646 0.8874 0.2631 1.332 0952 0.8939 0.1119 1.828 0.1697 1.406 1155 0.8283 0.0951 0.6375 0.1320 1.015 1400 0.88 Q DEQ iodine continued decreasing and pCi/gram on 8-18-80.
stabilized at approximately 0.025
4e A
~
4
Florida Power 5 Light Company FUEL BURNUP PER ASSEMBLY St. Lucie Plant Unit No. 1 g~~~ ~>>~~
LlcF~K Ev&~ NEPh~
gas-zo PAre M A~ca/w&vr A Y X N V T S R P NML K J HG F E D C 8 A
~
lL12. 1$ Ll 20
~
1 l.08 1.9X I.090 .15"l .t@ .135
.ez.:1'! .g@ .258 ( .)3$
.~?1 ZW1 .220
,lQ, 5'1 1.W .Sg 1.QS . >? I.lSS lg lAA5 ~
u3 ).)~6 Zi I&7 1.013 1.'1<4 KS 4101 ).SI5 ).H6 1 ).7oB,Sbh
),O15 A't& .ZlS )RO> .208 ),$ 1 Zl5 ).Gal .21 7 ).08tl 1.9z .ng 2041 [.C )xR z@S ).187 1<) ) lb' >,Sob
).%5 341 ~ 211 1.@2
.13'l
.nZ .'l'l5 )ASl .a01 l 70l SQ bio .Sm
.2%
1 IO 135 .95
.)g.
0