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{{#Wiki_filter:. S. NUCLEAR REGULATORY COMMISSION NRC FORM 366 I7-77)
LICENSEE EVENT REPORT CONTROL BLOCK:                                                  Q1                (PLEASE PRINT OR TYPE ALL REQUIRED INFORIVIATION)
I                                6 7      8    9 M      I    DCC1Qs00000000000Qs41 LICENSEE CODE              14    15                    LICENSE NUMBER                        25      26 1
LICENSE TYPE 11Qs~Qs30    57 CAT 58 CON'T
[QD1]              R'RE ~LQB                    0    5    0    0    0    3    1    5 Q7      0    2    1    8    7      9    QBO          3                        QB 7        8                      60            61            DOCKET NUMBER                68    69      EVENT DATE                74      75      REPORT DATE        80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                              Q10 DURING NORMAL OPERATION WHILE VALVING. OUT THE WEST CENTRI'FUGAL CHARGING PUMP FOR
~O3                MAINTENANCE, THE SUCTION VALVE WAS FOUND CLOSED CONTRARY TO                                                            T.S, 3.5,2, INVESTIGATION REVEALED THAT THE VALVE HAD BEEN MISTAKENLY CLOSED FOLLOWING
~os                SURVEILLANCE TESTING.                          THE WEST TRAIN WAS INOPERABLE FOR A.PERIOD OF                                              52.5  HOURS.
~os                DURING THIS TIME THE EAST PUMP WAS CONTINUOUSLY OPERABLE.
~O7
~OS                                                                                                                                                                              80 7      8 SYSTEM            CAUSE          CAUSE                                                          COMP.            VALVE CODE              CODE        SUBCODE                  COMPONENT CODE                      SUBCODE          SUBCODE F    Qii      A Qis      ~BQis            V    A    L    V    E    X    Gs        ~2Qis            ~0 7      8                        9          10        11            12              13                              18          19              20 SEQUENTIAL                          OCCURRENCE              REPORT                      REVISION Qii LERiRO REPORT ACTION FUTURE EVENT YEAR
                                    ~79 21        22 EFFECT
                                                          +
23 SHUTDOWN
                                                                        ~gp 24 REPORT NO.
p 26 Qw 27
                                                                                                                  ~03 28 ATTACHMENT CODE 29 NPRDQ TYPE
                                                                                                                                          +C 30 PRIME COMP.
31 NO.
Qp 32 COMPONENT TAKEN ACTION                    ON PLANT          METHOD                    HOURS +22        SUBMITTED          FORM SUB.          SUPPLIER            MANUFACTURER
              ~XQis ~HQis                      ~ZQss            ~ZQsi              0    0    0  11            Y  Qn          ~NQss            ~ZQss              2  9    9 9  Qss 33          34                  sI 5              36              37                    40    41                  42                43              44            47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27
  ~io              UPON COMPLETION OF THE SURVEILLANCE TEST RUN OF THE                                                      UM        AN    AUXILIARY E UIPMENT OPERATOR WAS INSTRUCTED TO PLACE THE PUMP B CK THE DISCHARGE VALVE AND CLOSED THE SUCTION VALVE WHICH                                                        IS THE CONDITION IN WHICH 3            HE FOUND THE PUMP BEFORE THE TEST RUN.                                                  CONTINUED            --    P GE      2 4
80 7      8  9 FACILITY STATUS
                            ~pp  99POWER                      OTHER STATUS      ~        METHOD OF DISCOVERY                                DISCOVERY DESCRIPTION Q32 OPERAT R            BSERVATIO 5      ~E    Qss                            Qss              NA                        LAJQ31 7      8  9              10                12                                      44    45        46                                                                      80 CONTENT ACTIVITY AMOUNT OF ACTIVITY                                                          LOCATION OF RELEASE        Q EZ 7      8
            ~Q LLIS RELEASED OF RElEASE 9              10 PERSONNEL EXPOSURES 11                                          44          45                                                                          80 NUMBER                TYPE        DESCRIPTION 7      8
            ~00 9
0 Qsi ~ZQss 11      12          13 NA 80 PERSONNEL INJURIES NUMBER                DESCRIPTION Q41
[iisJ8 ~Op 7          9 p Qss 11        12 NA 80 LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                    Q s          ZQ42                        NA 80 7      8  9 ISSUED PUB  ll10 CITY DESCRIPTION ".
NRC USE ONLY KZ      8 WNQ44 9          10 NA 68    69                        80 ~
c ss NAME OF PREPARER                  H~    M. ChadWel        1                                            PHONE          616      465-5901 X-316            c
 
0 n
 
CONTINUATION OF LER  879-007/03L-0 PAGE 2 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS THE SUCTION VALVE HAD BEEN CLOSED BY A DIFFERENT OPERATOR TO PERFORM ANOTHER TEST. THE SECOND OPERATOR RETURNED THE PUMP TO THE CONDITION WHICH HE FOUND IT. THE ERROR OCCURRED BECAUSE OF A LACK OF COORDINATION BETWEEN THE TWO AUXILIARY EQUIPMENT OPERATORS AND ALSO BECAUSE THE INSTRUCTIONS  WERE NOT EXPLICIT  ENOUGH. A LETTER HAS BEEN SENT TO EACH SHIFT OPERATING ENGINEER REQUESTING A REVIEW OF THIS INCIDENT WITH HIS PERSONNEL.
                                            \}}

Latest revision as of 02:11, 4 February 2020

LER 79-007/03L-0 on 790218:suction Valve of West Centrifugal Charging Pump Found Closed.Caused by Mistaken Closing Following Surveillance Testing.Incident Is Being Reviewed
ML17317B005
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/13/1979
From: Chadwell H
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B004 List:
References
LER-79-007-03L-01, LER-79-7-3L-1, NUDOCS 7903190293
Download: ML17317B005 (3)


Text

. S. NUCLEAR REGULATORY COMMISSION NRC FORM 366 I7-77)

LICENSEE EVENT REPORT CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORIVIATION)

I 6 7 8 9 M I DCC1Qs00000000000Qs41 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 1

LICENSE TYPE 11Qs~Qs30 57 CAT 58 CON'T

[QD1] R'RE ~LQB 0 5 0 0 0 3 1 5 Q7 0 2 1 8 7 9 QBO 3 QB 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 DURING NORMAL OPERATION WHILE VALVING. OUT THE WEST CENTRI'FUGAL CHARGING PUMP FOR

~O3 MAINTENANCE, THE SUCTION VALVE WAS FOUND CLOSED CONTRARY TO T.S, 3.5,2, INVESTIGATION REVEALED THAT THE VALVE HAD BEEN MISTAKENLY CLOSED FOLLOWING

~os SURVEILLANCE TESTING. THE WEST TRAIN WAS INOPERABLE FOR A.PERIOD OF 52.5 HOURS.

~os DURING THIS TIME THE EAST PUMP WAS CONTINUOUSLY OPERABLE.

~O7

~OS 80 7 8 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE F Qii A Qis ~BQis V A L V E X Gs ~2Qis ~0 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Qii LERiRO REPORT ACTION FUTURE EVENT YEAR

~79 21 22 EFFECT

+

23 SHUTDOWN

~gp 24 REPORT NO.

p 26 Qw 27

~03 28 ATTACHMENT CODE 29 NPRDQ TYPE

+C 30 PRIME COMP.

31 NO.

Qp 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS +22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~XQis ~HQis ~ZQss ~ZQsi 0 0 0 11 Y Qn ~NQss ~ZQss 2 9 9 9 Qss 33 34 sI 5 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27

~io UPON COMPLETION OF THE SURVEILLANCE TEST RUN OF THE UM AN AUXILIARY E UIPMENT OPERATOR WAS INSTRUCTED TO PLACE THE PUMP B CK THE DISCHARGE VALVE AND CLOSED THE SUCTION VALVE WHICH IS THE CONDITION IN WHICH 3 HE FOUND THE PUMP BEFORE THE TEST RUN. CONTINUED -- P GE 2 4

80 7 8 9 FACILITY STATUS

~pp 99POWER OTHER STATUS ~ METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32 OPERAT R BSERVATIO 5 ~E Qss Qss NA LAJQ31 7 8 9 10 12 44 45 46 80 CONTENT ACTIVITY AMOUNT OF ACTIVITY LOCATION OF RELEASE Q EZ 7 8

~Q LLIS RELEASED OF RElEASE 9 10 PERSONNEL EXPOSURES 11 44 45 80 NUMBER TYPE DESCRIPTION 7 8

~00 9

0 Qsi ~ZQss 11 12 13 NA 80 PERSONNEL INJURIES NUMBER DESCRIPTION Q41

[iisJ8 ~Op 7 9 p Qss 11 12 NA 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q s ZQ42 NA 80 7 8 9 ISSUED PUB ll10 CITY DESCRIPTION ".

NRC USE ONLY KZ 8 WNQ44 9 10 NA 68 69 80 ~

c ss NAME OF PREPARER H~ M. ChadWel 1 PHONE 616 465-5901 X-316 c

0 n

CONTINUATION OF LER 879-007/03L-0 PAGE 2 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS THE SUCTION VALVE HAD BEEN CLOSED BY A DIFFERENT OPERATOR TO PERFORM ANOTHER TEST. THE SECOND OPERATOR RETURNED THE PUMP TO THE CONDITION WHICH HE FOUND IT. THE ERROR OCCURRED BECAUSE OF A LACK OF COORDINATION BETWEEN THE TWO AUXILIARY EQUIPMENT OPERATORS AND ALSO BECAUSE THE INSTRUCTIONS WERE NOT EXPLICIT ENOUGH. A LETTER HAS BEEN SENT TO EACH SHIFT OPERATING ENGINEER REQUESTING A REVIEW OF THIS INCIDENT WITH HIS PERSONNEL.

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