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| | issue date = 01/29/1999 | | | issue date = 01/29/1999 |
| | title = LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr | | | title = LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr |
| | author name = BRASSART G, SAMPSON J R | | | author name = Brassart G, Sampson J |
| | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG | | | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:CATEGORY1REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDE)ACCESSION NBR:9902030311 DOC.DATE: | | {{#Wiki_filter:CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDE) |
| 99/01/29NOTARIZED: | | ACCESSION NBR:9902030311 DOC.DATE: 99/01/29 NOTARIZED: NO DOCKET ¹ FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 AUTH. NAME AUTHOR AFFILIATION BRASSART, G. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele SAMPSON,J.R. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION |
| NODOCKET¹FACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,IndianaM05000315AUTH.NAMEAUTHORAFFILIATION
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| : BRASSART, G.IndianaMichiganPowerCo.(formerly Indiana&MichiganEleSAMPSON,J.R.
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| IndianaMichiganPowerCo.(formerly Indiana&MichiganEleRECIP.NAME RECIPIENT AFFILIATION
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER98-059-00:on 981230,interim LER-singlefailureincontainment spraysyscouldresultincontainment spraypHoutsidedesignoccurred.
| | LER 98-059-00:on 981230,interim LER -single failure in containment spray sys could result in containment spray pH outside design occurred. Investigation into condition continuing. Update will be submitted by 990514 ltr. |
| Investigation intocondition continuing. | | DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL I SIZE: |
| Updatewillbesubmitted by990514ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR IENCLISIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RECIPIENT IDCODE/NAME PD3-3PDCOPIESLTTRENCL11RECIPIENT IDCODE/NAME STANG,JCOPIESLTTRENCL110INTERNAL:
| | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. |
| AEOD/SPDRABNRR/DE/EELB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RGN3FILE01EXTERNAL: | | NOTES: |
| LSTLOBBYWARDNOACPOORE,W.NRCPDR221111111111111'1111AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HOHB NRR/DRPM/PECB RES/DET/EIB LITCOBRYCE,JHNOACQUEENER,DS NUDOCSFULLTXT111111111111111111DUNNOTETOALLMRIDSMRECIPIENTS:
| | RECIPIENT COPIES RECIPIENT COPIES 0 ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 PD 1 1 STANG,J 1 1 INTERNAL: AEOD/SPD RAB 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOHB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/EIB 1 1 RGN3 FILE 01 1 1 D |
| PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
| | LITCO BRYCE,J H EXTERNAL: L ST LOBBY WARD 1 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 U |
| LTTR22ENCL22 0
| | N NOTE TO ALL MRIDSM RECIPIENTS: |
| IndianaMichigan~PowerCompanyGxkBuaer~>asxexr,-aiBridyncn.
| | PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 22 ENCL 22 |
| ha49106ele-'ea~sZINDIANAMICHIGANIaOM%RJanuary29,1999UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, DC20555Operating LicenseDPR-58DocketNo.50-315DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventLER315/98-059-00,"Single FailureInContainment SpraySystemCouldResultlnContainment SpraypHOutsideDesign"Nocommitments wereidentified inthissubmittal.
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| Sincerely, i.k4~J.R.SampsonSiteVicePresident
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| /mbdAttachment c:J.L.Caldwell(Acting),
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| RegionIIIR.P.PowersP.A.BarrettD.F.Kunsemiller R.WhaleD.HahnRecordsCenter,INPONRCResidentInspector
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| +f1l''rr99020303ii 990i29PDRADQCK050003i5SPDR
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| aNRCForm366U.S.NUCLEARREGULATORY COMMISSION (6-1998)LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEDBYOMBNo.3160.0104 EXPIRES06/30/2001 ESTIMATED SVRDENPERRESPONSETOCOMPLYWITHTIOSMANDATORY INFORMATION COLLECTION REOVEST500HRSREPORTEDLESSONSLEARNEDAREWCORPORATED INTOTHEUCENSINGPROCESSANOFEDSACKTOINDVSTRY.
| | 0 Indiana Michigan Power Company Gxk Buaer >as |
| FORWARDCOMMENTSREGARDING SVRDENESTasATETOTHEINFORMATION ANDRECORDSMANACEMENT SRANCHIT%F55).V.S.NUCLEARREGIAATORY COMMISSlON, WASHINGTON.
| | ~ |
| DC20555400I.
| | xe xr,-a i Bridyncn. ha 491 06 |
| ANDTOTHEPAPERWORK REDVCTION PRO)ECTts)50o)0I)
| | ~s Z |
| OFFICEOFMANAGEMENT ANOBVDCET.WASICNGTON.
| | ele -'ea INDIANA MICHIGAN IaOM%R January 29, 1999 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Operating License DPR-58 Docket No. 50-315 Document Control Manager: |
| DC20505FACIUTYNAMEtl)CookNuclearPlantUnit1DOCKETNUMBERI2)05000-315 PAGEIS)1of1TITLE14)InterimLER-SingleFailureInContainment SpraySystemCouldResultInContainment SpraypHOutsideDesignEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MONTHDAY1230YEARYEAR19981998SEQUENTIAL NUMBER0590001291999REVISIONNUMBERMONTHDAYYEARAILINAMDCCook-Unit2ACILINAMDNUMB05000-316 KNUMOPERATING MODE(9)POWERLEVEL(10) 000e)(11)20.2201(b)20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(v) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(viii) 50.73(a)(2)(x) 73.71THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFRg:(Checkoneormor20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(4) 50.36(c)(1) 50.36(c)(2)
| | In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event LER 315/98-059-00,"Single Failure In Containment Spray System Could Result ln Containment Spray pH Outside Design" No commitments were identified in this submittal. |
| LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii)
| | Sincerely, i.k4 ~ |
| OTHERSpeci/rIr)AbstractDeicerornNRCForm366ANAMEMr.GaryBrassart, NuclearSafetyAnalysisSupervisor TELEPHONE NUMBER(IncsvdeAreaCode)616/697-5106 COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXslMuNSUPPLEMENTAL REPORTEXPECTED(14)XYES(IfYes,completeEXPECTEDSUBMISSION DATE)NOEXPECTEDSUBMISSION DATE(15)MONTH05DAY141999Abstract(Limitto1400spaces,i.e.,approximately 15single-spaced typewritten lines)(16)InDecember1998,plantpersonnel identified anissueregarding asinglefailureintheContainment Spray(CTS)Systemwhichcouldresultinlossofsodiumhydroxide chemicaladditiontoasingletrainofCTSduringinjection phase.OnDecember30,1998,itwasdetermined thatthisrepresented acondition outsidethedesignbases.Therefore, thisinterimreportisbeingsubmitted inaccordance with10CFR50.73(a)(2)(ii)(B) asacondition outsidethedesignbasesoftheplant.TheContainment SpraySystemoperatesinresponsetoaLossofCoolantAccident(LOCA)orMSLBinsidecontainment.
| | J. R. Sampson Site Vice President |
| Sodiumhydroxide solutionfromthesprayadditivetankisaddedtothesprayusinganeductor,andensuresthatthepHofthesprayandsumparemaintained withintheestablished limits.Ifasinglevalvesupplying CTSflowthroughtheeductorforonetrainofCTSfailsclosed,chemicaladditiontothattrainwouldbestopped.Lackofsodiumhydroxide additionresultsinboratedwaterfromtheRWST,withapHof4.5,beingsprayedoncomponents insidecontainment fromtheaffectedtrainofCTS.Theequipmentincontainmentisqualified forapHrangeof6.8to12.9.
| | /mbd Attachment c: J. L. Caldwell (Acting), Region III R. P. Powers P. A. Barrett D. F. Kunsemiller R. Whale D. Hahn Records Center, INPO NRC Resident Inspector |
| Therefore, sprayingRWSTwaterwithoutsodiumhydroxide additiveresultsinspraypHoutsidetherangeusedforequipment qualification. | | +''rr f1 l 99020303ii 990i29 PDR ADQCK 050003i5 S PDR |
| Thiscondition appearstobepartoftheoriginaldesignoftheplant.Investigation intothiscondition iscontinuing, andisexpectedtobecompleteApril30.AnupdatetothisinterimLERwillbesubmitted byMay14,1999.NRCFORM366(6-1998)}}
| | |
| | a NRC Form 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160.0104 EXPIRES 06/30/2001 (6-1998) ESTIMATED SVRDEN PER RESPONSE TO COMPLY WITH TIOS MANDATORY INFORMATIONCOLLECTION REOVEST 500 HRS REPORTED LESSONS LEARNED ARE WCORPORATED INTO THE UCENSING PROCESS ANO FED SACK TO INDVSTRY. |
| | LICENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING SVRDEN ESTasATE TO THE INFORMATIONAND RECORDS MANACEMENT SRANCH IT% F55). V.S. NUCLEAR REGIAATORY COMMISSlON, WASHINGTON. DC 20555400I. AND TO THE PAPERWORK REDVCTION PRO)ECT ts)50o)0I) OFFICE OF MANAGEMENT ANO BVDCET. WASICNGTON. DC (See reverse for required number of 20505 digits/characters for each block) |
| | FACIUTY NAME tl) DOCKET NUMBER I2) PAGE IS) |
| | Cook Nuclear Plant Unit 1 05000-315 1 of 1 TITLE 14) |
| | Interim LER - Single Failure In Containment Spray System Could Result In Containment Spray pH Outside Design EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| | A ILI NAM D NUMB SEQUENTIAL REVISION DC Cook - Unit 2 05000-316 MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR ACILI NAM K NUM 12 30 1998 1998 059 00 01 29 1999 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR g: (Check one or mor e) (11) |
| | MODE (9) 20.2201 (b) 20.2203(a)(2)(v) 50.73(a)(2)(i) 50.73(a)(2)(viii) |
| | POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x) |
| | LEVEL(10) 000 73.71 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50.73(a)(2)(v) |
| | Speci/r Ir) Abstract Deicer 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) or n NRC Form 366A LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER (Incsvde Area Code) |
| | Mr. Gary Brassart, Nuclear Safety Analysis Supervisor 616/697-5106 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | REPORTABLE REPORTABLE TO CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX CAUSE SYSTEM COMPONENT MANUFACTURER EPIX sl Mu N |
| | SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY X YES SUBMISSION 05 14 1999 (If Yes, complete EXPECTED SUBMISSION DATE) NO DATE (15) |
| | Abstract (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) |
| | In December 1998, plant personnel identified an issue regarding a single failure in the Containment Spray (CTS) System which could result in loss of sodium hydroxide chemical addition to a single train of CTS during injection phase. On December 30, 1998, it was determined that this represented a condition outside the design bases. Therefore, this interim report is being submitted in accordance with 10 CFR 50.73 (a)(2)(ii)(B) as a condition outside the design bases of the plant. |
| | The Containment Spray System operates in response to a Loss of Coolant Accident (LOCA) or MSLB inside containment. |
| | Sodium hydroxide solution from the spray additive tank is added to the spray using an eductor, and ensures that the pH of the spray and sump are maintained within the established limits. If a single valve supplying CTS flow through the eductor for one train of CTS fails closed, chemical addition to that train would be stopped. Lack of sodium hydroxide addition results in borated water from the RWST, with a pH of 4.5, being sprayed on components inside containment from the affected train ofCTS. Theequipmentincontainmentisqualified fora pHrangeof6.8to12.9. Therefore, spraying RWST water without sodium hydroxide additive results in spray pH outside the range used for equipment qualification. |
| | This condition appears to be part of the original design of the plant. Investigation into this condition is continuing, and is expected to be complete April 30. An update to this interim LER will be submitted by May 14, 1999. |
| | NRC FORM 366 (6-1998)}} |
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Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:RO)
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDE)
ACCESSION NBR:9902030311 DOC.DATE: 99/01/29 NOTARIZED: NO DOCKET ¹ FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 AUTH. NAME AUTHOR AFFILIATION BRASSART, G. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele SAMPSON,J.R. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 98-059-00:on 981230,interim LER -single failure in containment spray sys could result in containment spray pH outside design occurred. Investigation into condition continuing. Update will be submitted by 990514 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL I SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES 0 ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 PD 1 1 STANG,J 1 1 INTERNAL: AEOD/SPD RAB 2 2 AEOD/SPD/RRAB 1 1 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOHB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/EIB 1 1 RGN3 FILE 01 1 1 D
LITCO BRYCE,J H EXTERNAL: L ST LOBBY WARD 1 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 U
N NOTE TO ALL MRIDSM RECIPIENTS:
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ele -'ea INDIANA MICHIGAN IaOM%R January 29, 1999 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Operating License DPR-58 Docket No. 50-315 Document Control Manager:
In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event LER 315/98-059-00,"Single Failure In Containment Spray System Could Result ln Containment Spray pH Outside Design" No commitments were identified in this submittal.
Sincerely, i.k4 ~
J. R. Sampson Site Vice President
/mbd Attachment c: J. L. Caldwell (Acting), Region III R. P. Powers P. A. Barrett D. F. Kunsemiller R. Whale D. Hahn Records Center, INPO NRC Resident Inspector
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a NRC Form 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160.0104 EXPIRES 06/30/2001 (6-1998) ESTIMATED SVRDEN PER RESPONSE TO COMPLY WITH TIOS MANDATORY INFORMATIONCOLLECTION REOVEST 500 HRS REPORTED LESSONS LEARNED ARE WCORPORATED INTO THE UCENSING PROCESS ANO FED SACK TO INDVSTRY.
LICENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING SVRDEN ESTasATE TO THE INFORMATIONAND RECORDS MANACEMENT SRANCH IT% F55). V.S. NUCLEAR REGIAATORY COMMISSlON, WASHINGTON. DC 20555400I. AND TO THE PAPERWORK REDVCTION PRO)ECT ts)50o)0I) OFFICE OF MANAGEMENT ANO BVDCET. WASICNGTON. DC (See reverse for required number of 20505 digits/characters for each block)
FACIUTY NAME tl) DOCKET NUMBER I2) PAGE IS)
Cook Nuclear Plant Unit 1 05000-315 1 of 1 TITLE 14)
Interim LER - Single Failure In Containment Spray System Could Result In Containment Spray pH Outside Design EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
A ILI NAM D NUMB SEQUENTIAL REVISION DC Cook - Unit 2 05000-316 MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR ACILI NAM K NUM 12 30 1998 1998 059 00 01 29 1999 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR g: (Check one or mor e) (11)
MODE (9) 20.2201 (b) 20.2203(a)(2)(v) 50.73(a)(2)(i) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL(10) 000 73.71 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50.73(a)(2)(v)
Speci/r Ir) Abstract Deicer 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) or n NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Incsvde Area Code)
Mr. Gary Brassart, Nuclear Safety Analysis Supervisor 616/697-5106 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE REPORTABLE TO CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX CAUSE SYSTEM COMPONENT MANUFACTURER EPIX sl Mu N
SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY X YES SUBMISSION 05 14 1999 (If Yes, complete EXPECTED SUBMISSION DATE) NO DATE (15)
Abstract (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
In December 1998, plant personnel identified an issue regarding a single failure in the Containment Spray (CTS) System which could result in loss of sodium hydroxide chemical addition to a single train of CTS during injection phase. On December 30, 1998, it was determined that this represented a condition outside the design bases. Therefore, this interim report is being submitted in accordance with 10 CFR 50.73 (a)(2)(ii)(B) as a condition outside the design bases of the plant.
The Containment Spray System operates in response to a Loss of Coolant Accident (LOCA) or MSLB inside containment.
Sodium hydroxide solution from the spray additive tank is added to the spray using an eductor, and ensures that the pH of the spray and sump are maintained within the established limits. If a single valve supplying CTS flow through the eductor for one train of CTS fails closed, chemical addition to that train would be stopped. Lack of sodium hydroxide addition results in borated water from the RWST, with a pH of 4.5, being sprayed on components inside containment from the affected train ofCTS. Theequipmentincontainmentisqualified fora pHrangeof6.8to12.9. Therefore, spraying RWST water without sodium hydroxide additive results in spray pH outside the range used for equipment qualification.
This condition appears to be part of the original design of the plant. Investigation into this condition is continuing, and is expected to be complete April 30. An update to this interim LER will be submitted by May 14, 1999.
NRC FORM 366 (6-1998)